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| issue date = 12/19/1980
| issue date = 12/19/1980
| title = LER 80-044/03L-0:on 801124,pump 2-SI-P-1A Declared Inoperable Due to Low Resistance.Caused by Connection Box Grounded Out by Rainwater.Box Dried Out,Roof Hatch Repaired & Pump & Motor Tested
| title = LER 80-044/03L-0:on 801124,pump 2-SI-P-1A Declared Inoperable Due to Low Resistance.Caused by Connection Box Grounded Out by Rainwater.Box Dried Out,Roof Hatch Repaired & Pump & Motor Tested
| author name = WILSON J L
| author name = Wilson J
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| addressee name =  
| addressee name =  
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:l'JRC FORNI 366 (7-77) e LICENSEE EVENT REPORT -NUCLEAR REGULATORY COMMISSION CONTROL BLOCK: I I I,\ (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
{{#Wiki_filter:l'JRC FORNI 366 (7-77)                                                               e           LICENSEE EVENT REPORT
!--1 _..____.__  
                                                                                                                                                  -NUCLEAR REGULATORY COMMISSION CONTROL BLOCK:             I
....... __.... ___ 6 \..!.) CU2J I v1 Al s I PI s I 2101 o I o I -I o I o I o I o I o I -I o I o 101 4 ! 1 I 1 I 1 I 1 101 I I © 7 8 9 LICENSEE.
                                          !--1_..____.__.......__...._ _ _6          I\..!.)
CODE 14 1S LICENSE NUMBER 2S 26 LICEllfSE TYPE JO S7 CAT SB CON'T [IE] 7 8  
I,\                            (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
~©I o I s I o I o I o I 2 I s I 1 101 1 11 I 2 I 4 I s I o IG)! 1 12 11 I 9 1 s Io 10 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 7S REPORT DATE* 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
CU2J I v1 7      8    9 Al   sI PI sI 2101 o I oI - I o I oI oI o I o I - I o I o 101 4 ! 1 I 1 I 1 I 1 101 I I © LICENSEE. CODE               14       1S                           LICENSE NUMBER                               2S   26             LICEllfSE TYPE                     JO             S7 CAT SB CON'T
I On November 24, 1980, with Unit No. 2 at 100 percent power, 2-SI-P-lA was declared inoperable due to low resistance*.
[IE]
Thi" s 1* s contrary t T S 3 3 A 6 d
7       8
* t []JI] LI -----------------------------0
                    ;~~~~~      ~©I               oI s I DOCKET  oI o INUMBER  oI 2 I s I 16810169 1 11EVENT                        4 I s I o IG)! 1 12 11 I 9 1s Io 10 I 2 IDATE 60             61                                                                                                 74             7S               REPORT DATE*                               80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
__ . __ . __ . _. _. __ an __ i_s_r_e..:..p_o_r_-_
I   On November 24, 1980, with Unit No. 2 at 100 percent power, 2-SI-P-lA was declared inoperable due to low resistance*.                                                     Thi" s 1* s contrary t T S 3 3 A 6
[[EJ IIITJ [ill] able per T. *s. 6.6.2.b(2).
[]JI]       LI-----------------------------0                                                                                               __.__.__. _._.__an_d _i_s_r_e..:..p_o_r_-_
The redundant pump was operable.
* t
Therefore the health and safety of the public were not affected.
((EJ             able per T.             *s.     6.6.2.b(2).                   The redundant pump was operable. Therefore the health and safety of the public were not affected.
[IE] [[I]] 7 8 9 [ill] 7 8 SYSTEM CODE Isl Fl@ 9 10 LER/RO CVENT YEAR REPORT 1 8 1 0 1 NUMBER 21 22 CAUSE CAUSE CODE SUBCODE COMPONENT CODE w@ L...z.1@)
IIITJ
I Mio Ir I al Rix I@ 11 12 13 18 SEQUENTIAL OCCURRENCE REPORT NO. CODE I I I a I 4 I 4 I l /I I o I 3 I 23 24 26 27 28 29 COMP, SUBCOOE w@ 19 REPORT TYPE LL.J 30 VALVE SUBCODE w@ 20 l.=l 31 ACTlON FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP. SUPPLIER REVISION NO. L.uJ 32 COMPONENT MANUFACTURER*
[ill]
80 TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED FOAM :;us. l.JLJ@l.xJ@)
[IE]
Lz.J@ Lz.J la la la la I LYJ@). W 33 34 3S 36 37 40 41 42 ln.J@) I w I I 2 1.o.J@ CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @ 43 44 I Rain water from a leaking roof batch groirnded out the moto:r' connection box. o:::IIJ I motor connection box dried out. The pump and motor were tested and returned -to DJ]] I service. The roof hatch was repaired.
((I))
o::m [JJTI 7 8 9 FACILITY '3Q\ STATUS % POWER OTHER STATUS \::::;/ METHOD OF (.;'.;\ 47 The BO tITIJ ~ I 1 1 0 I O l@)I ...... __ N.;..../A
7       8   9                                                                                                                                                                                                                           80 SYSTEM                CAUSE                CAUSE                                                                  COMP,                          VALVE CODE                  CODE              SUBCODE                              COMPONENT CODE                SUBCOOE                          SUBCODE
__ _,r 8 9 10 12 1'3 DISCOVERY DISCOVERY DESCRIPTION
[ill]
\:;I W@L.I ___ R:.;:o:;.u::.t::.:1::.:*n::.:e:......::T:..:e:..::s;..::t:___.  
7       8 Isl Fl@
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9           10 w@ 12L...z.1@) 13I Mio Ir I al Rix 18I@
ACTIVITY CONTENT Q\ RELEASED OF RELEASE AMOUNT OF ACTIVITY [QI] LU@) l2J@I . N/ A 7 8 9 10 11 4S 46 44 so 44 4S LOCATION OF RELEASE  N/A. 80 PERSONNEL EXPOSURES NUMBER c;;.. TYPE ~DESCRIPTION
11 w@ w@
[IE] I 01 01 OJ~~L......-------..:.:N.t...:./
19                              20 SEQUENTIAL                                     OCCURRENCE               REPORT                                                  REVISION
A;:_ ____ ..;._ _ _..;.. _________
              ~      LER/RO CVENT YEAR                                            REPORT NO.                                         CODE                     TYPE                                                      NO.
