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| issue date = 06/05/1981
| issue date = 06/05/1981
| title = LER 81-009/01T-0:on 810522,Westinghouse Identified Potential Sys Interaction Involving Vol Control Tank Level Control Sys & Charging Pumps.Caused by Design Criteria Misinterpretation.Procedure Mods Will Be Made
| title = LER 81-009/01T-0:on 810522,Westinghouse Identified Potential Sys Interaction Involving Vol Control Tank Level Control Sys & Charging Pumps.Caused by Design Criteria Misinterpretation.Procedure Mods Will Be Made
| author name = WILSON J L
| author name = Wilson J
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| addressee name =  
| addressee name =  
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:NRC FORM 366 (7-77) -.CLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK: ! 10 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI 1'--------"--'----''---"----:,6 LU2] l V I A I s I p I s I 1 101 0 I 0 I -I o I o I a I o I a I -I o I o 101 4 I 1 ! 11 1 ! 1101 I I  LICENSE NUMBER 2S 26 LICENSE TYPE 30 :7 CAT 58
{{#Wiki_filter:NRC FORM 366 (7-77)
* 8 9 i.lCENSE!:
CONTROL BLOCK:             !
CODE 1" 15 ::JN'T I o I , I 7 8  
1'--------"--'----''---"----:,6 ~
~© I o I s I o I o I o I 2 I s i o 101 o I s 12 J 2 I s I 1 IG) I o I 6 I o I 5 J_ s I 1 I G) 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 7S RE?ORTDA,c; 80 :VENT D:SCRIPTION AND PROBABLE CONSEQUENCES  
LICENSEE EVENT REPORT 10
@ I Westinghouse has identified a potential system interaction concern involving the [£ID I volume control tank (VCT) level control .system and charging pumps. A postulated
                                                                                                                                                  . C L E A R REGULATORY COMMISSION (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI LU2]
[ill] I failure of the VCT level control system,' without operator intervention, could lead [QJ]J I to a loss of suction fluid for the charging pumps. Numerous visual and audible [IJTI / indications are available to the operator to pemit the termination of this [£JJJ jpostulated event. The health*and safety of the public were not affected.
    ~      8 lV 9
This *[II]] 1 event is reportable per T.S.-6.6.2.a(9).
IA I s         I p I s I 1 101 0 i.lCENSE!: CODE              1"      15 I0 I- I           o I o I a I o I a I - I o I o2S10126 4 I 1! 11 TYPE LICENSE NUMBER                                                LICENSE 1! 1101     30         :7       CAT I 58I*
7 8 9 [ill] 7 B SYSTEM CODE IP \CI@ 9 10 Q. LER/RO CVENT YEAR '0 REPOR7 l8 I 11 NUMBER 21 . 22 CAUSE CAUSE CODE SUBCODE COMPONENT CODE w@ ~@ I z I z I z 1 z I z I z 1@ 11 12 1:l SEQUENTIAL REPORT NO. Io 10 I 9 I 24 26 18 OCCURRENCE CODE 10 11 I 28 29 COMP. SUBCODE ~@ 19 REPORT TYPE Lu 30 VALVE SUBCDDE Lu@ 20 AC.ION FUTURE 7AKEN ACTION EFFECT SHUTDOWN . '* (.;::::\ ATTACHMENT*
::JN'T Io 7
* NPRD~ PRIME COMP.,--***
I,I 8
SUPPLIER ** ** REVISION NO. L~J *:i:z . COMPONEN":".
                        ~~~~~        ~© I o I 60            61 s I oI oI oI DOCKET NUMBER 2I      s i o 101 o I s 68      69 12   J 2 EVENT DATE I s I1      IG) I7So I 6 I o I 5 J_ s I 1 IG) 74                   RE?ORTDA,c;                                   80
MANUFACTURER I 80 ON PLANT ME;THOD . HOURS SUBMITTED FOAM SUB. I 11 l@l£J@) ~@ l..Ll Io I 01 *oJ o 1* LlJ@-l1l.J@) J:l 34 JS 3B 37 40 41 4'2 W@l_-*. *1 z I 9 l 9 I 9 )@ CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @ 43 44 47 The cause of this concern appeared to be one of design criteria interpretatio1J..,_~
:VENT D:SCRIPTION AND PROBABLE CONSEQUENCES                                           @
__ Jb~ operating staff has been alerted to this potential problem and rhe _consequences.
I Westinghouse                 has identified a potential system interaction concern involving the
IT]]] I Mi.nor. modifications to Unit No. l and 2 pr_ocedures wi 11 be made to provide additional!
[£ID I volume control tank (VCT) level control .system and charging pumps.                                                                                                   A postulated
CiJdJ I guidance.
[ill] I failure of the VCT level control system,' without operator intervention, could lead
ITEl 1 a 9 FAClLITY (JO' STATUS % FOWER OTHER STATUS \::::::,1 t2TIJ ~:@) ! 0 I O j O 111...._D_e_fu_e_l_ed
[QJ]J       I to a loss of suction fluid for the charging pumps.                                                                   Numerous visual and audible
__ .__j 7 8 9 10 11 1'3 ACTIVITY CONTENT Q\ RELEASEO OF RELEASE AMOUNT OF ACTIVITY~
[IJTI / indications are available to the operator to pemit the termination of this
C::fil L1J@ I z 1@)11...._.;.:.N:,.:./A~-----.....J 7 3 9 10 11 80 ~00~ DISCOVERY DISCOVERY DESCRIPTION
[£JJJ         jpostulated event.                         The health*and safety of the public were not affected.                                                                                     This
'5 Ll2.J<22)~1~F~~x~t~e~r~n~a~l=--~S~ou=r=-=-c=e
  *[II))        1 event is reportable per T.S.- 6.6.2.a(9).
.........
I 7       8   9                                                                                                                                                                                                                               80 SYSTEM               CAUSE              CAUSE                                                                COMP.              VALVE CODE               CODE          SUBCODE                        COMPONENT CODE                      SUBCODE              SUBCDDE
_..,.....
[ill]                              IP \CI@ w@ ~@ Iz Iz I z 1 z I z I z 1@ ~@ Lu@
..................
7      B                          9          10          11                12                  1:l                               18            19                  20 SEQUENTIAL                                 OCCURRENCE            REPORT                                        REVISION Q.      LER/RO CVENT YEAR                                            REPORT NO.                                     CODE                TYPE                                                NO.
-.............................................  
                  '0    REPOR7 NUMBER l8 I 11 Io 10 I 9 I                                   10 11 I                 Lu                                                L~J .
---i 45 46 44 80 _LOCATION OF RELEASE @ 44 45 80 ?!:RSONNEL EXPOSURES r::;:;,..
21        22                            24                  26                        28       29           30                                               *:i:z AC.ION FUTURE                     EFFECT           SHUTDOWN                             .   '* (.;::::\ ATTACHMENT*
NUMBE"l A TYP: DESCRIPTiON U2] JO I OJ ':lJ0L.B@L.........
* NPRD~           PRIME COMP.,--***                           COMPONEN":".
