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| issue date = 12/10/1993
| issue date = 12/10/1993
| title = LER 93-006-00:on 931110,feedwater Transient Occurred,Due to Loss of Ability to Control Feedwater Regulating Valve.Caused by low-low SG Level Reactor Trip.New Screw & Nut Installed in Linkage arm.W/931210 Ltr
| title = LER 93-006-00:on 931110,feedwater Transient Occurred,Due to Loss of Ability to Control Feedwater Regulating Valve.Caused by low-low SG Level Reactor Trip.New Screw & Nut Installed in Linkage arm.W/931210 Ltr
| author name = MECREDY R C, ST MARTIN J T
| author name = Mecredy R, St Martin J
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| addressee name = JOHNSON A R
| addressee name = Johnson A
| addressee affiliation = NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM), NRC OFFICE OF NUCLEAR REACTOR REGULATION (NRR)
| addressee affiliation = NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM), NRC OFFICE OF NUCLEAR REACTOR REGULATION (NRR)
| docket = 05000244
| docket = 05000244
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=Text=
=Text=
{{#Wiki_filter:ACCELERATED DISTRIBUTION DEMONS~TION SYSTEMREGULATORY INFORMATION DISTRIBUTION SYSTEM(RIDS)ACCESSION NBR:9312270027 DOC.DATE:
{{#Wiki_filter:ACCELERATED                                     DEMONS~TION               SYSTEM DISTRIBUTION REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
93/12/10NOTARIZED:
ACCESSION NBR:9312270027               DOC.DATE: 93/12/10      NOTARIZED: NO        DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester                 G 05000244 AUTH. NAME            AUTHOR AFFILIATION ST.MARTIN,J.T.       Rochester Gas & Electric Corp.
NODOCKETFACIL:50-244 RobertEmmetGinnaNuclearPlant,Unit1,Rochester G05000244AUTH.NAMEAUTHORAFFILIATION ST.MARTIN,J.T.
MECREDY,R.C.         Rochester Gas & Electric Corp.
Rochester Gas&ElectricCorp.MECREDY,R.C.
RECIP.NAME             RECIPIENT AFFILIATION
Rochester Gas&ElectricCorp.RECIP.NAME RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER93-006-00:on 931110,feedwater transient occured,due toabilitycontrollfeedwater regulating valve.CausedbyLOLOsteamgenorator levelreactortrip.Newscrew&nutinstalled inleakagearm.w/931210 ltr.DISTRIBUTION CODE:IE22TCOPIESRECEIVED:LTR iENCL/SIZE:T1TLE:50.73/50.9 LicenseeEventReport(LER),IncidentRpt,etc.DNOTES:License Expdateinaccordance with10CFR2,2.109(9/19/72).
LER    93-006-00:on 931110,feedwater transient occured,due to ability controll          feedwater regulating valve. Caused by LO LO steam genorator level reactor trip. New screw & nut installed                      D in leakage arm.w/931210 ltr.