___. 7 8 9 11 12 13 PERSONNEL INJURIES t,;:;\ so NUMBER DESCRIPTION6 f2TIJ l O I O IO l@'------,-------....:N~/.;.:.A
              ~ REPORT              1 81 01                  I23 I               I a I 4 I 426I                      l27/I         I o I 329I                                              l.=l NUMBER 21          22                              24                                               28 LL.J 30                           31 L.uJ 32 ACTlON FUTURE                     EFFECT             SHUTDOWN                                           ~      ATTACHMENT       NPRD-4                   PRIME COMP.                                     COMPONENT TAKEN     ACTION               ON PLANT             METHOD                             HOURS ~                SUBMITTED     FOAM :;us.                   SUPPLIER                                MANUFACTURER*
________________
l.JLJ@l.xJ@)
__. 7 8 9 11 12 . LOSS OF OR DAMAGE TO FACILITY '4J' TYPE DESCRIPTION  
33        34 Lz.J@
\::::;) 80 ~(S}r........
3S Lz.J la la la la I 36                  37                              40 LYJ@).
______ ~-----=N~/=A~----~----------------'
41 W
7 a 1:su:i;:~o;;CRIPTION@
42 ln.J@)
8012290 "I< C) NRC USE ONLY 80"' IIli] ~e,~ __________  
43 I wI I 21.o.J@
----:;N.:.i..:.:..A
44                      47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS                                     @
________ ___. l I II II* 1 II I II I 8 9 -{\ 10 68 69 80 ; NAME OF PREPARER ____ ....;J:;..;...*  
I Rain     water from a leaking roof batch groirnded out the moto:r' ~ connection box.                                                                                                                           The o:::IIJ I motor           connection box dried out.                                       The pump and motor were tested and returned -to DJ)) I service.                     The roof hatch was repaired.
....;L;;;,,,,;,,.'
o::m
_W;,,;,.1;;;.*
[JJTI 7       8   9                                                                                                                                                                                                                         BO FACILITY                                                                       '3Q\           METHOD OF                                                                                            (.;'.;\
l;;;.s:;.o;:;.n;;;_
STATUS               % POWER                           OTHER STATUS           \::::;/         DISCOVERY                                DISCOVERY DESCRIPTION                                      \:;I tITIJ ~                   I   1 1 0 I O l@)I. . . _ _                N.;..../A_ __ , r                       W@L.I___R:.;:o:;.u::.t::.:1::.:*n::.:e:......::T:..:e:..::s;..::t:___.- - - - - - - - - - '
_____ _ PHONE: _ _.(_..8...,.0...,,4u)-3i...5:.L7....;-
8    9 ACTIVITY 10 CONTENT 12      1'3 Q\
.. 31...1l.i..8'-"4:__
44            4S          46                                                                                                        so RELEASED OF RELEASE                           AMOUNT OF ACTIVITY ~                                                                      LOCATION OF RELEASE
__ _ 0 a. "
[QI] LU@) l2J@I .                                                       N/ A                                                                N/A.
a*, *. ***-r, ... ATTACHMENT 1 SURRY POWER DOCKET NO: e STATION, UNIT 2 50-281 80-044/03L-0 11-24-80 e REfOR.! NO: EVENT DATE: SUBJECT 2-SI-P-lA INOPERABLE
7       8   9             10           11                                                       44                   4S                                                                                                             80 PERSONNEL EXPOSURES                                 ~
: 1. Description of Event: On 24 November 1980, with Unit No. 2 at 100% power, rain water from a heavy rain storm was observed leaking th~ough a roof hatch on 2-SI-P-lA.
NUMBER         c;;.. TYPE ~DESCRIPTION
Operability of the redundant pump (2-SI-P-lB) was verified by PT 18.1 and 2-SI-P-lA was removed from service. Investigation revealed that the motor.connection was grounded .. This is contra1:y to Technical Specification 3.3.A.6 *and-* is reportable*
[IE] I 01 01                 OJ~~L......-------..:.:N.t...:./A;:__ _ _ _..;.__ _..;.._ _ _ _ _ _ _ _ ____.
7       8   9               11 PERSONNEL INJURIES 12           13 t,;:;\
so NUMBER               DESCRIPTION6 f2TIJ l O I O IO 7      8    9                11 l@'------,-------....:N~/.;.:.A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ___.
12                   .                                                                                                                                                                         80 LOSS OF OR DAMAGE TO FACILITY               '4J' TYPE       DESCRIPTION                     \::::;)
~ ~(S}r........______~ - - - - - = N ~ / = A ~ - - - - ~ - - - - - - - - - - - - - - - - '
7       a 1:su:i;:~o;;CRIPTION@
IIli] ~e,~__________----:;N.:.i..:.:..A_ _ _ _ _ _ _ ____. l I II II* 1 II I II I ~
8012290                            "I<      C)                                                                NRC USE ONLY                      80"'
8   9 -{\       10                                                                                                                                               68       69                                                 80 ;
0 NAME OF PREPARER _ _ _ _....;J:;..;...*. . ;L; ;, , ;, .'_W;,,;,.1;;;.*l;;;.s:;.o;:;.n;;;__ _ _ _ __                PHONE: _                 _.(_..8...,.0...,,4u)-3i...5:.L7....;-.31...1l.i..8'
                                                                                                                                                                                                                .            -"4:___ __     a.
 
