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| issue date = 01/31/1988 | | issue date = 01/31/1988 | ||
| title = Monthly Operating Repts for Jan 1988.W/880215 Ltr | | title = Monthly Operating Repts for Jan 1988.W/880215 Ltr | ||
| author name = | | author name = Benson D, Stewart W, Warren L | ||
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) | | author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) | ||
| addressee name = | | addressee name = | ||
Line 16: | Line 16: | ||
=Text= | =Text= | ||
{{#Wiki_filter:VIRGINIA ELECTRIC AND POWER COMPANY | {{#Wiki_filter:POW 34-04 VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT 88-01 APPROVED: | ||
STATION MANAGER | |||
-SECTION Operating Data Report -Unit No. 1 Operating Data Report -Unit No. 2 | **6*f: 88 0 1'31,,oo | ||
-Unit No. 1 Unit Shutdowns and Power Reductions | *aso2220 1. :- osooo ,,.,o . | ||
-Unit No. 2 Average Daily Unit Power Level -Unit No. 1 Average Daily Unit Power Level -Unit No. 2 Summary of Operating Experience | pDR ADDCK - ncD. | ||
-Unit No. 1 Summary of Operating Experience | R | ||
-Unit No. 2 Facility Changes Requiring NRC Approval Facility Changes That Did Not Require NRC Approval Procedure or Method of Operation Changes that Did Not Require NRC Approval Tests and Experiments Requiring NRC Approval Tests and Experiments That Did Not Require NRC Approval Other Changes, Tests and Experiments Chemistry Report Fuel Handling -Unit No. 1 Fuel Handling -Unit No. 2 Procedure Revisions That Changed the Operating Mode Described in the FSAR Description of Periodic Test Which Were Not Completed Within the Time Limits Specified in Technical Specifications | |||
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: 9. Power Level Io Which Restricted, If Any (Net MWe): 10. Reasons For Restrictions, If Any: This Month Yr.-to-Date | - 1 SECTION PAGE Operating Data Report - Unit No. 1 1 Operating Data Report - Unit No. 2 2 Unit Shutdowns and Power Reductions - Unit No. 1 3 Unit Shutdowns and Power Reductions - Unit No. 2 4 Average Daily Unit Power Level - Unit No. 1 5 Average Daily Unit Power Level - Unit No. 2 6 Summary of Operating Experience - Unit No. 1 7 Summary of Operating Experience - Unit No. 2 7 Facility Changes Requiring NRC Approval 8 Facility Changes That Did Not Require NRC Approval 9 - 11 Procedure or Method of Operation Changes that Did Not Require NRC Approval 12 Tests and Experiments Requiring NRC Approval 13 Tests and Experiments That Did Not Require NRC Approval 14 Other Changes, Tests and Experiments 15 Chemistry Report 16 Fuel Handling - Unit No. 1 17 Fuel Handling - Unit No. 2 18 Procedure Revisions That Changed the Operating Mode Described in the FSAR 19 Description of Periodic Test Which Were Not Completed Within the Time Limits Specified in Technical Specifications 20 | ||
: 11. Hours In Reporting Period 744.0 744.0 | |||
: 17. Gross Electrical Energy Generated (MWH) 614935 614935 | OPERATING DAIA REPORT DOCKEI NO. 50-280 DAIE 2/5/88 COMPLETED BY L. A. warren TELEPHONE 804-357-3184 OPERATING STATUS | ||
INITIAL CRI'.CICALI!Y INil'IAL ELECl'RICil'Y COMMERCIAL OPERAl'ION | : 1. Unit Name: Surry I Notes | ||
: 2. Reporting Period: Jan~ 01 thru Jan. 31, 19 8 8 | |||
: 11. Hours In Reporting Period 744.0 744.0 12. Number of Hours Reactor Was Critical 744.0 744.0 13. Reactor Reserve Shutdown Hours o.o o.o 14. Hours Generator On-Line 744.0 744.0 15. Unit Reserve Shutdown Hours 0.0 o.o 16. Gross Thermal -Energy Generated (MWH) 1811065.7 1811065. 7 17. Gross Electrical Energy Generated (MWH) 606540.0 606540.0 18. Net Electrical Energy Generated (MWH) 577580.0 577580.0 19. Unit Service Factor 100% 100% 20. Unit Available Factor 100% 100% 21. Unit Capacity Factor (Using MDC Net) 99.4% 99.4% 22. Unit Capacity Factor (Using DER Net) 98. 5% 98.5% 23. Unit Forced Rate 0% 001 10 24. Shutdowns Scheduled over Next 6 Months (Type, Date, and Duration of Each): 25. If Shut Down At End Of Report Period Estimated Date of Startup: 26. Units In Test Status (Prior to Commercial Operation): | : 3. Licensed thermal Power (MWt): 2441 | ||
INITIAL CRITICALITY INITIAL ELEC'.rRICirY COMMERCIAL OPERATION | : 4. Nameplate Rating (Gross MWe): 847.5 5. | ||
6. | |||
7. | |||
Design Electrical Rating (Net MWe): | |||
Maximum Dependable Capacity (Gross MWe): | |||
Maxi.mum Dependable Capacity (Net MWe): | |||
788 | |||
" | _820 7 81 | ||
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: | |||
: 9. Power Level Io Which Restricted, If Any (Net MWe): | |||
: 10. Reasons For Restrictions, If Any: | |||
This Month Yr.-to-Date Cumulative | |||
DATE ___ 02~/_0~5~/8~8~------~ | : 11. Hours In Reporting Period 744.0 744.0 132456.0 | ||
: 12. Number of Hours Reactor Was Critical 744.0 744.0 85467.4 | |||
==~8:o:4-:3:5~7:-:3:1:8:4======~ | : 13. Reactor Reserve Shutdown Hours 0.0 o.o 3774.5 | ||
: 14. Hours Generator On-Line 744.0 744.0 83715.2 | |||
: 15. Unit Reserve Shutdown Hours 0.0 0.0 3736.2 | |||
: 16. Gross Thermal Energy Generated (MWH) 1811710.2 1811710.2 194531931.6 | |||
: 17. Gross Electrical Energy Generated (MWH) 614935 614935 62990108.0 | |||
: 18. Net Electrical Energy Generated (MWH) 585817 585817 59741193.0 | |||
: 19. Unit Service Factor 100% 100% 63.2% | |||
: 20. Unit Available Factor 100% 100% 66% | |||
(9/77) | : 21. Unit Capacity Factor (Using MDC Net) 100.8% 100.8% 58.3% | ||
: 22. Unit Capacity Factor (Using DER Net) 99. 9% 99. 9% 57.2% | |||
: 23. Unit Forced Rate 0% 0% 17 .5% | |||
: 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each): | |||
Refueling Outage April 8, 48 Days | |||
: 25. If Shut Down At End Of Report Period Estimated Date of Startup: | |||
: 26. Units In Iest Status (Prior to COl!Dllercial Operation): Forecast Achieved INITIAL CRI'.CICALI!Y INil'IAL ELECl'RICil'Y COMMERCIAL OPERAl'ION (9/77) | |||
