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{{#Wiki_filter:!+ACCELERATED DISTRIBUTION DEMONSTRATION SYSTEM REGULATOR INFORMATION DISTRlBUTION pTEM (RIDS)ACCESSION NBR:9203110291 DOC.DATE: 92/03/04 NOTARIZED:
{{#Wiki_filter:!
NO DOCKET¹FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH.NAME AUTHOR AFFILIATION BACKUSiW.H.
  +   ACCELERATED DISTRIBUTION DEMONSTRATION SYSTEM REGULATOR       INFORMATION DISTRlBUTION           pTEM (RIDS)
Rochester Gas&Electric Corp.MECREDY,R.C.
ACCESSION NBR:9203110291             DOC.DATE: 92/03/04         NOTARIZED: NO           DOCKET ¹ FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester                       G 05000244 AUTH. NAME           AUTHOR AFFILIATION BACKUSiW.H.         Rochester Gas & Electric Corp.
Rochester Gas&Electric Corp.RECIP.NAME RECiPIENT AFFILIATION
MECREDY,R.C.         Rochester Gas & Electric Corp.
RECIP.NAME           RECiPIENT AFFILIATION R


==SUBJECT:==
==SUBJECT:==
LER 92-002-00:on 920203,reactor trip occurred w/reactor at approx 23%full power just subsequent to turbine trip while at 47%power.Caused by lo lo level in SG A due to design perturbations.New setting calculated.W/920304 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
LER   92-002-00:on 920203,reactor trip occurred w/reactor at approx 23% full power just subsequent to turbine trip while at 47% power. Caused by lo lo level in SG A due to design perturbations.New setting calculated.W/920304                 ltr.                     D DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR                     ENCL     SIZE:
R D/05000244 A RECIPIENT ID CODE/NAME PDl-3 LA JOHNSON,A COPIES LTTR ENCL 1 1 1 1 RECIPIENT ID CODE/NAME PD1-3 PD COPIES LTTR ENCL 1 1 D D INTERNAL: ACNW AEOD/DSP/TPAB NRR/DET/EMEB 7E NRR/DLPQ/LPEB10 NRR/DREP/PRPBll NRR/DST/SICB8H3 NRR/DST/SRXB 8E RES/DSIR/EIB EXTERNAL'G&G BRYCE i J~H NRC PDR NSIC POOREiW.AEOD/DOA AEOD/ROAB/DSP NRR/DLPQ/LHFB10" NRR/DOEA/OEAB NRR/DST/SELB 8D gNR~D-.LB8Dl-G~02 RGN1 FILE 01 3 3 L ST LOBBY WARD 1 1 1 1 NSIC MURPHYgG.A 1 1 1.1 NUDOCS FULL TXT 1 1 2 2 1 1 1 1 2 2 1 1 1 1 1 1 1 1 2 2 1~1'1 1 1 1 1 1 1 1 1 1 1 1 D NOTE TO ALL"RIDS" RECIPIENTS:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!A D D S FULL'TEXT CONVERSION REQUIRED TOTAL NUMB R OF COPIES REQUIRED: LTTR 30 ENCL 30 I
                                                                                                        /
rr f~'I~zotrr.sT4 M ROCHESTER GAS AND ELECTRIC CORPORATION 4 89 EAST AVENUE, ROCHESTER N.K-74649-0001 ROBER't (, hlECRjtpY Vrr<Vresidenl Crnna No<lcm Prodursrorr TELE&>0'ME ARErr COM 716 546'2700 March 4, 1992 U.S.Nuclear Regulatory Commission Document Control Desk Washington, DC 20555  
NOTES:License Exp date       in accordance with 10CFR2,2.109(9/19/72).                 05000244 A
RECIPIENT              COPIES              RECIPIENT            COPIES              D ID CODE/NAME            LTTR ENCL        ID CODE/NAME         LTTR ENCL PDl-3 LA                     1   1     PD1-3 PD                   1     1             D JOHNSON,A                    1    1 INTERNAL: ACNW                         2    2      AEOD/DOA                  1      1 AEOD/DSP/TPAB                 1    1      AEOD/ROAB/DSP              2      2 NRR/DET/EMEB 7E               1    1      NRR/DLPQ/LHFB10"          1      1 NRR/DLPQ/LPEB10               1    1      NRR/DOEA/OEAB              1      1 NRR/DREP/PRPBll               2    2      NRR/DST/SELB 8D            1    ~ 1
                                            '1 G~ FILELB8Dl gNR~D      -.
NRR/DST/SICB8H3                   1                                1      1 NRR/DST/SRXB 8E               1    1      -                02      1      1 RES/DSIR/EIB                 1    1      RGN1              01      1      1 EXTERNAL'G&G BRYCE i J ~ H               3   3     L ST LOBBY WARD           1     1 NRC PDR                      1   1     NSIC MURPHYgG.A           1     1 NSIC POOREiW.                1. 1     NUDOCS FULL TXT           1     1 D
A D
D NOTE TO ALL "RIDS" RECIPIENTS:
S PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL 'TEXT CONVERSION REQUIRED TOTAL NUMB R OF COPIES REQUIRED: LTTR                 30   ENCL     30
 
I
                                                                                            'I ~
f rr ~
zotrr.
sT4 M ROCHESTER GAS AND ELECTRIC CORPORATION             4 89 EAST AVENUE, ROCHESTER N. K 74649-0001 ROBER't   (, hlECRjtpY                                                               TELE&>0'ME Vrr< Vresidenl                                                                ARErr COM 716 546'2700 Crnna No<lcm Prodursrorr March 4, 1992 U.S. Nuclear Regulatory Commission Document           Control Desk Washington,             DC   20555


==Subject:==
==Subject:==
LER 92-002, Feedwater Transient, Due To Loss Of Excitation Induced Turbine/Generator Trip, Causes Lo Lo Steam Gen'erator Level Reactor Trip-R.E.Ginna Nuclear Power Plant Docket No.50-244In accordance with 10CFR50.73, Licensee.Event Report System, item (a)(2)(iv), which requires a report of,"any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)", the attached Event Report LER 92-002 is hereby submitted.
LER   92-002, Feedwater Transient, Due To Loss                       Of Excitation Induced Turbine/Generator Trip, Causes                     Lo Lo Steam Gen'erator Level Reactor Trip
This event has in no way affected the public's health and safety.Very truly yours, Robert C.Mecredy.xco U.S.Nuclear Regulatory Commission Re'gion I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector f)~g(4~(q'l 92031i0291
                              -R.E. Ginna Nuclear Power   Plant Docket No. 50-244 In accordance with 10CFR50.73, Licensee. Event Report System, item         (a)(2)(iv), which requires a report of, "any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System           (RPS)",     the attached Event Report LER 92-002             is       hereby submitted.
'720304 PDR ADOCK 05000244 5 PDR I t'l  
This event has in no way affected the public's health and safety.
<<AC crea<<I 4ASI LICENSEE EVENT REPORT LER)Ug, IRILSAR RIRVLATCAT coe>>e<<voce Aeeaavla Oeet NO,$1<<.aiav ISIIAIS I/SQIS eACILITY NAeel Ill R.E.in'na Nuclear Power Plant: OOCRtT IA>>eOIR Ql A o6ooo244>ot
Very truly yours, Robert C. Mecredy.
'" Feedwater Transient, Due to Loss of Excitation n uced Tur z.ne Generator Trip, Causes Lo Lo Steam Generator Level Reactor Trip I VINS OATS III LtR NueettA III AIMRT OATI III OTHIA eACILITISI INVOLVIO Nl VO<<TH OAY YIA1 YIAR 0 2 3 9 2 9 2~save<<ewe<<vee~IA 0 0 2 Ae v orcee Irueee~A 0 IION TH 0 3 OAY 0 4 YIAR 9 2 eACIUTY<<Aeeee OOCAIT<<uee~SAISI 0 6 0 0 O 0 6 0 0 0 Oel1*TINO eeOOI Itl~Oeel1 LlvlL 0 2 3 THIS 1leOAT N SuteeITTIO euAWANT I$Lea$4I SO.NQ Nl ll I II Sa.calle III I III St.e le I II I I RI$OAOllel ll I l<<l SO.OOS lelll llel St.cell el~OMW III~OMWQI~O.T SN I QI I I~O.T tie I Q I I II IO.TSNIQIIVO
xco               U. S. Nuclear Regulatory Commission Re'gion   I 475   Allendale Road King of Prussia, PA     19406 Ginna   USNRC   Senior Resident Inspector f) q'l ~g(4
~O.T SNI Q I I<<I~O.TSlalQ)lel
                                                                                        ~(
~O.TSlalQlleOI IO.T I lel Qll era IAI~0.$SIeIQIleetl QI SO.TSWQll el 0 THI 1$ovl1tlelNTI Oe I tel 1$." lceeee err er cere el eee eeeeree>>Ill l M714I TLTllel OTHSR lteeeeV Ie Aeeeeee erer ere ee TeeL<<RC/>>4<<AUI LICINSII CONTACT MR THQ LSA llll TILteleONI NVLQIA Wesley JI.Backus ARIA COOl Technical Assist:ant to the Operations Manager 3 1 5 5 2 4 44 CCAVLST I ONS LINC>OR tACH CaeeMNINT OAILUAI 0tlCA Illa Iel THIS RIM AT lltl CAUSI SYSTIN COIIMNINT VA<<u>ACr TVAIA IMRTAILI'gent,~H<@t To NeRos r~P4;":~Qj C VSI SYSTSN coeeMN IN T HANVSA4 TV AIR IMATAI L TO NOAOS X B T B W 3 1 5 g~NAN$3'.~e'rte rr%g~rr3>vVjj~4~e:
92031i0291 '720304 PDR         ADOCK 05000244 5                           PDR
.II~I,>>~C.~,y;$$4 SVTTLININT*L AIMAT tteICTIO IIAI V II Ill Tee.er<<e>>N SRJSCTSO SVINISSIO>>
 
OATII AJSTA*cT ILeevl 4 Ieco eeeer.I A, eeereee<<e>>re AY>>ee ree>>eeeee eeoer<<I>>e<<eev lltl ttetCTSO LVINISSION OA'll ll~I eeONTH CAY YIAR On February 3, 1992 with the reactor at approximately 23%full power, just subsequent to a turbine trip while at 474 reactor power, a reactor trip occurred due to Lo Lo Level (</=17%)in the"A" Steam Generator (S/G).The Control Room operators immediately performed the appropriate actions of Emergency Operating Procedures E-0 (Reactor Trip or Safety Injection) and ES-0.1 (Reactor Trip Response).