05000244ARECIPIENT IDCODE/NAME PDl-3LAJOHNSON,A INTERNAL:
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR               i  ENCL T1TLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
AEOD/DOAAEOD/ROAB/DSP NRR/DE/EMEB NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRSS/PRPB NRR/DSSA/SRXB RES/DSIR/EIB COPIESLTTRENCL11111122111111221111RECIPIENT IDCODE/NAME PD1-3PDAEOD/DSP/TPAB NRR/DE/EELB NRR/DORS/OEAB NRR/DRCH/HICB NRR/DRIL/RPEB NRR--DSSA
                                                                          /  SIZE:
-PLBEGIEE02RGN-1~PIE01COPIESLTTRENCL111111111111111111DDEXTERNALEG&GBRYCEIJ~HNRCPDRNSICPOORE,W.22LSTLOBBYWARD11NSICMURPHYIG~A11NUDOCSFULLTXT111111DNOTETOALL"RIDS"RECIPIENTS:
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).                   05000244 A RECIPIENT                COPIES          RECIPIENT                              D COPIES ID CODE/NAME              LTTR ENCL      ID CODE/NAME       LTTR ENCL PDl-3 LA                      1    1    PD1-3 PD                1    1            D JOHNSON,A                     1    1 INTERNAL: AEOD/DOA                        1    1    AEOD/DSP/TPAB          1    1 AEOD/ROAB/DSP                 2    2    NRR/DE/EELB            1    1 NRR/DE/EMEB                   1    1    NRR/DORS/OEAB          1    1 NRR/DRCH/HHFB                 1    1    NRR/DRCH/HICB          1    1 NRR/DRCH/HOLB                 1    1    NRR/DRIL/RPEB          1    1 NRR/DRSS/PRPB                 2    2    NRR--DSSA PLB 1    1 NRR/DSSA/SRXB                 1    1      EG    IEE      02    1    1 RES/DSIR/EIB                 1    1    RGN-1~ PIE      01    1    1 EXTERNAL    EG&G BRYCE I J ~ H            2    2    L ST LOBBY    WARD      1    1 NRC PDR                      1    1    NSIC MURPHYIG A  ~      1    1 NSIC POORE,W.                 1    1    NUDOCS FULL TXT        1    1 D
PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMP1-37(EXT.20079)TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEED!DDSFULLTEXTCONVERSION REQUIREDTOTALNUMBEROFCOPIESREQUIRED:
D D
LTTR28ENCL28 E  
NOTE TO ALL "RIDS" RECIPIENTS:
<g(~VifiFNT If'ifl&#xc3;Jilif is'fiIitiiiiffffillliiiiiii ROCHESTER GASANDELECTRICCORPORATION sNeoIml~0w/',.r"eoec'ssnsc~89EASTAVENUE,ROCHESTER N.Y.14649.0001
S PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
*"ROBERTC.MECREDYVicePiesfdent OlnnnNuclearPsoducsion December10,1993TELEPHONE AREACODE71B5462700U.S.NuclearRegulatory Commission Attn:AllenR.JohnsonProjectDirectorate I-3DocumentControlDeskWashington, DC20555
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR                28  ENCL    28
 
E Neo
              <g(~VifiFNT If'ifl&#xc3;Jilif s
I ml ~ 0 w/           ',.r " eoec is 'fiIitiiiiffffillliiiiiii                                                                              'ssnsc ROCHESTER GAS AND ELECTRIC CORPORATION                    ~                                                               *"
89 EAST AVENUE, ROCHESTER N. Y. 14649.0001 ROBERT C. MECREDY                                                                          TELEPHONE Vice Piesfdent                                                                        AREA CODE 7 1B 546  2700 Olnnn Nuclear Psoducsion December 10, 1993 U.S. Nuclear Regulatory Commission Attn: Allen R. Johnson Project Directorate I-3 Document                  Control Desk Washington,                       DC  20555


==Subject:==
==Subject:==
LER93-006,Feedwater Transient, DuetoLossofAbilitytoControlFeedwater Regulating Valve,CausesaLoLoSteamGenerator LevelReactorTripR.E.GinnaNuclearPowerPlantDocketNo.50-244Inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),whichrequiresareportof,"anyeventorcondition thatresultedinamanualorautomatic actuation ofanyengineered safetyfeature(ESF),including thereactorprotection system(RPS)",theattachedLicenseeEventReportLER93-006isherebysubmitted.
LER    93-006, Feedwater Transient, Due to Loss of Ability to Control      Feedwater Regulating Valve, Causes a Lo Lo Steam Generator Level Reactor Trip R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (iv), which requires a report of, "any event or condition that resulted in a manual or automatic actuation of any engineered safety feature (ESF), including the reactor protection system (RPS)", the attached Licensee Event Report LER 93-006 is hereby submitted.
