ML20202F195: Difference between revisions
StriderTol (talk | contribs) (StriderTol Bot insert) |
StriderTol (talk | contribs) (StriderTol Bot change) |
||
Line 18: | Line 18: | ||
=Text= | =Text= | ||
{{#Wiki_filter: | {{#Wiki_filter:- _ | ||
, | |||
< | |||
. | |||
. | |||
U.S. NUCLEAR REGULATORY COMMill860N | |||
REGION 111 | |||
Docket Nos: 50 456,50-457 | |||
Uoense Nos: NPF 72 NPF 77 | |||
Report No: 50-456/97019(DRP); 50-457/97019(DRP) | |||
Ucensee: Commonwealth Edison (Comed) | |||
Facility: Braidwood Nuclear Plant, Units 1 and 2 | |||
- Location: RR #1, Box 84 | |||
Braceville,IL 60407 | |||
Dates: November 4 December 15,1997 | |||
Inspectors: C. Phillips, Senior Resident inspector | |||
J. Adams, Resident inspector | |||
D. Pelton, Resident inspector | |||
T. Tongue, Project Engineer | |||
T. Esper, Illinois Department of Nuclear Safety | |||
Approved by: Michael J. Jordan, Chief | |||
Reactor Projects Branch 3 | |||
: | |||
9902190148 900102 | |||
PDR | |||
8 ADOCK 05000456 | |||
PDR | |||
s j | |||
. | |||
4 | |||
. | |||
' | |||
EXECUTIVE SUMMARY | |||
Braidwood Nuclear Plant, Unita 1 and 2 | |||
NRC inspection Report No. 50 456/97019(DRP); 50 457/97019(DRP) | |||
l | |||
t | |||
I | |||
This inspection included aspects of licensee operations, maintenance, engineering, and plant | |||
sup,x>rt. The report covers a 6-week period of resdent inspection from November 4 through | |||
December 15,1997. | |||
Operatione | |||
+ | |||
The inspectors concluded that the operating crews performing the startup from the Unit 2 | |||
refueling outage demonstrated excellent human performance when challenged by a | |||
waterhammer event on the 2D tempering feedwater line on November 10 and a boron | |||
dilution prevention system actuation on November 14. The operators were observed to | |||
quickly identify the problem, enter the appropriate procedu,es and terminate the | |||
transients. The inspectors observed that throughout the startup, pre-evolution briefings | |||
met or exceeded management expectations, operators followed procedures, and there | |||
was continuous supervisory involvement and oversight. (Section 0.1) | |||
Maintenangs | |||
* | |||
On November 14, inspectors observed maintenance activities for the repair of hydraulic , | |||
actuator leakage on main steam isolation valve 1MS001C. The inspectors concluded that | |||
the work package was property preparsd and the work was property performed in | |||
accordance with the work package. However, the inspectors observed that the | |||
mechanics had to realign the hydraulic tubing and this was not documented in the work | |||
package. The inspectors concluded that not documenting as found conditions was a | |||
poor work practice. (Gection M1.1) | |||
+ | |||
The !nspectors concluded that licensee personnel failed to identify and remove all loose | |||
materials from the containment as required by a containment loose debris survollisnce | |||
conducted on November 2. A Notice of Violation was issued (Section Mt.1) | |||
+ | |||
On November 24, tho inspectors observed the parformance of 2BwVS 1.2.3.1 1, an | |||
American Society of Mechanical Engineers Code performance test, on the 2A centrifugal | |||
charging pump, and concluded that the surveillanca test was properly perfomied and | |||
acceptance criteria were met. (Section M4.2) | |||
Enalnes,rina | |||
* The inspectors performed a review of three safety-related modifications installed during | |||
the most recent Unit 2 refueling outage (A2R06) and concluded that the modifications and | |||
revisions were processed in accordance with the appropriate procedures, were property | |||
documented, and received proper safety evaluations. The inspectors concluded *Ast . | |||
post modification test procedures were well written and adequately verified that the | |||
modification performed as des!gned. The physicalinstallat'on of modification hardware | |||
appeared to match the work package specifications. (Section E2.1) | |||
a 2 | |||
. . _ _ _ - - - _ - _ . | |||
i | |||
< | |||
. | |||
. | |||
Plant tuonort | |||
* The inspectors concluded that threo vehicle searches observed on November 21 at the | |||
entrance to the protected area were performed in sooordance with the appropriate | |||
licensee procedure and that the pmper revision of the procedure was used. No problenis | |||
were observed. (Section 81.1) | |||
I | |||
N | |||
3 | |||
i | |||
. | |||
~ | |||
B | |||
la L ' . o | |||
, | |||
i | |||
' | |||
. | |||
' | |||
l | |||
i | |||
' | |||
Report Details | |||
Summary of Plant Status | |||
Unit i enterM the inspection period at '00 percent power and stayed at or near full power for the | |||
entirs period. On November 24, Unit 1 had run for 182 consecutive days exceeding a previous | |||
Unit i record run of 181 days. | |||
Unit 2 entered the inspedion period shutdown for refueling outage A2R06. The unit was made | |||
critical on November 14, was synchronized to the grid on November 15, reached full powwr on | |||
November 26, and operated at or near full power until the end of the period. | |||
L Operations | |||
01 Conduct of Operations | |||
01.1 Unit 2 Startuo From Refuelino Outaae A2R06 | |||
s. - Inspection Scope (71707) | |||
The inspectors observed portions of the licensee's preparation for startup of Unit 2 after , | |||
refueling outage A2R06 on November g and 10 and aga', on November 14. The | |||
inspectors observed the licensee's pre-evolution briefings and reviewwd BwAP 10012, | |||
" Human Performance Awareness of Pre Job Briefings / Meetings and Self Checking," | |||
Revision 5. The inspectors also reviewed BwGP 1001, * Plant Hestup," Revision 10; | |||
BwGP 100 2, * Plant Startup," Revision g; BwVS 500 3, " Reload Startup Physics Tests | |||
Following Refueling," Revision 13; BwVS 5004, " initial Criticality After Refueling and | |||
Nuclear Heating Level," Revision 12; and 2BwoA SEC 6, "Feedwater Tempering Line | |||
Loss of Subcooling," Revision 4. | |||
b. Observations and Findinah | |||
on November 10, the inspectors verified that the pre evolution briefings met the | |||
requirements of BwAP 10012. All the necessary personnel attended the meeting. The | |||
inspectors observed that at least one nuclear station operator (NSO) had received | |||
training on the startup and physics testing prior to the sairtup. The NSO specifically | |||
asked fc ' management expcetations on what contingency actions were to be taken if | |||
unexpected rod position indications were received at different points in the rod withdrawal | |||
sequence. | |||
iinspectors performed a partial verification of the lineup requirements of SwGP 100-1 | |||
and verified the prerequisites for RwGP 100 2 h6d been met. While performing steps of | |||
SwGP 100-2, just prior to control rod withdrawal, the licensee opened the prehester | |||
bypass valve 2FWO3gD. A inud waterhammer was heard in the control room. Shortly | |||
after that, indications were received in the control room that the 2D tempering feedwater | |||
line had lost flow. The inspectors verified that the operations crew identifkwi that there | |||
was m ioss of subcooling in the tempering feedwater line to the 'D' steam generator. The | |||
4 | |||
7i | |||
___ . . _ _ _ . _ _ _ ._--_ _ _ _ _ .._ _ _ _ . _ . _ __ | |||
' | |||
. | |||
, | |||
' | |||
operations crew entered and followed 2BwoA SEO 4 for loss of foedwater tempering line | |||
subcooling. At that point the startup was terminated until further troubleshooting could be | |||
completed. | |||
Further inspection on November 11, revealed significant damage to the 20 tempering | |||
feedwater line piping supports inside the Unit 2 containment. Additional details regarding | |||
the cause of the waterhammer, the adequacy of procedures, and the extent of the | |||
3 | |||
damage will be discussed in inspection Report No. 97021. | |||
j | |||
Repairs were made to the feedwater line supports and sanctor startup recommenood on | |||
November 14. Within minutes of reactor criticality, a boron dilution prevention system | |||
(BDPS) actuation occurred and borated water was iriected into the reactor. Tho | |||
actuation occurred due to the slow power ascent at a 0.1 decade per minute startup rate. | |||
One intermediate range instrument associated with the 'B" train BDPS momentarily went | |||
abovo 10 X 10* amps which unblocked the BDPS actuation signal and then dropped | |||
below 5 X 10-" amps which reanned the SDPS actuation system. Concurrently, source | |||
range counts had doubled within the last 10 minutes which actuated BDPS. The | |||
actuation did not occur due to operator error. The operators were observed taking the ; | |||
appropriate actions to secure the borated water irQoction. An estimated 120 gallons c7 | |||
borated water was irSected. Attar the boration was secured, a positive 0.1 decade per | |||
minute startup rate was observed. Thus, the negative reactivity inserted from the borated | |||
water injection had little offect on the powerlevel. The sta: tup then continued witho t * | |||
Incident up to 1X104 arrips. | |||
; | |||
c. Concheulo.a | |||
l The inspe ctors concluded that the opemting crews prforming the startup from the Unit 2 | |||
refueling outage demonstrated excalient human perfom'anoe when challenged by , | |||
equipment failures. On November 10, the inspectors observed operator action after a | |||
waterhammer event on the 20 tempering feedwater line. The operators entered the | |||
appropriate procedure and quickly terminated the event. On November 14, a BDP8 - | |||
actuat!on occurred moments after the reactor was made critical. The operators were | |||
obswrved tenninsting the BDPS actuation quickly and appropriately. The inspectors | |||
observed that throughout the startup, pre-evolution briefings met or exceeded | |||
, | |||
' | |||