I t
Both Main Steam Isolation Valves (MSIVs)were subsequently closed to limit a Reactor Coolant System (RCS)cooldown and the plant was stabil-ized at hot shutdown.The underlying cause of the event was the inability to control the"A" S/G level above the reactor trip setpoint due to design and transient induced perturbations.(This event is NUREG-1022 (x)Cause Code).Corrective action taken or planned are discussed in Section V of the text.<<AC e<<r<<I 4 4$I I f IIAC tv'040 ILICENSEE EVENT REPORT ILER)TEXT CONTINUATION V l.4VCLlAA AIOVLATOAV CeaWIllIISI A>>AOVlO 0+1 4O IIQI~IQA l)et<All II)I'lS SACILITY IIAIAl III" OOCIIKZ IIVIACCA Ill%lA A LlA IIIAAI~II Ill S~QMA4TIAL'V U A ACVOIOH V IA~AOl IlI R.E.Ginna Nuclear Power Plant tlXTOr~aeOee~.
    'l
~~~AAC~~'sIIlll o s o o o24 4 92 002 00020F].PRE-L?V1?NT PLANT CONDITIONS The plant was at approximately 47%reactor power due to a load reduction earlier in the day.Part of this load.reduction (i.e.to approximately 60%reactor power)was requested by the Rochester Gas and Electric Corporation (RG&E)Power Control Dispatcher to remove a major trans-mission line from service (circuit 908)for repair.The remainder of this load reduction (from 60%to 47%reactor power)was made to reduce reactor power below permissive P-9 (i.e.Reactor Trip From Turbine Trip Blocked)to perform condenser water box maintenance and turbine on-line trip testing and valve testing.The main generator voltage control was in the manual mode due to voltage oscillations experienced earlier in tQe day.The reactor control rods were also in the manual mode to maintain the core axial flux within its operating band.Turbine on-line trip testing and'alve testing was in progress with the last test's initial conditions being verified prior to performance of the test.II DESCRIPTION OF EVENT A.DATES AND APPROXIMATE TIMES OP MAZOR OCCUEGU9iCES:
 
o February 3, 1992, 2220 EST: due to loss of excitation.
  <<AC crea 4ASI
Main Generator.
              <<I                                                                                                                                             Ug, IRILSAR RIRVLATCATcoe>>e<<voce Aeeaavla Oeet NO, $ 1<<.aiav LICENSEE EVENT REPORT LER)                                                                      ISIIAIS I/SQIS eACILITY NAeel     Ill                                                                                                                         OOCRtT IA>>eOIR Ql                              A R.E. in'na Nuclear Power Plant:
Trip 0 February 3, 1992, 2220 EST: Main Turbine trip due=to main generator trip.0 February,3, 1992, 2224 EST: Event date and time.0 February 3, 1992, 2224 EST: Discovery date and time.0 February 3,'992, 2224 EST: Control Room operators verify both reactor trip breakers open, and all control and shutdown rods inserted.VAC~QALI lAAA Il 4$I
          '" Feedwater Transient, Due to Loss o6ooo244>ot of Excitation n uced Tur z.ne Generator Trip, Causes Lo Lo Steam Generator Level Reactor Trip I VINS OATS III                       LtR NueettA III                           AIMRT OATI III                                   OTHIA eACILITISI INVOLVIO Nl
                                                ~ save<<ewe          Ae v orcee                            YIAR                   eACIUTY <<Aeeee                      OOCAIT <<uee ~ SAISI VO<<TH        OAY      YIA1    YIAR              <<vee ~ IA       Irueee ~ A IIONTH          OAY 0   6    0     0   O 0 2            3    9    2 9       2       0 0 2                0         0     3 0 4              9  2                                                      0     6   0     0   0 Oel1*TINO THIS 1leOAT N SuteeITTIO euAWANT               I0 THI 1$ ovl1tlelNTI Oe I tel 1      $ ." lceeee  err er cere el  eee  eeeeree>>  Illl eeOOI  Itl                  $ Lea$ 4I                                 St.cell el                                  ~ O.T SNI Q I I<<I                              M714I
    ~ Oeel1                          SO.NQ Nl Ill II                            ~ OMW III                                   ~ O.TSlalQ)lel                                TLTllel LlvlL 0    2 3            Sa.calle IIII III                          ~ OMWQI                                      ~ O.TSlalQlleOI                                OTHSR lteeeeV Ie Aeeeeee erer ere  ee TeeL <<RC />>4 St.e le I IIII RI                          ~ O.T SN I QI I I                                I IO.T lel Qllera IAI
                                      $ OAOllelllI l<<l                            ~ O.T tie I Q II II                          ~ 0.$ SIeIQIleetl QI SO.OOS lelllllel                            IO.TSNIQIIVO                                SO.TSWQll el LICINSII CONTACT MR THQ LSA llll
<<AUI                                                                                                                                                                  TILteleONI NVLQIA Wesley JI. Backus                                                                                                                            ARIA COOl Technical Assist:ant to the Operations Manager                                                                                              3    1 5 5          2 4              44 I
CCAVLST ONS LINC >OR tACH CaeeMNINT OAILUAI 0tlCA                    Illa Iel THIS RIM AT lltl VA<<u>ACr          IMRTAILI 'gent, ~H <@t                                                                  HANVSA4            IMATAIL CAUSI SYSTIN            COIIMNINT            TVAIA            To NeRos        r~P4;":~Qj                  C VSI SYSTSN        coeeMN    IN T          TV AIR          TO NOAOS g~NAN $3'.~                                                                                              g~rr3 >vVjj~4~e:
X        B              T        B    W    3      1   5                             e'rte rr%
II~I, >>~      C.~,y; $$4 SVTTLININT*LAIMAT tteICTIO IIAI                                                                                                eeONTH      CAY    YIAR ttetCTSO LVINISSION OA'll ll~ I V II IllTee. er<<e>>N  SRJSCTSO SVINISSIO>> OATII AJSTA*cT ILeevl      4 Ieco eeeer. I A, eeereee<<e>>re    AY>>ee ree>>eeeee    eeoer<<I>>e <<eev        lltl On      February 3, 1992 with the reactor at approximately 23% full power, just subsequent to a turbine trip while at 474 reactor power, a reactor trip occurred due to Lo Lo Level (</=17%) in the "A" Steam Generator (S/G).
The          Control Room operators immediately performed the appropriate actions of Emergency Operating Procedures E-0 (Reactor Trip or Safety Injection) and ES-0.1 (Reactor Trip Response).                                                                                                              Both Main Steam Isolation Valves (MSIVs) were subsequently closed to limit a Reactor Coolant System (RCS) cooldown and the plant was stabil-ized at hot shutdown.
The underlying cause of the event was the inability to control the "A" S/G level above the reactor trip setpoint due to design and transient induced perturbations.                                                                               (This event is NUREG-1022 (x) Cause Code).
Corrective action taken or planned are discussed in Section                                                                                                                        V  of the text.
<<AC  e<<r <<I 4 4$ I
 
I f IIAC 040 I tv'                                                                                V l. 4VCLlAA AIOVLATOAVCeaWIllIISI LICENSEE EVENT REPORT ILER) TEXT CONTINUATION                        A>>AOVlO 0+1 4O IIQI~IQA l)et<All II)I'lS SACILITY IIAIAlIII"                          OOCIIKZ IIVIACCA Ill          LlA IIIAAI~ II Ill                  ~ AOl IlI
                                                                        %lA A   S ~ QMA4TIAL         ACVOIOH
                                                                                    'V U   A           V IA R.E. Ginna Nuclear Power Plant           o  s    o    o  o24 4 92        002                00020F].
tlXTOr~aeOee~.       ~~~AAC~~'sIIlll PRE-L?V1?NT PLANT CONDITIONS The plant was at approximately 47% reactor power due to a load reduction     earlier in the day. Part of this load .
reduction (i.e. to approximately 60% reactor power) was requested by the Rochester Gas and Electric Corporation (RG&E) Power Control Dispatcher to remove a major trans-mission line from service (circuit 908) for repair. The remainder of this load reduction (from 60% to 47% reactor power) was made to reduce reactor power below permissive P-9 (i.e. Reactor Trip From Turbine Trip Blocked) to perform condenser water box maintenance and turbine on-line trip testing and valve testing.
The main generator voltage control was in the manual mode due to voltage oscillations experienced earlier in tQe day. The reactor control rods were also in the manual mode to maintain the core axial flux within its operating band. Turbine on-line trip testing and'alve testing was in progress with the last test's initial conditions being verified prior to performance of the test.
II     DESCRIPTION OF EVENT A. DATES AND APPROXIMATE TIMES OP MAZOR OCCUEGU9iCES:
o     February 3, 1992, 2220 EST:             Main Generator.                    Trip due to loss of excitation.
0     February 3, 1992, 2220 EST:                 Main Turbine                   trip due =to main generator trip.
0     February,3, 1992, 2224           EST:   Event date and time.
0     February 3, 1992, 2224 EST:               Discovery date and time.
0     February    3,      '992, 2224 EST:                      Control Room operators      verify both reactor                    trip          breakers open, and    all      control and shutdown rods inserted.