___J | |||
OPERATING DATA REPORT DOCKET NO 50-2 8 1 DATE*_-_-_,2;1:5:1=:88:::::: | |||
COMPLETED BY L. A. warren TELEPHONE 804-357-3184 OPERATING STATUS | |||
: 1. Unit Name: Surry 2 Notes | |||
: 2. Reporting Period: Jan. 01 thru Jan. 3 L 1988 2441 3. | |||
4. | |||
Licensed Thermal Power (MWt): | |||
Nameplate Rating (Gross MWe): | |||
847.5 5. | |||
6. | |||
7. | |||
Design Electrical Rating (Net MWe): 788 820 Maximum Dependable Capacity (Gross MWe): .....;..;;;.;;.. | |||
Maxi.mum Dependable Capacity (Net MWe): 781 | |||
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: | |||
: 9. Power Level To Which Restricted, If Any (Net MWe): | |||
: 10. Reasons For Restrictions, If Any: | |||
This Month Yr.-to-Date Cumulative | |||
: 11. Hours In Reporting Period 744.0 744.0 129336.0 | |||
: 12. Number of Hours Reactor Was Critical 744.0 744.0 85410.0 | |||
: 13. Reactor Reserve Shutdown Hours o.o o.o 328.1 | |||
: 14. Hours Generator On-Line 744.0 744.0 84042.3 | |||
: 15. Unit Reserve Shutdown Hours 0.0 o.o o.o | |||
: 16. Gross Thermal -Energy Generated (MWH) 1811065.7 1811065. 7 196981428.4 | |||
: 17. Gross Electrical Energy Generated (MWH) 606540.0 606540.0 63979364.0 | |||
: 18. Net Electrical Energy Generated (MWH) 577580.0 577580.0 60654057.0 | |||
: 19. Unit Service Factor 100% 100% 65% | |||
: 20. Unit Available Factor 100% 100% 65% | |||
: 21. Unit Capacity Factor (Using MDC Net) 99.4% 99.4% 60.2% | |||
: 22. Unit Capacity Factor (Using DER Net) 98. 5% 98.5% 59.5% | |||
: 23. Unit Forced Rate 0% 001 10 14.3% | |||
: 24. Shutdowns Scheduled over Next 6 Months (Type, Date, and Duration of Each): | |||
: 25. If Shut Down At End Of Report Period Estimated Date of Startup: | |||
: 26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY INITIAL ELEC'.rRICirY COMMERCIAL OPERATION (9/77) | |||
UNIT SHUTDOWNS AND POWER REDUCTIONS . DOCKET NO. __ ______... | |||
UNIT NAME _ | |||
PAGE 3 50-280 | |||
_..;S~u::;.:*r_rv | |||
..*....:1:..______ | |||
DATE~--.0=2~/0~5./~88~~~---_, | |||
* . tw.Z.:ai,4.r,. .r. ... | |||
COMPLETED BY _ _..,..L1a.,....A....._ ie n"---~ | |||
REPORT t-ENTH JANUARY 19 8 8 TELEPHONE ___--,;:;8.:::.0..;..4-_,.3~5.:..7-...,3.;l..:.:;8..:.4~---~ | |||
Cl D | |||
-* C D | |||
"'CD D C .. | |||
LICENSEE C u E .:r II in "O | |||
GI Ill II C II NO. DAIE a. :, | |||
EVENT | |||
> D Ill D | |||
.I: :, | |||
II | |||
~ | |||
a, "O | |||
D D | |||
0. | |||
"O D | |||
CAUSE & CORRECTIVE ACTION IO I- :c II | |||
~ E 0 | |||
~ | |||
~ II | |||
::E | |||
.I: | |||
(I] C D | |||
REPORT# t) | |||
D t) tl PREVENT RECURRENCE . | |||
0 88-01 1/9/88 s 0.0 B 1 Unit was reduced to 69% power, 572 MW's to allow monthly testing of turbine valves (PT-29. | |||
e 1 2 3 4 F: Forced Reason: Method: Exhibit G - Instructions S: Scheduled A - Equipment Failure (Explain) 1 - Manual for Preparation of Data B - Maintenance or Test 2 - Manual Scram. Entry Sheets for Licensee C - Refueling 3 - Automatic Scram. Event Report (LER) File D - Regulatory Restriction 4 - Other (Explain) (NUREG 0161) | |||
E - Operator Training & License Examination 5 | |||
F - Administrative Exhibit 1 - Same Source G - Operational Error (Explain) | |||
(9/77) H - Other (Explain) | |||
PAGE 4 UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. _..,,,s_o-_2_8_1,,.....______:.. | |||
UNIT NAME __S'""'u"'"r_ry'-"'2'-------- | |||
DATE ___ 02~/_0~5~/8~8~------~ | |||
COMPLETED BY L. A. warren REPORT MONTH JANUARY 1988 TELEPHONE ==~8:o:4-:3:5~7:-:3:1:8:4======~ | |||
....D L C Cl D N C ., | |||
D u LICENSEE C C E :r L D "C II m ., ll"' | |||
C m NO. DATE a. II | |||
:, II D ll EVENT .. "C D "C CAUSE & CORRECTIVE ACTION TO | |||
>- L D II .c :, a: a, D a. D I-0 I II a: ll | |||
:E | |||
.c en C D | |||
REPORT# ;:; CJ E D | |||
CJ CJ PREVENT RECURRENCE . | |||
0 88-01 01/23/88 s o.o B 1 Unit was reduced to 70% power, 590 MW's to allow monthly testing of turbine valves (PT-29.1 e | |||
1 2 3 4 F: Forced Reason: Method: Exhibit G - Instructions S: Scheduled A - Equipment Failure (Explain) l - Manual for Preparation of Data B - Maintenance or Test 2 - Manual Scram. Entry Sheets for Licensee C - Refueling 3 - Automatic Scram. Event Report (LER) File D - Regulatory Restriction 4 - Other (Explain) (NUREG 0161) | |||
E - Operator Training & License Examination 5 | |||
F - Administrative Exhibit l - Same Source G - Operational Error (Explain) | |||
(9/77) H - Other (Explain) | |||
e AVERACE DAILY UNIT POWER LEVEL DOCICE'r No. _ _ | |||
UNI-.r s o_-_2_8_0_ __ | |||
Surry 1 DA'IE 2/08/88 COMPLETED BY L. A. warren TELEPHONE 804-357-3184 MONTH JANUARY 1988 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 787 17 791 2 787 18 791 | |||
'3 788 19 791 4 788 20 791 5 787 21 791 6 787 22 791 7 788 23 791 8 788 24 791 9 728 25 790 10 789 26 791 11 788 27 791 12 789 28 790 l'3 788 29 -791 14 789 30 | |||
* 791 15 789 31 790 16 790 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt. | |||
(9/77) | |||
AVERACE DAILY UNIT POWER LEVEL DOCKET No. | |||
UNIT Surry 2 | |||
_so_-_2__s_1____ | |||
DATE 2/08/88 COHPLETED BY L, 8. warren | |||
'rELEPHONE 804-357-3184 MONTH I8N!.L8.EY 1988 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 779 17 778 2 778 18 779 | |||
'3 778 19 778 4 777 20 778 | |||
'5 778 21 779 6 778 22 778 7 778 2 '3 731 8 779 24 776 9 777 25 777 10 778 26 776 11 778 27 776 12 778 28 777 1'3 779 29 777 14 778 30 778 1 '5 778 31 779 16 778 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt. | |||
(9/77) | |||
==SUMMARY== | ==SUMMARY== | ||
OF OPERATING EXPERIENCE MONTH/YEAR January 1988 | OF OPERATING EXPERIENCE MONTH/YEAR January 1988 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents. | ||
