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   !TIIJ                ~~~~;      LlJ@ I o I 5 I oI o I o I 2 I 7 I 2 101 o I 2 I o I 3 I 7 I a I© I o 12 I 2 I 3 I 7 1s I@                                                                                      -
   !TIIJ                ~~~~;      LlJ@ I o I 5 I oI o I o I 2 I 7 I 2 101 o I 2 I o I 3 I 7 I a I© I o 12 I 2 I 3 I 7 1s I@                                                                                      -
7        B                      60                61                  DOCKET NUMBER                        68    69 . EVENT OATE              74      75      REPORT CATE        . ao EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES @
7        B                      60                61                  DOCKET NUMBER                        68    69 . EVENT OATE              74      75      REPORT CATE        . ao EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES @
* [§]]] I During a planned power reduction BIT boron sample showed 19,991 ppm                                                                                                                                I
* [§))] I During a planned power reduction BIT boron sample showed 19,991 ppm                                                                                                                                I
   !]JI]              boron.Action Statement 3. 5. 4.1 implemented.Fast Speed recircula:tion
   !]JI]              boron.Action Statement 3. 5. 4.1 implemented.Fast Speed recircula:tion
   !Im                started.One batch boric acid added.BIT samples showed 21, 270 ppm bor.on. r
   !Im                started.One batch boric acid added.BIT samples showed 21, 270 ppm bor.on. r
   !]]]]             Total inoperable time, 1 hr 40 minutes. This is the third occurrence
   !))))             Total inoperable time, 1 hr 40 minutes. This is the third occurrence
[[[[]            of this type.
((((]            of this type.
[ill]
[ill]
[[[[]
((((]
7        8 9                                                                                                                                                                                            ao SYSTEM                    CAUSE                CAUSE                                                            COMP.            VAi.VE cooE                      cooE              suBcooE                    COMPONENT cooE                    SUBCOOE          SUBCOCE
7        8 9                                                                                                                                                                                            ao SYSTEM                    CAUSE                CAUSE                                                            COMP.            VAi.VE cooE                      cooE              suBcooE                    COMPONENT cooE                    SUBCOOE          SUBCOCE
   !Im 7        8 lslFI@ LPJ@ W@ lxlxlxlxlx Ix I@ t1.J@
   !Im 7        8 lslFI@ LPJ@ W@ lxlxlxlxlx Ix I@ t1.J@

Latest revision as of 00:03, 17 March 2020

LER 1978-008-03 for Salem Unit 1 Boron Concentration
ML19031A902
Person / Time
Site: Salem  PSEG icon.png
Issue date: 03/02/1978
From: Librizzi F
Public Service Electric & Gas Co
To: Grier B
NRC/IE, NRC Region 1
References
LER 1978-008-03
Download: ML19031A902 (4)


Text

PS~G e

  • ' Public Service Electric and Gas Company i

March 2, 1978 Mr. Boyce H. Grier Director of USNRC Off ice of Inspections and Enforcements Region 1 631 Park Avenu~

King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 78-08/03L P~rsuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1.b, we are submitting Licensee Event Report for Reportable Occurrence 78-08/03L. This report is required within thirty (30) days of the occurrence.

Sincerely yours,

~L~_.f.l.Y-F. P. Librizzi General Manager -

Electric Production CC: Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control 95-2001 300M 8-75

~eport Number:

e 78-08/03L Report Date: February 23, 1978 Occurrence Date: February 3, 1978 Facility: Salem Generating Station Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Inoperable Boron Injection Tank CONDITIONS PRIOR TO OCCURRENCE:

Operational Mode 1 Reactor Power: 89%

DESCRIPTION OF OCCURRENCE:

At 1520 hours0.0176 days <br />0.422 hours <br />0.00251 weeks <br />5.7836e-4 months <br /> while decreasing reactor power to clean condensate pump strainers, boron samples showed 19,991 ppm boron in the BIT. BAT's showed 20,200 ppm boron. BIT concentration being below the 20,100 ppm boron allowed by Technical Specifications required Action Statement 3.5.4.1 to be implemented. Boric Acid Transfer Pumps were placed in fast speed to increase recirculation flow. At 1608 hours0.0186 days <br />0.447 hours <br />0.00266 weeks <br />6.11844e-4 months <br />, one batch of boric acid was added to the BAT's and fast recirculation flow continued.

BIT sampling continued on a 1/2 hour schedule. At 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br /> BIT samples showed 21,270 ppm boron and Action Statement 3.5.4.1 was terminated.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

The cause of this occurrence was lack of mixing resulting from low recirculation flow.

