ML14058A033: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
 
(Created page by program invented by StriderTol)
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:V pOconee Nuclear Station ExternalFlood Protection ConcernMay 5, 2009 presentation to theLessons Learned Oversight BoardJeff CircleDivision of Risk Assessment Office of Nuclear Reactor Regulation dcial Use 0 -SecuU ..R "ltenfor t
{{#Wiki_filter:V p Oconee Nuclear Station External Flood Protection Concern May 5, 2009 presentation to the Lessons Learned Oversight Board Jeff Circle Division of Risk Assessment Office of Nuclear Reactor Regulation dcial Use 0 -Secu U ..R "ltenfor t Background of Issue NRC initiated the Systematic Evaluation Program (SEP) in 1977 to review the design of older, operating nuclear power plants with the current Standard Review Plan (SRP).-Opened Generic Safety Issue GSI-156.1.2, "Dam Integrity and Site Flooding".
Background of IssueNRC initiated the Systematic Evaluation Program (SEP) in 1977 to review the designof older, operating nuclear power plants withthe current Standard Review Plan (SRP).-Opened Generic Safety Issue GSI-156.1.2, "DamIntegrity and Site Flooding".
-Oconee Nuclear Station (ONS) was identified as one such plant with flooding vulnerability.
-Oconee Nuclear Station (ONS) was identified asone such plant with flooding vulnerability.
-GSI-156 scheduled to be closed out by licensees in the Generic Letter 88-20, Supplement 4, the Individual Plant Examination of External Events (IPEEE) program.USNRC 2-Rd I nm.t.
-GSI-156 scheduled to be closed out by licensees in the Generic Letter 88-20, Supplement 4, theIndividual Plant Examination of External Events(IPEEE) program.USNRC 2-Rd I nm.t.
and Oconee Nuclear Station Three-unit site with unique flooding vulnerability.
and Oconee Nuclear StationThree-unit site with unique flooding vulnerability.
-On Lake Keowee near Seneca, SC-No emergency diesel generators
-On Lake Keowee near Seneca, SC-No emergency diesel generators
-Reliance of 2-unit Keowee Dam as sole source emergency ac power-Site is downstream of Jocassee Dam, A 385-ft high pumped storage hydro-station holding back LakeJocassee-Licensee constructed the Standby Shutdown Facility (SSF)on site to address several issues including flooding, Houses equipment to safely shut down all 3 units in the eventof catastrophic flood to Mode 3* Licensee constructed 5-ft walls around entrances to addressexternal flooding vulnerability.
-Reliance of 2-unit Keowee Dam as sole source emergency ac power-Site is downstream of Jocassee Dam , A 385-ft high pumped storage hydro-station holding back Lake Jocassee-Licensee constructed the Standby Shutdown Facility (SSF)on site to address several issues including flooding , Houses equipment to safely shut down all 3 units in the event of catastrophic flood to Mode 3* Licensee constructed 5-ft walls around entrances to address external flooding vulnerability., Licensees extended these walls to 7.5-ft in February 2009.OiNRCial Use Y -SeTY- 3 Prolkif Ptople aa at h .rIm ,ommne Flooding* Licensee performed an ONS inundation study in 1992-Required by Federal Energy Regulatory Commission (FERC) Emergency Action Plan (EAP) on Jocassee license to Duke Hydro-Only reproducible calculation on record., Inundation levels calculated ranged from 12.5 to 16.8 feet , NRC service water inspection in 1994 identified potential deficiency in the 5-ft entrance wall height to that of the inundation study.P Lv .r: y cl r Licensee Disposition Licensee argued that Jocassee Dam floods are outside of licensing basis for ONS.Licensee committed to disposition of this deficiency as part of their IPEEE submittal in 1995 , An assessment of the Jocassee Dam flood hazard was included in the IPEEE without mention of the inspection issue., The staffs evaluation did not take issue with:-The derivation of the dam break frequency-Other factors that the licensee used to reduce their risk estimates of external flood events-The lack of arguments to justify plant protection for floods in excess of the eight of the protective walls at the SSF grade level.The licensee failed to note in the submittal or subsequent updates that there existed a recent inundation study that was the subject of an NRC inspection issue.SNficial s nly Secu -(;&UpS.NRC hddrInrnn NRC Staff Review of IPEEE Submittals