management expectat!ons, operators followed procedures, and there was continuous | |||
supervisory involvement and ovansight. | |||
02 Operational Status of Facilities and Equipment | |||
L | |||
' | |||
02.1 Out of Service (003) Review | |||
: | |||
a. Inspection Scoon (71707) | |||
, | |||
i | |||
' | |||
The inspectors reviewed an OOS in effect and an OOS recently closind. The inspectors | |||
also interviewed operations personnel in the work control center, | |||
b. htoatientandfbdinali | |||
The inspectors uviewed OOS 050001122, which was placed on essential service watSr | |||
components for admini:Wative control to assure compliance with TS 4.7.4. The OOS was | |||
. | |||
5 | |||
i | |||
l | |||
; | |||
I | |||
' | |||
: | |||
_ | |||
_ , _ - - , . _ - , . , . . - . - . _ _ . . _ , , , . - - ... - . . _ . . _ . _ _ . _ , . . - - . _ _ _ . , _ _ . _ _ _ . - _ ~ , _ . - , - . _ , . . , - | |||
e | |||
< | |||
. . | |||
. | |||
property prepared and authortred. M components listed on the 008 were in thu required | |||
position with appropriate 008 cards affixed. Documentation for the 000 was compWo. | |||
# | |||
The inspectors also reviewed recently cleared 008 970012343. The 008 was placed | |||
on 18 emergency diesel poneretor Ltarting air compressor #2 in order to perform | |||
lubrication of the compressor motor. M components were retumed to the required | |||
position listed for the retum-to service of the starting air compressor. M 008 tags were | |||
removed from components. Documentation for the cleared 008 was complete.- | |||
c. Conclusions | |||
The inspectors concluded that the two out-of-services reviewed c wfety related | |||
components were property placed, removed, and documented. | |||
08 Mlaoellaneous Operatione issues (92700 and 92901)) | |||
08.1 Institute For Nuclegr Power Operations (INPO) Recod Review | |||
The inspectors reviewed the INPO evaluation repost of Exidwood Station 1997 | |||
- performance dated October 6,1997, on November 28. The inspectors concluded that - | |||
- there were neither findinos that effected too health and safety of the public nor that | |||
required additional followup tr/ the resident inspectors. | |||
08.2 (Closed) Ucensee Event Report (i PR) 50 fAZl20004-03: On Mry 23, and again on | |||
May 24,1996, T8 3.0.3 was not entered as required by TS 3.4.6.1 when leak detection | |||
systems woru inopereblo. The plant was placed in this condition during routine filter | |||
changes on the containment atmosphere monitor with tim containmer.t floor drain leak | |||
L | |||
' | |||
detection system flow transmltter inoperable. The containment atmosphere monitor was | |||
returned to service prior to the expiration of the limiting candition for operation. The | |||
licensee determined that both events were caused by Saman error. The inspectors | |||
reviewed the licensee's completed corrective actions and considered them appropriate. | |||
This item is closed. | |||
11. Maintenanott | |||
M1 Conduct of Maintenance , | |||
M1.1 Maintenance Activities Performed w Main Steam Isolation Valve (MSM 1MS001C | |||
. a. Insoection8523 (62707) | |||
On November 12,'.he inspectors observed rnanntenance actises on MSIV iMS001C. | |||
The inspectors reviewed work request 970119298-01, *2 Drop per Second Fyrquel Leak - | |||
on Hydraulic Pump Discherge! (no revision); reviewed and monitored the establishment | |||
of required system status; monitored the performance of maintenance work; reviewed the- | |||
completed wost package, and interviewed licensee po.mel at the job site. | |||
6 | |||
, _ | |||
n- | |||
4 | |||
, | |||
b. Qb.es,tions end Findinas | |||
l | |||
l | |||
Work request 970119798 O'l was written 10 provide instructions for the removal, | |||
inspection and replacement of a portion of tubing tc repair leakage on the hydraulic | |||
operator of 1MS001C. The inspectors reviewed the work package f rior to the start of the | |||
l work, no problems were observed. | |||
The inspectors monitored the performance of work laciuding tae estabilshment of | |||
required system status and the removal, inspection, and reinttcIlation of the tubing. | |||
During reinstallation of the tubing, the mechanica identified that the tubing was | |||
misaligned which was the probsble cause of the reported leak. The tubing was property | |||
aligned tr.d cubsequently did not leak. No problems were noted with the performance of | |||
the work. | |||
The inspectors reviewed the completed work package. Mhough the work package | |||
includes a section for the documenting of as found conditlens, work performed, and root | |||
cause, the tubing misalignment problem was not documented. Th!s was discussed with | |||
the field supervisor. No other problems were noted w;th the completed work package. | |||
c. Coriciusione | |||
On November 14, inspectors observed maintenance retivities for the repair of hydrau;ic | |||
actuator leakage oa MSlV 1MS001C. The inspectors concluded that the work package | |||
was property prepared and the work was property performed in accordance with the work | |||
package. However, the inspectors observed that the mechanics had to realign the | |||
hydraul;c tubing a.id this was not documented in the work package. The inspectors | |||
concluded that not documenting as-found conditions was a poor work practice. | |||
M1.2 Cold Weather Preparationg : | |||
a. Jnspection Seppjt (71714) | |||
The inspectors reviewed the licenssa's preparations for protection from cold weather. | |||
The inspectors reviev'ed procedure OBwCS XFT A1, ' Freezing Temperature Equipment | |||
Protection Annual Surveillance," Revision 5. The inspectors also intery;ewed operations | |||
and system engineering personnel, | |||
b, Observations and Findinas | |||
The inspectors reviewed the completed surveillance procedure OBwOS XFT-A1. The | |||
procedure was property completed and all discrepancies were addressed with action | |||
requests. The inspectcre verified that procedure OBwCS XFT-A1 checked safaty-related | |||
' | |||
systems and components that are susceptible to cold weather effects. | |||
Only one item identified in the completed procedure was a icng standing deficiency. The | |||
deficient item was a turbine building louver which was required to be closed for secondary | |||
system (non safety-related) protection. Ar action request was written on June 19,1996, | |||
to repair damper OHS VT404 LV 7. | |||
7 | |||
l | |||
- .. . - _ _ - - _ _ _ _ _ _ _ _ | |||
y . . | |||
. | |||
' | |||
. | |||
? . | |||
The inspectors checked for licensee response to deficient items idenufled during | |||
performance of the cold weather choolm. Actions to repair deflolerd items were | |||
scheduled for repair soon after discovery. For example, the security diesel generator | |||
jacket water cooling system did not meet saceptance criteda for anti freeze protection. | |||
The licensee scheduled and implemented repairs within five weeks of dismvery, and | |||
before extreme cold weather conditions were experienced. | |||
c. Conclusions | |||
The inspedors concluded that the licensee propedy completed cold weather | |||
preparshs. The licensee implemented appopdate and timely corrocuve actions to | |||
address the deficionoles identified while performing the annual oold weather surveillance | |||
procedure. Safety-related components appeared to be protected from the effects of cold | |||
weather. | |||
M4 Maintenance Staff Knowledge and Performance | |||
M4.1 Unit 2 Containment closeout inspection | |||
a. inspection Scogi(61726) | |||
The inspectors pe,1ormed an independent inspection of the Unit 2 containment following | |||
the licensee's contalament locss debris inspection prior to entry into Mode 4 (hot | |||
shutdown) from refueling outage A2R06. Tho inspectors reviewed BwV8 5.2.d.2.1, | |||
" Visual Surveillance of Containment Recimulation Sumps,' Revision 4: 2BwoS 5.2.01, | |||
" Containment Loose Dobrts inspection,' Revision 6; Braidwood Problem identification | |||
Form (PlF) # 456 20196 0979; Operability Scrooning Form for PlF #456 201-96 0979; | |||
Braidwood Updated Final Gafety Analysis Report (UFSAR), Appendix A, ' Application of | |||
NRC Regulatory Guida," Regulatory Guide 1.82; and NRC Regulator / Guide 1.82, | |||
" Water Sources For Long-Term Recirculation Cooling Following A Lnss-Of-Coolant | |||
Accident,' Revision 2. | |||
b, Observations and Findinas | |||
on November 2, the inspecters performed a containment loose debris inspection of the | |||
Unit 2 containment following notification from licensee management that operations | |||
department personnel had completed the containment loose debria surveillance | |||
inspection 2BwoS 6.2.c4. The inspectors walked down all accessible elevations inside | |||
and outside of the missile barrier, inspectors found that all trash, rags, protective | |||
clothing, and foreign material exclusion barrier matedals had boon removed. The | |||
containment sump covers and screens were found free of debris. However, the | |||
inspectors did observe several material condition problems, and loose materials. For | |||
example, the inspectors identified the following material condition problems: | |||
a | |||
the 2B charcoal unit door was found unnatched; | |||
+ | |||
charging valve,2AOV-CV8147, had a minor packing leak; _ | |||
. | |||
seal table area radiation monitor meter,2RIA-AR303, was erroneously reading | |||
10,000 millirem per tour; | |||
8 | |||
. _ | |||
_ , . . . .. .. | |||
. | |||
. . . | |||
' | |||
. | |||
. | |||
* surface gaps larger than the 3/8 inch mesh in the outer containment toolroulation | |||
sump screens and a hole larger than the 7/16 inch mesh in the Intermediate | |||
containment roolroulation sump screen covers; and . | |||
* | |||
the 28 reactor cooling pump number 2 seal leakoff flow indicator reading less than | |||
aero. | |||
