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NAME              EPARER
NAME              EPARER
* Y PHONE:
* Y PHONE:
* _sio_2 ss0MoF P                                      -
* _sio_2 ss0MoF P                                      -


                                                                                                ;
Mr. Boyce H. Grier, Director                                      No. 2-81-06/3L ,
Mr. Boyce H. Grier, Director                                      No. 2-81-06/3L ,
Office of Inspection & Enforcement, Region 1                                      i U.S. Nuclear Regulatory Conrnission                                              I 631 Park Avenue King of Prussia, PA      19M6
Office of Inspection & Enforcement, Region 1                                      i U.S. Nuclear Regulatory Conrnission                                              I 631 Park Avenue King of Prussia, PA      19M6

Latest revision as of 17:47, 15 March 2020

LER 81-006/03L-0:on 810117,main Steam Line D Radiation Monitor Failed & During Repairs Line a Monitor Cable Was Disconnected.Caused by Technician Error.Techniques Reviewed W/Technicians
ML19351G421
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 02/13/1981
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
LER-81-006-03L, LER-81-6-3L, NUDOCS 8102230669
Download: ML19351G421 (1)


Text

- -- - ~ ~ " - ~

U.S. NuCL f AH HEGuLATGHY COMMISSION I

LICENSEE EVENT REPORT l

j CON 1HuL ULOCK: l i

l l l l l]e (PLEAsE PRINT OR TYF 4 ALL HEQulHED INFORMATION) l0 l t8 l9 lP l LICENSEE l A l P CODE l 8 l S l 2 l@l 0 l0 l- LICENSE 14 15 l0 l0 NUMBERl0 l0 l0 l- l0 l020 l@l4l1 26 l1 l1 l1 l@lbl LATl bdl@

LICENSE TYPE Ju CON'T loIiI 3",M Ql0 l 5 10 l- 10 l2 I7 i 7 l@l 0 l 1 l 1 l 7 l 8 l 1 l@l 012 l 1 l 3 l 8 l 1 l@

41 60 61 DOCKET NUVBER 68 b3 EVENT DATE 74 7b HEPORT DATE 80 EVENT DEsCniPTION AND PROBABLE CONSEOuENCES h lo lzl 1 With the plant at power the 'D' main steam line (MSL) rad monitor failed l-l- 1T1 I in the tripped condition, and was maintained tripped per Tech. Spec. I J

10187 I Tabl e 3.1.1. During repairs the ' A' monitor cable was erroneously dis- 1 i

in t sj i connected. A plant shutdown was initiated per Tech. Spec. Tabic 3.1.1. l lo le 1 i until the monitor was returned to service in approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. Be- I l o l 71 I cause the 'D' monitor remained tripped durina the event, the required l I O ,s i i protective action would have been initiated on MSL hiah rad levels. I

? 8 9 80 SYSTEM CAUSE CAUSE CODE COMP. VALVE CODE SUBCODE COYPONENT CODE SUSCODE SUBCODE

[o19l8

/ 9 lI lA l @ lA l@ l C l@ lI lN lS lT lR lU l@ { j@ W @

10 11 12 13 18 19 20 SEQUE N TI AL OCCURRENCE REPORT REVISION LE EVENT YEAR REPORT NO. CODE TYPE NO.

O a'R?S RO L8111 1-1 I o lo 161 l-l l28 0l 3l y t_j l 0l

_2a 2/ 2J 74 2b // ?J Ju 31 32 AK A T ON ON PL A T TH HOURS S B IT D FO b B. SUPPLIE MANUFACTURER lHl@lXl@

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l 0 l0 l0 l2 l 3/ lN 41 l@ [Y l@ lN l@ lG l0 l8 l0 l@

4G 42 43 44 4)

CAUSE CESCRIPTioN AND CORRECTIVE ACTIONS

[I.) OJ L _Ilm cause was technician error. Reoair work was beina done hurried 1v due l L.LL Jl to extremelv hioh temocratures in ih? area a it was assumed the 'D' I

,,,,,I monitor was next to the 'D' MS line. Proper instrument identification i j ilaj l techniques were reviewed with the technicians. The rad monitor cables l l i 14 I i will be more clearly marked during the next appropriate outage. l_

I B 9 80 STA S  % POWE R OTHER STATUS Di O RY DISCOVERY DESCRIPTION

!I i l'> l l El@ l 0 l 3 l 0 l@l N/A l l Al@l ' Operator Observation l A TiVITY CONTENT RELE ASE D OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE l1 l6ul 9[_Zj @ [,Z_j@l

/

N/A l l N/A l to 13 44 4b PERSONNEL EXFOSURES 40 NUMBER TYPE DESCRIPTION

'liIillO!01Ol@lZl@l N/A ,

.O ,hc l

PERSONNEt,~;UWiES NUMuER

  • ~". c t
  • li la l 101010 l@lDtSCmPriON@ /A t 8 if 11 12 N _,,,5, Q M *"*'

l LOSS OF OR DAMAGE TO FACILITV p' nu TYPE DESCRIP TION @* h. o 's3.f II I >l" Lz_l@l N/A l

,UensTY tem o a oESCRiPisON O ' NRC W ONI Y I>lof r.sUt r@l N /A / . [ H0llDpp ' _ _

l lj liIlllll ll l$

u 9 IU .

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NAME EPARER

  • Y PHONE:
  • _sio_2 ss0MoF P -

Mr. Boyce H. Grier, Director No. 2-81-06/3L ,

Office of Inspection & Enforcement, Region 1 i U.S. Nuclear Regulatory Conrnission I 631 Park Avenue King of Prussia, PA 19M6

Dear Mr. Grier:

This L.E.R. concerns loss of a main steam line radiation monitor j while a half logic trip was inserted due to another monitor being inoperable. (

\,

I Governing Tech. Spec. is Table 3.1.1. . L