VAC ~ QALI lAAA Il4$ I
 
IIAC Svv (041 I
              ~                      LICENSEE EVENT REPORT ILERI TEXT CONTINUATION U  l, vUCLSAA Al<<ULATOAY <<OvvlllIOAI ArrrovlO Ovl SvO IISO~IOs l)erirf5 llII%$    C SACILITY VAVl Ill                                              CO<<II CT IIUVClr l1I              LlA lsUVCSA lll                          ~ AOl Ill
                                                                                                        $ I 4 v Svr 7 I A I. ASVISIOH r                      V 1 R.E. Ginna Nuclear Power Plant                                o    s      o    o  2 4  4  92  0                      0              30>
TlxT III ~  vSSS r rrsrvr. vv SrrrrAv Ivrc svrl ~'ll I ITI o                                0 2                    0 0              1 2 o        February 3, 1992, 2229 EST:                                        Control Room operators close both Main Steam Isolation Valves (MSIVs) to limit a Reactor Coolant System (RCS) cooldown.
o        February 3, 1992, 2307 EST:                  Plant stabilized at hot shutdown condition.
B.          EVENT:
On    February 3, 1992 at approximately 2220 EST, with the reactor at approximately 47% stable reactor power, the Control Room received turbine trip first out annunciator alarm K-26 (Generator Lockout Relay).
As reactor power was less than 50% full power with the main condenser available, (i.e. less than permis-sive P-9), reactor trip from turbine trip was automatically blocked.                        The Control Room operators immediately          entered-              Abnormal    Procedure AP-TURB.'1 (Turbine Trip          Without            Reactor    Trip Required) and performed        its  applicable            actions.
The responses of the Steam Generator (S/G) Feedwater Regulating Valves (FRVs) for different control configurations are noted here for clarity of subsequent events:
o        When all FRVs (Main and Bypass)                                        are in the automatic mode, they                  will  go          full            open on a turbine trip          with      RCS  average    temperature                        (Tavg) greater than 554 F. When temperature goes below 554 F, these valves will go full closed.
0        All FRVs, both main and bypass, will fully close upon receiving a HI S/G Level ()/= 674) or safety injection signal regardless of their auto/manual status (feedwater isolation).
When  the Main FRVs are placed in the, manual mode from the above configuration, they will assume the position abased on the                      current controller manual    demand            signal and        stay there until adjusted by the responsible                  operator. Assuming that the bypass FRVs are                      left in auto, the bypass FRVs will continue                      to respond to the automatic feedwater control                  demand.
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                                                                                                                          $ Ilr<A$5 IISI '$$
AACIUI'TY HAMI I 1 I                                                OOCIICT HUMOIA 111              Cli HUMOti I ~ I                              SA0$  1$ 1 SSOU  HTIAI,        ASvlQIOr
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M    r RAT R.E. Ginna Nuclear Power Plant lr mar MSrs r Hssrsr. ~sr srrrsAM Hrc Ilsrr ~ $ 1 11TI o  s    o o    o 2 4  4  9 2 -0          .'2" 0'            0 4 os                  l    2 Prior to the turbine trip all FRVs were in the automatic control mode with the bypass FRVs full open and the main FRVs controlling S/G level in some midposition.
Subsequent          to the turbine trip, the                    ma'in FRVs went full open          per design (the bypass FRVs were already full open)          and the Control Room operator transferred the main FRVs to manual control and adjusted them to control S/G levels. The bypass FRVs were left in the automatic control mode.
The narrow range S/G levels were at approximately 534 and rapidly increasing when the main FRVs were shifted to the manual mode. The Control Room operator the main FRVs to approximately 10-134 open to closed'own control S/G levels. During this time the "A" S/G FRV isolated on HI Level (i.e. )/= 67% narrow range level). During approximately this same time the full open bypass FRVs rapidly clo".ed because their automatic controlling setpoint was now 394 S/G level. The Control Room operator 'continued to make adjustments to the main FRVs to compensate for the transient perturbations,            but    was      unsuccessful.              At 2224 EST, February 3, 1992, with                      the  reactor    at approximately 234 full power a reactor trip occurred due to Lo Lo Level ((/= 174) in the "A" S/G.
The Control Room operators performed the immediate actions of Emergency Operating Procedure E-0 (Reactor Trip Or Safety Injection) and transitioned to Emergency Operating Procedure ES-O.l (Reactor Trip Response) when were open, it  was verified that both reactor trip breakers all control and shutdown rods were inserted, and safety injection was not actuated or required.
Both MSIVs were subsequently closed at 2229 EST to limit the RCS cooldown. The closing of the MSIVs subsequently mitigated the RCS cooldown and the plant was stabilized in hot shutdown at 2307 EST.
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LICENSEE EVENT REPORT {LER) TEXT CONTINUATION                                ASSAOV lO Oul
                                                                                                                          /IO TISO&104 l~>All SINAI 1$
SACILITV IIASSt III                                    OOCKtt IIUI&lAITI            Llll IIUSSCIA ISI                    SAOl ISI vSAA    S ~ 4USatiAL U  1 R.E. Ginna Nuclear Power Plant TlXT IIT ~ ~ ~. e  We eerCeW +AC Arm WS S I UTI osooo244                9  2      0      2        0 0 0          50vl      2 Equipment problems            that occurred during the event                            were as  follows:
0'heindicationSteam "ALT showed Generator MSIV Main Control Board the valve to be not fully closed. An auxiliary operator was immediately sent out to check and reported the valve closed based on viewing the valve external indicator.
Subsequently, the Main Control Board indicated the valve fully closed approximately 23 minutes after signal receipt.
0          Following the start of the Turbine ,Driven Auxiliary Feedwater (TDAFW) pump on Lo Lo S/G Levels, it exhibited some oscillations in flow, however    total flow remained above the required 400  gallons per minute (GPM) as recorded on the Plant Process Computer System (PPCS).
0          The Intermediate Range Nuclear Instrumentation, Channel N-35, after tracking consistant with Channel N-36 down'to approximately 10 E-10 amps, had its indication continue to drop below 10 E-11 amps.      The N channel returned to normal (10 E-11 amps) approximately ten hours following the trip.
C.        INOPERABLE STRUCTURES g COMPONENTS l                        OR        SYSTEMS            THAT CONTRIBUTED TO THE KG9iT:
None.
D.        OWNER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
                                  ~
None.
E.        METHOD OF DISCOVERY:
The event was immediately apparent                        due      to alarms              and indications in the Control                Room.
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SACILITY HAltt Ill                                                OOCKET IIUoottA Itl          Lt1 HUOSOEA III                      ~ AOE  IEI
                                                                                                    $ $ 4v ~ rrYIOL        otveOI<
M    o                o R.E. Ginna Nuclear Power Plant TEXT lrs rrreo HIOoo ~ rotreoS. re oroorror HPC AHe ~$ I IITI o so        oo244        9 2 0        0    2                  0 60F 1        2 OPERATOR ACTION:
After the reactor trip, the Control Room operators performed the actions of Emergency Operating Procedures E-O, (Reactor Trip Or Safety Injection) and ES-0.1, (Reactor Trip Response).                  The MSIVs were manually actuated closed approximately four (4) minutes after the trip to prevent further plant cooldown.                                              The plant was subsequently stabilized at hot shutdown.
                                                . Subsequently,        the Control Room operators notified higher supervision and the Nuclear Regulatory Com-mission per 10 CFR 50.72, non-emergency, 4 hour notification.
G.          SAFETX SXSTEM RESPONSES:
The "A" S/G FRVs closed                automatically from                a  feedwatdr isolation signal.
III.              CAUSE OF KGDFZ A.          IMMEDIATE CAUSE:
The    reactor  trip      was      due to  "Att S/G              Lo Lo Level
(</=>>4)
B.          ROOT CAUSE:
The    underlying cause of she "A" S/G Lo Lo Level                                              ~
(</=174) was determined to be the Control Room operator's inability to control the "A" S/G level above its reactor trip setpoint due to the following contributing factors:
The transient perturbations that were occurring due to design (i.e. the design of the FRVs to go full open, when in automatic mode, following a turbine trip, and the design of having the bypass FRVs open at the higher power levels).
0        The shrink and swell phenomenon of the S/G water levels due to the above design induced perturba-tions and the transient induced perturbations.
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                                                                                                                                          $ I$O~ION lNNI1$ $ $ I$ I 1$
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                            ,  ANALYSIS OF EV19iT This event is reportable in accordance with 10CFR50.73, Licensee Event Report system, item (a)(2)(iv), which requires reporting of, "any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF) including the Reactor'rotection System (RPS)".                    The "A" S/G Lo Lo Level reactor trip was an automatic actuation of the RPS.
An assessment                  was  performed considering both the safety consequences.                and  implications of this event with the following results and conclusions:
There were no safety consequences or implications attributed to the reactor trip because:
o        The two reactor trip breakers opened as required.
o        All control and shutdown rods inserted as designed.
o        The plant was stabilized at hot shutdown.
The Ginna Updated Final Safety Analysis Report (UFSAR)
Chapter 15.2.2, "Loss of External Electrical Load", was reviewed and compared to the plant response for this event.            The plant is designed to accept a 50% loss of electrical load while operating at full power or a complete loss of electrical load while operating below 50%,
without initiating a reactor trip.
Although plant design can accept a 50% loss of load, past experience has'hown a vulnerability to S/G shrink and swell.              Since the S/G main FRVs are placed in manual, actual plant response will be dependent upon operator response to indicated S/G level.
Ginna UFSAR Chapter 15.2.2 evaluates the plant behavior for a complete loss of load from full power without a direct reactor trip, primarily to show the adequacy of the pressure-relieving devices and also to show that no core damage occurs.                  Complete loss of load analysis shows that DNBR does not drop below 2.0 and pressurizer pressure does not exceed 2500 psia. Only a small pressure spike (approxi-mately 30 psig) and a small temperature spike (2.5 F) was encountered during this transient.