, Licensees extended these walls to 7.5-ft in February 2009.OiNRCial Use Y -SeTY- 3Prolkif Ptople aa at h .rIm ,ommne Flooding* Licensee performed an ONS inundation studyin 1992-Required by Federal Energy Regulatory Commission (FERC) Emergency Action Plan(EAP) on Jocassee license to Duke Hydro-Only reproducible calculation on record., Inundation levels calculated ranged from 12.5to 16.8 feet, NRC service water inspection in 1994identified potential deficiency in the 5-ftentrance wall height to that of the inundation study.P Lv .r: y cl r Licensee Disposition Licensee argued that Jocassee Dam floods are outside oflicensing basis for ONS.Licensee committed to disposition of this deficiency as part oftheir IPEEE submittal in 1995, An assessment of the Jocassee Dam flood hazard was includedin the IPEEE without mention of the inspection issue., The staffs evaluation did not take issue with:-The derivation of the dam break frequency
* Review of submittals for NRR was managed by RES e RES contracted national laboratories to conduct reviews s Region II staff met with NRR staff on September 1, 1994 which was documented in a memo-The Jocassee Dam rupture flood issue was discussed-NRR staff stated that the external event hazards preliminary review of Oconee would take several months-The memo stated that NRR staff considered the issue of minimal importance without any bases for these views-In light of this, RES staff was not informed of this issue 0 i Ue On6 UjSI RCR rmto 1CB~1T~WO NRC Staff Disposition of the Oconee IPEEE Submittal o Given the submittal information, the staffs closeout letter in 2000 stated-Duke's process is capable of identifying potential vulnerabilities associated with these issues at Oconee-Considered external event issues resolved.* The closeout letter cites a dominant contributor to residual risk involved Jocassee Dam failures and flood heights exceeding the 5-foot high SSF flood barrier, thus rendering the SSF inoperable.
-Other factors that the licensee used to reduce their riskestimates of external flood events-The lack of arguments to justify plant protection for floods inexcess of the eight of the protective walls at the SSF gradelevel.The licensee failed to note in the submittal or subsequent updates that there existed a recent inundation study that wasthe subject of an NRC inspection issue.SNficial s nly Secu -(;&UpS.NRC hddrInrnn NRC Staff Review of IPEEESubmittals
7 Re-emergence of Issue# The Reactor Oversight Program (ROP) identified a performance deficiency against the licensee by their making and keeping an opening in the side of the SSF below the 5-ft level for 2 years without an adequate evaluation.
* Review of submittals for NRR was managed by RESe RES contracted national laboratories to conductreviewss Region II staff met with NRR staff on September 1,1994 which was documented in a memo-The Jocassee Dam rupture flood issue was discussed
e The flood height calculation resurfaced during evaluation of the performance deficiency using the Significance Determination Process (SDP) in 2006 NRC staff reviewed the dam failure probability frequency and discovered a major flaw in the licensee's calculation in 2007.jUSNRC 'ftici NPepk aud thef Empiometn r " ., : j -Actions Taken by NRC Staff# The NRC staff took the following actions to assess the Oconee facility's ability to withstand severe flood events from a postulated Jocassee Dam break:-Initiated a design adequacy review-Developed an action plan-Staff assessed the design basis-Researched prior licensing actions related to flood protection s Reviewed other information to determine if the current plant design meets NRC regulatory expectations , The staff used a collaborative, consensus-building approach among 4 NRR Divisions and OGC to ensure appropriate regulatory practices were followed (e.g., backfit analysis)., A draft backfit analysis was prepared (1U.SS RC 9no PIucdq Pe~ opte ard 11w Eior Results of Actions Taken by NRC Staff , NRC concluded that an adequate protection backfit exception may be the appropriate approach., Further determined that additional information from the licensee was required before additional regulatory action is to be taken.