_____ N_/A _____________________
7AKEN        ACTION            ON PLANT            ME;THOD                          . HOURS ~              SUBMITTED        FOAM SUB.            SUPPLIER ** **                     MANUFACTURER I 11 l@l&#xa3;J@)
.........
J:l          34
,, _ _.. a s n 12 13 80 ~ERSONNEL INJURIES Q NUMBER DESCRIPTIONO GliJ OJ O I O l@L..........------~t.:.:..1/.:.:.A
                                                    ~@
__________________
JS l..Ll Io I 01 *oJ o 1*
-___. a s *
3B                  37                            40 LlJ@-
* 11 12 eo LOSS OF OR DAMAGE TO FACILITY ;-vpe DESCRIPTION
41 l1l.J@)
\::;J [2]Ij ~{&sect;)L.........._.
4'2 W@l_-*. *1 z I 9 l 9 I 9 )@
_______ ___;.,:.:1/~A:..........
43                          44                                            47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS                                  @
_________________
The cause of this concern appeared to be one of design criteria interpretatio1J..,_~__Jb~
____. ; 8 9 10 so PUBLICITY G\ NRC USE ONLY ISSUED(,:";\
operating staff has been alerted to this potential problem and rhe _consequences.
DESCRIPTION~  
IT))] I Mi.nor. modifications to Unit No. l and 2 pr_ocedures wi 11 be made to provide additional!
"' LiliJ IN 1e, N A 1 1 1 , 1 1 1 1 1 1 1 S 9 10. 68 69 80 ; ,'\JAME c,pc;;;plpE"l J, L. Wilson ~'-'ONEf 804) 357-3184 _____ 81 fJ6 o.~ '~-siJ-----------
CiJdJ        I  guidance.
_ ----------
ITEla 1           9                                                                                                                                                                                                                              80 FAClLITY                                                                    (JO'            ~00~                                                                                  ~
_---------
STATUS                % FOWER                        OTHER STATUS          \::::::,1      DISCOVERY                                DISCOVERY DESCRIPTION                        '5 t2TIJ ~:@) ! 0 I O j                          O 111...._D_e_fu_e_l_ed_ _                     .__j Ll2.J<22)~1~F~~x~t~e~r~n~a~l=--~S~ou=r=-=-c=e........._..,.......................- .............................................---i 7      8    9                10              11      1'3                                      44      45            46                                                                                                                  80 ACTIVITY        CONTENT                                                  Q\
___ **-.* _ ---~-------~--------------
RELEASEO OF RELEASE                          AMOUNT OF ACTIVITY~                                                                    _LOCATION OF RELEASE                      @
*--
C::fil L1J@ I z 1@)11...._.;.:.N:,.:./A~-----.....J 7      3    9                10          11                                                    44              45                                                                                                                        80
-ATTACHMENT 1 SURRY POWER STATION, UNIT NO. DOCKET NO: 50-280 REPORT NO: 81-009/017-0 EVENT DATE: 05-22-81 TITLE OF EVENT: VCT LEVEL SYSTEM DESIGN PROBLEM 1. DESCRIPTION OF EVENT: Westinghouse has identified a potential system interaction involving the volume control tank (VCT) level control system and the charging pumps. A postulated failure (failed high) of the VCT level control system, without operator intervention, could lead to a possible loss of suction fluid for the charging pumps. This is reportable per Tech. Spec. 6.6.2.a (9). 2. PROBABLE CONSEQUENCES arid STATUS of REDUNDANT EQUIPMENT:
                      ?!:RSONNEL EXPOSURES                              r::;:;,..
The VCT is the normal supply to the charging pumps. The RWST is the alternate and accident supply to the charging pumps. If VCT level. transmitter (LT-115) failed high, letdown* to the VCT would be diverted to the Primary Drain Tank. The auto~attc mak~ up to the VCT and the automatic transfer to the RWST, on .. *VCH.. Low*-low level, would not_be funq,ional; Throughout this event, numerous ,set.onda ry *ind i caFons (VCT pressure, charging pressure and f 1 ow) and a 1 arms would be available to the operator for system evalua~ion.
NUMBE"l          A    TYP:        DESCRIPTiON U2] JO I OJ ':lJ0L.B@L........._____N_/A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _.........,,__..
In addition, redundant VCT level indication (Ll-112), located near the VCT, would be available.
a s                    n        12          13                                                                                                                                                                                    80
Westinghouse has indicated that the operator would have approximately 10 minutes to transfer the charging pump suction from the VCT to the RWST or initiate other appropriate corrective actions to prevent possible damage to the operating charging pump. The failure of the VCT level control system will not prevent the manual transfer of charging pump suction* to the RWST or the automatic transfer to the RWST during an accident.
                      ~ERSONNEL INJURIES                    Q NUMBER                DESCRIPTIONO GliJ            OJ O I O l@L..........------~t.:.:..1/.:.:.A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _-___.
a s       *
* 11      12                                                                                                                                                                                                 eo LOSS OF OR DAMAGE TO FACILITY ~
                ;-vpe        DESCRIPTION                    \::;J
[2]Ij ~{&sect;)L.........._.__________;.,:.:1/~A:.........._ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _____.
    ;       8    9            10                                                                                                                                                                                                              so PUBLICITY                  G\                                                                                                                                        NRC USE ONLY ISSUED(,:";\ DESCRIPTION~                                                                                                                                                                                                           "'
LiliJ IN 1e, S    9            10.
NA 68 1 1 1, 1 1 1 69 1      1 1 1~
80 ;
                              ,'\JAME c,pc;;;plpE"l              J, L. Wilson                                                                  ~'-'ONEf    804) 357-3184                                                                          ~
_____81 fJ6        o.~    '~-siJ----------- _---------- _-- - - - ___ * -.* _---~-------~-------------- *-
 