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2 4  9    2      0 0 2                                1 2 Following the reactor trip, pressurizer'level decreased to approximately 54 level as a result of the cooldown. This is an expected observed'ransient.                                The S/G levels both decreased to the narrow range taps.                              This is an expected transient based upon the encountered shrink in the S/Gs.
A slow cooldown resulted during the post trip recovery period. This cooldown is bounded by the plant accident
                              'nalysis and does not exceed the Technical Specification limit of 100 F per hour. Additional protection was provided by closure of the MSIVs.
Based on the above and a review of post trip data and past plant transients,              it    can be concluded that the plant has operated as designed and that there'as no unreviewed safety questions and that the public's health and safety was assured at all times.
CORRECTIVE ACTION A.          ACTION TAKEN TO RRKZJBN AFFECTED SYSTEMS TO PRE-&TENT NORMAL STATUS:
0        The    S/G  levels were returned to their normal operating        levels by addition of Auxiliary Feedwater, subsequent to the reactor trip.
0        The "A" MSIV, manufactured by Atwood and Morrill, is a 30 inch air operated swing check valve, installed in the reverse direction to use S/G steam flow to ensure proper closure. As with any swing check valve, the closing moment must be large enough to overcome the friction on the valve shaft due to the valve packing-. . Complete closure is accomplished by the force of the fluid flow on the valve disc. The "A" MSIV was subsequently        stroked several times successfully to ensure operability and adequate closure capability. Results of these tests                              support the conclusion that failure of the "A" MSIV to fully seat during the reactor trip was not due to internal valve distortion and bending, but was the result of a lack of flow across the valve disc. Failure to close is attributed to the closure      operation          occurring        in        a        quiescent environment.
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AitAOVEO OVI W )ISOWIOC E)ctiACS ~ ITI %S S*CILITY IIANI III                                      DOCKCT IIVINIAITI                L41 IILNNI1 III                    ~ ACE Iel vTAA      SICVINTiAL        VIVOS<
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R.E. Ginna Nuclear P'ower Plant
          ~~          vm eeeaaeV IIAC AVVI~'llIITl 0  s  0  0  o  2 4  4  9  2    p      p 2            p p 0 90~              1 2 Valve closure is dependent upon two factors:
The moment, developed by the weight of the valve disc and the spring provided to assist in valve
                                              .closure,      plus sufficient steam flow across the valve disc, without which the valve was not capable of completing its clc                              g operation.
When the demand signal for MSI~                              =o close was ger
                                                    . ated d/p    across    the  A    MSIV      was        lower than th-. d/p across the B MSIV.                    The d/p across the B =. IV was enough to fully seat the valve while the d/p across the A MSIV did not provide enough force to overcome shaft packing frictional forces. Approximately 23 minutes later, the d/p across the A MSIV increased approximately 2 psid which resulted in complete closure of the valve.
For  all design basis accidents, where MSIV closure is required, the accident transients
                                                                                          =-
would develop a large enough differential pressure to obtain complete valve closure. RG&E is continuing to evaluate various packing materials which have a low friction coefficient and can perform the required sealing function.
o      The TDAFW pump was subsequently                                      tested to determine the cause of the flow oscillations, but the test had to be aborted due to a steam leak on the governor valve. The governor valve was disassembled,            inspected and placed back in service.      The steam leak was the result of gasket leak (probably caused due to excessive travel of the governor valve). The gasket was replaced with a qualified spare.                            The cause of the flow oscillations was due to the "hunting" of the governor valve. The hunting of the governor valve was caused by a feedback nut being out of proper position., The position of the feedback nut was corrected and the TDAFW pump was subsequently              tested successfully and returned to service.
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IIAC Svv~(041 I LICENSEE EVENT REPORT ILERI TEXT CONTINUATION U l, vUCLSAA Al<<ULATOA Y<<OvvlllIOAI S ArrrovlO Ovl vO IISO~IOs l)erirf5 llII%$C SACILITY VAVl Ill CO<<II CT IIUVClr l1I LlA lsUVCSA lll$I 4 v S r 7 I A I.r v ASVISIOH V 1~AOl Ill R.E.Ginna Nuclear Power Plant o s o o o 2 4 4 TlxT III~vSSS r rrsrvr.vv SrrrrAv Ivrc svrl~'ll I ITI 92-0 0 2-0 0 0 30>1 2 o February 3, 1992, 2229 EST: Control Room operators close both Main Steam Isolation Valves (MSIVs)to limit a Reactor Coolant System (RCS)cooldown.o February 3, 1992, 2307 EST: Plant stabilized at hot shutdown condition.
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B.EVENT: On February 3, 1992 at approximately 2220 EST, with the reactor at approximately 47%stable reactor power, the Control Room received turbine trip first out annunciator alarm K-26 (Generator Lockout Relay).As reactor power was less than 50%full power with the main condenser available, (i.e.less than permis-sive P-9), reactor trip from turbine trip was automatically blocked.The Control Room operators immediately entered-Abnormal Procedure AP-TURB.'1 (Turbine Trip Without Reactor Trip Required)and performed its applicable actions.The responses of the Steam Generator (S/G)Feedwater Regulating Valves (FRVs)for different control configurations are noted here for clarity of subsequent events: o When all FRVs (Main and Bypass)are in the automatic mode, they will go full open on a turbine trip with RCS average temperature (Tavg)greater than 554 F.When temperature goes below 554 F, these valves will go full closed.0 All FRVs, both main and bypass, will fully close upon receiving a HI S/G Level ()/=674)or safety injection signal regardless of their auto/manual status (feedwater isolation).
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'When the Main FRVs are placed in the, manual mode from the above configuration, they will assume the position abased on the current controller manual demand signal and stay there until adjusted by the responsible operator.Assuming that the bypass FRVs are left in auto, the bypass FRVs will continue to respond to the automatic feedwater control demand.VAC sOAv SCCA<l4$I tl HISC Term~IMMI e LICENSEE EVENT REPORT ILERI TEXT CONTINUATION U.S.HUclcAA itoUUAToir cossssls$loi/ASSAOV CO OH$HO$1$OWIOS$Ilr<A$5 IISI'$$AACIUI'TY HAMI I 1 I OOCIICT HUMOIA 111 Cli HUMOti I~I SSOU~HTIAI, ASvlQIOr M r SA0$1$1 R.E.Ginna Nuclear Power Plant RAT lr mar MSrs r Hssrsr.~sr srrrsAM Hrc Ilsrr~$1 11TI o s o o o 2 4 4 9 2--0.'2"-0'0 4 os l 2 Prior to the turbine trip all FRVs were in the automatic control mode with the bypass FRVs full open and the main FRVs controlling S/G level in some midposition.
            ~               LICENSEE EVENT REPORT ILER) TEXT CONTINUATION M  5, ~IICLSAA AlauLASOAV CO<<AIISSIOII Alt1OVSO OUI NO SISO~IO4 5)cttII55 SISI 'SS FACILITY HAAIS I'l                                OOCIIS7 HUIAllAISI            Llll NIIIASSII I ~ I                     AAOl ISI SSQMSle  TILL          8'IYCIOR
Subsequent to the turbine trip, the ma'in FRVs went full open per design (the bypass FRVs were already full open)and the Control Room operator transferred the main FRVs to manual control and adjusted them to control S/G levels.The bypass FRVs were left in the automatic control mode.The narrow range S/G levels were at approximately 534 and rapidly increasing when the main FRVs were shifted to the manual mode.The Control Room operator closed'own the main FRVs to approximately 10-134 open to control S/G levels.During this time the"A" S/G FRV isolated on HI Level (i.e.)/=67%narrow range level).During approximately this same time the full open bypass FRVs rapidly clo".ed because their automatic controlling setpoint was now 394 S/G level.The Control Room operator'continued to make adjustments to the main FRVs to compensate for the transient perturbations, but was unsuccessful.
                                                                                          ~  U                  <<SA raXt W  ~ eeae e ~. v<< ~
At 2224 EST, February 3, 1992, with the reactor at approximately 234 full power a reactor trip occurred due to Lo Lo Level ((/=174)in the"A" S/G.The Control Room operators performed the immediate actions of Emergency Operating Procedure E-0 (Reactor Trip Or Safety Injection) and transitioned to Emergency Operating Procedure ES-O.l (Reactor Trip Response)when it was verified that both reactor trip breakers were open, all control and shutdown rods were inserted, and safety injection was not actuated or required.Both MSIVs were subsequently closed at 2229 EST to limit the RCS cooldown.The closing of the MSIVs subsequently mitigated the RCS cooldown and the plant was stabilized in hot shutdown at 2307 EST.MAC sorv sAAA I$441 I
R.E. Ginna Nuclear Power Plant
IIAC Soew%CA I%45>LICENSEE EVENT REPORT{LER)TEXT CONTINUATION y,l, IIUCLSAA AlOULATOA V COSSMISCIOII
                              +AC A<< ~'iIIm o   s   o o   o   2 4 4 9 2         p    2           p p        1 poi:1     2 0       As  the Intermediate Range NIS Channel N-35 tracked NIS Channel N-36 for, its normal operating range. and returned to normal approximately ten (10) hours after the trip, no immediate action was deemed necessary.             This abnormality has been observed and         researched      extensively in the past in cooperation        with    the NSSS vendor, Westinghouse.
/ASSAOV lO Oul IO TISO&104 l~>All SINAI 1$SACILITV IIASSt III OOCKtt IIUI&lA ITI vSAA Llll IIUSSCIA ISI S~4USatiAL U 1 SAOl ISI R.E.Ginna Nuclear Power Plant TlXT IIT~~e~.We eerCeW+AC Arm WS S I UTI osooo244 9 2 0 2 0 0 0 50vl 2 Equipment problems that occurred during the event were as follows: 0'he"ALT Steam Generator MSIV Main Control Board indication showed the valve to be not fully closed.An auxiliary operator was immediately sent out to check and reported the valve closed based on viewing the valve external indicator.