The inspectors also identifled the following examples of loose materials: | |||
+ | |||
tools were staged near the reactor head area (426 foot elevation) with no work | |||
requiring the tools being performed; and | |||
* | |||
sheet metal covers on two of the incore drive units were not fastened down. | |||
The inspecaors discussed their findings with licenses managemord. The inspectors were | |||
told that the surface gaps in the outer containmord toolroulation sump scroon had been | |||
previously identified in May of 1996, and documented by PlF #456 201-96-0979. The | |||
licensee told the inspectors that modification E200 97 298 woeld eliminate the surface | |||
gaps and would be completed prior to the change from mode five to mode four. The | |||
inspectors later verified that the modification was instal;sd. The inspootors asked if | |||
; | |||
modification E2M 97 298 would also eliminate the holes in the covers of the | |||
Intermediate screen. The licensee told inspectors that it would not, but provided the | |||
inspectors a copy of the operability screening justifying continued operation with the holes | |||
in the intermediate screen covers. The inspectors reviewed the operability scrooning for | |||
PlF #456-20196-0979 and found that the licensee had based the operebility of the | |||
containment recirculation sump on the existence of a verticalinner screen also | |||
constructed of 3/16 inch mesh located on the collection side of the containmord | |||
recirculation sump weir plate. The inspectors found that the containment recirculation ' | |||
sump met the minimum design guidance found in NRC Regulatory Guide 1.82, | |||
- Section C.1.3, with the holes in the intermediate screen covers. | |||
\ | |||
The inspectors were concemed with the amourd of loose equipment identified during the | |||
inspection. The inspectors obtaired a copy of 2Bwo8 5.2.o 1 that was performed on | |||
' November 2, at 4:40 p.m. Step F.2.c required that loose tools and equipment that were | |||
not needed for approved work in progress be removed from containment. Tlw inspectors | |||
found that loose materials and tools were not removed; tut none of the discrepancies | |||
were documented co the surveillance data shoot; that the'ro yas no work in p: ogress ; | |||
associated with the incore neutron detector drives or the tools staged near the reactor | |||
head area; and supervisory personnel were not aware that the (r. core drive mechanism | |||
covers wste unfastened. Ucensee persomel that performed the surveillance test | |||
procedure indicated on the surveillsnoe test data sheet tt at the requhments of | |||
Step F.2.c were met with the exception of a clock that ricaded to be traowd. | |||
Technical Specification 6.8.1.o states, ',n part, that mitten orocedures shall be | |||
established, implement 6d, snd maintained covefirsg the applicable precedures. , | |||
recommended in Appendix A of Regulatory Guide 1.33, Revision 2. Februg 1978. 3 | |||
' ~ | |||
Regulatory Guide 1.33, Appenutr. A, Secticn 3.f. statse that there shail be instrucll",ns for | |||
the staitup, uperat;on, and shutdown of safettrelated systems. Tha failure to fot!7.v | |||
2RwoS 5.2.o 1 was a viola' ion of T6 6.8.1.a. (SO457/97019-01(ORP)). | |||
9 | |||
, ,_ , - -- | |||
s | |||
' | |||
. | |||
. | |||
! | |||
c. Conclusions | |||
On November 2, the inspedors performed an inspecuon of the Unit 2 containmord | |||
following noufication by the licensee that they had completed their okscout inspection | |||
survelhanos, inspedors concluded that licensee personnel failed to identify and remove | |||
aN loose materials from the containment. The inspectors identiflod unfastened covers on | |||
two incore neutron detector drive mechanisms and unattended tools near the reactor | |||
head. These were conditions that did not meet the acceptance critetta of 2Bwo8 6.2.01, | |||
Step F.2.c. | |||
M4.2 Burveillanos Testino of the 2A Centrifunal Chaminn Pumo | |||
a. Inspection Soone (61726) | |||
The inspecbra observed the performance of and reviewed procedure 2BwV81.2.3.1 1, | |||
'American Society of Mechanical Engineers (ASME) Survenslance Requiremends For 2A | |||
Centrifugal Charging Pump And Check Valve 2CV8480A 8troke Test," Revis!on 1. The | |||
inspedors discussed the performance of the test with the system engineer, | |||
b. Observations and Findinos --- | |||
On November 24, the inspedors observed the performance of 28wV81.2.3.1 1. During | |||
the pre-job brtefing, the system engineer discusseo the purpose of the surveillance test, | |||
precautions and limitations, prerequisites, responslolilt!ss, contingency actions, and key | |||
steps that required operator actions. The inspectors observed the system oncineer | |||
obtain the required approvals for the commencement of the surveillance test and property | |||
wmpiele the prorsquisites. During the performance of 28wV81.2.3.1 1, the inspedors | |||
observed proper communications between the unit supervisor, nuclear station operators, | |||
and the system engineer; proper self checkir.g; and proper independent verifications.' | |||
' | |||
The inspectors found that the required soceptance orlierta for pump suction p; essure,- | |||
pump differential pressure, total flow, and pump vibration were met. The inspootors . | |||
- observed an soceptable flow rate through 2CV8480A, the 2A centrifugal charging pump | |||
minimum flow check valve, to varify a full stroke of the valve. The inspectors observed | |||
the proper operation of the 2A charging pump hMcating oil system and cubical coolers. | |||
The inspectors verilled that the pump's perfon. .ece exceeded the UFSAR pump | |||
performance curve's minimum design performance. | |||
g c. .QQDdilAl ons | |||
On November 24, the incpedors observed the performance of 2BwV81.2.3.1 1 and - | |||
corwiudod that the survoitlance test was property performed and soceptance critetta were | |||
met. The pump's performance exceedad the minimum required performance specified in | |||
the UFSAR. | |||
. | |||
MS Miscotlaneous Maintenance issues (92902) | |||
~ | |||
M8.1 {Qjgiq$ Violation 50-40'//g6011-04a and 50-457/99011-04b: Failure To Follow Two | |||
Procedures Regarding Maintenance Mterations and Operational Electrical Uneups. The | |||
Ncensee retumed a redweste building ventilation damper to servios in the failed open | |||
y 10 | |||
( , , | |||
. . | |||
- .--.- | |||
, - | |||
' | |||
. | |||
. | |||
condition following maintenance, and fskd to complete Procedure BwoP MP.08, | |||
" Restoring Unit 2 Mein Osntrator, Main Power Transfermars 2E and 2W and | |||
Unit Auxiliary Transformers 241 1 and 2414 * The inspectors verified that the licensee | |||
completed the corrocuve act!ons for both eumples and that there has been no | |||
recurrence of these spoolfic problems, This violation is closed. | |||
M8.2 (Closed) LER 60-458/95020-Of}: On D6cember 23,1995, power range channel N43 was | |||
placed in test for caliwst!on. Power re.nge N42 Indication began swinging by 10 percent | |||
power, causing spurious rate inps. No other indications of changing roantor power were | |||
present. The licensee invoked TS 3.0.3 s,nce both N42 and N43 were inoperable. | |||
Channel N43 was rectored end TO 3.0.3 was axited. Power range channel N42 was | |||
subsequently determined to have a pews,f suppii failure. The power supply was | |||
replaced. The IWnssa perfomwd an anwyd: cf the failure mode for maintenance rule | |||
applicability and determined that the bih c? not maintenance preventable. The | |||
inspectors concluded that the licensee's correcuve actions were appropriate. This item is | |||
closed. | |||
E.gapineerina | |||
E2 Engineering Support of Foollities and Equipment | |||
E2.1 Review of Plant Modifications | |||
. | |||
a. inanection Scoot (37551) | |||
The inspectors reviewed the work packages, modiilcation approval letters, modification , | |||
approval letter addendums, modification test procedures, and 10 CFR 50.59 safety | |||
evaluations, for modifications E20 2-96 250, *2CV 110A/2CV 111A Trim Change"; | |||
E20 2-96 256, ' installation of Permanent Power Source For Temporary 125 Volt DC | |||
Battery Chargers"; and E20 2 97 225, " Containment Recirculation Sump Enhancement." | |||
The inspectors reviewed procedures NEP 04-02, " Exempt Changes," Revision 0; . | |||
SWAP 232121, * Exempt Changes," Revision 3; and NSWP A-04, *10 CFR 50.59 Safety | |||
Evaluation Process," Revision 0. The inspectors performed a walkdown of accessible | |||
portions of the installed modifications, | |||
b. Observations and Findinns | |||
The inspectors reviewed the completed work packages for mor'ificationc E20 2 96 250, | |||
E242 96 256, and E20 2 97 225. The inspectors noted that the work packages were | |||
complets, Work procedures appeared to contain sufficient detail for the installation of the | |||
mod;fications. Procedure steps were propertf initialed and verified where required. The | |||
pre-job briefing, foreign material exclusion, and calibration documentation were included | |||
and appeared complete. | |||
The inspectors reviewed the modification approval letters and any modification approval | |||
letter addendums for modifications E20 2 96 250, E20-2-96-236, and E20-2-97-225. | |||
Each letter included a description of the modification, a discussion of applicable oodos | |||
and specifications, a brief discussion of the 10 CFR 50.59 safety evaluation, a list of | |||
11 | |||
) | |||
. | |||
t * | |||
__ | |||
, | |||
_ _ _ _ - | |||
_. _ _ _ _ _ _ _ _ _ _ . | |||
' | |||
. | |||
I | |||
' | |||
, l | |||
l dmwings effected by the modification, cor.3truction and modification testing requirements, | |||
t aining requirements, and a list procedures requiring review and revision. When the | |||
modifications were required to be changed following their initial approval, the inspectors | |||