a*,*. ~ ***- r, ...
ATTACHMENT 1 e                                  e SURRY POWER STATION, UNIT 2 DOCKET NO:    50-281 REfOR.! NO:    80-044/03L-0 EVENT DATE: 11-24-80 SUBJECT                           2-SI-P-lA INOPERABLE
: 1. Description of Event:
On 24 November 1980, with Unit No. 2 at 100% power, rain water from a heavy rain storm was observed leaking th~ough a roof hatch on 2-SI-P-lA. Operability of the redundant pump (2-SI-P-lB) was verified by PT 18.1 and 2- SI-P-lA was removed from service. Investigation revealed that the motor.connection was grounded . . This is contra1:y to Technical Specification 3.3.A.6 *and-* is reportable*
as per Tech. Spec. 6.6.2.b(2).
as per Tech. Spec. 6.6.2.b(2).
: 2. Probable Consequences and Status of Redundant Equipment:
: 2. Probable Consequences and Status of Redundant Equipment:
The low head Safety Injection
The low head Safety Injection :Bumps provide*. cooling and makeup water to.2'the reactor during the LOCA. The redundant pump*(2-SI-P-1B) was operable and would have functioned as designed. 2-SI-P-lA was returned to service in 12 hours, well within the 24 hours allowed. Therefore, the health and safety of the public were not affected.
:Bumps provide*.
: 3. Cause:
cooling and makeup water to.2'the reactor during the LOCA. The redundant pump*(2-SI-P-1B) was operable and would have functioned as designed.
Rain water from a leaking roof hatch above the pump leaked into the motor con-nection box and created a ground.
2-SI-P-lA was returned to service in 12 hours, well within the 24 hours allowed. Therefore, the health and safety of the public were not affected.
: 4. Immediate Corrective Action:
: 3. Cause: Rain water from a leaking roof hatch above the pump leaked into the motor nection box and created a ground. 4. Immediate Corrective Action: The redundant pump (2-SI-P-lB) was verified operable as required by Technical Specification 3.3.B.3. Water was removed from the connection box and heat was applied. 5. Subsequent Corrective Action: The motor connection box was dried using temporary electrical heaters. sequently the pump and motor were verified operable and returned to service. 6. Action Taken to Prevent Recurrance  
The redundant pump (2-SI-P-lB) was verified operable as required by Technical Specification 3.3.B.3. Water was removed from the connection box and heat was applied.
-The leaking roof hatch was repaired and.inspected during a subsequent rain storm. 7. Generic Implications:
: 5. Subsequent Corrective Action:
The motor connection box was dried using temporary electrical heaters. Sub-sequently the pump and motor were verified operable and returned to service.
: 6. Action Taken to Prevent Recurrance -
The leaking roof hatch was repaired and.inspected during a subsequent rain storm.
: 7. Generic Implications:
None.}}
None.}}