No technical basis has been identified as to why the 10 E-11 idle current does not maintain indication at 10 E-11 amps; RG&E and Westinghouse concurred that the channel was operable and capable of performing all intended functions.
Subsequently, the Main Control Board indicated the valve fully closed approximately 23 minutes after signal receipt.0 0 Following the start of the Turbine ,Driven Auxiliary Feedwater (TDAFW)pump on Lo Lo S/G Levels, it exhibited some oscillations in flow, however total flow remained above the required 400 gallons per minute (GPM)as recorded on the Plant Process Computer System (PPCS).The Intermediate Range Nuclear Instrumentation, Channel N-35, after tracking consistant with Channel N-36 down'to approximately 10 E-10 amps, had its indication continue to drop below 10 E-11 amps.The N-35-channel returned to normal (10 E-11 amps)approximately ten hours following the trip.C.INOPERABLE STRUCTURES g COMPONENTS l OR SYSTEMS THAT CONTRIBUTED TO THE KG9iT: D.None.OWNER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:~None.E.METHOD OF DISCOVERY:
Further evaluations of the response characteris-tics of NIS channel N-35 will be performed during the 1992 Annual Refueling and Maintenance Outage.
The event was immediately apparent due to alarms and indications in the Control Room.hAC SOAIS SASA ISASI 0~~1 HAC Sore M I$4$I LICENSEE EVENT REPORT ILERI TEXT CONTINUATION v t.IIUCLEA+AtOULATCAY coooorlttrorr AssAOYEO Ovt HO$I$0aIOo-t)eOIAES trtI 1$SACILITY HAltt Ill OOCKET IIUoottA Itl Lt1 HUOSOEA III$$4v~rrYIOL M o otveOI<o~AOE IEI R.E.Ginna Nuclear Power Plant TEXT lrs rrreo HIOoo~rotreoS.re oroorror HPC AHe~$I IITI o so oo244 9 2-0 0 2-0 60F 1 2 OPERATOR ACTION: After the reactor trip, the Control Room operators performed the actions of Emergency Operating Procedures E-O, (Reactor Trip Or Safety Injection) and ES-0.1, (Reactor Trip Response).
0     This event was initiated by a main generator trip due to loss of excitation.                                       Extensive examination, evaluation and testing was performed on the main generator voltage control system, with the following results and conclusions:
The MSIVs were manually actuated closed approximately four (4)minutes after the trip to prevent further plant cooldown.The plant was subsequently stabilized at hot shutdown..Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Com-mission per 10 CFR 50.72, non-emergency, 4 hour notification.
The   automatic and manual voltage control units were  extensively tested and found to operate satisfactorily.               The Minimum  Excitation Limiter (MEL) data taken during the testing indicated that the setting was too close to normal operating points of the generator. A new MEL setting was calculated, reviewed by .Westinghouse (the vendor) and implemented. The revised setting will allow operation to approximately 190 MVAR underexcited at 500 MW.
G.SAFETX SXSTEM RESPONSES:
h1C BOA<<SASA il4$ I
The"A" S/G FRVs closed automatically from a feedwatdr isolation signal.III.CAUSE OF KGDFZ A.IMMEDIATE CAUSE: The reactor trip was due to"Att S/G Lo Lo Level (</=>>4)B.ROOT CAUSE: The underlying cause of she"A" S/G Lo Lo Level~(</=174)was determined to be the Control Room operator's inability to control the"A" S/G level above its reactor trip setpoint due to the following contributing factors: The transient perturbations that were occurring due to design (i.e.the design of the FRVs to go full open, when in automatic mode, following a turbine trip, and the design of having the bypass FRVs open at the higher power levels).0 The shrink and swell phenomenon of the S/G water levels due to the above design induced perturba-tions and the transient induced perturbations.
HAC Soaks ttAA rtttl 4 4 IINC Notes~I$4$I 0 LICENSEE EVENT REPORT ILER)TEXT CONTINUATION V l.1VCLlAA 1$OVLATO1Y COMMI$$IO1 N ANNAOVlO OVNAO$I$O~ION lNNI1$$$I$I 1$NACILITY IIANlt Ill OOCIIlZ IIVINCCA Ill Ll1 IIINNC$1 I~I slavlseviAL M alv+IO<I>AOl I$I R.E.Ginna Nuclear Power Plant TEXT IN'1INNN 1~.vNN OeeeaW IYNC/erat~$I I ITI 0 5IO 0 0 2 4 4 9 2-00 2-0 0 0 70'2 , ANALYSIS OF EV19iT This event is reportable in accordance with 10CFR50.73, Licensee Event Report system, item (a)(2)(iv), which requires reporting of,"any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF)including the Reactor'rotection System (RPS)".The"A" S/G Lo Lo Level reactor trip was an automatic actuation of the RPS.An assessment was performed considering both the safety consequences.
and implications of this event with the following results and conclusions:
There were no safety consequences or implications attributed to the reactor trip because: o The two reactor trip breakers opened as required.o All control and shutdown rods inserted as designed.o The plant was stabilized at hot shutdown.The Ginna Updated Final Safety Analysis Report (UFSAR)Chapter 15.2.2,"Loss of External Electrical Load", was reviewed and compared to the plant response for this event.The plant is designed to accept a 50%loss of electrical load while operating at full power or a complete loss of electrical load while operating below 50%, without initiating a reactor trip.Although plant design can accept a 50%loss of load, past experience has'hown a vulnerability to S/G shrink and swell.Since the S/G main FRVs are placed in manual, actual plant response will be dependent upon operator response to indicated S/G level.Ginna UFSAR Chapter 15.2.2 evaluates the plant behavior for a complete loss of load from full power without a direct reactor trip, primarily to show the adequacy of the pressure-relieving devices and also to show that no core damage occurs.Complete loss of load analysis shows that DNBR does not drop below 2.0 and pressurizer pressure does not exceed 2500 psia.Only a small pressure spike (approxi-mately 30 psig)and a small temperature spike (2.5 F)was encountered during this transient.
wAC NOAIN$NAA I$44I


ISAC Tens 444A I4431 LICENSEE EVENT REPORT ILER)TEXT CONTINUATION U.S.HUCLSAA ASOULATOAY CO>>>>ISSIOSI ASSAOYSO OU4'SO)ISO~IOs 4)ctiA 4$41SI SS FACILITY IIA>>4 Ill OOCIIST HUIS44A ISI T~AA LSA KUSA44A ISI SSQUSNT<AL U A ASYhlOR U SA SAO4 ISI R.E.Ginna Nuclear Power Plant TSXT/IT~>>S>>h>>SUse4.v>>>>h>>On>>hfISC A>>>>~'S1 1171 I 0 5 0 0 0 2 4 9 2 0 0 2-0 OF 1 2 Following the reactor trip, pressurizer'level decreased to approximately 54 level as a result of the cooldown.This is an expected observed'ransient.
l 4
The S/G levels both decreased to the narrow range taps.This is an expected transient based upon the encountered shrink in the S/Gs.A slow cooldown resulted during the post trip recovery period.This cooldown is bounded by the plant accident'nalysis and does not exceed the Technical Specification limit of 100 F per hour.Additional protection was provided by closure of the MSIVs.Based on the above and a review of post trip data and past plant transients, it can be concluded that the plant has operated as designed and that there'as no unreviewed safety questions and that the public's health and safety was assured at all times.CORRECTIVE ACTION A.ACTION TAKEN TO RRKZJBN AFFECTED SYSTEMS TO PRE-&TENT NORMAL STATUS: 0 The S/G levels were returned to their normal operating levels by addition of Auxiliary Feedwater, subsequent to the reactor trip.0 The"A" MSIV, manufactured by Atwood and Morrill, is a 30 inch air operated swing check valve, installed in the reverse direction to use S/G steam flow to ensure proper closure.As with any swing check valve, the closing moment must be large enough to overcome the friction on the valve shaft due to the valve packing-..Complete closure is accomplished by the force of the fluid flow on the valve disc.The"A" MSIV was subsequently stroked several times successfully to ensure operability and adequate closure capability.
Results of these tests support the conclusion that failure of the"A" MSIV to fully seat during the reactor trip was not due to internal valve distortion and bending, but was the result of a lack of flow across the valve disc.Failure to close is attributed to the closure operation occurring in a quiescent environment.
'eAC AOASI 444A iSWI Lh 0 IIAC tovv%CA 104ll UCENSEE EVENT REPORT{LER)TEXT CONTINUATION V l.IIVCLtAA AlCULATCAY CISALIIQQCII
/AitAOVEO OVI W)ISOWIOC E)ctiACS~ITI%S S*CILITY IIANI III DOCKCT IIVINIA ITI L41 IILNNI1 III vTAA SICVINTiAL VIVOS<V 1 V~ACE Iel R.E.Ginna Nuclear P'ower Plant 0 s 0 0 o 2 4 4 9 2-p p 2 p p ftXT W~~1~vm eeeaaeV IIAC AVVI~'ll IITl 0 90~1 2 Valve closure is dependent upon two factors: The moment, developed by the weight of the valve disc and the spring provided to assist in valve.closure, plus sufficient steam flow across the valve disc, without which the valve was not capable of completing its clc g operation.