' | |||
four.d appropriate addendums to the modification approval letters cordaining a discussion | |||
d the reasons for the change. The inspectors verified compliance with procedures | |||
NEP 04-02, * Exempt Changes," and BwAP 232121, * Exempt Changes,' in tn. | |||
processing of the modihations. | |||
! The inspectom reviewed the post-modification test procedures performed following the | |||
completion of the installation of each of the modifications. The inspecters found detailed | |||
procedures for each of the modifications. The post-modification test procedures I | |||
appeared adequate to ensure the modification performed as designed. l | |||
' | |||
The inspa Mors reviewed the 10 CFR 50.59 safety evaluat!ons for each modification. The | |||
inspectors concluded th at each safety evaluation was well written, complete, and | |||
prepared in scoordance with Procedure NSWP-A-04, *10 CFR 50.59 Safety Evaluation | |||
' | |||
Process." The safsty evaluations appeared adequate to determine if an unroviewed | |||
safety questim existed. The inspectors noted that changes to approved modification | |||
packages receive 4 additional 10 CFR 50.59 safety evaluations prior to their approval and | |||
installation. | |||
The inspectors looked at the physical inttallation of socessible modification hardware and | |||
compared the installatien to the documentation contained in the work osckar,es and _ | |||
' | |||
noted that the field installation appeared to match specifications in the work package. ; | |||
c. Conclus;ons I | |||
The inspectors performed a review of three safety-related A2R06 modifications and | |||
concluded that the modifications were processed in accordance with the appropriate | |||
procedures, were property documented, and received a proper safety evaluation. | |||
Revisions to the modifications were property documented and received additional safety | |||
evaluations prior to approval end installation. The inspectors co.wiudod that post- | |||
modification test procedures were well written and adequately verified that the | |||
, | |||
' | |||
modification performed as designed. The physicalinstallation of modification hardware | |||
appeared to match the work package specifWsPons. | |||
ES. Miscellaneous Engineering issues (92903) | |||
E6.1 (Closed) Unresolved item 50-456/g6014-06: - Roll Up Fire Doors Failure To Close. On | |||
' | |||
July 3,1996, mechanical maintenance personnel performed surveillance | |||
BwMS 3350-001, " Fire and Security Door Semi-Annual Inspection," Revision 0, and | |||
several roll-up doors did not go closed as expected with outside air ventilation to the | |||
room. A violation was issued in inspection Report No. 96016 (50456/96016-04(DRS); | |||
50-457/96016 04(DRS)) for the failure of the doors to close. This issue will be tracked by | |||
that vlotation. This item is closed. | |||
* | |||
E8.2 ' (Closed) Violation 50-456/oO21-03(DRP): 50-457/96021-03(DRP): On December 23, | |||
- | |||
1996, the licensee identified a through wall leak on ASME Class 3 piping in the 1A | |||
essential service water (SX) system. The licensee failed 'o remove the 1 A SX train from , | |||
' | |||
l service and take corrective actions as required by ASME Boiler and Pressure Vessel | |||
, | |||
12 | |||
. | |||
em m- see +s-.-e.h. istm -s & m' eve rw- -ea+--a-+--um.er-w---ww--e+-enww--*e& w-ry-wa .-----,----a, ,,m,+ w+ ;+--+--rr 's--he us -++'s aw- erW '- vvv'--'Y-v'-'r -*-N t'w*r ftvt-- -* mew yTw-1---yr | |||
- - _ . _ _ _ _ _ _ | |||
, | |||
' | |||
. | |||
. | |||
Code, Soodon XI. Part 60.55s(9)(4) of 10 CFR requires that aN components which are | |||
classi6ed as ASME Code Class 3 must meet the requirements set forth in ASME | |||
' | |||
Secuon XI. The inspectors reviewed the corrective acGons taken by the licensee in | |||
response to this violation and considered them to be adequate.1Es violation is closed. | |||
4 | |||
E8.3 (Closed) Violation 50 456/g7005 04fDRP): 50-457/97005 04fDRP): Failure To Wdte ! | |||
4 | |||
10 CFR 50.59 Safety Evaluation. The licensee tecked open the door between the | |||
auxiliary building ventilation exhaust plenum and the auxiliary building to perform , | |||
modification work on the auxiliary building exhaust fans and did not perform a | |||
' | |||
10 CFR 50.5g safety evaluation. The inspectors vedfied that the licenses changed | |||
DwAP 1110 3, *Plard Barder impairment Program,' Revision 5, to clarify that impairments | |||
to ventilation bounderles described in the UFSAR need to be screened for safety | |||
evaluations. The inspedots had no further concems. This item is closed. | |||
' | |||
, | |||
E8.4 (Closed) LER 64456/9601100: On September 24,1996, the licensee determined, during | |||
the performance of a surveillance test, that four rou-up doors separoung areas containing | |||
, | |||
safety-related equipment from the turbine building failed to fully close under full ventilation | |||
+ | |||
cond,tions. A review performed by system engineering personnel indicated that the | |||
, roll-up doors were not tested following installation. The licensets immediate corrective | |||
scuons were to close the four roll-up doors. The event was documented in inspec6on | |||
Report No. 50-456/96014 as an Unresolved item pending the results of additional rolo-up - | |||
door testing and a follow up inspection by regional fire protection specialists. The | |||
inspectors det6rrr.ined that since 1991 the roll-up doors were inoperable and did not meet | |||
the 3 hour rated fire barrier lequirement. An apparent violation was written and | |||
i documented in inspection Report No. 50 456/96016. The licensee's immediate correcGve | |||
' | |||
. uctions have been completed and were appropnate. The licensee's long-term corrective | |||
actions have been identified but have not been completed. The tracking of the licensee's | |||
long-term conective actions will be done by Violation 50 456/96016-04. This item is- | |||
closed. | |||
E8,5 ff& lid). : On October 12 and 25,1995, the | |||
licensee identified that several incorrect cable separations assumptions could potentially | |||
result in the inability to achieve and maintain safe shutdown conditions if a fire occurred in | |||
certain fire zones. An apparent violation was written and documented in inspection , | |||
Report No. 50-456/96016, and subsequently received escalated enforcement without a | |||
civil penalty. Design modifications are currently in progress to correct the deficiencies. 1 | |||
The tracking of the licensee's long-term corrective actions will be done by Violation | |||
50 456/96016-03. This item is closed. | |||
IV. Plant Support | |||
- | |||
l | |||
; 31 Conduct of Security and Safeguards Activities | |||
! 81.1 Vehicle Search. | |||
, | |||
s. Inspection Scope (71750) | |||
J | |||
' | |||
The inspectors performed an inspecuon of the licensees vehicle search program. The | |||
i. Inspectors reviewed BSP-09, " Vehicle Entry / Exit Procedure", Revision 7; reviewed | |||
t | |||
' | |||
13 | |||
, | |||
+-e, e- e- y,--,,,- e-,,,, ~ -~p ,m,,-,..,w-,.. - , ,_. _n,,,-n,nn. . , . , . _ . , , , . - - - , . - . . - - - , | |||
- | |||
e,,-.,mme,,,,,,w--.n.. ,, , , , ,- , , , , , . - . . , | |||
o | |||
. | |||
. | |||
. | |||
associated special security instructions; interviewed security personnel; and observed the | |||
performance of three vehicle searches. | |||
b. Observations and Findinos | |||
on November 21, the inspectors monitored the performance of two vehicle entry | |||
searches and one exit search performed at the entrance to the protected area in | |||
socordance with B8P Og, All required areas of the vehicles were searched including the | |||
engine, passenger compartment, cargo compartment, and the undercaninge. No | |||
prohibited llams were discovered, and no problems were noted by the inspectors. The | |||
inspectors (nonitored security personnel control of the vehicle drivers within the gate | |||
. area. Driver access was controlled in accordaru with 88P Og. Inspectors also | |||
monitored the control of the main gates during the vehicle searches. Actions taken by the | |||
security individuals including ooordinating the opening and closing of the outer gate, | |||
raising and lowering the vehicle barrier gate arm, and opening and closing the inner gate | |||
were in socordance with BSP Og, inspectors reviewed the security procedures | |||
maintained at the main entrance guard shack. The onpy of BSP-Og mahtained at the.. | |||
guard shack was the latest revision and all special security instructions applicable to | |||
BSP-Og were enclosed, | |||
c. 99aclusions | |||
' | |||
The inspectors concluded that three vehicle searches observed on November 21 at the | |||
. | |||
. entrance to the protected arsa were performed in socordance with the appropriate | |||
l licensee procedure and that the proper revision of the procedure was used. No problems | |||
were observed. | |||
V. Mananoment Meetinas | |||
X1 Exit Meeting Summary | |||
The inspectors presented the inspection results to members of licensee management at | |||
the conclusion of th9 inspection on December .15,1997. The licensee acknowledged the | |||
findings presented. The inspectors asked i Nnsee whether any materials examined | |||
during the inspection should be conslered ; arietary. No proprietary information was | |||
identified. | |||
_ | |||
14 | |||
m | |||
. . | |||
. . . . . . . . | |||
. | |||
. | |||
. _ _ _ _ _ . _ . _ . | |||
" | |||
, | |||
' | |||
. | |||
! . | |||
PARTIAL LIST OF PERSONS CONTACTED | |||
Lloensee | |||
'T. Tulon, site Vice President | |||
*K. Schwartz, Station Manager | |||
A. Haeger, Health Physics and Chemistry Supervisor | |||
'R. Byers, Maintenance Superintendent | |||
R. Graham, Work Control Superintendent | |||