UNIT ONE 01-01-88 0000 | UNIT ONE 01-01-88 0000 This reporting period begins with the unit at 100% power, 830MW's. | ||
Holding power at 69% power, 572 MW's. Commenced power increase at 150 MW /hr. Unit at 100% power, 830 MW's. This reporting period ends with the unit at 100% power, 830 MW's. This reporting period begins with the unit at 100% power, 820 MW's. Commenced power reduction at 150 MW's/hr for scheduled testing of turbine valves (PT-29.1 ). Holding power at 70%, 590 MW's. Commenced power increase at 150 MW /hr. Unit at 100% power, 815 MW's. This reporting period ends with the unit at 100% power, 815 MW's. _J | 01-09-88 1000 Commenced power reduction at 150MW /hr. for scheduled testing of turbine valves (PT-29.1). | ||
\ . | 1136 Holding power at 69% power, 572 MW's. | ||
1445 Commenced power increase at 150 MW /hr. | |||
REPLACE MAIN STEAM VALVE (1-MS-104) | 1845 Unit at 100% power, 830 MW's. | ||
UNIT 1 This engineering work request installed an equivalent safety related gate valve to replace l-MS-104, an isolation globe valve for the auxiliary feedwater pump steam flow transmitter which had a bonnet steam cut. The replacement valve is of the same pressure class and material as the original valve. Therefore, there are no changes in the probability or consequences of accidents analyzed in the UFSAR, nor has the possibility of a new accident being created. The margin of safety is not affected. | 01-31-88 2400 This reporting period ends with the unit at 100% power, 830 MW's. | ||
MODIFY FEEDWATER VALVES (1/2-FW-MOV-lSOA, B/250A, B) | UNIT TWO 01-01-88 0000 This reporting period begins with the unit at 100% power, 820 MW's. | ||
EVALUATE GLAND BOLT MATERIAL CHANGE {1-CH-163, 164) UNIT 1 This engineering work request compared chemical and* mechanical properties of the old (A 19 3) and the new (A582) gland bolt materials for Westinghouse valves (2 11 -T58) to determine if the new material was acceptable. | 01-23-88 1213 Commenced power reduction at 150 MW's/hr for scheduled testing of turbine valves (PT-29.1 ). | ||
1346 Holding power at 70%, 590 MW's. | |||
1650 Commenced power increase at 150 MW /hr. | |||
1930 Unit at 100% power, 815 MW's. | |||
01-31-88 2400 This reporting period ends with the unit at 100% power, 815 MW's. | |||
_J | |||
\ . | |||
FACIIJTY CHANGES REQUIRING NRG APPROVAL MONTH/YEAR JANUARY 1988 NONE DURING THIS PERIOD | |||
F ACIUTY .NGES THAT DID NOT REQUIRE C APPROVAL MONTH/YEAR Jartuary 1988 EW.R 87-331 ADDITION OF FP CARDOX ODORIZER UNITS 1 & 2 1/29/88 This engineering work request added an odorizer to the Cardox System to enhance worker safety by providing another means of detecting a discharge of the system. | |||
The addition of odorizers does not effect the function of the Cardox System. Therefore, the enhancement does not impact plant or public health and safety nor result in an unreviewed safety question. | |||
EWR 87-400 REPLACE MAIN STEAM VALVE (1-MS-104) UNIT 1 1/12/88 This engineering work request installed an equivalent safety related gate valve to replace l-MS-104, an isolation globe valve for the auxiliary feedwater pump steam flow transmitter which had a bonnet steam cut. | |||
The replacement valve is of the same pressure class and material as the original valve. Therefore, there are no changes in the probability or consequences of accidents analyzed in the UFSAR, nor has the possibility of a new accident being created. The margin of safety is not affected. | |||
EWR 87-403 MODIFY FEEDWATER VALVES UNITS 1 & 2 1/05/88 (1/2-FW-MOV-lSOA, B/250A, B) | |||
This engineering work request evaluated modifications to the Unit 1 and 2 feedwater pump discharge valves (1-FW-MOV-150 A/B and 2-FW-MOV-250 A/B) to prevent the operator mounting studs from pulling loose from the operator body. | |||
The installation of: 1) all thread rod studs to ensure thread engagement, 2) one new stud between existing holes for support and 3) a new yoke flange will not result in an unreviewed safety question. | |||
EWR 87-410 EVALUATE GLAND BOLT MATERIAL CHANGE 1/05/88 | |||
{1-CH-163, 164) UNIT 1 This engineering work request compared chemical and* mechanical properties of the old (A 19 3) and the new (A582) gland bolt materials for Westinghouse valves (2 11 - T58) to determine if the new material was acceptable. | |||
An analysis of the impact of the valve failure as analyzed in UFSAR was mad.e. As the material's properties are equivalent, there is no effect on the UFSAR analyses. | An analysis of the impact of the valve failure as analyzed in UFSAR was mad.e. As the material's properties are equivalent, there is no effect on the UFSAR analyses. | ||
FACILITY IANGES THAT DID NOT REQUIRE.C APPROVAL MONTH/YEAR ) anuary I 988 N/A SCAFFOLD REQUEST 1/29/88 A temporary scaffold platform was constructed in | |||
Conclusion is that assumptions, bases and probabilities of accident analyses and equipment malfunctions are not affected. | # 1 EDG Room to work # 1 Diesel Room Dampers. | ||
SCAFFOLD REQUEST A temporary scaffold platform was constructed in Auxiliary Building to work FT-VS-118 and FT-VS-218. | Installation of this temporary scaffolding was reviewed for affect on accident analyses and equipment operability/function. Conclusion is that assumptions, bases and probabilities of accident analyses and equipment malfunctions are not affected. | ||
Installation of this temporary scaffolding was reviewed for affect on accident analyses and equipment operability/function. | N/A SCAFFOLD REQUEST 1/20/88 A temporary scaffold platform was constructed in Auxiliary Building to work FT-VS-118 and FT-VS-218. | ||
Conclusion is that assumptions, bases and probabilities of accident analyses and equipment malfunctions are not affected. | Installation of this temporary scaffolding was reviewed for affect on accident analyses and equipment operability/function. Conclusion is that assumptions, bases and probabilities of accident analyses and equipment malfunctions are not affected. | ||
