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| issue date = 03/07/2008
| issue date = 03/07/2008
| title = Summary of Conference Call and Request for Additional Information Regarding the Fall 2006 Steam Generator Inspections
| title = Summary of Conference Call and Request for Additional Information Regarding the Fall 2006 Steam Generator Inspections
| author name = Miller G E
| author name = Miller G
| author affiliation = NRC/NRR/ADRO/DORL/LPLI-2
| author affiliation = NRC/NRR/ADRO/DORL/LPLI-2
| addressee name = St.Pierre G F
| addressee name = St.Pierre G
| addressee affiliation = Florida Power & Light Energy Seabrook, LLC
| addressee affiliation = Florida Power & Light Energy Seabrook, LLC
| docket = 05000443
| docket = 05000443
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=Text=
=Text=
{{#Wiki_filter:March 7, 2008  
{{#Wiki_filter:March 7, 2008 Mr. Gene F. St. Pierre, Site Vice President c/o James M. Peschel Seabrook Station FPL Energy Seabrook, LLC P.O. Box 300 Seabrook, NH 03874
 
Mr. Gene F. St. Pierre, Site Vice President c/o James M. Peschel Seabrook Station FPL Energy Seabrook, LLC P.O. Box 300 Seabrook, NH 03874  


==SUBJECT:==
==SUBJECT:==
Line 26: Line 24:


==SUMMARY==
==SUMMARY==
OF CONFERENCE CALL AND REQUEST FOR ADDITIONAL INFORMATION REGARDING THE FALL 2006 STEAM GENERATOR INSPECTIONS (TAC NO. MD2791)  
OF CONFERENCE CALL AND REQUEST FOR ADDITIONAL INFORMATION REGARDING THE FALL 2006 STEAM GENERATOR INSPECTIONS (TAC NO. MD2791)


==Dear Mr. St. Pierre:==
==Dear Mr. St. Pierre:==


By letters dated October 26, 2006 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML063040324), and May 23, 2007 (ADAMS Accession No.
By letters dated October 26, 2006 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML063040324), and May 23, 2007 (ADAMS Accession No. ML071510197), FPL Energy Seabrook, LLC (FPLE) submitted information summarizing the results of the steam generator (SG) tube inspection activities at Seabrook Station, Unit No. 1 (Seabrook) during the eleventh refueling outage, which took place in October 2006. In addition, on October 17, 2006, FPLE staff participated in a conference call with the Nuclear Regulatory Commission (NRC) staff regarding the stats of the ongoing SG tube inspection activities.
ML071510197), FPL Energy Seabrook, LLC (FPLE) submitted information summarizing the results of the steam generator (SG) tube inspection activities at Seabrook Station, Unit No. 1 (Seabrook) during the eleventh refueling outage, which took place in October 2006. In addition, on October 17, 2006, FPLE staff participated in a conference call with the Nuclear Regulatory Commission (NRC) staff regarding the stats of the ongoing SG tube inspection activities.
A summary of this teleconference is provided in Enclosure 1 to this letter.
A summary of this teleconference is provided in Enclosure 1 to this letter.  
The NRC staff has reviewed the information provided and requests that additional information be submitted for the staff to complete its review. The requested information is identified in to this letter.
 
Sincerely,
The NRC staff has reviewed the information provided and requests that additional information be submitted for the staff to complete its review. The requested information is identified in   to this letter.  
                                              /ra/
 
G. Edward Miller, Project Manager Plant Licensing Branch I-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-443
Sincerely, /ra/
G. Edward Miller, Project Manager Plant Licensing Branch I-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation  
 
Docket No. 50-443  


==Enclosure:==
==Enclosure:==
: 1. Teleconference Summary  
: 1. Teleconference Summary
: 2. Request for Additional Information  
: 2. Request for Additional Information cc w/encls: See next page


cc w/encls:  See next page March 7, 2008 Mr. Gene F. St. Pierre, Site Vice President c/o James M. Peschel Seabrook Station FPL Energy Seabrook, LLC P.O. Box 300 Seabrook, NH 03874  
March 7, 2008 Mr. Gene F. St. Pierre, Site Vice President c/o James M. Peschel Seabrook Station FPL Energy Seabrook, LLC P.O. Box 300 Seabrook, NH 03874


==SUBJECT:==
==SUBJECT:==
Line 51: Line 45:


==SUMMARY==
==SUMMARY==
OF CONFERENCE CALL AND REQUEST FOR ADDITIONAL INFORMATION REGARDING THE FALL 2006 STEAM GENERATOR INSPECTIONS (TAC NO. MD2791)  
OF CONFERENCE CALL AND REQUEST FOR ADDITIONAL INFORMATION REGARDING THE FALL 2006 STEAM GENERATOR INSPECTIONS (TAC NO. MD2791)