Latest revision as of 12:42, 17 March 2020

LER 80-044/03L-0:on 801124,pump 2-SI-P-1A Declared Inoperable Due to Low Resistance.Caused by Connection Box Grounded Out by Rainwater.Box Dried Out,Roof Hatch Repaired & Pump & Motor Tested
ML18139A942
Person / Time
Site: Surry Dominion icon.png
Issue date: 12/19/1980
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139A940 List:
References
LER-80-044-03L-03, LER-80-44-3L-3, NUDOCS 8012290460
Download: ML18139A942 (2)


Text

{{#Wiki_filter:l'JRC FORNI 366 (7-77) e LICENSEE EVENT REPORT

                                                                                                                                                 -NUCLEAR REGULATORY COMMISSION CONTROL BLOCK:             I
                                          !--1_..____.__.......__...._ _ _6          I\..!.)

I,\ (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) CU2J I v1 7 8 9 Al sI PI sI 2101 o I oI - I o I oI oI o I o I - I o I o 101 4 ! 1 I 1 I 1 I 1 101 I I © LICENSEE. CODE 14 1S LICENSE NUMBER 2S 26 LICEllfSE TYPE JO S7 CAT SB CON'T [IE] 7 8

                    ;~~~~~      ~©I               oI s I DOCKET  oI o INUMBER   oI 2 I s I 16810169 1 11EVENT                         4 I s I o IG)! 1 12 11 I 9 1s Io 10 I 2 IDATE 60             61                                                                                                 74              7S                REPORT DATE*                                80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@

I On November 24, 1980, with Unit No. 2 at 100 percent power, 2-SI-P-lA was declared inoperable due to low resistance*. Thi" s 1* s contrary t T S 3 3 A 6 []JI] LI-----------------------------0 __.__.__. _._.__an_d _i_s_r_e..:..p_o_r_-_

  • t

((EJ able per T. *s. 6.6.2.b(2). The redundant pump was operable. Therefore the health and safety of the public were not affected. IIITJ [ill] [IE] ((I)) 7 8 9 80 SYSTEM CAUSE CAUSE COMP, VALVE CODE CODE SUBCODE COMPONENT CODE SUBCOOE SUBCODE [ill] 7 8 Isl Fl@ 9 10 w@ 12L...z.1@) 13I Mio Ir I al Rix 18I@ 11 w@ w@ 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION

             ~       LER/RO CVENT YEAR                                             REPORT NO.                                         CODE                     TYPE                                                       NO.
             ~ REPORT              1 81 01                   I23 I               I a I 4 I 426I                      l27/I         I o I 329I                                              l.=l NUMBER 21           22                               24                                                28 LL.J 30                            31 L.uJ 32 ACTlON FUTURE                     EFFECT             SHUTDOWN                                           ~       ATTACHMENT       NPRD-4                   PRIME COMP.                                      COMPONENT TAKEN      ACTION               ON PLANT              METHOD                             HOURS ~                 SUBMITTED      FOAM :;us.                    SUPPLIER                                MANUFACTURER*