TEMPORARY MODIFICATION Temporary modification removed and blanked the piping connection on the PG tank heat exchanger thermal relief valves, l-RV-BR-114A, B. It was determined that maintaining the PG tank heat exchanger inlet and outlet isolation valves open prevents heat exchanger overpressurization while the thermal relief valves are removed. Therefore, the radioactive liquid release probability is not increased. | TM Sl-88-2 TEMPORARY MODIFICATION 1/29/88 Temporary modification removed and blanked the piping connection on the PG tank heat exchanger thermal relief valves, l-RV-BR-114A, B. | ||
TEMPORARY MODIFICATION This temporary procedure closed manual valve 2-SW-117 and placed it under administrative control to prevent over-cooling of lube oil for 2-CH-P-lB while the pump is off. Closure of 2-SW-117 does not constitute an unreviewed safety question because it is under administrative control ensuring it will be opened if needed before operability of any plant equipment is affected. | It was determined that maintaining the PG tank heat exchanger inlet and outlet isolation valves open prevents heat exchanger overpressurization while the thermal relief valves are removed. Therefore, the radioactive liquid release probability is not increased. | ||
TM S2-88-2 TEMPORARY MODIFICATION 1/07 /88 This temporary procedure closed manual valve 2-SW-117 and placed it under administrative control to prevent over-cooling of lube oil for 2-CH-P-lB while the pump is off. | |||
TEMPORARY MODIFICATION This temporary modification placed the emergency borate valve, 2-CH-MOV-2350, under administrative control because the normal boric acid flow path from the blender was inoperable due to a heat tracing failure. Placing 2-CH-MOV-2350 under administrative control will ensure two boric-acid flow paths are available to the charging pump suction as required. | Closure of 2-SW-117 does not constitute an unreviewed safety question because it is under administrative control ensuring it will be opened if needed before operability of any plant equipment is affected. | ||
TEMPORARY MODIFICATION This temporary modification locked closed 2-RC-133 to isolate containment penetration | |||
#57 and the pressurizer vent and vapor space sample. The pressurizer vent system is used as a backup bleed path in case of a loss of heat sink transient. | FACIIJTY 'ANGES THAT DID NOT REQUIRE MONTH/YEAR January 1988 le APPROVAL TM S2-88-3 TEMPORARY MODIFICATION 1/11/88 This temporary modification closed manual valve 2-SW-168 (lube oil cooler SW isolation) under administrative control to prevent over cooling of lube oil for 2-CH-P-IA while the pump is shut down. | ||
However, the preferred path remained available. | Closure of 2-SW-168 does not constitute an unreviewed safety question since it is under administrative control ensuring it will be opened, if required, before operability of any plant equipment is affected. | ||
The pressurizer vent system can also be used to vent non-condensible gases from the pressurizer vapor space. However, the PORV's remain available if this function is required. | TM S2-88-5 TEMPORARY MODIFICATION l/26/88 This temporary modification placed the emergency borate valve, 2-CH-MOV-2350, under administrative control because the normal boric acid flow path from the blender was inoperable due to a heat tracing failure. | ||
Placing 2-CH-MOV-2350 under administrative control will ensure two boric- acid flow paths are available to the charging pump suction as required. | |||
TM S2-88-7 TEMPORARY MODIFICATION 1/26/88 This temporary modification locked closed 2-RC-133 to isolate containment penetration #57 and the pressurizer vent and vapor space sample. | |||
NONE DURING THIS PERIOD | The pressurizer vent system is used as a backup bleed path in case of a loss of heat sink transient. However, the preferred path remained available. The pressurizer vent system can also be used to vent non-condensible gases from the pressurizer vapor space. However, the PORV's remain available if this function is required. | ||
NONE DURING TIIlS PERIOD e | PROC.URE OR METHOD OF OPERATIO-HANGES THAT DID NOT REQUIRE NRG APPROVAL MONTH/YEAR January 1988 2-TOP-2015 AUXIUARY FEEDWATER CHECK VALVE 1/05/88 LEAKAGE GUIDEIJNES UNIT 2 This temporary operating procedure isolated steam generator auxiliary feedwater flow paths on Unit 2 to determine potential check valve leakage paths. | ||
UNIT NO. 1 MAX. MIN. AVG. 1.42 7.78E-1 1.24 o.o o.o o.o 7.82E-2 3.22E-2 S.43E-2 l.48E-2 6.41E-3 9.87E-3 0.26 0.12 0.19 39.3 31.0 33.3 0.66 0.41 0.54 37.6 15.1 25.1 | Since the flow paths were under administrative control during the temporary operations and since automatic actuation will return the system to the required operating condition, it was determined that an unreviewed safety question was not created. | ||
2-TOP-2015 AUXIIJARY FEEDWATER CHECK VALVE 1/26/88 LEAKAGE GUIDEIJNE UNIT 2 The temporary operating procedure was revised to extend the implementation date. | |||
'.fhe administrative control and automatic actuations remain in place; therefore, the evaluation above remains valid. | |||
SUADM-ADM-21 STATION PROCEDURES 1/26/88 This procedure revision updated the procedure deviation process to reflect the 10CFRS0.59 screening and review process. | |||
The updated procedure incorporated more stringent requirements governing procedure deviations than outlined in the administration section of Technical Specification (section 6.4) | |||
'.I'ESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRG APPROVAL MONTH/YEAR JANUARY 1988 NONE DURING THIS PERIOD | |||