==Dear Mr. St. Pierre:==
==Dear Mr. St. Pierre:==


By letters dated October 26, 2006 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML063040324), and May 23, 2007 (ADAMS Accession No.
By letters dated October 26, 2006 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML063040324), and May 23, 2007 (ADAMS Accession No. ML071510197), FPL Energy Seabrook, LLC (FPLE) submitted information summarizing the results of the steam generator (SG) tube inspection activities at Seabrook Station, Unit No. 1 (Seabrook) during the eleventh refueling outage, which took place in October 2006. In addition, on October 17, 2006, FPLE staff participated in a conference call with the Nuclear Regulatory Commission (NRC) staff regarding the stats of the ongoing SG tube inspection activities.
ML071510197), FPL Energy Seabrook, LLC (FPLE) submitted information summarizing the results of the steam generator (SG) tube inspection activities at Seabrook Station, Unit No. 1 (Seabrook) during the eleventh refueling outage, which took place in October 2006. In addition, on October 17, 2006, FPLE staff participated in a conference call with the Nuclear Regulatory Commission (NRC) staff regarding the stats of the ongoing SG tube inspection activities.
A summary of this teleconference is provided in Enclosure 1 to this letter.
A summary of this teleconference is provided in Enclosure 1 to this letter.  
The NRC staff has reviewed the information provided and requests that additional information be submitted for the staff to complete its review. The requested information is identified in to this letter.
 
Sincerely,
The NRC staff has reviewed the information provided and requests that additional information be submitted for the staff to complete its review. The requested information is identified in   to this letter.  
                                                  /ra/
 
G. Edward Miller, Project Manager Plant Licensing Branch I-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-443
Sincerely,       /ra/ G. Edward Miller, Project Manager Plant Licensing Branch I-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation  
 
Docket No. 50-443  


==Enclosure:==
==Enclosure:==
: 1. Teleconference Summary  
: 1. Teleconference Summary
: 2. Request for Additional Information  
: 2. Request for Additional Information cc w/encls: See next page DISTRIBUTION RidsNRRLpl1-2   RidsOgcMailCenter       RidsRgn1MailCenter PUBLIC         RidsNrrRMGMiller         RidsAcrsAcnwMailCenter LPL1-2R/F       RidsNrrLAABaxter RidsNrrDorl     ABurrit, RI ADAMS Accession NO: ML073532041 OFFICE LPL1-2/PM LPL1-2/LA         DCI/CSGB/BC       LPL1-2/BC NAME     GEMiller     ABaxter     AHiser           HChernoff DATE     2/26/08     2/22/08     2/20/08           3/7/08 Official Record Copy
 
cc w/encls: See next page  
 
DISTRIBUTION RidsNRRLpl1-2 RidsOgcMailCenter RidsRgn1MailCenter PUBLIC RidsNrrRMGMiller RidsAcrsAcnwMailCenter   LPL1-2R/F RidsNrrLAABaxter RidsNrrDorl ABurrit, RI
 
ADAMS Accession NO: ML073532041 OFFICE LPL1-2/PM LPL1-2/LA DCI/CSGB/BC LPL1-2/BC NAME GEMiller ABaxter AHiser HChernoff
 
DATE 2/26/08 2/22/08 2/20/08 3/7/08 Official Record Copy Seabrook Station, Unit No. 1
 
cc:
 
Mr. J. A. Stall Senior Vice President, Nuclear and Chief Nuclear Officer Florida Power & Light Company P.O. Box 14000 Juno Beach, FL  33408-0420
 
Mr. Peter Brann Assistant Attorney General State House, Station #6 Augusta, ME  04333
 
Resident Inspector U.S. Nuclear Regulatory Commission Seabrook Nuclear Power Station P.O. Box 1149 Seabrook, NH  03874
 
Town of Exeter 10 Front Street Exeter, NH  03823
 
Regional Administrator, Region I U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA  19406
 
Office of the Attorney General One Ashburton Place, 20th Floor Boston, MA  02108
 
Board of Selectmen Town of Amesbury Town Hall Amesbury, MA  01913
 
Mr. Robert Poole Federal Emergency Management Agency Region I 99 High Street, 6 th Floor Boston, MA  02110
 
Mr. Tom Crimmins Polestar Applied Technology One First Street, Suite 4 Los Altos, CA  94019 John Giarrusso Massachusetts Emergency Management Agency 400 Worcester Road Framingham, MA  01702-5399
 
Ms. Kelly Ayotte, Attorney General Mr. Orvil Fitch, Deputy Attorney General 33 Capitol Street Concord, NH  03301
 
Mr. Christopher M. Pope, Director Homeland Security & Emergency Mgmt.
New Hampshire Department of Safety Bureau of Emergency Management 33 Hazen Drive Concord, NH  03301
 
Mr. M. S. Ross, Managing Attorney Florida Power & Light Company P.O. Box 14000 Juno Beach, FL  33408-0420
 
Mr. Rajiv S. Kundalkar Vice President - Nuclear Technical Services Florida Power & Light Company P.O. Box 14000 Juno Beach, FL  33408-0420
 
James M. Peschel Regulatory Programs Manager FPL Energy Seabrook, LLC PO Box 300 Seabrook, NH  03874
 
Ms. Marjan Mashhadi Senior Attorney Florida Power & Light Company 801 Pennsylvania Ave., NW Suite 220 Washington, DC  20004
 
Seabrook Station, Unit No. 1
 
cc:
 
Mr. Mark E. Warner Vice President, Nuclear Operations, North Region (Seabrook & Duane Arnold Plants)
Florida Power & Light Company P.O. Box 14000 Juno Beach, FL  33408-0420