When the demand signal for MSI~=o close was ger.ated d/p across the A MSIV was lower than th-.d/p across the B MSIV.The d/p across the B=.IV was enough to fully seat the valve while the d/p across the A MSIV did not provide enough force to overcome shaft packing frictional forces.Approximately 23 minutes later, the d/p across the A MSIV increased approximately 2 psid which resulted in complete closure of the valve.For all design basis accidents, where MSIV closure is required, the=-accident transients would develop a large enough differential pressure to obtain complete valve closure.RG&E is continuing to evaluate various packing materials which have a low friction coefficient and can perform the required sealing function.o The TDAFW pump was subsequently tested to determine the cause of the flow oscillations, but the test had to be aborted due to a steam leak on the governor valve.The governor valve was disassembled, inspected and placed back in service.The steam leak was the result of gasket leak (probably caused due to excessive travel of the governor valve).The gasket was replaced with a qualified spare.The cause of the flow oscillations was due to the"hunting" of the governor valve.The hunting of the governor valve was caused by a feedback nut being out of proper position., The position of the feedback nut was corrected and the TDAFW pump was subsequently tested successfully and returned to service.11C PCAIv~IIABI


IIAC t<<<<~IS45 I LICENSEE EVENT REPORT ILER)TEXT CONTINUATION M 5,~IICLSAA AlauLASOA V CO<<AIISSIOII Alt1OVSO OUI NO SISO~IO4 5)cttII55 SISI'SS FACILITY HAAIS I'l OOCIIS7 HUIAllA ISI Llll NIIIASSII I~I SSQMSle TILL~U 8'IYCIOR<<SA AAOl ISI R.E.Ginna Nuclear Power Plant o s o o o 2 4 4 9 2 p 2 p p raXt W~eeae e~.v<<~+AC A<<~'iI Im 1 poi:1 2 0 0 As the Intermediate Range" NIS Channel N-35 tracked NIS Channel N-36 for, its normal operating range.and returned to normal approximately ten (10)hours after the trip, no immediate action was deemed necessary.
IIAC IVn XW                                                                                          V,l. HVCLSAA ASOULATOISY COWHISSIOII IS@) I LICENSEE EVENT REPORT (LERI TEXT CONTINUATION                             AttrOvlO OUS JeO )ISOMI04 SIctirlS SI)I 'IS AACILITYHAAIS III                                           OOCIIlt HUUl1 111 Llr IIUMOlr I ~ I                   ~ AOl I)I S~ Ovlrt<AL e v R.E. Ginna Nuclear Power Plant                                                         0                 0           110' tt)IT IIt rrn ~r   never. vn rrreenr rrC Attn ~ s I Im 0 5    o  0   o 2 4  4 9          0     2          0                   2 The unit was     synchronized to the system with the-voltage   regulator         in manual and no unusual events were noted.             When the voltage regulator was placed in the- automatic mode, the loop within the voltage regulator system was unstable and the voltage regulator was returned to the manual mode.             The operation of the voltage regulator damping module was verified and the gain was reduced from maximum setting to the mid point on the potentiometer. The voltage regulator was returned to the automatic mode and operated satisfactorily.
This abnormality has been observed and researched extensively in the past in cooperation with the NSSS vendor, Westinghouse.
The plant   has now operated at approximately                             full power   and       has gone through several                               normal voltage adjustments such as lowering the voltaqe in the evening and raising the voltage in the morning as required by system load.                                             No abnormalities. have been encountered.
No technical basis has been identified as to why the 10 E-11 idle current does not maintain indication at 10 E-11 amps;RG&E and Westinghouse concurred that the channel was operable and capable of performing all intended functions.
B.       ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
Further evaluations of the response characteris-tics of NIS channel N-35 will be performed during the 1992 Annual Refueling and Maintenance Outage.This event was initiated by a main generator trip due to loss of excitation.
As   the underlying cause of the event was determined to be     the inability of the Control Room operator to control the "A" S/G leve above its reactor trip
Extensive examination, evaluation and testing was performed on the main generator voltage control system, with the following results and conclusions:
                                                                                      ~
The automatic and manual voltage control units were extensively tested and found to operate satisfactorily.
setpoint due to design and transient induced level perturbation, the following actions have been taken or are being planned:
The Minimum Excitation Limiter (MEL)data taken during the testing indicated that the setting was too close to normal operating points of the generator.
0           Applicable operating procedures have been changed to require that the bypass FRVs be placed in manual closed when increasing above approximately 304 reactor power.
A new MEL setting was calculated, reviewed by.Westinghouse (the vendor)and implemented.
0         Applicable operating procedures have been changed to require returning the bypass FRVs to automatic control when decreasing below 304 reactor power.
The revised setting will allow operation to approximately 190 MVAR underexcited at 500 MW.h1C BOA<<SASA il4$I l 4 IIAC IVn XW IS@)I LICENSEE EVENT REPORT (LERI TEXT CONTINUATION V,l.HVCLSAA ASOULATOISY COWHISSIOII J AttrOvlO OUS eO)ISOMI04 SIctirlS SI)I'IS AACILITY HAAIS III OOCIIlt HUUl1 111 Llr IIUMOlr I~I~AOl I)I R.E.Ginna Nuclear Power Plant 0 5 o 0 o 2 4 4 9 tt)IT IIt rrn~r never.vn rrreenr rrC Attn~s I I m S~Ovlrt<AL e v-0 0 2-0 0 110'2 The unit was synchronized to the system with the-voltage regulator in manual and no unusual events were noted.When the voltage regulator was placed in the-automatic mode, the loop within the voltage regulator system was unstable and the voltage regulator was returned to the manual mode.The operation of the voltage regulator damping module was verified and the gain was reduced from maximum setting to the mid point on the potentiometer.
eAC JOAN )SAA il4)1
The voltage regulator was returned to the automatic mode and operated satisfactorily.
The plant has now operated at approximately full power and has gone through several normal voltage adjustments such as lowering the voltaqe in the evening and raising the voltage in the morning as required by system load.No abnormalities.
have been encountered.
B.ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
As the underlying cause of the event was determined to be the inability of the Control Room operator to control the"A" S/G leve~above its reactor trip setpoint due to design and transient induced level perturbation, the following actions have been taken or are being planned: 0 Applicable operating procedures have been changed to require that the bypass FRVs be placed in manual closed when increasing above approximately 304 reactor power.0 Applicable operating procedures have been changed to require returning the bypass FRVs to automatic control when decreasing below 304 reactor power.eAC JOAN)SAA il4)1  


IIAC Isrse lAAA 104lI LICENSEE EVENT REPORT ILER)TEXT CONTINUATION v l.eevCLlAII AlOULATCAY coseseeClloee
IIAC Isrse lAAA                                                                                               v l. eevCLlAII AlOULATCAYcoseseeClloee Ovl /eeo 104lI LICENSEE EVENT REPORT ILER) TEXT CONTINUATION                                     AASSOvlo               IISOWIOe l>eseAl5 ~ rlI TS I'ACILITYIIAIIlIII                                              OOCIIKT eeULQlA 111 LlA IIUAOlAI ~ I                       ~ Aol IQ v TAA   SloulreveAL       SAVes~are v er               U ~s R.E. Ginna Nuclear Power. Plant TKXT rrr rsrers ~ r ~. vm e seseeeer rrreC Arse ~'gr IITI 0  6    <<      o  2 4 4 9   2 0     0   2                   1   2o~       1 2 o       A     modification is planned for the 1993 Annual Refueling and Maintenance Outage that would modify the existing feedwater isolation logic for fail-open or fail-closed of the main and bypass FRVs upon turbine trip with main FRVs in automatic control mode. The planned modification will delete the existing fail-open logic and replace the fail-closed logic with actuation upon reactor trip as opposed to turbine trip.
/AASSOvlo Ovl eeo IISOWIOe l>eseAl5~rlI TS I'ACILITY IIAIIl III OOCIIKT eeULQlA 111 LlA IIUAOlA I~I v TAA SloulreveAL SAVes~are v er U~s~Aol IQ R.E.Ginna Nuclear Power.Plant 0 6<<o 2 4 4 TKXT rrr rsrers~r~.vm e seseeeer rrreC Arse~'gr IITI 9 2-0 0 2-1 2o~1 2 o A modification is planned for the 1993 Annual Refueling and Maintenance Outage that would modify the existing feedwater isolation logic for fail-open or fail-closed of the main and bypass FRVs upon turbine trip with main FRVs in automatic control mode.The planned modification will delete the existing fail-open logic and replace the fail-closed logic with actuation upon reactor trip as opposed to turbine trip.As the event was initiated by the Main Generator trip due to loss of excitation, the following actions are planned to prevent recurrence'.
As the event was initiated by the Main Generator                                               trip due to loss of excitation, the following actions are planned to prevent recurrence'.
0 0 RG&E is planning to purchase and install a replacement voltage regulator unit.I Routine testing and maintenance will be performed on the existing voltage regulator unit during the 1992 Annual Refueling and Maintenance Outage to attain a high degree of confidence that the unit will operate without incident for the entire fuel cycle.ADDITIONAL INFORMATION A.FAILED COMPONENTS:
0       RG&E     is planning to purchase and                               install                 a replacement voltage regulator unit.
The TDAFW pump turbine is a 465 horsepower noncondensing steam turbine, serial number 26635, manufactured by the Worthington Corporation.
I 0        Routine testing and maintenance                     will be           performed on   the existing voltage regulator unit during the   1992 Annual Refueling and Maintenance Outage to attain a high degree of confidence that the unit will operate without incident for the entire fuel cycle.
B.PREVIOUS LERs ON SIMILAR EVENTS: A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same underlying cause at Ginna Station could be identified.
ADDITIONAL INFORMATION A.             FAILED COMPONENTS:
C.SPECIAL COMMENTS: None.~eAC SOAee 1AAA rl4lI}}
The       TDAFW     pump         turbine       is     a     465         horsepower noncondensing steam turbine, serial number                                               26635, manufactured by the Worthington Corporation.
B.             PREVIOUS LERs ON SIMILAR EVENTS:
A   similar LER event historical search was conducted with the following results:                           No documentation                             of similar LER events with the same underlying cause at Ginna Station could be identified.
C.             SPECIAL COMMENTS:
None.