___J | |||
TESTS AND EXPERIMENTS REQUIRING NRC APPROVAL MONTH/YEAR JANUARY 1988 NONE DURING THIS PERIOD | |||
OTHER CHANGES, TEST AND EXPERIMENTS MONTH/YEAR JANUARY 1988 NONE DURING TIIlS PERIOD | |||
e VIRGINIA .POWEil SURRY POWER STATION CHEMISTRY REPORT JANUARY 19 88 PRIMARY COOLANT ANALYSIS UNIT NO. 1 UNIT NO. 2 MAX. MIN. AVG. MAX. MIN. AVG. | |||
Gross Radioact., µCi/ml 1.42 7.78E-1 1.24 2.72E-1 l.27E-l 2.03E-l Suspended Solids, ppm o.o o.o o.o o.o o.o o.o Gross Tritium, µCi/ml 7.82E-2 3.22E-2 S.43E-2 1. 32E-1 2.78E-2 9.42E-2 Iodine 131 , µCi/ml l.48E-2 6.41E-3 9.87E-3 2.65E-4 7.88E-5 l.40E-4 Il'31 / Il '31 0.26 0.12 0.19 0.13 0.06 0.09 Hydrogen, cc/kg 39.3 31.0 33.3 34.7 30.3 32.0 Lithium, ppm 0.66 0.41 0.54 1. 05 o. 77 0.91 Boron-10, ppm* 37.6 15.1 25.1 87.2 70.2 78.2 oxygen, (DO), ppm <0.005 <0.005 <o.oos <0.005 <0.005 <o*. 005 Chloride, ppm 0.010 0.001 0.003 0.010 0.00? n _no3 PH@ 2c; degree Celsius 7.05 6.52 6.81 6.70 6.46 6.56 | |||
* Boron-10 | * Boron-10 | ||
* Total Boron X 0.196 | * Total Boron X 0.196 REMARKS: Unit 1: No LiOH additions made in Januarv, Deborating Bed placed in service for LiOH reroavaJ an 1-04-88 from 1115 to 1247; 1-19-88 from 1250 to 1430; 1-22-88 from 0950 to 1208; 1-29-88 from 1820 to 2031. | ||
Unit 2: No LiOH additions made in January. Cation Bed placed in service for LiOH removal on 1-3-88 from 0515 to 0844; 1-7-88 from 0945 to 1321; 1-9-88 from 1810 to 2239; 1-12-88 from 0925 to 1204; 1-15-88 from 0950 to 1326; 1-19-88 from 1810 to 2040; 1-22-88 from 1535 to 1705. | |||
RECEIVED PER SHIPMENT fl II ENRICHMENT CASK ACTIVITI LEVEL NONE D URING THIS PERIOD /\ i | |||
NONE DURING THIS PERIOD _J e* | PAGE 17 V | ||
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT | ~ | ||
e UNIT | |||
-- 1 FUEL HANDLING DATE JAN 1988 NEW OR DATE NUMBER OF NEW OR SPENT SPENT FUEL SHIPMENT I SHIPPED OR RECEIVED ASSEMBLIES PER SHIPMENT , | |||
ASSEMBLY ANSI INITIAL ENRICHMENT FUEL SHIPPINC CASK ACTIVIn LEVEL Cask #6 01-05-88 21 B02 NIA 2.57 NIA Cask #6 01-05-88 21 B03 NIA 2.57 NIA Cask #6 01-05-88 21 BOS NIA 2.57 NIA Cask #6 01-05-88 21 Bl 1 NIA 2.57 NIA Cask #6 01-05-88 21 Bl3 NIA . 2.57 NIA Cask #6 01-05-88 21 B37 NIA 2.57 NIA Cask #6 01-05-88 21 B46 NIA 2.57 NIA Cask #6 01-05-88 21 B51 NIA 2.57 NIA Cask #6 01-05-88 21 cos NIA 3.12 NIA Cask #6 01-05-88 21 Cl6 NIA 3.12 NIA Cask #6 01-05-88 21 C22 NIA 3.12 NIA Cask #6 01-05-88 21 C23 NIA 3.12 NIA Cask #6 01-05-88 21 C29 NIA 3.12 NIA Cask #6 01-05-88 21 C30 NIA 3.12 NIA Cask #6 01-05-88 21 C31 NIA 3.12 NIA Cask #6 01-05-88 n C33 NIA 3.12 NIA Cask #6 01-05-88 21 C34 NIA 3.12 N/A Cask #6 01-05-88 21 C39 NIA 3.12 Nil-. | |||
Cask #6 01-05-88 21 C41 NIA 3.12 NIA Cask #6 01-05-88 21 C45 NIA 3.12 N/A Cask* #6 01-05-88 21 C46 NIA 3.12 N/A | |||
C'.M.UJ.o J.U UNIT . 2 FUEL HANDLING DATE JAN 1988 NEW OR DATE NUMBER OF NEW OR SPENT SPENT FUEL SHIPPED OR ASSEMBLIES ASSEMBLY ANSI INITIAL FUEL SHIPPINC SHIPMENT# RECEIVED PER SHIPMENT fl II ENRICHMENT CASK ACTIVITI LEVEL NONE D URING THIS PERIOD | |||
/\ | |||
i | |||
.PAGE 19 PROCEDURE REVISIONS THAT CHANGED THE OPERATING MODE DESCRIBED IN THE FSAR MONTH/YEAR JANUARY 1988 NONE DURING THIS PERIOD | |||
e - | |||
V | |||
- DESCRIPTION OF PERIODIC TEST WHICH WERE NOT COMPLETED WITHIN THE TIME UMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR JANUARY 1988 NONE DURING THIS PERIOD | |||
_J | |||
e* | |||
VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 W. L, STEWART VxcE PRESIDENT February 15, 1988 NUCLEAR OPERATIONS U. S. Nuclear Regulatory Commission Serial No. 88-075 Attn: Document Control Desk NO/DAS:vlh Washington, D. C. 20555 Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37 Gentlemen: | |||
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of January 1988. | |||
Very truly yours, l~~ | |||
W. L. Stewart Enclosure cc: U. S. Nuclear Regulatory Commission 101 Marietta Street, N. W. | |||
Suite 2900 Atlanta, GA 30323 Mr. W. E. Holland NRC Senior Resident Inspector Surry Power Station}} |
Latest revision as of 02:56, 23 February 2020
ML18152A515 | |
Person / Time | |
---|---|
Site: | Surry |
Issue date: | 01/31/1988 |
From: | Benson D, Stewart W, Warren L VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
To: | NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM) |
References | |
88-075, 88-75, NUDOCS 8802220166 | |
Download: ML18152A515 (23) | |
Text
POW 34-04 VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT 88-01 APPROVED:
STATION MANAGER
- 6*f: 88 0 1'31,,oo
- aso2220 1. :- osooo ,,.,o .
pDR ADDCK - ncD.
R
- 1 SECTION PAGE Operating Data Report - Unit No. 1 1 Operating Data Report - Unit No. 2 2 Unit Shutdowns and Power Reductions - Unit No. 1 3 Unit Shutdowns and Power Reductions - Unit No. 2 4 Average Daily Unit Power Level - Unit No. 1 5 Average Daily Unit Power Level - Unit No. 2 6 Summary of Operating Experience - Unit No. 1 7 Summary of Operating Experience - Unit No. 2 7 Facility Changes Requiring NRC Approval 8 Facility Changes That Did Not Require NRC Approval 9 - 11 Procedure or Method of Operation Changes that Did Not Require NRC Approval 12 Tests and Experiments Requiring NRC Approval 13 Tests and Experiments That Did Not Require NRC Approval 14 Other Changes, Tests and Experiments 15 Chemistry Report 16 Fuel Handling - Unit No. 1 17 Fuel Handling - Unit No. 2 18 Procedure Revisions That Changed the Operating Mode Described in the FSAR 19 Description of Periodic Test Which Were Not Completed Within the Time Limits Specified in Technical Specifications 20
OPERATING DAIA REPORT DOCKEI NO. 50-280 DAIE 2/5/88 COMPLETED BY L. A. warren TELEPHONE 804-357-3184 OPERATING STATUS
- 1. Unit Name: Surry I Notes
- 2. Reporting Period: Jan~ 01 thru Jan. 31, 19 8 8
- 3. Licensed thermal Power (MWt): 2441
- 4. Nameplate Rating (Gross MWe): 847.5 5.
6.
7.