Mr. Joseph Roy Director of Operations Massachusetts Municipal Wholesale Electric Company Moody Street Ludlow, MA 01056 Mr. Don E. Grissette Vice President, Nuclear Training and Performance Improvement Florida Power & Light Company P.O. Box 14000 Juno Beach, FL 3340
Seabrook Station, Unit No. 1 cc:
Mr. J. A. Stall Senior Vice President, Nuclear and  John Giarrusso Chief Nuclear Officer              Massachusetts Emergency Management Agency Florida Power & Light Company      400 Worcester Road P.O. Box 14000                      Framingham, MA 01702-5399 Juno Beach, FL 33408-0420 Ms. Kelly Ayotte, Attorney General Mr. Peter Brann                    Mr. Orvil Fitch, Deputy Attorney General Assistant Attorney General          33 Capitol Street State House, Station #6            Concord, NH 03301 Augusta, ME 04333 Mr. Christopher M. Pope, Director Resident Inspector                  Homeland Security & Emergency Mgmt.
U.S. Nuclear Regulatory Commission  New Hampshire Department of Safety Seabrook Nuclear Power Station      Bureau of Emergency Management P.O. Box 1149                      33 Hazen Drive Seabrook, NH 03874                  Concord, NH 03301 Town of Exeter                      Mr. M. S. Ross, Managing Attorney 10 Front Street                    Florida Power & Light Company Exeter, NH 03823                    P.O. Box 14000 Juno Beach, FL 33408-0420 Regional Administrator, Region I U.S. Nuclear Regulatory Commission  Mr. Rajiv S. Kundalkar 475 Allendale Road                  Vice President - Nuclear Technical Services King of Prussia, PA 19406          Florida Power & Light Company P.O. Box 14000 Office of the Attorney General      Juno Beach, FL 33408-0420 One Ashburton Place, 20th Floor Boston, MA 02108                    James M. Peschel Regulatory Programs Manager Board of Selectmen                  FPL Energy Seabrook, LLC Town of Amesbury                    PO Box 300 Town Hall                          Seabrook, NH 03874 Amesbury, MA 01913 Ms. Marjan Mashhadi Mr. Robert Poole                    Senior Attorney Federal Emergency Management Agency Florida Power & Light Company Region I                            801 Pennsylvania Ave., NW Suite 220 99 High Street, 6th Floor          Washington, DC 20004 Boston, MA 02110 Mr. Tom Crimmins Polestar Applied Technology One First Street, Suite 4 Los Altos, CA 94019


Mr. Michael W. Kiley Plant General Manager FPL Energy Seabrook, LLC P.O. Box 300 Seabrook, NH 03874 Enclosure 1
Seabrook Station, Unit No. 1 cc:
Mr. Mark E. Warner Vice President, Nuclear Operations, Mr. Don E. Grissette North Region                        Vice President, Nuclear Training and (Seabrook & Duane Arnold Plants)    Performance Improvement Florida Power & Light Company      Florida Power & Light Company P.O. Box 14000                      P.O. Box 14000 Juno Beach, FL 33408-0420          Juno Beach, FL 3340 Mr. Joseph Roy                      Mr. Michael W. Kiley Director of Operations              Plant General Manager Massachusetts Municipal            FPL Energy Seabrook, LLC Wholesale Electric Company          P.O. Box 300 Moody Street                        Seabrook, NH 03874 Ludlow, MA 01056


==SUMMARY==
==SUMMARY==
OF OCTOBER 17, 2006, TELECONFERENCE
OF OCTOBER 17, 2006, TELECONFERENCE RELATED TO STEAM GENERATOR INSPECTIONS PERFORMED DURING THE ELEVENTH REFUELING OUTAGE FPL ENERGY SEABROOK, LLC SEABROOK STATION, UNIT NO. 1 DOCKET NO. 50-443 On October 17, 2006, FPL Energy Seabrook, LLC (FPLE) staff participated in a conference call with the Nuclear Regulatory Commission (NRC) staff regarding the, at the time, ongoing steam generator (SG) tube inspection activities at Seabrook Station, Unit No. 1 (Seabrook) during the eleventh refueling outage (OR11).
 
During this call, FPLE reported that there was no primary to secondary leakage during the previous operating cycle and that there would be no secondary-side pressure tests performed during OR11. FPLE reported that one exception was taken to the Electric Power Research Institute (EPRI) Pressurized Water Reactor SG Examination Guidelines, Revision 6. It is important to note that the guidelines do not constitute NRC requirements, but are documented here for completeness.
RELATED TO STEAM GENERATOR INSPECTIONS PERFORMED DURING THE ELEVENTH REFUELING OUTAGE
The exception taken was that examination of SG tubing was not performed fully, in accordance with EPRI SG Examination Guidelines, Section 3.3.10. Section 3.3.10 states, in part, that if an active damage mechanism associated with cracking is present and a critical area cannot be defined, all tubing, full length, shall be examined. Additionally, the area must be inspected every fuel cycle. FPLE indicated that the cracking reported during previous outages was repaired and that they have not found any signs of further cracking. Based on its root cause assessment, FPLE believes that all tubes potentially susceptible to the previously observed cracking mechanism have been plugged. Therefore, FPLE will return to the normal schedule of examining the SG every other refueling outage (RFO) as opposed to every RFO.
 