~ eAC SOAee 1AAA rl4lI}}

Latest revision as of 09:45, 4 February 2020

LER 92-002-00:on 920203,reactor Trip Occurred W/Reactor at Approx 23% Full Power Just Subsequent to Turbine Trip While at 47% Power.Caused by Lo Lo Level in SG a Due to Design Perturbations.New Setting calculated.W/920304 Ltr
ML17262A758
Person / Time
Site: Ginna Constellation icon.png
Issue date: 03/04/1992
From: Backus W, Mecredy R
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LER-92-002, LER-92-2, NUDOCS 9203110291
Download: ML17262A758 (28)


Text

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+ ACCELERATED DISTRIBUTION DEMONSTRATION SYSTEM REGULATOR INFORMATION DISTRlBUTION pTEM (RIDS)

ACCESSION NBR:9203110291 DOC.DATE: 92/03/04 NOTARIZED: NO DOCKET ¹ FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION BACKUSiW.H. Rochester Gas & Electric Corp.

MECREDY,R.C. Rochester Gas & Electric Corp.

RECIP.NAME RECiPIENT AFFILIATION R

SUBJECT:

LER 92-002-00:on 920203,reactor trip occurred w/reactor at approx 23% full power just subsequent to turbine trip while at 47% power. Caused by lo lo level in SG A due to design perturbations.New setting calculated.W/920304 ltr. D DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

/

NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 A

RECIPIENT COPIES RECIPIENT COPIES D ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PDl-3 LA 1 1 PD1-3 PD 1 1 D JOHNSON,A 1 1 INTERNAL: ACNW 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DET/EMEB 7E 1 1 NRR/DLPQ/LHFB10" 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB 1 1 NRR/DREP/PRPBll 2 2 NRR/DST/SELB 8D 1 ~ 1

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S PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

FULL 'TEXT CONVERSION REQUIRED TOTAL NUMB R OF COPIES REQUIRED: LTTR 30 ENCL 30

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sT4 M ROCHESTER GAS AND ELECTRIC CORPORATION 4 89 EAST AVENUE, ROCHESTER N. K 74649-0001 ROBER't (, hlECRjtpY TELE&>0'ME Vrr< Vresidenl ARErr COM 716 546'2700 Crnna No<lcm Prodursrorr March 4, 1992 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Subject:

LER 92-002, Feedwater Transient, Due To Loss Of Excitation Induced Turbine/Generator Trip, Causes Lo Lo Steam Gen'erator Level Reactor Trip

-R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10CFR50.73, Licensee. Event Report System, item (a)(2)(iv), which requires a report of, "any event or condition that resulted in manual or automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)", the attached Event Report LER 92-002 is hereby submitted.

This event has in no way affected the public's health and safety.

Very truly yours, Robert C. Mecredy.

xco U. S. Nuclear Regulatory Commission Re'gion I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector f) q'l ~g(4

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92031i0291 '720304 PDR ADOCK 05000244 5 PDR

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II~I, >>~ C.~,y; $$4 SVTTLININT*LAIMAT tteICTIO IIAI eeONTH CAY YIAR ttetCTSO LVINISSION OA'll ll~ I V II IllTee. er<<e>>N SRJSCTSO SVINISSIO>> OATII AJSTA*cT ILeevl 4 Ieco eeeer. I A, eeereee<<e>>re AY>>ee ree>>eeeee eeoer<>e <<eev lltl On February 3, 1992 with the reactor at approximately 23% full power, just subsequent to a turbine trip while at 474 reactor power, a reactor trip occurred due to Lo Lo Level (</=17%) in the "A" Steam Generator (S/G).

The Control Room operators immediately performed the appropriate actions of Emergency Operating Procedures E-0 (Reactor Trip or Safety Injection) and ES-0.1 (Reactor Trip Response). Both Main Steam Isolation Valves (MSIVs) were subsequently closed to limit a Reactor Coolant System (RCS) cooldown and the plant was stabil-ized at hot shutdown.

The underlying cause of the event was the inability to control the "A" S/G level above the reactor trip setpoint due to design and transient induced perturbations. (This event is NUREG-1022 (x) Cause Code).

Corrective action taken or planned are discussed in Section V of the text.

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tlXTOr~aeOee~. ~~~AAC~~'sIIlll PRE-L?V1?NT PLANT CONDITIONS The plant was at approximately 47% reactor power due to a load reduction earlier in the day. Part of this load .

reduction (i.e. to approximately 60% reactor power) was requested by the Rochester Gas and Electric Corporation (RG&E) Power Control Dispatcher to remove a major trans-mission line from service (circuit 908) for repair. The remainder of this load reduction (from 60% to 47% reactor power) was made to reduce reactor power below permissive P-9 (i.e. Reactor Trip From Turbine Trip Blocked) to perform condenser water box maintenance and turbine on-line trip testing and valve testing.

The main generator voltage control was in the manual mode due to voltage oscillations experienced earlier in tQe day. The reactor control rods were also in the manual mode to maintain the core axial flux within its operating band. Turbine on-line trip testing and'alve testing was in progress with the last test's initial conditions being verified prior to performance of the test.

II DESCRIPTION OF EVENT A. DATES AND APPROXIMATE TIMES OP MAZOR OCCUEGU9iCES:

o February 3, 1992, 2220 EST: Main Generator. Trip due to loss of excitation.

0 February 3, 1992, 2220 EST: Main Turbine trip due =to main generator trip.

0 February,3, 1992, 2224 EST: Event date and time.

0 February 3, 1992, 2224 EST: Discovery date and time.

0 February 3, '992, 2224 EST: Control Room operators verify both reactor trip breakers open, and all control and shutdown rods inserted.

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TlxT III ~ vSSS r rrsrvr. vv SrrrrAv Ivrc svrl ~'ll I ITI o 0 2 0 0 1 2 o February 3, 1992, 2229 EST: Control Room operators close both Main Steam Isolation Valves (MSIVs) to limit a Reactor Coolant System (RCS) cooldown.

o February 3, 1992, 2307 EST: Plant stabilized at hot shutdown condition.

B. EVENT:

On February 3, 1992 at approximately 2220 EST, with the reactor at approximately 47% stable reactor power, the Control Room received turbine trip first out annunciator alarm K-26 (Generator Lockout Relay).

As reactor power was less than 50% full power with the main condenser available, (i.e. less than permis-sive P-9), reactor trip from turbine trip was automatically blocked. The Control Room operators immediately entered- Abnormal Procedure AP-TURB.'1 (Turbine Trip Without Reactor Trip Required) and performed its applicable actions.

The responses of the Steam Generator (S/G) Feedwater Regulating Valves (FRVs) for different control configurations are noted here for clarity of subsequent events:

o When all FRVs (Main and Bypass) are in the automatic mode, they will go full open on a turbine trip with RCS average temperature (Tavg) greater than 554 F. When temperature goes below 554 F, these valves will go full closed.

0 All FRVs, both main and bypass, will fully close upon receiving a HI S/G Level ()/= 674) or safety injection signal regardless of their auto/manual status (feedwater isolation).

When the Main FRVs are placed in the, manual mode from the above configuration, they will assume the position abased on the current controller manual demand signal and stay there until adjusted by the responsible operator. Assuming that the bypass FRVs are left in auto, the bypass FRVs will continue to respond to the automatic feedwater control demand.

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M r RAT R.E. Ginna Nuclear Power Plant lr mar MSrs r Hssrsr. ~sr srrrsAM Hrc Ilsrr ~ $ 1 11TI o s o o o 2 4 4 9 2 -0 .'2" 0' 0 4 os l 2 Prior to the turbine trip all FRVs were in the automatic control mode with the bypass FRVs full open and the main FRVs controlling S/G level in some midposition.

Subsequent to the turbine trip, the ma'in FRVs went full open per design (the bypass FRVs were already full open) and the Control Room operator transferred the main FRVs to manual control and adjusted them to control S/G levels. The bypass FRVs were left in the automatic control mode.

The narrow range S/G levels were at approximately 534 and rapidly increasing when the main FRVs were shifted to the manual mode. The Control Room operator the main FRVs to approximately 10-134 open to closed'own control S/G levels. During this time the "A" S/G FRV isolated on HI Level (i.e. )/= 67% narrow range level). During approximately this same time the full open bypass FRVs rapidly clo".ed because their automatic controlling setpoint was now 394 S/G level. The Control Room operator 'continued to make adjustments to the main FRVs to compensate for the transient perturbations, but was unsuccessful. At 2224 EST, February 3, 1992, with the reactor at approximately 234 full power a reactor trip occurred due to Lo Lo Level ((/= 174) in the "A" S/G.

The Control Room operators performed the immediate actions of Emergency Operating Procedure E-0 (Reactor Trip Or Safety Injection) and transitioned to Emergency Operating Procedure ES-O.l (Reactor Trip Response) when were open, it was verified that both reactor trip breakers all control and shutdown rods were inserted, and safety injection was not actuated or required.

Both MSIVs were subsequently closed at 2229 EST to limit the RCS cooldown. The closing of the MSIVs subsequently mitigated the RCS cooldown and the plant was stabilized in hot shutdown at 2307 EST.

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SACILITV IIASSt III OOCKtt IIUI&lAITI Llll IIUSSCIA ISI SAOl ISI vSAA S ~ 4USatiAL U 1 R.E. Ginna Nuclear Power Plant TlXT IIT ~ ~ ~. e We eerCeW +AC Arm WS S I UTI osooo244 9 2 0 2 0 0 0 50vl 2 Equipment problems that occurred during the event were as follows:

0'heindicationSteam "ALT showed Generator MSIV Main Control Board the valve to be not fully closed. An auxiliary operator was immediately sent out to check and reported the valve closed based on viewing the valve external indicator.

Subsequently, the Main Control Board indicated the valve fully closed approximately 23 minutes after signal receipt.

0 Following the start of the Turbine ,Driven Auxiliary Feedwater (TDAFW) pump on Lo Lo S/G Levels, it exhibited some oscillations in flow, however total flow remained above the required 400 gallons per minute (GPM) as recorded on the Plant Process Computer System (PPCS).