T. Simpkin, Regulatory Assurance Supervisor | |||
C. Dunn, System Engineering Supervisor | |||
*J. Nalewajka, industrial Safety Engineering Group Cupervisor , | |||
*C, Herzog, Executive Assistant | |||
*J. Meister, Engineering Manager | |||
*R. Wegner, Operations Manager | |||
*M. Cassidy, Regulatory Assurance NRC Coordinator | |||
HBQ | |||
M. Jordan, Chief, Reactor Projects Branch 3 | |||
*C Phillips, Senior Resident inspector | |||
*J. Adams, Resident inspector | |||
D. Pelton, Resident inspector | |||
T. Tongue, Project Engineer | |||
IQNA | |||
*T. Esper | |||
* Denotes those who attended the exit interview conk Wn December 15,19g7. | |||
, | |||
__ - _ _ -_ | |||
15 | |||
i | |||
_ | |||
._ _ _- | |||
, | |||
.- | |||
, | |||
. | |||
INSPECTION PROCEDURES USED | |||
IP 37551: Onsite Engineering | |||
! IP 627C7: Maintenance Observations | |||
IP 61726: Surveillance Observations | |||
IP 71707: Plant Operations | |||
IP 71714: Cold Weather Preparations | |||
IP 71750: Plant Support Activities | |||
IP 92700: Onsite Followup of Written Reports of Nontoutine E"ents at Power Reactor | |||
Facliilles | |||
IP 92901: Followup PlantOperations | |||
IP 92902: Followup- Plant Maintenance | |||
IP 92903: Followup - Engineering | |||
ITEMS OPENED, CLOSED, AND DISCUSSED | |||
Opened | |||
50-456/97019 01 VIO Failure to follow procedures | |||
Chtits | |||
50-457/9601104a VIO Failure to follow procedures | |||
50-457/96011-04b VIO Failure to follow procedures | |||
50 456/96014-06 URI Roll up fire doors failure to close | |||
50-456/9602103(DRP); VIO Failure to meet ASME Boller and Pressure Vessel | |||
50-457/96021 n3(DRP) Code | |||
50-456/97005 04(DRP); VIO Failure to write a 10 CFR 50.59 safety evaluation | |||
50457/97005 04(DRP) | |||
50-456/95013-00 LER locorrect cable separations for fire protection | |||
50 456/95013-01 LER Incorrect cable separations for fire protection | |||
50 456/95020 @ LER Power range channel indication oscillations | |||
50-457/96004-00 LER TS 3.0.3 was not entered as required by TS 3,4.6.1 | |||
when leak detection systems were inoperable | |||
504 56/96011-00 LER Fire doors failure to close | |||
Discussed | |||
50-456/96016-03(DRS); VIO Incorrect cable separation assumptions | |||
50-457/96016-03(DRS) | |||
50-456/96016-04(DRS); VIO Roll up fire doors failure to test | |||
50-457/96016-04(DRS) | |||
_ _ __ | |||
16 | |||
) | |||
I | |||
* | |||
. | |||
! ' | |||
, | |||
, | |||
, | |||
; | |||
UST OF ACRONYMS USED | |||
ASME American Society of Mechanical Engineers | |||
l BDP8 Boron Dilution Prevention System | |||
l CFR Code of Federal Regulations | |||
' | |||
INPO Institute for Nuclear Power | |||
LER Licensee Event Report | |||
MSIV Main Steam isolation Valve | |||
NRC Nuclear Regulatory Commission | |||
NSO Nuclear Station Operator | |||
. | |||
008 Out-of-service | |||
l PDR PutJic Document Room | |||
l PlF Problem identification Form | |||
SX Essential Service Water | |||
l T8 Technica: Specification | |||
UFSAR Updated Finst safety Analysis Report | |||
URI Unresolved item | |||
VIO Violation | |||
, | |||
17 | |||
_ __9 | |||
}} | }} |
Latest revision as of 20:18, 1 January 2021
ML20202F195 | |
Person / Time | |
---|---|
Site: | Braidwood |
Issue date: | 01/02/1998 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
To: | |
Shared Package | |
ML20202F168 | List: |
References | |
50-456-97-19, 50-457-97-19, NUDOCS 9802190148 | |
Download: ML20202F195 (17) | |
See also: IR 05000456/1997019
Text
- _
,
<
.
.
U.S. NUCLEAR REGULATORY COMMill860N
REGION 111
Docket Nos: 50 456,50-457
Uoense Nos: NPF 72 NPF 77
Report No: 50-456/97019(DRP); 50-457/97019(DRP)
Ucensee: Commonwealth Edison (Comed)
Facility: Braidwood Nuclear Plant, Units 1 and 2
- Location: RR #1, Box 84
Braceville,IL 60407
Dates: November 4 December 15,1997
Inspectors: C. Phillips, Senior Resident inspector
J. Adams, Resident inspector
D. Pelton, Resident inspector
T. Tongue, Project Engineer
T. Esper, Illinois Department of Nuclear Safety
Approved by: Michael J. Jordan, Chief
Reactor Projects Branch 3
9902190148 900102
8 ADOCK 05000456
s j
.
4
.
'
EXECUTIVE SUMMARY
Braidwood Nuclear Plant, Unita 1 and 2
NRC inspection Report No. 50 456/97019(DRP); 50 457/97019(DRP)
l
t
I
This inspection included aspects of licensee operations, maintenance, engineering, and plant
sup,x>rt. The report covers a 6-week period of resdent inspection from November 4 through
December 15,1997.
Operatione
+
The inspectors concluded that the operating crews performing the startup from the Unit 2
refueling outage demonstrated excellent human performance when challenged by a
waterhammer event on the 2D tempering feedwater line on November 10 and a boron
dilution prevention system actuation on November 14. The operators were observed to
quickly identify the problem, enter the appropriate procedu,es and terminate the
transients. The inspectors observed that throughout the startup, pre-evolution briefings
met or exceeded management expectations, operators followed procedures, and there
was continuous supervisory involvement and oversight. (Section 0.1)
Maintenangs
On November 14, inspectors observed maintenance activities for the repair of hydraulic ,
actuator leakage on main steam isolation valve 1MS001C. The inspectors concluded that
the work package was property preparsd and the work was property performed in
accordance with the work package. However, the inspectors observed that the
mechanics had to realign the hydraulic tubing and this was not documented in the work
package. The inspectors concluded that not documenting as found conditions was a
poor work practice. (Gection M1.1)
+
The !nspectors concluded that licensee personnel failed to identify and remove all loose
materials from the containment as required by a containment loose debris survollisnce
conducted on November 2. A Notice of Violation was issued (Section Mt.1)
+
On November 24, tho inspectors observed the parformance of 2BwVS 1.2.3.1 1, an
American Society of Mechanical Engineers Code performance test, on the 2A centrifugal
charging pump, and concluded that the surveillanca test was properly perfomied and
acceptance criteria were met. (Section M4.2)
Enalnes,rina
- The inspectors performed a review of three safety-related modifications installed during
the most recent Unit 2 refueling outage (A2R06) and concluded that the modifications and
revisions were processed in accordance with the appropriate procedures, were property
documented, and received proper safety evaluations. The inspectors concluded *Ast .
post modification test procedures were well written and adequately verified that the
modification performed as des!gned. The physicalinstallat'on of modification hardware
appeared to match the work package specifications. (Section E2.1)
a 2
. . _ _ _ - - - _ - _ .
i
<
.
.
Plant tuonort
- The inspectors concluded that threo vehicle searches observed on November 21 at the
entrance to the protected area were performed in sooordance with the appropriate
licensee procedure and that the pmper revision of the procedure was used. No problenis
were observed. (Section 81.1)
I
N
3
i
.
~
B
la L ' . o
,
i
'
.
'
l
i
'
Report Details
Summary of Plant Status
Unit i enterM the inspection period at '00 percent power and stayed at or near full power for the
entirs period. On November 24, Unit 1 had run for 182 consecutive days exceeding a previous
Unit i record run of 181 days.
Unit 2 entered the inspedion period shutdown for refueling outage A2R06. The unit was made
critical on November 14, was synchronized to the grid on November 15, reached full powwr on
November 26, and operated at or near full power until the end of the period.
L Operations
01 Conduct of Operations
01.1 Unit 2 Startuo From Refuelino Outaae A2R06
s. - Inspection Scope (71707)
The inspectors observed portions of the licensee's preparation for startup of Unit 2 after ,
refueling outage A2R06 on November g and 10 and aga', on November 14. The
inspectors observed the licensee's pre-evolution briefings and reviewwd BwAP 10012,
" Human Performance Awareness of Pre Job Briefings / Meetings and Self Checking,"
Revision 5. The inspectors also reviewed BwGP 1001, * Plant Hestup," Revision 10;
BwGP 100 2, * Plant Startup," Revision g; BwVS 500 3, " Reload Startup Physics Tests
Following Refueling," Revision 13; BwVS 5004, " initial Criticality After Refueling and
Nuclear Heating Level," Revision 12; and 2BwoA SEC 6, "Feedwater Tempering Line
Loss of Subcooling," Revision 4.
b. Observations and Findinah
on November 10, the inspectors verified that the pre evolution briefings met the
requirements of BwAP 10012. All the necessary personnel attended the meeting. The
inspectors observed that at least one nuclear station operator (NSO) had received
training on the startup and physics testing prior to the sairtup. The NSO specifically
asked fc ' management expcetations on what contingency actions were to be taken if
unexpected rod position indications were received at different points in the rod withdrawal
sequence.
iinspectors performed a partial verification of the lineup requirements of SwGP 100-1
and verified the prerequisites for RwGP 100 2 h6d been met. While performing steps of
SwGP 100-2, just prior to control rod withdrawal, the licensee opened the prehester
bypass valve 2FWO3gD. A inud waterhammer was heard in the control room. Shortly
after that, indications were received in the control room that the 2D tempering feedwater
line had lost flow. The inspectors verified that the operations crew identifkwi that there
was m ioss of subcooling in the tempering feedwater line to the 'D' steam generator. The
4
7i
___ . . _ _ _ . _ _ _ ._--_ _ _ _ _ .._ _ _ _ . _ . _ __
'
.
,
'
operations crew entered and followed 2BwoA SEO 4 for loss of foedwater tempering line
subcooling. At that point the startup was terminated until further troubleshooting could be
completed.