This exception was consistent with the requirements contained in a proposed Technical Specification (TS) change that was under NRC staff review at the time of the inspection. This amendment to the TSs was approved on March 28, 2007 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML070510629).
FPL ENERGY SEABROOK, LLC
 
SEABROOK STATION, UNIT NO. 1
 
DOCKET NO. 50-443
 
On October 17, 2006, FPL Energy Seabrook, LLC (FPLE) staff participated in a conference call with the Nuclear Regulatory Commission (NRC) staff regarding the, at the time, ongoing steam generator (SG) tube inspection activities at Seabrook Station, Unit No. 1 (Seabrook) during the eleventh refueling outage (OR11).  
 
During this call, FPLE reported that there was no primary to secondary leakage during the previous operating cycle and that there would be no secondary-side pressure tests performed during OR11. FPLE reported that one exception was taken to the Electric Power Research Institute (EPRI) Pressurized Water Reactor SG Examination Guidelines, Revision 6. It is important to note that the guidelines do not constitute NRC requirements, but are documented here for completeness.  
 
The exception taken was that examination of SG tubing was not performed fully, in accordance with EPRI SG Examination Guidelines, Section 3.3.10. Section 3.3.10 states, in part, that if an active damage mechanism associated with cracking is present and a critical area cannot be defined, all tubing, full length, shall be examined. Additionally, the area must be inspected every fuel cycle. FPLE indicated that the cracking reported during previous outages was repaired and that they have not found any signs of further cracking. Based on its root cause assessment, FPLE believes that all tubes potentially susceptible to the previously observed cracking mechanism have been plugged. Therefore, FPLE will return to the normal schedule of examining the SG every other refueling outage (RFO) as opposed to every RFO.  
 
This exception was consistent with the requirements contained in a proposed Technical Specification (TS) change that was under NRC staff review at the time of the inspection. This amendment to the TSs was approved on March 28, 2007 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML070510629).  
 
The Seabrook inspection scope consisted of the following:
The Seabrook inspection scope consisted of the following:
* 100 percent of the inservice tubes were inspected full length with a bobbin coil;
* 100 percent of the inservice tubes were inspected full length with a bobbin coil;
* 30 percent of the Row 1 and 2 tubes were inspected in the U-bend region with a rotating probe;
* 30 percent of the Row 1 and 2 tubes were inspected in the U-bend region with a rotating probe;
* 30 percent of the tubes were inspected using a rotating probe from 3-inches above to 3-inches below the top of the hot-leg tube-sheet;
* 30 percent of the tubes were inspected using a rotating probe from 3-inches above to 3-inches below the top of the hot-leg tube-sheet;
* 30 percent of the dents and dings greater than 5 volts were inspected using a rotating probe;
* 30 percent of the dents and dings greater than 5 volts were inspected using a rotating probe; Enclosure 1
* 50 percent of the bulges and over-expansions in the top 17-inches of the tube-sheet on the hot-leg side of the SG were inspected using a rotating probe;
* 50 percent of the bulges and over-expansions in the top 17-inches of the tube-sheet on the hot-leg side of the SG were inspected using a rotating probe;
* 100 percent of the I-codes were inspected using a rotating probe;
* 100 percent of the I-codes were inspected using a rotating probe;
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* Visual inspections were performed on all mechanical weld plugs;
* Visual inspections were performed on all mechanical weld plugs;
* Visual inspections were performed to confirm loose parts; and
* Visual inspections were performed to confirm loose parts; and
* Foreign object search and retrieval was performed in the tube bundle to shell annulus and the open tube lane.  
* Foreign object search and retrieval was performed in the tube bundle to shell annulus and the open tube lane.
 
At the time of the call, SGs C and D were reported to have three anti-vibration bar wear indications exceeding the plugging limit of 40 percent through-wall. FPLE indicated that these wear indications were 41 to 44 percent through-wall, and that these tubes would be plugged.
At the time of the call, SGs C and D were reported to have three anti-vibration bar wear indications exceeding the plugging limit of 40 percent through-wall. FPLE indicated that these wear indications were 41 to 44 percent through-wall, and that these tubes would be plugged.
Additionally, no indications were identified at the top or in the tube-sheet.  
Additionally, no indications were identified at the top or in the tube-sheet.
 
At the time of the call, FPLE stated that there were no plans for in-situ pressure testing or for tube pulls.
At the time of the call, FPLE stated that there were no plans for in-situ pressure testing or for tube pulls.  
 
With regard to loose parts, FPLE reported the following:
With regard to loose parts, FPLE reported the following:
* In SG A, a 0.25 inch by 0.12 inch hard piece of socket screw was found and removed;
* In SG A, a 0.25 inch by 0.12 inch hard piece of socket screw was found and removed;
* A twisted piece of wire and a thin piece of metal were found and removed from SG B;
* A twisted piece of wire and a thin piece of metal were found and removed from SG B;
* In SG C, a dumbbell-shaped foreign object was located between two tubes. The object was reported to have been present since the first RFO, and is bounded by plugged tubes; and
* In SG C, a dumbbell-shaped foreign object was located between two tubes. The object was reported to have been present since the first RFO, and is bounded by plugged tubes; and
* No loose parts were found in SG D.  
* No loose parts were found in SG D.
 