ATTACHMENT 1 SURRY POWER STATION, UNIT NO.
DOCKET NO:          50-280 REPORT NO:          81-009/017-0 EVENT DATE:          05-22-81 TITLE OF EVENT:            VCT LEVEL SYSTEM DESIGN PROBLEM
: 1. DESCRIPTION OF EVENT:
Westinghouse has identified a potential system interaction involving the volume control tank (VCT) level control system and the charging pumps.
A postulated failure (failed high) of the VCT level control system, without operator intervention, could lead to a possible loss of suction fluid for the charging pumps.
This is reportable per Tech. Spec. 6.6.2.a (9).
: 2. ~  PROBABLE CONSEQUENCES arid STATUS of REDUNDANT EQUIPMENT:
The VCT is the normal supply to the charging pumps. The RWST is the alternate and accident supply to the charging pumps. If VCT level. transmitter (LT-115) failed high, letdown* to the VCT would be diverted to the Primary Drain Tank.
The auto~attc mak~ up to the VCT and the automatic transfer to the RWST, on
  .. *VCH.. Low*-low level, would not_be funq,ional; Throughout this event, numerous
      ,set.onda ry *ind i caFons (VCT pressure, charging pressure and f 1ow) and a 1arms would be available to the operator for system evalua~ion. In addition, redundant VCT level indication (Ll-112), located near the VCT, would be available.
Westinghouse has indicated that the operator would have approximately 10 minutes to transfer the charging pump suction from the VCT to the RWST or initiate other appropriate corrective actions to prevent possible damage to the operating charging pump.
The failure of the VCT level control system will not prevent the manual transfer of charging pump suction* to the RWST or the automatic transfer to the RWST during an accident.
Since num~r6us visual and audible indications are available to the operator to permit the termination of this postulated event, the health and safety of the public would not be affected.
Since num~r6us visual and audible indications are available to the operator to permit the termination of this postulated event, the health and safety of the public would not be affected.
: 3. CAUSE: The cause .. of this.cconcern .appeared to be one of design criteria interpretation.
: 3. CAUSE:
: 4. IMMEDIATE CORRECTIVE ACTl'ON: The operating staff was alerted to this potential problem and the consequences.
The cause . of this.cconcern .appeared to be one of design criteria interpretation.
-ATTACHMENT 1 (continued)
: 4. IMMEDIATE CORRECTIVE ACTl'ON:
SURRY POWER STATION, UNIT NO. DOCKET NO: 50-280 REPORT NO: 81-009-017-0 EVENT DATE: 05-22-81 5. SUBSEQUENT CORRECTIVE ACTION: A review of station procedures was conducted, and as a result, minor cations (clarifications) will be made. )n addition, the postulated event, the consequences and the required corrective actions will be included in the operator's training/retraining program. 6. ACTION TAKEN TO PREVENT RECURRENCE:
The operating staff was alerted to this potential problem and the consequences.
 