-A 10 CFR 50.54(f) request for information letter was sent to licensee on August 15, 2008.-Licensee responded to the letter on September 26, 2008-The NRC staff has reviewed licensee's response letter to the 50.54(f) letter and is issuing a formal response.ij u 10 USoAR .,. Inf .,,,  
-NRR staff stated that the external event hazardspreliminary review of Oconee would take several months-The memo stated that NRR staff considered the issue ofminimal importance without any bases for these views-In light of this, RES staff was not informed of this issue0 i Ue On6UjSI RCR rmto1CB~1T~WO NRC Staff Disposition of theOconee IPEEE Submittal o Given the submittal information, the staffs closeoutletter in 2000 stated-Duke's process is capable of identifying potential vulnerabilities associated with these issues at Oconee-Considered external event issues resolved.
-, -1,, Yv. 0 I.- -Generic Implications s NRC staff has identified six (6) sites which may have a similar flood vulnerability s NRC staff planning on reviewing closeout of GS1-156.1.2 s A proposed B.5.b review of possible strategies to mitigate core damage s A generic communication via an Information Notice has been drafted and is in the process of concurrence.
* The closeout letter cites a dominant contributor toresidual risk involved Jocassee Dam failures andflood heights exceeding the 5-foot high SSF floodbarrier, thus rendering the SSF inoperable.
(ýtUS.NRC ORc Us In -Sn PfakimfPeapk a.4 WA Fm ,o,.mt}}
7 Re-emergence of Issue# The Reactor Oversight Program (ROP) identified aperformance deficiency against the licensee by theirmaking and keeping an opening in the side of theSSF below the 5-ft level for 2 years without anadequate evaluation.
e The flood height calculation resurfaced duringevaluation of the performance deficiency using theSignificance Determination Process (SDP) in 2006NRC staff reviewed the dam failure probability frequency and discovered a major flaw in thelicensee's calculation in 2007.jUSNRC 'ftici NPepk aud thef Empiometn r " ., : j -Actions Taken by NRC Staff# The NRC staff took the following actions to assess the Oconeefacility's ability to withstand severe flood events from apostulated Jocassee Dam break:-Initiated a design adequacy review-Developed an action plan-Staff assessed the design basis-Researched prior licensing actions related to flood protection s Reviewed other information to determine if the current plantdesign meets NRC regulatory expectations
, The staff used a collaborative, consensus-building approachamong 4 NRR Divisions and OGC to ensure appropriate regulatory practices were followed (e.g., backfit analysis).
, A draft backfit analysis was prepared(1U.SS RC 9noPIucdq Pe~ opte ard 11w Eior Results of Actions Taken by NRCStaff, NRC concluded that an adequate protection backfit exception may be the appropriate approach.
, Further determined that additional information from the licensee was required beforeadditional regulatory action is to be taken.-A 10 CFR 50.54(f) request for information letterwas sent to licensee on August 15, 2008.-Licensee responded to the letter on September 26, 2008-The NRC staff has reviewed licensee's responseletter to the 50.54(f) letter and is issuing a formalresponse.
ij u 10USoAR .,. Inf .,,,  
-, -1,, Yv. 0 I.- -Generic Implications s NRC staff has identified six (6) sites whichmay have a similar flood vulnerability s NRC staff planning on reviewing closeout ofGS1-156.1.2 s A proposed B.5.b review of possiblestrategies to mitigate core damages A generic communication via an Information Notice has been drafted and is in the processof concurrence.
(ýtUS.NRC ORc Us In -SnPfakimfPeapk a.4 WA Fm ,o,.mt}}