At the time of the call, FPLE reported two distorted support indications (DSIs) above the baffle plate using the bobbin probe. The DSIs were further inspected using a +PointTM probe and were discovered to be two PLPs with some apparent wall loss. As a result of the two PLPs, additional inspections of neighboring tubes were performed at the same axial elevation where the original PLPs were identified. These additional inspections resulted in identifying five additional PLPs.
At the time of the call, FPLE reported two distorted support indications (DSIs) above the baffle plate using the bobbin probe. The DSIs were further inspected using a +Point TM probe and were discovered to be two PLPs with some apparent wall loss. As a result of the two PLPs, additional inspections of neighboring tubes were performed at the same axial elevation where the original PLPs were identified. These additional inspections resulted in identifying five additional PLPs.
FPLE plugged a 16 tube zone bounding the location of the 7 PLPs. No indications were present at these locations during the previous outage. FPLE reported that it is difficult to perform a visual inspection of the location where the 7 PLPs were found.
FPLE plugged a 16 tube zone bounding the location of the 7 PLPs. No indications were present at these locations during the previous outage. FPLE reported that it is difficult to perform a visual inspection of the location where the 7 PLPs were found.  
While inspecting SG D, FPLE identified a DSI with a bobbin probe just below a support plate on the cold-leg side. The DSI was further inspected using a +PointTM coil. The +PointTM inspection of the location revealed a volumetric indication of 40 percent through-wall loss. FPLE stated that this tube would be plugged. In addition, inspections of the adjacent tubes using a +PointTM coil were performed yielding no indications, including no indications of loose parts.
 
While inspecting SG D, FPLE identified a DSI with a bobbin probe just below a support plate on the cold-leg side. The DSI was further inspected using a +Point TM coil. The +Point TM inspection of the location revealed a volumetric indication of 40 percent through-wall loss. FPLE stated that this tube would be plugged. In addition, inspections of the adjacent tubes using a +Point TM coil were performed yielding no indications, including no indications of loose parts.
Enclosure 2 REQUEST FOR ADDITIONAL INFORMATION
 
RELATED TO STEAM GENERATOR INSPECTIONS PERFORMED DURING THE ELEVENTH REFUELING OUTAGE
 
FPL ENERGY SEABROOK, LLC
 
SEABROOK STATION, UNIT NO. 1
 
DOCKET NO. 50-443


By letters dated October 26, 2006 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML063040324), and May 23, 2007 (ADAMS Accession No.
REQUEST FOR ADDITIONAL INFORMATION RELATED TO STEAM GENERATOR INSPECTIONS PERFORMED DURING THE ELEVENTH REFUELING OUTAGE FPL ENERGY SEABROOK, LLC SEABROOK STATION, UNIT NO. 1 DOCKET NO. 50-443 By letters dated October 26, 2006 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML063040324), and May 23, 2007 (ADAMS Accession No. ML071510197), FPL Energy Seabrook, LLC (FPLE) submitted information summarizing the results of the steam generator (SG) tube inspections performed in October 2006, during the eleventh refueling outage (OR11). The Nuclear Regulatory Commission (NRC) staff has reviewed the information provided and requests that the following additional information be submitted for the staff to complete its review:
ML071510197), FPL Energy Seabrook, LLC (FPLE) submitted information summarizing the results of the steam generator (SG) tube inspections performed in October 2006, during the eleventh refueling outage (OR11). The Nuclear Regulatory Commission (NRC) staff has reviewed the information provided and requests that the following additional information be submitted for the staff to complete its review:  
: 1. For each refueling outage or SG inspection outage, since the beginning of the second inspection interval, please provide the cumulative effective full power months (or years) of operation that the SGs had accumulated at the time of the outage.
: 1. For each refueling outage or SG inspection outage, since the beginning of the second inspection interval, please provide the cumulative effective full power months (or years) of operation that the SGs had accumulated at the time of the outage. 2. In the May 23, 2007, letter, Table 1 identifies SG B, tube R27C97 (Row 27, Column 97) as having been plugged in OR11 due to potentially elevated residual stress. In previous letters dated October 12, 2004 (ADAMS Accession No. ML042940501), and October 26, 2006, you indicated SG B, tube R29C97 as having potentially elevated residual stress that would result in plugging in OR11. Please clarify which tube was plugged and which tube had the elevated residual stress. 3. Please provide the scope and results of any secondary side inspections (including foreign object search and retrieval) performed during OR11. 4. With respect to the inspections performed in the u-bend region of the tubes in rows one and two, and at dings and dents whose voltage exceeds five volts, please discuss whether 50 percent of these locations have been inspected since the start of the 90 effective full power month period. 5. Regarding the tubes in SG C with foreign object wear and the surrounding tubes, please identify those which were plugged and also stabilized. If plugged and not stabilized, discuss how the condition of these tubes will be monitored or why no monitoring is necessary. 6. The May 23, 2007, submittal does not appear to provide the location and percentage of wall thickness for all indications of an imperfection. Specifically, it appears that this information is not provided for wear at the anti-vibration bars and wear at the flow distribution baffle (FDB). Please provide this information for all imperfections.       7. You indicated that two tubes in SG C with possible loose part (PLP) signals could not be accessed for removal of the foreign object. Since both of these tubes are in the periphery of the tube bundle, please discuss the location of the indications and the challenges in removing any PLPs at these locations. 8. Please discuss how pressure pulse cleaning caused indications at the FDB. In addition, discuss the purpose of the pressure pulse cleaning.}}
: 2. In the May 23, 2007, letter, Table 1 identifies SG B, tube R27C97 (Row 27, Column 97) as having been plugged in OR11 due to potentially elevated residual stress. In previous letters dated October 12, 2004 (ADAMS Accession No. ML042940501), and October 26, 2006, you indicated SG B, tube R29C97 as having potentially elevated residual stress that would result in plugging in OR11. Please clarify which tube was plugged and which tube had the elevated residual stress.
: 3. Please provide the scope and results of any secondary side inspections (including foreign object search and retrieval) performed during OR11.
: 4. With respect to the inspections performed in the u-bend region of the tubes in rows one and two, and at dings and dents whose voltage exceeds five volts, please discuss whether 50 percent of these locations have been inspected since the start of the 90 effective full power month period.
: 5. Regarding the tubes in SG C with foreign object wear and the surrounding tubes, please identify those which were plugged and also stabilized. If plugged and not stabilized, discuss how the condition of these tubes will be monitored or why no monitoring is necessary.
: 6. The May 23, 2007, submittal does not appear to provide the location and percentage of wall thickness for all indications of an imperfection. Specifically, it appears that this information is not provided for wear at the anti-vibration bars and wear at the flow distribution baffle (FDB). Please provide this information for all imperfections.
Enclosure 2
: 7. You indicated that two tubes in SG C with possible loose part (PLP) signals could not be accessed for removal of the foreign object. Since both of these tubes are in the periphery of the tube bundle, please discuss the location of the indications and the challenges in removing any PLPs at these locations.
: 8. Please discuss how pressure pulse cleaning caused indications at the FDB. In addition, discuss the purpose of the pressure pulse cleaning.}}