0 The Intermediate Range Nuclear Instrumentation, Channel N-35, after tracking consistant with Channel N-36 down'to approximately 10 E-10 amps, had its indication continue to drop below 10 E-11 amps. The N channel returned to normal (10 E-11 amps) approximately ten hours following the trip.

C. INOPERABLE STRUCTURES g COMPONENTS l OR SYSTEMS THAT CONTRIBUTED TO THE KG9iT:

None.

D. OWNER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:

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None.

E. METHOD OF DISCOVERY:

The event was immediately apparent due to alarms and indications in the Control Room.

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After the reactor trip, the Control Room operators performed the actions of Emergency Operating Procedures E-O, (Reactor Trip Or Safety Injection) and ES-0.1, (Reactor Trip Response). The MSIVs were manually actuated closed approximately four (4) minutes after the trip to prevent further plant cooldown. The plant was subsequently stabilized at hot shutdown.

. Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Com-mission per 10 CFR 50.72, non-emergency, 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> notification.

G. SAFETX SXSTEM RESPONSES:

The "A" S/G FRVs closed automatically from a feedwatdr isolation signal.

III. CAUSE OF KGDFZ A. IMMEDIATE CAUSE:

The reactor trip was due to "Att S/G Lo Lo Level

(</=>>4)

B. ROOT CAUSE:

The underlying cause of she "A" S/G Lo Lo Level ~

(</=174) was determined to be the Control Room operator's inability to control the "A" S/G level above its reactor trip setpoint due to the following contributing factors:

The transient perturbations that were occurring due to design (i.e. the design of the FRVs to go full open, when in automatic mode, following a turbine trip, and the design of having the bypass FRVs open at the higher power levels).

0 The shrink and swell phenomenon of the S/G water levels due to the above design induced perturba-tions and the transient induced perturbations.

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2 4 9 2 0 0 2 1 2 Following the reactor trip, pressurizer'level decreased to approximately 54 level as a result of the cooldown. This is an expected observed'ransient. The S/G levels both decreased to the narrow range taps. This is an expected transient based upon the encountered shrink in the S/Gs.

A slow cooldown resulted during the post trip recovery period. This cooldown is bounded by the plant accident

'nalysis and does not exceed the Technical Specification limit of 100 F per hour. Additional protection was provided by closure of the MSIVs.

Based on the above and a review of post trip data and past plant transients, it can be concluded that the plant has operated as designed and that there'as no unreviewed safety questions and that the public's health and safety was assured at all times.

CORRECTIVE ACTION A. ACTION TAKEN TO RRKZJBN AFFECTED SYSTEMS TO PRE-&TENT NORMAL STATUS:

0 The S/G levels were returned to their normal operating levels by addition of Auxiliary Feedwater, subsequent to the reactor trip.

0 The "A" MSIV, manufactured by Atwood and Morrill, is a 30 inch air operated swing check valve, installed in the reverse direction to use S/G steam flow to ensure proper closure. As with any swing check valve, the closing moment must be large enough to overcome the friction on the valve shaft due to the valve packing-. . Complete closure is accomplished by the force of the fluid flow on the valve disc. The "A" MSIV was subsequently stroked several times successfully to ensure operability and adequate closure capability. Results of these tests support the conclusion that failure of the "A" MSIV to fully seat during the reactor trip was not due to internal valve distortion and bending, but was the result of a lack of flow across the valve disc. Failure to close is attributed to the closure operation occurring in a quiescent environment.

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~~ vm eeeaaeV IIAC AVVI~'llIITl 0 s 0 0 o 2 4 4 9 2 p p 2 p p 0 90~ 1 2 Valve closure is dependent upon two factors:

The moment, developed by the weight of the valve disc and the spring provided to assist in valve

.closure, plus sufficient steam flow across the valve disc, without which the valve was not capable of completing its clc g operation.

When the demand signal for MSI~ =o close was ger

. ated d/p across the A MSIV was lower than th-. d/p across the B MSIV. The d/p across the B =. IV was enough to fully seat the valve while the d/p across the A MSIV did not provide enough force to overcome shaft packing frictional forces. Approximately 23 minutes later, the d/p across the A MSIV increased approximately 2 psid which resulted in complete closure of the valve.

For all design basis accidents, where MSIV closure is required, the accident transients

=-

would develop a large enough differential pressure to obtain complete valve closure. RG&E is continuing to evaluate various packing materials which have a low friction coefficient and can perform the required sealing function.

o The TDAFW pump was subsequently tested to determine the cause of the flow oscillations, but the test had to be aborted due to a steam leak on the governor valve. The governor valve was disassembled, inspected and placed back in service. The steam leak was the result of gasket leak (probably caused due to excessive travel of the governor valve). The gasket was replaced with a qualified spare. The cause of the flow oscillations was due to the "hunting" of the governor valve. The hunting of the governor valve was caused by a feedback nut being out of proper position., The position of the feedback nut was corrected and the TDAFW pump was subsequently tested successfully and returned to service.

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+AC A<< ~'iIIm o s o o o 2 4 4 9 2 p 2 p p 1 poi:1 2 0 As the Intermediate Range NIS Channel N-35 tracked NIS Channel N-36 for, its normal operating range. and returned to normal approximately ten (10) hours after the trip, no immediate action was deemed necessary. This abnormality has been observed and researched extensively in the past in cooperation with the NSSS vendor, Westinghouse.

No technical basis has been identified as to why the 10 E-11 idle current does not maintain indication at 10 E-11 amps; RG&E and Westinghouse concurred that the channel was operable and capable of performing all intended functions.

Further evaluations of the response characteris-tics of NIS channel N-35 will be performed during the 1992 Annual Refueling and Maintenance Outage.

0 This event was initiated by a main generator trip due to loss of excitation. Extensive examination, evaluation and testing was performed on the main generator voltage control system, with the following results and conclusions:

The automatic and manual voltage control units were extensively tested and found to operate satisfactorily. The Minimum Excitation Limiter (MEL) data taken during the testing indicated that the setting was too close to normal operating points of the generator. A new MEL setting was calculated, reviewed by .Westinghouse (the vendor) and implemented. The revised setting will allow operation to approximately 190 MVAR underexcited at 500 MW.

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IIAC IVn XW V,l. HVCLSAA ASOULATOISY COWHISSIOII IS@) I LICENSEE EVENT REPORT (LERI TEXT CONTINUATION AttrOvlO OUS JeO )ISOMI04 SIctirlS SI)I 'IS AACILITYHAAIS III OOCIIlt HUUl1 111 Llr IIUMOlr I ~ I ~ AOl I)I S~ Ovlrt<AL e v R.E. Ginna Nuclear Power Plant 0 0 110' tt)IT IIt rrn ~r never. vn rrreenr rrC Attn ~ s I Im 0 5 o 0 o 2 4 4 9 0 2 0 2 The unit was synchronized to the system with the-voltage regulator in manual and no unusual events were noted. When the voltage regulator was placed in the- automatic mode, the loop within the voltage regulator system was unstable and the voltage regulator was returned to the manual mode. The operation of the voltage regulator damping module was verified and the gain was reduced from maximum setting to the mid point on the potentiometer. The voltage regulator was returned to the automatic mode and operated satisfactorily.

The plant has now operated at approximately full power and has gone through several normal voltage adjustments such as lowering the voltaqe in the evening and raising the voltage in the morning as required by system load. No abnormalities. have been encountered.

B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:

As the underlying cause of the event was determined to be the inability of the Control Room operator to control the "A" S/G leve above its reactor trip

~

setpoint due to design and transient induced level perturbation, the following actions have been taken or are being planned:

0 Applicable operating procedures have been changed to require that the bypass FRVs be placed in manual closed when increasing above approximately 304 reactor power.

0 Applicable operating procedures have been changed to require returning the bypass FRVs to automatic control when decreasing below 304 reactor power.

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IIAC Isrse lAAA v l. eevCLlAII AlOULATCAYcoseseeClloee Ovl /eeo 104lI LICENSEE EVENT REPORT ILER) TEXT CONTINUATION AASSOvlo IISOWIOe l>eseAl5 ~ rlI TS I'ACILITYIIAIIlIII OOCIIKT eeULQlA 111 LlA IIUAOlAI ~ I ~ Aol IQ v TAA SloulreveAL SAVes~are v er U ~s R.E. Ginna Nuclear Power. Plant TKXT rrr rsrers ~ r ~. vm e seseeeer rrreC Arse ~'gr IITI 0 6 << o 2 4 4 9 2 0 0 2 1 2o~ 1 2 o A modification is planned for the 1993 Annual Refueling and Maintenance Outage that would modify the existing feedwater isolation logic for fail-open or fail-closed of the main and bypass FRVs upon turbine trip with main FRVs in automatic control mode. The planned modification will delete the existing fail-open logic and replace the fail-closed logic with actuation upon reactor trip as opposed to turbine trip.

As the event was initiated by the Main Generator trip due to loss of excitation, the following actions are planned to prevent recurrence'.

0 RG&E is planning to purchase and install a replacement voltage regulator unit.

I 0 Routine testing and maintenance will be performed on the existing voltage regulator unit during the 1992 Annual Refueling and Maintenance Outage to attain a high degree of confidence that the unit will operate without incident for the entire fuel cycle.

ADDITIONAL INFORMATION A. FAILED COMPONENTS:

The TDAFW pump turbine is a 465 horsepower noncondensing steam turbine, serial number 26635, manufactured by the Worthington Corporation.

B. PREVIOUS LERs ON SIMILAR EVENTS:

A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same underlying cause at Ginna Station could be identified.

C. SPECIAL COMMENTS:

None.

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