l.JLJ@l.xJ@) 33 34 Lz.J@ 3S Lz.J la la la la I 36 37 40 LYJ@). 41 W 42 ln.J@) 43 I wI I 21.o.J@ 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @ I Rain water from a leaking roof batch groirnded out the moto:r' ~ connection box. The o:::IIJ I motor connection box dried out. The pump and motor were tested and returned -to DJ)) I service. The roof hatch was repaired. o::m [JJTI 7 8 9 BO FACILITY '3Q\ METHOD OF (.;'.;\ STATUS  % POWER OTHER STATUS \::::;/ DISCOVERY DISCOVERY DESCRIPTION \:;I tITIJ ~ I 1 1 0 I O l@)I. . . _ _ N.;..../A_ __ , r W@L.I___R:.;:o:;.u::.t::.:1::.:*n::.:e:......::T:..:e:..::s;..::t:___.- - - - - - - - - - ' 8 9 ACTIVITY 10 CONTENT 12 1'3 Q\ 44 4S 46 so RELEASED OF RELEASE AMOUNT OF ACTIVITY ~ LOCATION OF RELEASE [QI] LU@) l2J@I . N/ A N/A. 7 8 9 10 11 44 4S 80 PERSONNEL EXPOSURES ~ NUMBER c;;.. TYPE ~DESCRIPTION [IE] I 01 01 OJ~~L......-------..:.:N.t...:./A;:__ _ _ _..;.__ _..;.._ _ _ _ _ _ _ _ ____. 7 8 9 11 PERSONNEL INJURIES 12 13 t,;:;\ so NUMBER DESCRIPTION6 f2TIJ l O I O IO 7 8 9 11 l@'------,-------....:N~/.;.:.A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ___. 12 . 80 LOSS OF OR DAMAGE TO FACILITY '4J' TYPE DESCRIPTION \::::;) ~ ~(S}r........______~ - - - - - = N ~ / = A ~ - - - - ~ - - - - - - - - - - - - - - - - ' 7 a 1:su:i;:~o;;CRIPTION@ IIli] ~e,~__________----:;N.:.i..:.:..A_ _ _ _ _ _ _ ____. l I II II* 1 II I II I ~ 8012290 "I< C) NRC USE ONLY 80"' 8 9 -{\ 10 68 69 80 ; 0 NAME OF PREPARER _ _ _ _....;J:;..;...*. . ;L; ;, , ;, .'_W;,,;,.1;;;.*l;;;.s:;.o;:;.n;;;__ _ _ _ __ PHONE: _ _.(_..8...,.0...,,4u)-3i...5:.L7....;-.31...1l.i..8'

                                                                                                                                                                                                               .            -"4:___ __      a.

a*,*. ~ ***- r, ... ATTACHMENT 1 e e SURRY POWER STATION, UNIT 2 DOCKET NO: 50-281 REfOR.! NO: 80-044/03L-0 EVENT DATE: 11-24-80 SUBJECT 2-SI-P-lA INOPERABLE

1. Description of Event:

On 24 November 1980, with Unit No. 2 at 100% power, rain water from a heavy rain storm was observed leaking th~ough a roof hatch on 2-SI-P-lA. Operability of the redundant pump (2-SI-P-lB) was verified by PT 18.1 and 2- SI-P-lA was removed from service. Investigation revealed that the motor.connection was grounded . . This is contra1:y to Technical Specification 3.3.A.6 *and-* is reportable* as per Tech. Spec. 6.6.2.b(2).

2. Probable Consequences and Status of Redundant Equipment:

The low head Safety Injection :Bumps provide*. cooling and makeup water to.2'the reactor during the LOCA. The redundant pump*(2-SI-P-1B) was operable and would have functioned as designed. 2-SI-P-lA was returned to service in 12 hours, well within the 24 hours allowed. Therefore, the health and safety of the public were not affected.

3. Cause:

Rain water from a leaking roof hatch above the pump leaked into the motor con-nection box and created a ground.

4. Immediate Corrective Action:

The redundant pump (2-SI-P-lB) was verified operable as required by Technical Specification 3.3.B.3. Water was removed from the connection box and heat was applied.

5. Subsequent Corrective Action:

The motor connection box was dried using temporary electrical heaters. Sub-sequently the pump and motor were verified operable and returned to service.

6. Action Taken to Prevent Recurrance -

The leaking roof hatch was repaired and.inspected during a subsequent rain storm.

7. Generic Implications:

None.}}