ATTACHMENT 1 (continued)
SURRY POWER STATION, UNIT NO.
                                                                    -                      DOCKET NO:                     50-280 REPORT NO:                     81-009-017-0 EVENT DATE:                     05-22-81
: 5.     SUBSEQUENT CORRECTIVE ACTION:
A review of station procedures was conducted, and as a result, minor modifi-cations (clarifications) will be made. )n addition, the postulated event, the consequences and the required corrective actions will be included in the operator's training/retraining program.
: 6.     ACTION TAKEN TO PREVENT RECURRENCE:
At this time, none is deemed necessary.
At this time, none is deemed necessary.
: 7. GENERIC IMPLICATIONS:
: 7.     GENERIC IMPLICATIONS:
This concern is generic to both Unit No. 1 and 2, therefore, Unit No. 2 procedures will be modified . . ,.,,_~~-.-*,----,,..  
This concern is generic to both Unit No. 1 and 2, therefore, Unit No. 2 procedures will be modified .
,...._. --,---,--~.  
.,.,,_~~-.-*,----,,.. ,...._. --,---,--~. -- ~ -- *.-.--*-~---~----}}
----*.-.--*-~---~----}}

Latest revision as of 12:34, 17 March 2020

LER 81-009/01T-0:on 810522,Westinghouse Identified Potential Sys Interaction Involving Vol Control Tank Level Control Sys & Charging Pumps.Caused by Design Criteria Misinterpretation.Procedure Mods Will Be Made
ML18139B385
Person / Time
Site: Surry Dominion icon.png
Issue date: 06/05/1981
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139B384 List:
References
LER-81-009-01T, LER-81-9-1T, NUDOCS 8106090523
Download: ML18139B385 (3)


Text

NRC FORM 366 (7-77)

CONTROL BLOCK:  !

1'--------"--'-------"----:,6 ~

LICENSEE EVENT REPORT 10

. C L E A R REGULATORY COMMISSION (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI LU2]

~ 8 lV 9

IA I s I p I s I 1 101 0 i.lCENSE!: CODE 1" 15 I0 I- I o I o I a I o I a I - I o I o2S10126 4 I 1! 11 TYPE LICENSE NUMBER LICENSE 1! 1101 30 :7 CAT I 58I*

