05000313/LER-1982-010: Difference between revisions

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| document report number = LER-82-010-03L-01, LER-82-10-3L-1, NUDOCS 8206220277
| document report number = LER-82-010-03L-01, LER-82-10-3L-1, NUDOCS 8206220277
| package number = ML20054G759
| package number = ML20054G759
| document type = LICENSEE EVENT REPORT (SEE ALSO AO,RO), TEXT-SAFETY REPORT
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 2
| page count = 2
}}
}}

Revision as of 14:06, 15 March 2020

LER 82-010/03L-0:on 820511,while at 45% Full Power,Standby Hydrogen Purge Sys Failed Monthly Surveillance Test,Failing to Meet Tech Spec Requirements.Caused by Filter Saturated W/Water.Filter Replaced
ML20054G762
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 06/08/1982
From: Moeggenberg D
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20054G759 List:
References
LER-82-010-03L-01, LER-82-10-3L-1, NUDOCS 8206220277
Download: ML20054G762 (2)


LER-2082-010,
Event date:
Report date:
3132082010R00 - NRC Website

text

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NnC FORM 3f,6 U. S. NUCLE AR REGULATORY COMMISSION LICENSEE EVENT REPORT EXHlBIT A coNTRot stoCo 1 1 l l l l l@ (PLEASE PRINT OR TYPE ALL REOUIRED INFORMATION) lo j i j l AlR l A l Nj 0 l 1 lgl 010 l - 10 l0 l 0l 0l 0 l- l 0 l0tactN>t LectNSE Nuvetn 25 26 lg;4ay,6 l1l1;ll1[gl JJ l lg 6 8 C A F 6e 7 8 9 LacENSit COog .4 is CON'T lolil 3",3 LL_J@l015 9 1010131113 l@l015111118121@l01610181812 69 34 HF,OH1 DAf f 90 l@

7 8 60 6' DOCet t T Nuug g m td, EvtNT DaTE FS EVE NT DESCRIPTION AND PROBAOLE CONSEQUENCES h t o lai 10n 5/11/82 while at 45% full power, the standby Hydrogen Purge System 1 o 3 i failed the monthly surveillance test, therefore, the system failed to e o . I meet the requir_ements of T.S.3.14.1. The lead Hvdrogen Purge System wasj n s ioperable at the time of the occurrence. This occurrence is reportable I o r, iper T.S.6.12.3.2.b. Similar occurrences were reported in LER's i Io1ilI313/80-037 & 79-001. I O H l i

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, o 1 Investigation revealed that the filter was saturated with water. The i l i isource of the moisture is believed to be the seal water for the enmnrossnys i,i?i i in the system. The filter was replaced and the system was returned to 1 FTTil 1 ooerable status. In view of the history of system fouling and seal watert i i leakaae. a comnrehensive studv was initi-ated in early Aoril 1982. This

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ATTACiffENT LER N0. 50-313/82-010/03L-0 l CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (Continued) study should provide long and short term corrective action and is expected to be completed in June 1982. An LER update will be provided when appro-priate long and short tenn corrective actions have been determined.

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