Further inspection on November 11, revealed significant damage to the 20 tempering
feedwater line piping supports inside the Unit 2 containment. Additional details regarding
the cause of the waterhammer, the adequacy of procedures, and the extent of the
3
damage will be discussed in inspection Report No. 97021.
j
Repairs were made to the feedwater line supports and sanctor startup recommenood on
November 14. Within minutes of reactor criticality, a boron dilution prevention system
(BDPS) actuation occurred and borated water was iriected into the reactor. Tho
actuation occurred due to the slow power ascent at a 0.1 decade per minute startup rate.
One intermediate range instrument associated with the 'B" train BDPS momentarily went
abovo 10 X 10* amps which unblocked the BDPS actuation signal and then dropped
below 5 X 10-" amps which reanned the SDPS actuation system. Concurrently, source
range counts had doubled within the last 10 minutes which actuated BDPS. The
actuation did not occur due to operator error. The operators were observed taking the ;
appropriate actions to secure the borated water irQoction. An estimated 120 gallons c7
borated water was irSected. Attar the boration was secured, a positive 0.1 decade per
minute startup rate was observed. Thus, the negative reactivity inserted from the borated
water injection had little offect on the powerlevel. The sta: tup then continued witho t *
Incident up to 1X104 arrips.
c. Concheulo.a
l The inspe ctors concluded that the opemting crews prforming the startup from the Unit 2
refueling outage demonstrated excalient human perfom'anoe when challenged by ,
equipment failures. On November 10, the inspectors observed operator action after a
waterhammer event on the 20 tempering feedwater line. The operators entered the
appropriate procedure and quickly terminated the event. On November 14, a BDP8 -
actuat!on occurred moments after the reactor was made critical. The operators were
obswrved tenninsting the BDPS actuation quickly and appropriately. The inspectors
observed that throughout the startup, pre-evolution briefings met or exceeded
,
'
management expectat!ons, operators followed procedures, and there was continuous
supervisory involvement and ovansight.
02 Operational Status of Facilities and Equipment
L
'
02.1 Out of Service (003) Review
a. Inspection Scoon (71707)
,
i
'
The inspectors reviewed an OOS in effect and an OOS recently closind. The inspectors
also interviewed operations personnel in the work control center,
b. htoatientandfbdinali
The inspectors uviewed OOS 050001122, which was placed on essential service watSr
components for admini:Wative control to assure compliance with TS 4.7.4. The OOS was
.
5
i
l
I
'
_
_ , _ - - , . _ - , . , . . - . - . _ _ . . _ , , , . - - ... - . . _ . . _ . _ _ . _ , . . - - . _ _ _ . , _ _ . _ _ _ . - _ ~ , _ . - , - . _ , . . , -
e
<
. .
.
property prepared and authortred. M components listed on the 008 were in thu required
position with appropriate 008 cards affixed. Documentation for the 000 was compWo.
The inspectors also reviewed recently cleared 008 970012343. The 008 was placed
on 18 emergency diesel poneretor Ltarting air compressor #2 in order to perform
lubrication of the compressor motor. M components were retumed to the required
position listed for the retum-to service of the starting air compressor. M 008 tags were
removed from components. Documentation for the cleared 008 was complete.-
c. Conclusions
The inspectors concluded that the two out-of-services reviewed c wfety related
components were property placed, removed, and documented.
08 Mlaoellaneous Operatione issues (92700 and 92901))
08.1 Institute For Nuclegr Power Operations (INPO) Recod Review
The inspectors reviewed the INPO evaluation repost of Exidwood Station 1997
- performance dated October 6,1997, on November 28. The inspectors concluded that -
- there were neither findinos that effected too health and safety of the public nor that
required additional followup tr/ the resident inspectors.
08.2 (Closed) Ucensee Event Report (i PR) 50 fAZl20004-03: On Mry 23, and again on
May 24,1996, T8 3.0.3 was not entered as required by TS 3.4.6.1 when leak detection
systems woru inopereblo. The plant was placed in this condition during routine filter
changes on the containment atmosphere monitor with tim containmer.t floor drain leak
L
'
detection system flow transmltter inoperable. The containment atmosphere monitor was
returned to service prior to the expiration of the limiting candition for operation. The
licensee determined that both events were caused by Saman error. The inspectors
reviewed the licensee's completed corrective actions and considered them appropriate.
This item is closed.
11. Maintenanott
M1 Conduct of Maintenance ,
M1.1 Maintenance Activities Performed w Main Steam Isolation Valve (MSM 1MS001C
. a. Insoection8523 (62707)
On November 12,'.he inspectors observed rnanntenance actises on MSIV iMS001C.
The inspectors reviewed work request 970119298-01, *2 Drop per Second Fyrquel Leak -
on Hydraulic Pump Discherge! (no revision); reviewed and monitored the establishment
of required system status; monitored the performance of maintenance work; reviewed the-
completed wost package, and interviewed licensee po.mel at the job site.
6
, _
n-
4
,
b. Qb.es,tions end Findinas
l
l
Work request 970119798 O'l was written 10 provide instructions for the removal,
inspection and replacement of a portion of tubing tc repair leakage on the hydraulic
operator of 1MS001C. The inspectors reviewed the work package f rior to the start of the
l work, no problems were observed.
The inspectors monitored the performance of work laciuding tae estabilshment of
required system status and the removal, inspection, and reinttcIlation of the tubing.
During reinstallation of the tubing, the mechanica identified that the tubing was
misaligned which was the probsble cause of the reported leak. The tubing was property
aligned tr.d cubsequently did not leak. No problems were noted with the performance of
the work.
The inspectors reviewed the completed work package. Mhough the work package
includes a section for the documenting of as found conditlens, work performed, and root
cause, the tubing misalignment problem was not documented. Th!s was discussed with
the field supervisor. No other problems were noted w;th the completed work package.
c. Coriciusione
On November 14, inspectors observed maintenance retivities for the repair of hydrau;ic
actuator leakage oa MSlV 1MS001C. The inspectors concluded that the work package
was property prepared and the work was property performed in accordance with the work
package. However, the inspectors observed that the mechanics had to realign the
hydraul;c tubing a.id this was not documented in the work package. The inspectors
concluded that not documenting as-found conditions was a poor work practice.
M1.2 Cold Weather Preparationg :
a. Jnspection Seppjt (71714)
The inspectors reviewed the licenssa's preparations for protection from cold weather.
The inspectors reviev'ed procedure OBwCS XFT A1, ' Freezing Temperature Equipment
Protection Annual Surveillance," Revision 5. The inspectors also intery;ewed operations
and system engineering personnel,
b, Observations and Findinas
The inspectors reviewed the completed surveillance procedure OBwOS XFT-A1. The
procedure was property completed and all discrepancies were addressed with action
requests. The inspectcre verified that procedure OBwCS XFT-A1 checked safaty-related
'
systems and components that are susceptible to cold weather effects.
Only one item identified in the completed procedure was a icng standing deficiency. The
deficient item was a turbine building louver which was required to be closed for secondary
system (non safety-related) protection. Ar action request was written on June 19,1996,
to repair damper OHS VT404 LV 7.
7
l
- .. . - _ _ - - _ _ _ _ _ _ _ _
y . .
.
'
.
? .
The inspectors checked for licensee response to deficient items idenufled during
performance of the cold weather choolm. Actions to repair deflolerd items were
scheduled for repair soon after discovery. For example, the security diesel generator
jacket water cooling system did not meet saceptance criteda for anti freeze protection.
The licensee scheduled and implemented repairs within five weeks of dismvery, and
before extreme cold weather conditions were experienced.
c. Conclusions
The inspedors concluded that the licensee propedy completed cold weather
preparshs. The licensee implemented appopdate and timely corrocuve actions to
address the deficionoles identified while performing the annual oold weather surveillance
procedure. Safety-related components appeared to be protected from the effects of cold
weather.
M4 Maintenance Staff Knowledge and Performance
M4.1 Unit 2 Containment closeout inspection
a. inspection Scogi(61726)
The inspectors pe,1ormed an independent inspection of the Unit 2 containment following
the licensee's contalament locss debris inspection prior to entry into Mode 4 (hot
shutdown) from refueling outage A2R06. Tho inspectors reviewed BwV8 5.2.d.2.1,
" Visual Surveillance of Containment Recimulation Sumps,' Revision 4: 2BwoS 5.2.01,
" Containment Loose Dobrts inspection,' Revision 6; Braidwood Problem identification
Form (PlF) # 456 20196 0979; Operability Scrooning Form for PlF #456 201-96 0979;
Braidwood Updated Final Gafety Analysis Report (UFSAR), Appendix A, ' Application of
NRC Regulatory Guida," Regulatory Guide 1.82; and NRC Regulator / Guide 1.82,
" Water Sources For Long-Term Recirculation Cooling Following A Lnss-Of-Coolant
Accident,' Revision 2.
b, Observations and Findinas
on November 2, the inspecters performed a containment loose debris inspection of the
Unit 2 containment following notification from licensee management that operations
department personnel had completed the containment loose debria surveillance
inspection 2BwoS 6.2.c4. The inspectors walked down all accessible elevations inside
and outside of the missile barrier, inspectors found that all trash, rags, protective
clothing, and foreign material exclusion barrier matedals had boon removed. The
containment sump covers and screens were found free of debris. However, the
inspectors did observe several material condition problems, and loose materials. For
example, the inspectors identified the following material condition problems:
a
the 2B charcoal unit door was found unnatched;
+
charging valve,2AOV-CV8147, had a minor packing leak; _
.
seal table area radiation monitor meter,2RIA-AR303, was erroneously reading
10,000 millirem per tour;
8
. _
_ , . . . .. ..
.
. . .
'
.
.
- surface gaps larger than the 3/8 inch mesh in the outer containment toolroulation
sump screens and a hole larger than the 7/16 inch mesh in the Intermediate
containment roolroulation sump screen covers; and .
the 28 reactor cooling pump number 2 seal leakoff flow indicator reading less than
aero.