This'eventhasinnowayaffectedthepublic',s healthandsafety.Verytrulyyours,RobertC.Meedyxc:U.S.NuclearRegulatory Commission RegionI475Allendale RoadKingofPrussia,PA19406GinnaUSNRCSeniorResidentInspector 4j.OOa99312270027 931210PDRADOCK05000244SPDRy~
This 'event has in no way affected the public',s health and safety.
p~rt.l~alii*
Very  truly  yours, Robert C. Me  edy xc: U.S. Nuclear Regulatory Commission Region                I 475          Allendale Road King of Prussia, PA                  19406 Ginna            USNRC    Senior Resident Inspector 4j.OOa9 9312270027                931210 PDR    ADOCK            05000244 S                                    PDR      y~
MRCFORH366(5-92)Us.IH)cLEARREGULATDRY ccsallssioN APPROVEDBY(NBNO3150-0104 EXPIRES5/31/95LXCENSEEEVENTREPORT(LER)(Seereverseforrequirednumberofdigits/characters foreachblock)ESTIHATED BURDENPERRESPONSETOCOHPLYMITHTHISINFORHATIOH COLLECTION REQUEST:50.0HRS.FORMARDCOHHEHTSREGARDIHG BURDENESTINATETOTHEINFORNATION ANDRECORDSHANAGEHENT BRAHCH(HHBB7714),U.S.NUCLEARREGULATORY COHHISSIDM, WASHINGTON, DC20555-0001 ANDTOTHEPAPERUORK REDUCTION PROJECT(3140.0104),
 
OFFICEOFHAMAGEHENT AMDBUDGETllASHINGTOM DC20503.FAclLITYNba(1)R.E~GinnaNuclearPowerPlantDOCKETIRNBER(2)05000244PAGE(3)1OF11TITLE(4)Feeckater Transient, DuetoLossofAbilitytoControlFee>hater Regulating Valve,CausesaLoLoSteamGenerator LevelReactorTripHOHTHDAYYEAREVENTDATE5YEARLERNMBER6SEQUENTIAL NUHBERREVISIOHNUMBERHOHTHDAYYEARREPORTDATE7OTHERFACILITIES INVOLVED8FACILITYNAHEDOCKETNUNBER109393-006-00121093FACILITYHAHEDOCKETHUHBEROPERATING H(X)E(9)PQKRLEVEL(10)N09720.402(b) 20.405(a)(1)(i)20.405(a)(1)(ii) 20.405(c) 50.36(c)(1) 50.36(c)(2) 50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii) 73.71(b)73.71(c)OTHERTHISREPORTISSUBMITTED PURSUANTTOTHEREQUIREHENTS OF10CFR:Checkoneormore1120.405(a)(1)(iii) 20.405(a)(1)(iv) 20.405(a)(1)(v) 50.73(a)(2)(i) 50.73(a)(2)(ii) 50.73(a)(2)(iii)
p
LICENSEECONTACTFORTHISLER1250.73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B) 50.73(a)(2)(x)
  ~ rt. l al
(SpecifyinAbstractbelowandinText,MRCForm366ANAHEJohnT.St.Hartin-Director, Operating Experience TELEPHONE HUNGER(IncludeAreaCode)(315)524-4446GNPLETEONELINEFOREACHGNRNEMTFAILUREDESCRIBED INTHISREPORT13CAUSESYSTEHCOMPONENT BJBLCVHAMUFACTURER B042REPORTABLE TOHPRDSCAUSESYSTEHCOMPONENT HAHUFACTURER REPORTABLE TOMPRDSSUPPLEMENTAL REPORTEXPECTED14'YES(Ifyes,completeEXPECTEDSUBHISSIOM DATE)~EXPECTEDSUBHISSION DATE(15)HOMTHOAYYEARABSTRACT(Limitto1400spaces,i.e.,approximately 15single-spaced typemritten lines)(16)OnNovember10,1993,atapproximately 0848EST,withthereactoratapproximately 974reactorpower,theabilitytocontrolthe>>A<<mainfeedwater regulating valvewaslost.Thisresultedinsteamgenerator leveltransients.