JN'T Io 7

I,I 8

~~~~~ ~© I o I 60 61 s I oI oI oI DOCKET NUMBER 2I s i o 101 o I s 68 69 12 J 2 EVENT DATE I s I1 IG) I7So I 6 I o I 5 J_ s I 1 IG) 74 RE?ORTDA,c; 80

VENT D:SCRIPTION AND PROBABLE CONSEQUENCES @

I Westinghouse has identified a potential system interaction concern involving the

[£ID I volume control tank (VCT) level control .system and charging pumps. A postulated

[ill] I failure of the VCT level control system,' without operator intervention, could lead

[QJ]J I to a loss of suction fluid for the charging pumps. Numerous visual and audible

[IJTI / indications are available to the operator to pemit the termination of this

[£JJJ jpostulated event. The health*and safety of the public were not affected. This

  • [II)) 1 event is reportable per T.S.- 6.6.2.a(9).

I 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCDDE

[ill] IP \CI@ w@ ~@ Iz Iz I z 1 z I z I z 1@ ~@ Lu@

7 B 9 10 11 12 1:l 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION Q. LER/RO CVENT YEAR REPORT NO. CODE TYPE NO.

'0 REPOR7 NUMBER l8 I 11 Io 10 I 9 I 10 11 I Lu L~J .

21 22 24 26 28 29 30 *:i:z AC.ION FUTURE EFFECT SHUTDOWN . '* (.;::::\ ATTACHMENT*

  • NPRD~ PRIME COMP.,--*** COMPONEN":".

7AKEN ACTION ON PLANT ME;THOD . HOURS ~ SUBMITTED FOAM SUB. SUPPLIER ** ** MANUFACTURER I 11 l@l£J@)

J:l 34

~@

JS l..Ll Io I 01 *oJ o 1*

3B 37 40 LlJ@-

41 l1l.J@)

4'2 W@l_-*. *1 z I 9 l 9 I 9 )@

43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @

The cause of this concern appeared to be one of design criteria interpretatio1J..,_~__Jb~

operating staff has been alerted to this potential problem and rhe _consequences.

IT))] I Mi.nor. modifications to Unit No. l and 2 pr_ocedures wi 11 be made to provide additional!

CiJdJ I guidance.

ITEla 1 9 80 FAClLITY (JO' ~00~ ~

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ATTACHMENT 1 SURRY POWER STATION, UNIT NO.

DOCKET NO: 50-280 REPORT NO: 81-009/017-0 EVENT DATE: 05-22-81 TITLE OF EVENT: VCT LEVEL SYSTEM DESIGN PROBLEM

1. DESCRIPTION OF EVENT:

Westinghouse has identified a potential system interaction involving the volume control tank (VCT) level control system and the charging pumps.

A postulated failure (failed high) of the VCT level control system, without operator intervention, could lead to a possible loss of suction fluid for the charging pumps.

This is reportable per Tech. Spec. 6.6.2.a (9).

2. ~ PROBABLE CONSEQUENCES arid STATUS of REDUNDANT EQUIPMENT:

The VCT is the normal supply to the charging pumps. The RWST is the alternate and accident supply to the charging pumps. If VCT level. transmitter (LT-115) failed high, letdown* to the VCT would be diverted to the Primary Drain Tank.

The auto~attc mak~ up to the VCT and the automatic transfer to the RWST, on

.. *VCH.. Low*-low level, would not_be funq,ional; Throughout this event, numerous

,set.onda ry *ind i caFons (VCT pressure, charging pressure and f 1ow) and a 1arms would be available to the operator for system evalua~ion. In addition, redundant VCT level indication (Ll-112), located near the VCT, would be available.

Westinghouse has indicated that the operator would have approximately 10 minutes to transfer the charging pump suction from the VCT to the RWST or initiate other appropriate corrective actions to prevent possible damage to the operating charging pump.

The failure of the VCT level control system will not prevent the manual transfer of charging pump suction* to the RWST or the automatic transfer to the RWST during an accident.

Since num~r6us visual and audible indications are available to the operator to permit the termination of this postulated event, the health and safety of the public would not be affected.

3. CAUSE:

The cause . of this.cconcern .appeared to be one of design criteria interpretation.

4. IMMEDIATE CORRECTIVE ACTl'ON:

The operating staff was alerted to this potential problem and the consequences.

ATTACHMENT 1 (continued)

SURRY POWER STATION, UNIT NO.

- DOCKET NO: 50-280 REPORT NO: 81-009-017-0 EVENT DATE: 05-22-81

5. SUBSEQUENT CORRECTIVE ACTION:

A review of station procedures was conducted, and as a result, minor modifi-cations (clarifications) will be made. )n addition, the postulated event, the consequences and the required corrective actions will be included in the operator's training/retraining program.

6. ACTION TAKEN TO PREVENT RECURRENCE:

At this time, none is deemed necessary.

7. GENERIC IMPLICATIONS:

This concern is generic to both Unit No. 1 and 2, therefore, Unit No. 2 procedures will be modified .

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