The inspectors also identifled the following examples of loose materials:
+
tools were staged near the reactor head area (426 foot elevation) with no work
requiring the tools being performed; and
sheet metal covers on two of the incore drive units were not fastened down.
The inspecaors discussed their findings with licenses managemord. The inspectors were
told that the surface gaps in the outer containmord toolroulation sump scroon had been
previously identified in May of 1996, and documented by PlF #456 201-96-0979. The
licensee told the inspectors that modification E200 97 298 woeld eliminate the surface
gaps and would be completed prior to the change from mode five to mode four. The
inspectors later verified that the modification was instal;sd. The inspootors asked if
modification E2M 97 298 would also eliminate the holes in the covers of the
Intermediate screen. The licensee told inspectors that it would not, but provided the
inspectors a copy of the operability screening justifying continued operation with the holes
in the intermediate screen covers. The inspectors reviewed the operability scrooning for
PlF #456-20196-0979 and found that the licensee had based the operebility of the
containment recirculation sump on the existence of a verticalinner screen also
constructed of 3/16 inch mesh located on the collection side of the containmord
recirculation sump weir plate. The inspectors found that the containment recirculation '
sump met the minimum design guidance found in NRC Regulatory Guide 1.82,
- Section C.1.3, with the holes in the intermediate screen covers.
\
The inspectors were concemed with the amourd of loose equipment identified during the
inspection. The inspectors obtaired a copy of 2Bwo8 5.2.o 1 that was performed on
' November 2, at 4:40 p.m. Step F.2.c required that loose tools and equipment that were
not needed for approved work in progress be removed from containment. Tlw inspectors
found that loose materials and tools were not removed; tut none of the discrepancies
were documented co the surveillance data shoot; that the'ro yas no work in p: ogress ;
associated with the incore neutron detector drives or the tools staged near the reactor
head area; and supervisory personnel were not aware that the (r. core drive mechanism
covers wste unfastened. Ucensee persomel that performed the surveillance test
procedure indicated on the surveillsnoe test data sheet tt at the requhments of
Step F.2.c were met with the exception of a clock that ricaded to be traowd.
Technical Specification 6.8.1.o states, ',n part, that mitten orocedures shall be
established, implement 6d, snd maintained covefirsg the applicable precedures. ,
recommended in Appendix A of Regulatory Guide 1.33, Revision 2. Februg 1978. 3
' ~
Regulatory Guide 1.33, Appenutr. A, Secticn 3.f. statse that there shail be instrucll",ns for
the staitup, uperat;on, and shutdown of safettrelated systems. Tha failure to fot!7.v
2RwoS 5.2.o 1 was a viola' ion of T6 6.8.1.a. (SO457/97019-01(ORP)).
9
, ,_ , - --
s
'
.
.
!
c. Conclusions
On November 2, the inspedors performed an inspecuon of the Unit 2 containmord
following noufication by the licensee that they had completed their okscout inspection
survelhanos, inspedors concluded that licensee personnel failed to identify and remove
aN loose materials from the containment. The inspectors identiflod unfastened covers on
two incore neutron detector drive mechanisms and unattended tools near the reactor
head. These were conditions that did not meet the acceptance critetta of 2Bwo8 6.2.01,
Step F.2.c.
M4.2 Burveillanos Testino of the 2A Centrifunal Chaminn Pumo
a. Inspection Soone (61726)
The inspecbra observed the performance of and reviewed procedure 2BwV81.2.3.1 1,
'American Society of Mechanical Engineers (ASME) Survenslance Requiremends For 2A
Centrifugal Charging Pump And Check Valve 2CV8480A 8troke Test," Revis!on 1. The
inspedors discussed the performance of the test with the system engineer,
b. Observations and Findinos ---
On November 24, the inspedors observed the performance of 28wV81.2.3.1 1. During
the pre-job brtefing, the system engineer discusseo the purpose of the surveillance test,
precautions and limitations, prerequisites, responslolilt!ss, contingency actions, and key
steps that required operator actions. The inspectors observed the system oncineer
obtain the required approvals for the commencement of the surveillance test and property
wmpiele the prorsquisites. During the performance of 28wV81.2.3.1 1, the inspedors
observed proper communications between the unit supervisor, nuclear station operators,
and the system engineer; proper self checkir.g; and proper independent verifications.'
'
The inspectors found that the required soceptance orlierta for pump suction p; essure,-
pump differential pressure, total flow, and pump vibration were met. The inspootors .
- observed an soceptable flow rate through 2CV8480A, the 2A centrifugal charging pump
minimum flow check valve, to varify a full stroke of the valve. The inspectors observed
the proper operation of the 2A charging pump hMcating oil system and cubical coolers.
The inspectors verilled that the pump's perfon. .ece exceeded the UFSAR pump
performance curve's minimum design performance.
g c. .QQDdilAl ons
On November 24, the incpedors observed the performance of 2BwV81.2.3.1 1 and -
corwiudod that the survoitlance test was property performed and soceptance critetta were
met. The pump's performance exceedad the minimum required performance specified in
the UFSAR.
.
MS Miscotlaneous Maintenance issues (92902)
~
M8.1 {Qjgiq$ Violation 50-40'//g6011-04a and 50-457/99011-04b: Failure To Follow Two
Procedures Regarding Maintenance Mterations and Operational Electrical Uneups. The
Ncensee retumed a redweste building ventilation damper to servios in the failed open
y 10
( , ,
. .
- .--.-
, -
'
.
.
condition following maintenance, and fskd to complete Procedure BwoP MP.08,
" Restoring Unit 2 Mein Osntrator, Main Power Transfermars 2E and 2W and
Unit Auxiliary Transformers 241 1 and 2414 * The inspectors verified that the licensee
completed the corrocuve act!ons for both eumples and that there has been no
recurrence of these spoolfic problems, This violation is closed.
M8.2 (Closed) LER 60-458/95020-Of}: On D6cember 23,1995, power range channel N43 was
placed in test for caliwst!on. Power re.nge N42 Indication began swinging by 10 percent
power, causing spurious rate inps. No other indications of changing roantor power were
present. The licensee invoked TS 3.0.3 s,nce both N42 and N43 were inoperable.
Channel N43 was rectored end TO 3.0.3 was axited. Power range channel N42 was
subsequently determined to have a pews,f suppii failure. The power supply was
replaced. The IWnssa perfomwd an anwyd: cf the failure mode for maintenance rule
applicability and determined that the bih c? not maintenance preventable. The
inspectors concluded that the licensee's correcuve actions were appropriate. This item is
closed.
E.gapineerina
E2 Engineering Support of Foollities and Equipment
E2.1 Review of Plant Modifications
.
a. inanection Scoot (37551)
The inspectors reviewed the work packages, modiilcation approval letters, modification ,
approval letter addendums, modification test procedures, and 10 CFR 50.59 safety
evaluations, for modifications E20 2-96 250, *2CV 110A/2CV 111A Trim Change";
E20 2-96 256, ' installation of Permanent Power Source For Temporary 125 Volt DC
Battery Chargers"; and E20 2 97 225, " Containment Recirculation Sump Enhancement."
The inspectors reviewed procedures NEP 04-02, " Exempt Changes," Revision 0; .
SWAP 232121, * Exempt Changes," Revision 3; and NSWP A-04, *10 CFR 50.59 Safety
Evaluation Process," Revision 0. The inspectors performed a walkdown of accessible
portions of the installed modifications,
b. Observations and Findinns
The inspectors reviewed the completed work packages for mor'ificationc E20 2 96 250,
E242 96 256, and E20 2 97 225. The inspectors noted that the work packages were
complets, Work procedures appeared to contain sufficient detail for the installation of the
mod;fications. Procedure steps were propertf initialed and verified where required. The
pre-job briefing, foreign material exclusion, and calibration documentation were included
and appeared complete.
The inspectors reviewed the modification approval letters and any modification approval
letter addendums for modifications E20 2 96 250, E20-2-96-236, and E20-2-97-225.
Each letter included a description of the modification, a discussion of applicable oodos
and specifications, a brief discussion of the 10 CFR 50.59 safety evaluation, a list of
11
)
.
t *
__
,
_ _ _ _ -
_. _ _ _ _ _ _ _ _ _ _ .
'
.
I
'
, l
l dmwings effected by the modification, cor.3truction and modification testing requirements,
t aining requirements, and a list procedures requiring review and revision. When the
modifications were required to be changed following their initial approval, the inspectors
'
four.d appropriate addendums to the modification approval letters cordaining a discussion
d the reasons for the change. The inspectors verified compliance with procedures
NEP 04-02, * Exempt Changes," and BwAP 232121, * Exempt Changes,' in tn.
processing of the modihations.
! The inspectom reviewed the post-modification test procedures performed following the
completion of the installation of each of the modifications. The inspecters found detailed
procedures for each of the modifications. The post-modification test procedures I
appeared adequate to ensure the modification performed as designed. l
'
The inspa Mors reviewed the 10 CFR 50.59 safety evaluat!ons for each modification. The
inspectors concluded th at each safety evaluation was well written, complete, and
prepared in scoordance with Procedure NSWP-A-04, *10 CFR 50.59 Safety Evaluation
'
Process." The safsty evaluations appeared adequate to determine if an unroviewed
safety questim existed. The inspectors noted that changes to approved modification
packages receive 4 additional 10 CFR 50.59 safety evaluations prior to their approval and
installation.
The inspectors looked at the physical inttallation of socessible modification hardware and
compared the installatien to the documentation contained in the work osckar,es and _
'
noted that the field installation appeared to match specifications in the work package. ;
c. Conclus;ons I
The inspectors performed a review of three safety-related A2R06 modifications and
concluded that the modifications were processed in accordance with the appropriate
procedures, were property documented, and received a proper safety evaluation.