Latest revision as of 08:21, 13 March 2020

Summary of Conference Call and Request for Additional Information Regarding the Fall 2006 Steam Generator Inspections
ML073532041
Person / Time
Site: Seabrook NextEra Energy icon.png
Issue date: 03/07/2008
From: Geoffrey Miller
NRC/NRR/ADRO/DORL/LPLI-2
To: St.Pierre G
Florida Power & Light Energy Seabrook
Miller G, NRR/DORL, 415-2481
References
TAC MD2791
Download: ML073532041 (8)


Text

March 7, 2008 Mr. Gene F. St. Pierre, Site Vice President c/o James M. Peschel Seabrook Station FPL Energy Seabrook, LLC P.O. Box 300 Seabrook, NH 03874

SUBJECT:

SEABROOK STATION, UNIT NO. 1 -

SUMMARY

OF CONFERENCE CALL AND REQUEST FOR ADDITIONAL INFORMATION REGARDING THE FALL 2006 STEAM GENERATOR INSPECTIONS (TAC NO. MD2791)

Dear Mr. St. Pierre:

By letters dated October 26, 2006 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML063040324), and May 23, 2007 (ADAMS Accession No. ML071510197), FPL Energy Seabrook, LLC (FPLE) submitted information summarizing the results of the steam generator (SG) tube inspection activities at Seabrook Station, Unit No. 1 (Seabrook) during the eleventh refueling outage, which took place in October 2006. In addition, on October 17, 2006, FPLE staff participated in a conference call with the Nuclear Regulatory Commission (NRC) staff regarding the stats of the ongoing SG tube inspection activities.

A summary of this teleconference is provided in Enclosure 1 to this letter.

The NRC staff has reviewed the information provided and requests that additional information be submitted for the staff to complete its review. The requested information is identified in to this letter.

Sincerely,

/ra/

G. Edward Miller, Project Manager Plant Licensing Branch I-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-443

Enclosure:

1. Teleconference Summary
2. Request for Additional Information cc w/encls: See next page

March 7, 2008 Mr. Gene F. St. Pierre, Site Vice President c/o James M. Peschel Seabrook Station FPL Energy Seabrook, LLC P.O. Box 300 Seabrook, NH 03874

SUBJECT:

SEABROOK STATION, UNIT NO. 1 -

SUMMARY

OF CONFERENCE CALL AND REQUEST FOR ADDITIONAL INFORMATION REGARDING THE FALL 2006 STEAM GENERATOR INSPECTIONS (TAC NO. MD2791)

Dear Mr. St. Pierre:

By letters dated October 26, 2006 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML063040324), and May 23, 2007 (ADAMS Accession No. ML071510197), FPL Energy Seabrook, LLC (FPLE) submitted information summarizing the results of the steam generator (SG) tube inspection activities at Seabrook Station, Unit No. 1 (Seabrook) during the eleventh refueling outage, which took place in October 2006. In addition, on October 17, 2006, FPLE staff participated in a conference call with the Nuclear Regulatory Commission (NRC) staff regarding the stats of the ongoing SG tube inspection activities.

A summary of this teleconference is provided in Enclosure 1 to this letter.

The NRC staff has reviewed the information provided and requests that additional information be submitted for the staff to complete its review. The requested information is identified in to this letter.