ANALYSIS OF OCCURRENCE:

Technical Specification 3.5.4.1 states that with the Boron Injection Tank inoperable, restore the tank to operable status within one hour or be in Hot Standby and borated to a shutdown margin equivalent to 1% ~K/K at 200°F within the next six hours-; - restore the tank to operable status within the next seven days or be in Hot Standby within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

The Boron Injection Tank was returned to operable status in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> 40 minutes. The load reduction was continued until the BIT was within the boron limits.

CORRECTIVE ACTION:

Addition of boric acid to the BAT's and fast speed recirculation flow re-established BIT boron concentration.

, LER 78-08/03L

  • 2/23/78 A procedural revision will require fast speed recirculation flow to be run one shift per day to provide increased mixing.

FAILURE.DATA:

N/A Prepared by ~~~T~._L;;;;...;.."__;;;S~p~e~n~c~e~r~~

Manager Station SORC Meeting No. 10-78

  • ~ ~CONTROL BLOCK: I . I ... I - I . I0 (Pl.EASE PRINT OR TYP!6L REQUIRED INFORMATION) 1 . 6 *
  • I o*:.r 1.r1 N *,J~ I s I G Is I 1 JG)I 0 I o('-1 0 I0 I 0 I 0 I 0 I - I .QI 0 lI 4 I 1 11 1111101 I I© 7 8 9 . 1.1.CENSS! \=OOE 14 ;5 . l.ICENSE NUMBER 25 25
  • 1.ICENSE TYPE . JO 57 CAT 58 CON'T

!TIIJ ~~~~; LlJ@ I o I 5 I oI o I o I 2 I 7 I 2 101 o I 2 I o I 3 I 7 I a I© I o 12 I 2 I 3 I 7 1s I@ -

7 B 60 61 DOCKET NUMBER 68 69 . EVENT OATE 74 75 REPORT CATE . ao EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES @

  • [§))] I During a planned power reduction BIT boron sample showed 19,991 ppm I

!]JI] boron.Action Statement 3. 5. 4.1 implemented.Fast Speed recircula:tion

!Im started.One batch boric acid added.BIT samples showed 21, 270 ppm bor.on. r

!)))) Total inoperable time, 1 hr 40 minutes. This is the third occurrence

((((] of this type.

[ill]

((((]

7 8 9 ao SYSTEM CAUSE CAUSE COMP. VAi.VE cooE cooE suBcooE COMPONENT cooE SUBCOOE SUBCOCE

!Im 7 8 lslFI@ LPJ@ W@ lxlxlxlxlx Ix I@ t1.J@

9 10 11 12 1J 18 19 w@

20 SEQUENTIAi. OCCURRENCE REPORT REVISION

(.".;'\ I.EA RO L=VENTYEAA REPORT NO. COOE TYPE .'lie.

~* REPORT NUMBER I7 l 21 8

22 I l=.J 23 10 24 I 0101 26

~

27 I al 31 28 29 l.J;J JO l=1 Jl w

J2 ACTION FUTURE EFFECT SHUTDOWN (.;:;\ ATTACHMENT NPA0-4 PRIME COMP. COMPONENT TAKEN ACTION ON Pl.ANT METHOD HOURS ~ SUBMITTED FOAM :;us. SUPPt.JER MANUFACTURER W@l.QJ@)

JJ J4 w@*

JS w

JS .

I 0 I 0 I 0 111 J7 40 W@

41 ll!J@

42 l.Ll@

43 I z I9 44 19 I 9 !@

47 CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS @

(II[] I The cause of this occurrence was boron stratification caused by OJI] low recirculation flow. A procedure change will require fast speed CTIIJ recirculation flow to be established for approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> per day. I OJI]

1

  • a 9 80 FACll.ITY t3Q\ METHOD OF STATUS  % POWER OTHER STATUS \:.::J OISCOVERY DISCOVERY OESCRIPTlON @

[!JI] LLJ@ 10 I8 I 9 l@_I_ _N_/_A_ __I LlU@I Routine Boron Samples 7 8 9 10 12 11 44 45 46 80 ACTIVITY CONTENT r.;:\

. REL.EASED OF REL.EASE AMOUNT OF ACTIVITY ~ l.OCATION OF REI.EASE @

ITTIJ 7 B

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9 W(§I 10 11 N/A

. 44 45 NiA.

ao

- - PERSONNEi. EXPOSURES. - - - - ~ ---

IIITI 1 o1a 1 a NUMBER ~TYPE I.::\. OESCFllPTlON 10w~ ___N_/_A _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __.

7 8 9 11

?EFISONNEI. INJURIES 12 13

~

ao NUMBER OESCRIPTlON~

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69 NAMEOFPREPARER----*-T**..._r_~_.__s~e~e-*n.._c_e_r___________ PHONE: (609)365-7000.Salen Ext.~

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