Design Electrical Rating (Net MWe):
Maximum Dependable Capacity (Gross MWe):
Maxi.mum Dependable Capacity (Net MWe):
788
_820 7 81
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
- 9. Power Level Io Which Restricted, If Any (Net MWe):
- 10. Reasons For Restrictions, If Any:
This Month Yr.-to-Date Cumulative
- 11. Hours In Reporting Period 744.0 744.0 132456.0
- 12. Number of Hours Reactor Was Critical 744.0 744.0 85467.4
- 13. Reactor Reserve Shutdown Hours 0.0 o.o 3774.5
- 14. Hours Generator On-Line 744.0 744.0 83715.2
- 15. Unit Reserve Shutdown Hours 0.0 0.0 3736.2
- 16. Gross Thermal Energy Generated (MWH) 1811710.2 1811710.2 194531931.6
- 17. Gross Electrical Energy Generated (MWH) 614935 614935 62990108.0
- 18. Net Electrical Energy Generated (MWH) 585817 585817 59741193.0
- 19. Unit Service Factor 100% 100% 63.2%
- 20. Unit Available Factor 100% 100% 66%
- 21. Unit Capacity Factor (Using MDC Net) 100.8% 100.8% 58.3%
- 22. Unit Capacity Factor (Using DER Net) 99. 9% 99. 9% 57.2%
- 23. Unit Forced Rate 0% 0% 17 .5%
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
Refueling Outage April 8, 48 Days
- 25. If Shut Down At End Of Report Period Estimated Date of Startup:
- 26. Units In Iest Status (Prior to COl!Dllercial Operation): Forecast Achieved INITIAL CRI'.CICALI!Y INil'IAL ELECl'RICil'Y COMMERCIAL OPERAl'ION (9/77)
___J
OPERATING DATA REPORT DOCKET NO 50-2 8 1 DATE*_-_-_,2;1:5:1=:88::::::
COMPLETED BY L. A. warren TELEPHONE 804-357-3184 OPERATING STATUS
- 1. Unit Name: Surry 2 Notes
- 2. Reporting Period: Jan. 01 thru Jan. 3 L 1988 2441 3.
4.
Licensed Thermal Power (MWt):
Nameplate Rating (Gross MWe):
847.5 5.
6.
7.
Design Electrical Rating (Net MWe): 788 820 Maximum Dependable Capacity (Gross MWe): .....;..;;;.;;..
Maxi.mum Dependable Capacity (Net MWe): 781
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
- 9. Power Level To Which Restricted, If Any (Net MWe):
- 10. Reasons For Restrictions, If Any:
This Month Yr.-to-Date Cumulative
- 11. Hours In Reporting Period 744.0 744.0 129336.0
- 12. Number of Hours Reactor Was Critical 744.0 744.0 85410.0
- 13. Reactor Reserve Shutdown Hours o.o o.o 328.1
- 14. Hours Generator On-Line 744.0 744.0 84042.3
- 15. Unit Reserve Shutdown Hours 0.0 o.o o.o
- 16. Gross Thermal -Energy Generated (MWH) 1811065.7 1811065. 7 196981428.4
- 17. Gross Electrical Energy Generated (MWH) 606540.0 606540.0 63979364.0
- 18. Net Electrical Energy Generated (MWH) 577580.0 577580.0 60654057.0
- 19. Unit Service Factor 100% 100% 65%
- 20. Unit Available Factor 100% 100% 65%
- 21. Unit Capacity Factor (Using MDC Net) 99.4% 99.4% 60.2%
- 22. Unit Capacity Factor (Using DER Net) 98. 5% 98.5% 59.5%
- 23. Unit Forced Rate 0% 001 10 14.3%
- 24. Shutdowns Scheduled over Next 6 Months (Type, Date, and Duration of Each):
- 25. If Shut Down At End Of Report Period Estimated Date of Startup:
- 26. Units In Test Status (Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY INITIAL ELEC'.rRICirY COMMERCIAL OPERATION (9/77)
UNIT SHUTDOWNS AND POWER REDUCTIONS . DOCKET NO. __ ______...
UNIT NAME _
PAGE 3 50-280
_..;S~u::;.:*r_rv
..*....:1:..______
DATE~--.0=2~/0~5./~88~~~---_,
- . tw.Z.:ai,4.r,. .r. ...
COMPLETED BY _ _..,..L1a.,....A....._ ie n"---~
REPORT t-ENTH JANUARY 19 8 8 TELEPHONE ___--,;:;8.:::.0..;..4-_,.3~5.:..7-...,3.;l..:.:;8..:.4~---~
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GI Ill II C II NO. DAIE a. :,
EVENT
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CAUSE & CORRECTIVE ACTION IO I- :c II
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(I] C D
REPORT# t)
D t) tl PREVENT RECURRENCE .
0 88-01 1/9/88 s 0.0 B 1 Unit was reduced to 69% power, 572 MW's to allow monthly testing of turbine valves (PT-29.
e 1 2 3 4 F: Forced Reason: Method: Exhibit G - Instructions S: Scheduled A - Equipment Failure (Explain) 1 - Manual for Preparation of Data B - Maintenance or Test 2 - Manual Scram. Entry Sheets for Licensee C - Refueling 3 - Automatic Scram. Event Report (LER) File D - Regulatory Restriction 4 - Other (Explain) (NUREG 0161)
E - Operator Training & License Examination 5
F - Administrative Exhibit 1 - Same Source G - Operational Error (Explain)
(9/77) H - Other (Explain)
PAGE 4 UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. _..,,,s_o-_2_8_1,,.....______:..
UNIT NAME __S'""'u"'"r_ry'-"'2'--------
DATE ___ 02~/_0~5~/8~8~------~
COMPLETED BY L. A. warren REPORT MONTH JANUARY 1988 TELEPHONE ==~8:o:4-:3:5~7:-:3:1:8:4======~
....D L C Cl D N C .,
D u LICENSEE C C E :r L D "C II m ., ll"'
C m NO. DATE a. II
- , II D ll EVENT .. "C D "C CAUSE & CORRECTIVE ACTION TO
>- L D II .c :, a: a, D a. D I-0 I II a: ll
- E
.c en C D
REPORT# ;:; CJ E D
CJ CJ PREVENT RECURRENCE .
0 88-01 01/23/88 s o.o B 1 Unit was reduced to 70% power, 590 MW's to allow monthly testing of turbine valves (PT-29.1 e
1 2 3 4 F: Forced Reason: Method: Exhibit G - Instructions S: Scheduled A - Equipment Failure (Explain) l - Manual for Preparation of Data B - Maintenance or Test 2 - Manual Scram. Entry Sheets for Licensee C - Refueling 3 - Automatic Scram. Event Report (LER) File D - Regulatory Restriction 4 - Other (Explain) (NUREG 0161)
E - Operator Training & License Examination 5
F - Administrative Exhibit l - Same Source G - Operational Error (Explain)
(9/77) H - Other (Explain)
e AVERACE DAILY UNIT POWER LEVEL DOCICE'r No. _ _
UNI-.r s o_-_2_8_0_ __
Surry 1 DA'IE 2/08/88 COMPLETED BY L. A. warren TELEPHONE 804-357-3184 MONTH JANUARY 1988 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 787 17 791 2 787 18 791
'3 788 19 791 4 788 20 791 5 787 21 791 6 787 22 791 7 788 23 791 8 788 24 791 9 728 25 790 10 789 26 791 11 788 27 791 12 789 28 790 l'3 788 29 -791 14 789 30
- 791 15 789 31 790 16 790 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
(9/77)
AVERACE DAILY UNIT POWER LEVEL DOCKET No.