Sincerely,

/ra/

G. Edward Miller, Project Manager Plant Licensing Branch I-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-443

Enclosure:

1. Teleconference Summary
2. Request for Additional Information cc w/encls: See next page DISTRIBUTION RidsNRRLpl1-2 RidsOgcMailCenter RidsRgn1MailCenter PUBLIC RidsNrrRMGMiller RidsAcrsAcnwMailCenter LPL1-2R/F RidsNrrLAABaxter RidsNrrDorl ABurrit, RI ADAMS Accession NO: ML073532041 OFFICE LPL1-2/PM LPL1-2/LA DCI/CSGB/BC LPL1-2/BC NAME GEMiller ABaxter AHiser HChernoff DATE 2/26/08 2/22/08 2/20/08 3/7/08 Official Record Copy

Seabrook Station, Unit No. 1 cc:

Mr. J. A. Stall Senior Vice President, Nuclear and John Giarrusso Chief Nuclear Officer Massachusetts Emergency Management Agency Florida Power & Light Company 400 Worcester Road P.O. Box 14000 Framingham, MA 01702-5399 Juno Beach, FL 33408-0420 Ms. Kelly Ayotte, Attorney General Mr. Peter Brann Mr. Orvil Fitch, Deputy Attorney General Assistant Attorney General 33 Capitol Street State House, Station #6 Concord, NH 03301 Augusta, ME 04333 Mr. Christopher M. Pope, Director Resident Inspector Homeland Security & Emergency Mgmt.

U.S. Nuclear Regulatory Commission New Hampshire Department of Safety Seabrook Nuclear Power Station Bureau of Emergency Management P.O. Box 1149 33 Hazen Drive Seabrook, NH 03874 Concord, NH 03301 Town of Exeter Mr. M. S. Ross, Managing Attorney 10 Front Street Florida Power & Light Company Exeter, NH 03823 P.O. Box 14000 Juno Beach, FL 33408-0420 Regional Administrator, Region I U.S. Nuclear Regulatory Commission Mr. Rajiv S. Kundalkar 475 Allendale Road Vice President - Nuclear Technical Services King of Prussia, PA 19406 Florida Power & Light Company P.O. Box 14000 Office of the Attorney General Juno Beach, FL 33408-0420 One Ashburton Place, 20th Floor Boston, MA 02108 James M. Peschel Regulatory Programs Manager Board of Selectmen FPL Energy Seabrook, LLC Town of Amesbury PO Box 300 Town Hall Seabrook, NH 03874 Amesbury, MA 01913 Ms. Marjan Mashhadi Mr. Robert Poole Senior Attorney Federal Emergency Management Agency Florida Power & Light Company Region I 801 Pennsylvania Ave., NW Suite 220 99 High Street, 6th Floor Washington, DC 20004 Boston, MA 02110 Mr. Tom Crimmins Polestar Applied Technology One First Street, Suite 4 Los Altos, CA 94019

Seabrook Station, Unit No. 1 cc:

Mr. Mark E. Warner Vice President, Nuclear Operations, Mr. Don E. Grissette North Region Vice President, Nuclear Training and (Seabrook & Duane Arnold Plants) Performance Improvement Florida Power & Light Company Florida Power & Light Company P.O. Box 14000 P.O. Box 14000 Juno Beach, FL 33408-0420 Juno Beach, FL 3340 Mr. Joseph Roy Mr. Michael W. Kiley Director of Operations Plant General Manager Massachusetts Municipal FPL Energy Seabrook, LLC Wholesale Electric Company P.O. Box 300 Moody Street Seabrook, NH 03874 Ludlow, MA 01056

SUMMARY

OF OCTOBER 17, 2006, TELECONFERENCE RELATED TO STEAM GENERATOR INSPECTIONS PERFORMED DURING THE ELEVENTH REFUELING OUTAGE FPL ENERGY SEABROOK, LLC SEABROOK STATION, UNIT NO. 1 DOCKET NO. 50-443 On October 17, 2006, FPL Energy Seabrook, LLC (FPLE) staff participated in a conference call with the Nuclear Regulatory Commission (NRC) staff regarding the, at the time, ongoing steam generator (SG) tube inspection activities at Seabrook Station, Unit No. 1 (Seabrook) during the eleventh refueling outage (OR11).

During this call, FPLE reported that there was no primary to secondary leakage during the previous operating cycle and that there would be no secondary-side pressure tests performed during OR11. FPLE reported that one exception was taken to the Electric Power Research Institute (EPRI) Pressurized Water Reactor SG Examination Guidelines, Revision 6. It is important to note that the guidelines do not constitute NRC requirements, but are documented here for completeness.

The exception taken was that examination of SG tubing was not performed fully, in accordance with EPRI SG Examination Guidelines, Section 3.3.10. Section 3.3.10 states, in part, that if an active damage mechanism associated with cracking is present and a critical area cannot be defined, all tubing, full length, shall be examined. Additionally, the area must be inspected every fuel cycle. FPLE indicated that the cracking reported during previous outages was repaired and that they have not found any signs of further cracking. Based on its root cause assessment, FPLE believes that all tubes potentially susceptible to the previously observed cracking mechanism have been plugged. Therefore, FPLE will return to the normal schedule of examining the SG every other refueling outage (RFO) as opposed to every RFO.

This exception was consistent with the requirements contained in a proposed Technical Specification (TS) change that was under NRC staff review at the time of the inspection. This amendment to the TSs was approved on March 28, 2007 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML070510629).