Revision as of 22:24, 9 July 2018

Presentation to the Lessons Learned Oversight Board on Oconee Nuclear Station External Flood Protection Concern
ML14058A033
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 05/05/2009
From: Circle J A
NRC/NRR/DRA
To:
Shared Package
ML14055A421 List: ... further results
References
FOIA/PA-2012-0325
Download: ML14058A033 (11)


Text

V p Oconee Nuclear Station External Flood Protection Concern May 5, 2009 presentation to the Lessons Learned Oversight Board Jeff Circle Division of Risk Assessment Office of Nuclear Reactor Regulation dcial Use 0 -Secu U ..R "ltenfor t Background of Issue NRC initiated the Systematic Evaluation Program (SEP) in 1977 to review the design of older, operating nuclear power plants with the current Standard Review Plan (SRP).-Opened Generic Safety Issue GSI-156.1.2, "Dam Integrity and Site Flooding".

-Oconee Nuclear Station (ONS) was identified as one such plant with flooding vulnerability.

-GSI-156 scheduled to be closed out by licensees in the Generic Letter 88-20, Supplement 4, the Individual Plant Examination of External Events (IPEEE) program.USNRC 2-Rd I nm.t.

and Oconee Nuclear Station Three-unit site with unique flooding vulnerability.

-On Lake Keowee near Seneca, SC-No emergency diesel generators

-Reliance of 2-unit Keowee Dam as sole source emergency ac power-Site is downstream of Jocassee Dam , A 385-ft high pumped storage hydro-station holding back Lake Jocassee-Licensee constructed the Standby Shutdown Facility (SSF)on site to address several issues including flooding , Houses equipment to safely shut down all 3 units in the event of catastrophic flood to Mode 3* Licensee constructed 5-ft walls around entrances to address external flooding vulnerability., Licensees extended these walls to 7.5-ft in February 2009.OiNRCial Use Y -SeTY- 3 Prolkif Ptople aa at h .rIm ,ommne Flooding* Licensee performed an ONS inundation study in 1992-Required by Federal Energy Regulatory Commission (FERC) Emergency Action Plan (EAP) on Jocassee license to Duke Hydro-Only reproducible calculation on record., Inundation levels calculated ranged from 12.5 to 16.8 feet , NRC service water inspection in 1994 identified potential deficiency in the 5-ft entrance wall height to that of the inundation study.P Lv .r: y cl r Licensee Disposition Licensee argued that Jocassee Dam floods are outside of licensing basis for ONS.Licensee committed to disposition of this deficiency as part of their IPEEE submittal in 1995 , An assessment of the Jocassee Dam flood hazard was included in the IPEEE without mention of the inspection issue., The staffs evaluation did not take issue with:-The derivation of the dam break frequency-Other factors that the licensee used to reduce their risk estimates of external flood events-The lack of arguments to justify plant protection for floods in excess of the eight of the protective walls at the SSF grade level.The licensee failed to note in the submittal or subsequent updates that there existed a recent inundation study that was the subject of an NRC inspection issue.SNficial s nly Secu -(;&UpS.NRC hddrInrnn NRC Staff Review of IPEEE Submittals

  • Review of submittals for NRR was managed by RES e RES contracted national laboratories to conduct reviews s Region II staff met with NRR staff on September 1, 1994 which was documented in a memo-The Jocassee Dam rupture flood issue was discussed-NRR staff stated that the external event hazards preliminary review of Oconee would take several months-The memo stated that NRR staff considered the issue of minimal importance without any bases for these views-In light of this, RES staff was not informed of this issue 0 i Ue On6 UjSI RCR rmto 1CB~1T~WO NRC Staff Disposition of the Oconee IPEEE Submittal o Given the submittal information, the staffs closeout letter in 2000 stated-Duke's process is capable of identifying potential vulnerabilities associated with these issues at Oconee-Considered external event issues resolved.* The closeout letter cites a dominant contributor to residual risk involved Jocassee Dam failures and flood heights exceeding the 5-foot high SSF flood barrier, thus rendering the SSF inoperable.

7 Re-emergence of Issue# The Reactor Oversight Program (ROP) identified a performance deficiency against the licensee by their making and keeping an opening in the side of the SSF below the 5-ft level for 2 years without an adequate evaluation.

e The flood height calculation resurfaced during evaluation of the performance deficiency using the Significance Determination Process (SDP) in 2006 NRC staff reviewed the dam failure probability frequency and discovered a major flaw in the licensee's calculation in 2007.jUSNRC 'ftici NPepk aud thef Empiometn r " ., : j -Actions Taken by NRC Staff# The NRC staff took the following actions to assess the Oconee facility's ability to withstand severe flood events from a postulated Jocassee Dam break:-Initiated a design adequacy review-Developed an action plan-Staff assessed the design basis-Researched prior licensing actions related to flood protection s Reviewed other information to determine if the current plant design meets NRC regulatory expectations , The staff used a collaborative, consensus-building approach among 4 NRR Divisions and OGC to ensure appropriate regulatory practices were followed (e.g., backfit analysis)., A draft backfit analysis was prepared (1U.SS RC 9no PIucdq Pe~ opte ard 11w Eior Results of Actions Taken by NRC Staff , NRC concluded that an adequate protection backfit exception may be the appropriate approach., Further determined that additional information from the licensee was required before additional regulatory action is to be taken.-A 10 CFR 50.54(f) request for information letter was sent to licensee on August 15, 2008.-Licensee responded to the letter on September 26, 2008-The NRC staff has reviewed licensee's response letter to the 50.54(f) letter and is issuing a formal response.ij u 10 USoAR .,. Inf .,,,

-, -1,, Yv. 0 I.- -Generic Implications s NRC staff has identified six (6) sites which may have a similar flood vulnerability s NRC staff planning on reviewing closeout of GS1-156.1.2 s A proposed B.5.b review of possible strategies to mitigate core damage s A generic communication via an Information Notice has been drafted and is in the process of concurrence.

(ýtUS.NRC ORc Us In -Sn PfakimfPeapk a.4 WA Fm ,o,.mt