UNIT Surry 2
_so_-_2__s_1____
DATE 2/08/88 COHPLETED BY L, 8. warren
'rELEPHONE 804-357-3184 MONTH I8N!.L8.EY 1988 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 779 17 778 2 778 18 779
'3 778 19 778 4 777 20 778
'5 778 21 779 6 778 22 778 7 778 2 '3 731 8 779 24 776 9 777 25 777 10 778 26 776 11 778 27 776 12 778 28 777 1'3 779 29 777 14 778 30 778 1 '5 778 31 779 16 778 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.
(9/77)
SUMMARY
OF OPERATING EXPERIENCE MONTH/YEAR January 1988 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
UNIT ONE 01-01-88 0000 This reporting period begins with the unit at 100% power, 830MW's.
01-09-88 1000 Commenced power reduction at 150MW /hr. for scheduled testing of turbine valves (PT-29.1).
1136 Holding power at 69% power, 572 MW's.
1445 Commenced power increase at 150 MW /hr.
1845 Unit at 100% power, 830 MW's.
01-31-88 2400 This reporting period ends with the unit at 100% power, 830 MW's.
UNIT TWO 01-01-88 0000 This reporting period begins with the unit at 100% power, 820 MW's.
01-23-88 1213 Commenced power reduction at 150 MW's/hr for scheduled testing of turbine valves (PT-29.1 ).
1346 Holding power at 70%, 590 MW's.
1650 Commenced power increase at 150 MW /hr.
1930 Unit at 100% power, 815 MW's.
01-31-88 2400 This reporting period ends with the unit at 100% power, 815 MW's.
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FACIIJTY CHANGES REQUIRING NRG APPROVAL MONTH/YEAR JANUARY 1988 NONE DURING THIS PERIOD
F ACIUTY .NGES THAT DID NOT REQUIRE C APPROVAL MONTH/YEAR Jartuary 1988 EW.R 87-331 ADDITION OF FP CARDOX ODORIZER UNITS 1 & 2 1/29/88 This engineering work request added an odorizer to the Cardox System to enhance worker safety by providing another means of detecting a discharge of the system.
The addition of odorizers does not effect the function of the Cardox System. Therefore, the enhancement does not impact plant or public health and safety nor result in an unreviewed safety question.
EWR 87-400 REPLACE MAIN STEAM VALVE (1-MS-104) UNIT 1 1/12/88 This engineering work request installed an equivalent safety related gate valve to replace l-MS-104, an isolation globe valve for the auxiliary feedwater pump steam flow transmitter which had a bonnet steam cut.
The replacement valve is of the same pressure class and material as the original valve. Therefore, there are no changes in the probability or consequences of accidents analyzed in the UFSAR, nor has the possibility of a new accident being created. The margin of safety is not affected.
EWR 87-403 MODIFY FEEDWATER VALVES UNITS 1 & 2 1/05/88 (1/2-FW-MOV-lSOA, B/250A, B)
This engineering work request evaluated modifications to the Unit 1 and 2 feedwater pump discharge valves (1-FW-MOV-150 A/B and 2-FW-MOV-250 A/B) to prevent the operator mounting studs from pulling loose from the operator body.
The installation of: 1) all thread rod studs to ensure thread engagement, 2) one new stud between existing holes for support and 3) a new yoke flange will not result in an unreviewed safety question.
EWR 87-410 EVALUATE GLAND BOLT MATERIAL CHANGE 1/05/88
{1-CH-163, 164) UNIT 1 This engineering work request compared chemical and* mechanical properties of the old (A 19 3) and the new (A582) gland bolt materials for Westinghouse valves (2 11 - T58) to determine if the new material was acceptable.
An analysis of the impact of the valve failure as analyzed in UFSAR was mad.e. As the material's properties are equivalent, there is no effect on the UFSAR analyses.
FACILITY IANGES THAT DID NOT REQUIRE.C APPROVAL MONTH/YEAR ) anuary I 988 N/A SCAFFOLD REQUEST 1/29/88 A temporary scaffold platform was constructed in
Installation of this temporary scaffolding was reviewed for affect on accident analyses and equipment operability/function. Conclusion is that assumptions, bases and probabilities of accident analyses and equipment malfunctions are not affected.
N/A SCAFFOLD REQUEST 1/20/88 A temporary scaffold platform was constructed in Auxiliary Building to work FT-VS-118 and FT-VS-218.
Installation of this temporary scaffolding was reviewed for affect on accident analyses and equipment operability/function. Conclusion is that assumptions, bases and probabilities of accident analyses and equipment malfunctions are not affected.
TM Sl-88-2 TEMPORARY MODIFICATION 1/29/88 Temporary modification removed and blanked the piping connection on the PG tank heat exchanger thermal relief valves, l-RV-BR-114A, B.
It was determined that maintaining the PG tank heat exchanger inlet and outlet isolation valves open prevents heat exchanger overpressurization while the thermal relief valves are removed. Therefore, the radioactive liquid release probability is not increased.
TM S2-88-2 TEMPORARY MODIFICATION 1/07 /88 This temporary procedure closed manual valve 2-SW-117 and placed it under administrative control to prevent over-cooling of lube oil for 2-CH-P-lB while the pump is off.
Closure of 2-SW-117 does not constitute an unreviewed safety question because it is under administrative control ensuring it will be opened if needed before operability of any plant equipment is affected.
FACIIJTY 'ANGES THAT DID NOT REQUIRE MONTH/YEAR January 1988 le APPROVAL TM S2-88-3 TEMPORARY MODIFICATION 1/11/88 This temporary modification closed manual valve 2-SW-168 (lube oil cooler SW isolation) under administrative control to prevent over cooling of lube oil for 2-CH-P-IA while the pump is shut down.
Closure of 2-SW-168 does not constitute an unreviewed safety question since it is under administrative control ensuring it will be opened, if required, before operability of any plant equipment is affected.
TM S2-88-5 TEMPORARY MODIFICATION l/26/88 This temporary modification placed the emergency borate valve, 2-CH-MOV-2350, under administrative control because the normal boric acid flow path from the blender was inoperable due to a heat tracing failure.
Placing 2-CH-MOV-2350 under administrative control will ensure two boric- acid flow paths are available to the charging pump suction as required.
TM S2-88-7 TEMPORARY MODIFICATION 1/26/88 This temporary modification locked closed 2-RC-133 to isolate containment penetration #57 and the pressurizer vent and vapor space sample.
The pressurizer vent system is used as a backup bleed path in case of a loss of heat sink transient. However, the preferred path remained available. The pressurizer vent system can also be used to vent non-condensible gases from the pressurizer vapor space. However, the PORV's remain available if this function is required.