The Seabrook inspection scope consisted of the following:

  • 100 percent of the inservice tubes were inspected full length with a bobbin coil;
  • 30 percent of the Row 1 and 2 tubes were inspected in the U-bend region with a rotating probe;
  • 30 percent of the tubes were inspected using a rotating probe from 3-inches above to 3-inches below the top of the hot-leg tube-sheet;
  • 30 percent of the dents and dings greater than 5 volts were inspected using a rotating probe; Enclosure 1
  • 50 percent of the bulges and over-expansions in the top 17-inches of the tube-sheet on the hot-leg side of the SG were inspected using a rotating probe;
  • 100 percent of the I-codes were inspected using a rotating probe;
  • Tubes immediately surrounding tubes with possible loose part (PLP) indications were inspected;
  • Visual inspections were performed on all mechanical weld plugs;
  • Visual inspections were performed to confirm loose parts; and
  • Foreign object search and retrieval was performed in the tube bundle to shell annulus and the open tube lane.

At the time of the call, SGs C and D were reported to have three anti-vibration bar wear indications exceeding the plugging limit of 40 percent through-wall. FPLE indicated that these wear indications were 41 to 44 percent through-wall, and that these tubes would be plugged.

Additionally, no indications were identified at the top or in the tube-sheet.

At the time of the call, FPLE stated that there were no plans for in-situ pressure testing or for tube pulls.

With regard to loose parts, FPLE reported the following:

  • In SG A, a 0.25 inch by 0.12 inch hard piece of socket screw was found and removed;
  • A twisted piece of wire and a thin piece of metal were found and removed from SG B;
  • In SG C, a dumbbell-shaped foreign object was located between two tubes. The object was reported to have been present since the first RFO, and is bounded by plugged tubes; and
  • No loose parts were found in SG D.

At the time of the call, FPLE reported two distorted support indications (DSIs) above the baffle plate using the bobbin probe. The DSIs were further inspected using a +PointTM probe and were discovered to be two PLPs with some apparent wall loss. As a result of the two PLPs, additional inspections of neighboring tubes were performed at the same axial elevation where the original PLPs were identified. These additional inspections resulted in identifying five additional PLPs.

FPLE plugged a 16 tube zone bounding the location of the 7 PLPs. No indications were present at these locations during the previous outage. FPLE reported that it is difficult to perform a visual inspection of the location where the 7 PLPs were found.

While inspecting SG D, FPLE identified a DSI with a bobbin probe just below a support plate on the cold-leg side. The DSI was further inspected using a +PointTM coil. The +PointTM inspection of the location revealed a volumetric indication of 40 percent through-wall loss. FPLE stated that this tube would be plugged. In addition, inspections of the adjacent tubes using a +PointTM coil were performed yielding no indications, including no indications of loose parts.

REQUEST FOR ADDITIONAL INFORMATION RELATED TO STEAM GENERATOR INSPECTIONS PERFORMED DURING THE ELEVENTH REFUELING OUTAGE FPL ENERGY SEABROOK, LLC SEABROOK STATION, UNIT NO. 1 DOCKET NO. 50-443 By letters dated October 26, 2006 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML063040324), and May 23, 2007 (ADAMS Accession No. ML071510197), FPL Energy Seabrook, LLC (FPLE) submitted information summarizing the results of the steam generator (SG) tube inspections performed in October 2006, during the eleventh refueling outage (OR11). The Nuclear Regulatory Commission (NRC) staff has reviewed the information provided and requests that the following additional information be submitted for the staff to complete its review:

1. For each refueling outage or SG inspection outage, since the beginning of the second inspection interval, please provide the cumulative effective full power months (or years) of operation that the SGs had accumulated at the time of the outage.
2. In the May 23, 2007, letter, Table 1 identifies SG B, tube R27C97 (Row 27, Column 97) as having been plugged in OR11 due to potentially elevated residual stress. In previous letters dated October 12, 2004 (ADAMS Accession No. ML042940501), and October 26, 2006, you indicated SG B, tube R29C97 as having potentially elevated residual stress that would result in plugging in OR11. Please clarify which tube was plugged and which tube had the elevated residual stress.
3. Please provide the scope and results of any secondary side inspections (including foreign object search and retrieval) performed during OR11.
4. With respect to the inspections performed in the u-bend region of the tubes in rows one and two, and at dings and dents whose voltage exceeds five volts, please discuss whether 50 percent of these locations have been inspected since the start of the 90 effective full power month period.
5. Regarding the tubes in SG C with foreign object wear and the surrounding tubes, please identify those which were plugged and also stabilized. If plugged and not stabilized, discuss how the condition of these tubes will be monitored or why no monitoring is necessary.
6. The May 23, 2007, submittal does not appear to provide the location and percentage of wall thickness for all indications of an imperfection. Specifically, it appears that this information is not provided for wear at the anti-vibration bars and wear at the flow distribution baffle (FDB). Please provide this information for all imperfections.

Enclosure 2

7. You indicated that two tubes in SG C with possible loose part (PLP) signals could not be accessed for removal of the foreign object. Since both of these tubes are in the periphery of the tube bundle, please discuss the location of the indications and the challenges in removing any PLPs at these locations.
8. Please discuss how pressure pulse cleaning caused indications at the FDB. In addition, discuss the purpose of the pressure pulse cleaning.