Revisions to the modifications were property documented and received additional safety
evaluations prior to approval end installation. The inspectors co.wiudod that post-
modification test procedures were well written and adequately verified that the
,
'
modification performed as designed. The physicalinstallation of modification hardware
appeared to match the work package specifWsPons.
ES. Miscellaneous Engineering issues (92903)
E6.1 (Closed) Unresolved item 50-456/g6014-06: - Roll Up Fire Doors Failure To Close. On
'
July 3,1996, mechanical maintenance personnel performed surveillance
BwMS 3350-001, " Fire and Security Door Semi-Annual Inspection," Revision 0, and
several roll-up doors did not go closed as expected with outside air ventilation to the
room. A violation was issued in inspection Report No. 96016 (50456/96016-04(DRS);
50-457/96016 04(DRS)) for the failure of the doors to close. This issue will be tracked by
that vlotation. This item is closed.
E8.2 ' (Closed) Violation 50-456/oO21-03(DRP): 50-457/96021-03(DRP): On December 23,
-
1996, the licensee identified a through wall leak on ASME Class 3 piping in the 1A
essential service water (SX) system. The licensee failed 'o remove the 1 A SX train from ,
'
l service and take corrective actions as required by ASME Boiler and Pressure Vessel
,
12
.
em m- see +s-.-e.h. istm -s & m' eve rw- -ea+--a-+--um.er-w---ww--e+-enww--*e& w-ry-wa .-----,----a, ,,m,+ w+ ;+--+--rr 's--he us -++'s aw- erW '- vvv'--'Y-v'-'r -*-N t'w*r ftvt-- -* mew yTw-1---yr
- - _ . _ _ _ _ _ _
,
'
.
.
Code, Soodon XI. Part 60.55s(9)(4) of 10 CFR requires that aN components which are
classi6ed as ASME Code Class 3 must meet the requirements set forth in ASME
'
Secuon XI. The inspectors reviewed the corrective acGons taken by the licensee in
response to this violation and considered them to be adequate.1Es violation is closed.
4
E8.3 (Closed) Violation 50 456/g7005 04fDRP): 50-457/97005 04fDRP): Failure To Wdte !
4
10 CFR 50.59 Safety Evaluation. The licensee tecked open the door between the
auxiliary building ventilation exhaust plenum and the auxiliary building to perform ,
modification work on the auxiliary building exhaust fans and did not perform a
'
10 CFR 50.5g safety evaluation. The inspectors vedfied that the licenses changed
DwAP 1110 3, *Plard Barder impairment Program,' Revision 5, to clarify that impairments
to ventilation bounderles described in the UFSAR need to be screened for safety
evaluations. The inspedots had no further concems. This item is closed.
'
,
E8.4 (Closed) LER 64456/9601100: On September 24,1996, the licensee determined, during
the performance of a surveillance test, that four rou-up doors separoung areas containing
,
safety-related equipment from the turbine building failed to fully close under full ventilation
+
cond,tions. A review performed by system engineering personnel indicated that the
, roll-up doors were not tested following installation. The licensets immediate corrective
scuons were to close the four roll-up doors. The event was documented in inspec6on
Report No. 50-456/96014 as an Unresolved item pending the results of additional rolo-up -
door testing and a follow up inspection by regional fire protection specialists. The
inspectors det6rrr.ined that since 1991 the roll-up doors were inoperable and did not meet
the 3 hour3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> rated fire barrier lequirement. An apparent violation was written and
i documented in inspection Report No. 50 456/96016. The licensee's immediate correcGve
'
. uctions have been completed and were appropnate. The licensee's long-term corrective
actions have been identified but have not been completed. The tracking of the licensee's
long-term conective actions will be done by Violation 50 456/96016-04. This item is-
closed.
E8,5 ff& lid). : On October 12 and 25,1995, the
licensee identified that several incorrect cable separations assumptions could potentially
result in the inability to achieve and maintain safe shutdown conditions if a fire occurred in
certain fire zones. An apparent violation was written and documented in inspection ,
Report No. 50-456/96016, and subsequently received escalated enforcement without a
civil penalty. Design modifications are currently in progress to correct the deficiencies. 1
The tracking of the licensee's long-term corrective actions will be done by Violation
50 456/96016-03. This item is closed.
IV. Plant Support
-
l
- 31 Conduct of Security and Safeguards Activities
! 81.1 Vehicle Search.
,
s. Inspection Scope (71750)
J
'
The inspectors performed an inspecuon of the licensees vehicle search program. The
i. Inspectors reviewed BSP-09, " Vehicle Entry / Exit Procedure", Revision 7; reviewed
t
'
13
,
+-e, e- e- y,--,,,- e-,,,, ~ -~p ,m,,-,..,w-,.. - , ,_. _n,,,-n,nn. . , . , . _ . , , , . - - - , . - . . - - - ,
-
e,,-.,mme,,,,,,w--.n.. ,, , , , ,- , , , , , . - . . ,
o
.
.
.
associated special security instructions; interviewed security personnel; and observed the
performance of three vehicle searches.
b. Observations and Findinos
on November 21, the inspectors monitored the performance of two vehicle entry
searches and one exit search performed at the entrance to the protected area in
socordance with B8P Og, All required areas of the vehicles were searched including the
engine, passenger compartment, cargo compartment, and the undercaninge. No
prohibited llams were discovered, and no problems were noted by the inspectors. The
inspectors (nonitored security personnel control of the vehicle drivers within the gate
. area. Driver access was controlled in accordaru with 88P Og. Inspectors also
monitored the control of the main gates during the vehicle searches. Actions taken by the
security individuals including ooordinating the opening and closing of the outer gate,
raising and lowering the vehicle barrier gate arm, and opening and closing the inner gate
were in socordance with BSP Og, inspectors reviewed the security procedures
maintained at the main entrance guard shack. The onpy of BSP-Og mahtained at the..
guard shack was the latest revision and all special security instructions applicable to
BSP-Og were enclosed,
c. 99aclusions
'
The inspectors concluded that three vehicle searches observed on November 21 at the
.
. entrance to the protected arsa were performed in socordance with the appropriate
l licensee procedure and that the proper revision of the procedure was used. No problems
were observed.
V. Mananoment Meetinas
X1 Exit Meeting Summary
The inspectors presented the inspection results to members of licensee management at
the conclusion of th9 inspection on December .15,1997. The licensee acknowledged the
findings presented. The inspectors asked i Nnsee whether any materials examined
during the inspection should be conslered ; arietary. No proprietary information was
identified.
_
14
m
. .
. . . . . . . .
.
.
. _ _ _ _ _ . _ . _ .
"
,
'
.
! .
PARTIAL LIST OF PERSONS CONTACTED
Lloensee
'T. Tulon, site Vice President
- K. Schwartz, Station Manager
A. Haeger, Health Physics and Chemistry Supervisor
'R. Byers, Maintenance Superintendent
R. Graham, Work Control Superintendent
T. Simpkin, Regulatory Assurance Supervisor
C. Dunn, System Engineering Supervisor
- J. Nalewajka, industrial Safety Engineering Group Cupervisor ,
- C, Herzog, Executive Assistant
- J. Meister, Engineering Manager
- R. Wegner, Operations Manager
- M. Cassidy, Regulatory Assurance NRC Coordinator
HBQ
M. Jordan, Chief, Reactor Projects Branch 3
- C Phillips, Senior Resident inspector
- J. Adams, Resident inspector
D. Pelton, Resident inspector
T. Tongue, Project Engineer
IQNA
- T. Esper
- Denotes those who attended the exit interview conk Wn December 15,19g7.
,
__ - _ _ -_
15
i
_
._ _ _-
,
.-
,
.
INSPECTION PROCEDURES USED
IP 37551: Onsite Engineering
! IP 627C7: Maintenance Observations
IP 61726: Surveillance Observations
IP 71707: Plant Operations
IP 71714: Cold Weather Preparations
IP 71750: Plant Support Activities
IP 92700: Onsite Followup of Written Reports of Nontoutine E"ents at Power Reactor
Facliilles
IP 92901: Followup PlantOperations
IP 92902: Followup- Plant Maintenance
IP 92903: Followup - Engineering
ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
50-456/97019 01 VIO Failure to follow procedures
Chtits
50-457/9601104a VIO Failure to follow procedures
50-457/96011-04b VIO Failure to follow procedures
50 456/96014-06 URI Roll up fire doors failure to close
50-456/9602103(DRP); VIO Failure to meet ASME Boller and Pressure Vessel
50-457/96021 n3(DRP) Code
50-456/97005 04(DRP); VIO Failure to write a 10 CFR 50.59 safety evaluation
50457/97005 04(DRP)
50-456/95013-00 LER locorrect cable separations for fire protection
50 456/95013-01 LER Incorrect cable separations for fire protection
50 456/95020 @ LER Power range channel indication oscillations
50-457/96004-00 LER TS 3.0.3 was not entered as required by TS 3,4.6.1
when leak detection systems were inoperable
504 56/96011-00 LER Fire doors failure to close
Discussed
50-456/96016-03(DRS); VIO Incorrect cable separation assumptions
50-457/96016-03(DRS)
50-456/96016-04(DRS); VIO Roll up fire doors failure to test
50-457/96016-04(DRS)
_ _ __
16
)
I
.
! '
,
,
,
UST OF ACRONYMS USED
ASME American Society of Mechanical Engineers
l BDP8 Boron Dilution Prevention System
l CFR Code of Federal Regulations
'
INPO Institute for Nuclear Power
LER Licensee Event Report
MSIV Main Steam isolation Valve
NRC Nuclear Regulatory Commission
NSO Nuclear Station Operator
.
008 Out-of-service
l PDR PutJic Document Room
l PlF Problem identification Form
SX Essential Service Water
l T8 Technica: Specification
UFSAR Updated Finst safety Analysis Report
URI Unresolved item
VIO Violation
,
17
_ __9