PROC.URE OR METHOD OF OPERATIO-HANGES THAT DID NOT REQUIRE NRG APPROVAL MONTH/YEAR January 1988 2-TOP-2015 AUXIUARY FEEDWATER CHECK VALVE 1/05/88 LEAKAGE GUIDEIJNES UNIT 2 This temporary operating procedure isolated steam generator auxiliary feedwater flow paths on Unit 2 to determine potential check valve leakage paths.
Since the flow paths were under administrative control during the temporary operations and since automatic actuation will return the system to the required operating condition, it was determined that an unreviewed safety question was not created.
2-TOP-2015 AUXIIJARY FEEDWATER CHECK VALVE 1/26/88 LEAKAGE GUIDEIJNE UNIT 2 The temporary operating procedure was revised to extend the implementation date.
'.fhe administrative control and automatic actuations remain in place; therefore, the evaluation above remains valid.
SUADM-ADM-21 STATION PROCEDURES 1/26/88 This procedure revision updated the procedure deviation process to reflect the 10CFRS0.59 screening and review process.
The updated procedure incorporated more stringent requirements governing procedure deviations than outlined in the administration section of Technical Specification (section 6.4)
'.I'ESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRG APPROVAL MONTH/YEAR JANUARY 1988 NONE DURING THIS PERIOD
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TESTS AND EXPERIMENTS REQUIRING NRC APPROVAL MONTH/YEAR JANUARY 1988 NONE DURING THIS PERIOD
OTHER CHANGES, TEST AND EXPERIMENTS MONTH/YEAR JANUARY 1988 NONE DURING TIIlS PERIOD
e VIRGINIA .POWEil SURRY POWER STATION CHEMISTRY REPORT JANUARY 19 88 PRIMARY COOLANT ANALYSIS UNIT NO. 1 UNIT NO. 2 MAX. MIN. AVG. MAX. MIN. AVG.
Gross Radioact., µCi/ml 1.42 7.78E-1 1.24 2.72E-1 l.27E-l 2.03E-l Suspended Solids, ppm o.o o.o o.o o.o o.o o.o Gross Tritium, µCi/ml 7.82E-2 3.22E-2 S.43E-2 1. 32E-1 2.78E-2 9.42E-2 Iodine 131 , µCi/ml l.48E-2 6.41E-3 9.87E-3 2.65E-4 7.88E-5 l.40E-4 Il'31 / Il '31 0.26 0.12 0.19 0.13 0.06 0.09 Hydrogen, cc/kg 39.3 31.0 33.3 34.7 30.3 32.0 Lithium, ppm 0.66 0.41 0.54 1. 05 o. 77 0.91 Boron-10, ppm* 37.6 15.1 25.1 87.2 70.2 78.2 oxygen, (DO), ppm <0.005 <0.005 <o.oos <0.005 <0.005 <o*. 005 Chloride, ppm 0.010 0.001 0.003 0.010 0.00? n _no3 PH@ 2c; degree Celsius 7.05 6.52 6.81 6.70 6.46 6.56
- Boron-10
- Total Boron X 0.196 REMARKS: Unit 1: No LiOH additions made in Januarv, Deborating Bed placed in service for LiOH reroavaJ an 1-04-88 from 1115 to 1247; 1-19-88 from 1250 to 1430; 1-22-88 from 0950 to 1208; 1-29-88 from 1820 to 2031.
Unit 2: No LiOH additions made in January. Cation Bed placed in service for LiOH removal on 1-3-88 from 0515 to 0844; 1-7-88 from 0945 to 1321; 1-9-88 from 1810 to 2239; 1-12-88 from 0925 to 1204; 1-15-88 from 0950 to 1326; 1-19-88 from 1810 to 2040; 1-22-88 from 1535 to 1705.
PAGE 17 V
~
e UNIT
-- 1 FUEL HANDLING DATE JAN 1988 NEW OR DATE NUMBER OF NEW OR SPENT SPENT FUEL SHIPMENT I SHIPPED OR RECEIVED ASSEMBLIES PER SHIPMENT ,
ASSEMBLY ANSI INITIAL ENRICHMENT FUEL SHIPPINC CASK ACTIVIn LEVEL Cask #6 01-05-88 21 B02 NIA 2.57 NIA Cask #6 01-05-88 21 B03 NIA 2.57 NIA Cask #6 01-05-88 21 BOS NIA 2.57 NIA Cask #6 01-05-88 21 Bl 1 NIA 2.57 NIA Cask #6 01-05-88 21 Bl3 NIA . 2.57 NIA Cask #6 01-05-88 21 B37 NIA 2.57 NIA Cask #6 01-05-88 21 B46 NIA 2.57 NIA Cask #6 01-05-88 21 B51 NIA 2.57 NIA Cask #6 01-05-88 21 cos NIA 3.12 NIA Cask #6 01-05-88 21 Cl6 NIA 3.12 NIA Cask #6 01-05-88 21 C22 NIA 3.12 NIA Cask #6 01-05-88 21 C23 NIA 3.12 NIA Cask #6 01-05-88 21 C29 NIA 3.12 NIA Cask #6 01-05-88 21 C30 NIA 3.12 NIA Cask #6 01-05-88 21 C31 NIA 3.12 NIA Cask #6 01-05-88 n C33 NIA 3.12 NIA Cask #6 01-05-88 21 C34 NIA 3.12 N/A Cask #6 01-05-88 21 C39 NIA 3.12 Nil-.
Cask #6 01-05-88 21 C41 NIA 3.12 NIA Cask #6 01-05-88 21 C45 NIA 3.12 N/A Cask* #6 01-05-88 21 C46 NIA 3.12 N/A
C'.M.UJ.o J.U UNIT . 2 FUEL HANDLING DATE JAN 1988 NEW OR DATE NUMBER OF NEW OR SPENT SPENT FUEL SHIPPED OR ASSEMBLIES ASSEMBLY ANSI INITIAL FUEL SHIPPINC SHIPMENT# RECEIVED PER SHIPMENT fl II ENRICHMENT CASK ACTIVITI LEVEL NONE D URING THIS PERIOD
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.PAGE 19 PROCEDURE REVISIONS THAT CHANGED THE OPERATING MODE DESCRIBED IN THE FSAR MONTH/YEAR JANUARY 1988 NONE DURING THIS PERIOD
e -
V
- DESCRIPTION OF PERIODIC TEST WHICH WERE NOT COMPLETED WITHIN THE TIME UMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR JANUARY 1988 NONE DURING THIS PERIOD
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VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 W. L, STEWART VxcE PRESIDENT February 15, 1988 NUCLEAR OPERATIONS U. S. Nuclear Regulatory Commission Serial No.88-075 Attn: Document Control Desk NO/DAS:vlh Washington, D. C. 20555 Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37 Gentlemen:
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of January 1988.
Very truly yours, l~~
W. L. Stewart Enclosure cc: U. S. Nuclear Regulatory Commission 101 Marietta Street, N. W.
Suite 2900 Atlanta, GA 30323 Mr. W. E. Holland NRC Senior Resident Inspector Surry Power Station