          ~
At0850EST,thereactortrippedonLoLolevel(</=174)inthe<<A>>steamgenerator.
i i*
TheControlRoomoperators performed theactionsofprocedures E-0andES-0.1.Theunderlying causewasdetermined tobedisconnection ofthe<<A<<mainfeedwater regulating valvepositioner feedbacklinkagearmfromthevalveactuatorlinkagerod,duetodisengagement oftheconnecting screwandnut.(ThiseventisNUREG-1220 (B)causecode.)Corrective actionwastoinstallanewscrewandnut.Corrective actiontoprecluderepetition isoutlinedinSectionV(B).HRCFORH366(5-92)  
 
MRC FORH    366                                    U s. IH)cLEAR REGULATDRY  ccsallssioN           APPROVED BY    (NB  NO  3150-0104 (5-92)                                                                                                          EXPIRES  5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY MITH THIS INFORHATIOH COLLECTION REQUEST: 50.0 HRS.
LXCENSEE EVENT REPORT                      (LER)                      FORMARD COHHEHTS REGARDIHG  BURDEN ESTINATE TO THE INFORNATION AND RECORDS HANAGEHENT BRAHCH (HHBB 7714), U.S. NUCLEAR REGULATORY COHHISSIDM, (See reverse    for required  number  of digits/characters for each block)          WASHINGTON, DC 20555-0001       AND TO THE PAPERUORK REDUCTION   PROJECT     (3140.0104),       OFFICE    OF HAMAGEHENT AMD BUDGET llASHINGTOM DC 20503.
FAclLITY Nba (1)       R. E ~ Ginna          Nuclear Power Plant                            DOCKET IRNBER  (2)                       PAGE  (3) 05000244                          1  OF 11 TITLE (4) Feeckater Transient, Due to Loss of            Ability to    Control Fee>hater Regulating Valve, Causes      a Lo Lo Steam    Generator Level Reactor Trip EVENT DATE      5                  LER NMBER    6                  REPORT DATE    7              OTHER  FACILITIES INVOLVED 8 SEQUENTIAL        REVISIOH                          FACILITY NAHE                      DOCKET NUNBER HOHTH      DAY      YEAR    YEAR                                    HOHTH    DAY    YEAR NUHBER          NUMBER 10      93      93      006                 00        12      10      93 FACILITY HAHE                      DOCKET HUHBER OPERATING                  THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREHENTS OF 10        CFR:      Check one  or mor e    11 H(X)E (9)
N        20.402(b)                           20.405(c)                      50.73(a)(2)(iv)                73.71(b)
PQKR                      20.405(a   )(1)(i)                   50.36(c)(1)                    50.73(a)(2)(v)                 73.71(c) 097 LEVEL    (10)                 20.405(a)(1)(ii)                     50.36(c)(2)                   50.73(a)(2)(vii)               OTHER 20.405(a)(1)(iii)                   50.73(a)(2)(i)                 50.73(a)(2)(viii)(A) (Specify in 20.405(a)(1)(iv)                     50.73(a)(2)(ii)               50.73(a)(2)(viii)(B) Abstract and in Text, below 20.405(a)(1)(v)                     50.73(a)(2)(iii)               50.73(a)(2)(x)             MRC Form 366A LICENSEE CONTACT FOR THIS LER      12 NAHE      John T. St. Hartin - Director, Operating Experience                                     TELEPHONE HUNGER     (Include Area    Code)
(315) 524-4446 GNPLETE ONE LINE    FOR EACH  GNRNEMT FAILURE DESCRIBED IN THIS REPORT          13 REPORTABLE                                                                      REPORTABLE CAUSE        SYSTEH      COMPONENT    HAMUFACTURER                                CAUSE    SYSTEH    COMPONENT      HAHUFACTURER TO HPRDS                                                                        TO MPRDS B          JB            LCV            B042 SUPPLEMENTAL REPORT EXPECTED      14                                  EXPECTED              HOMTH      OAY        YEAR
    'YES                                                                                         SUBHISSION (If yes,   complete  EXPECTED SUBHISSIOM DATE) ~                                           DATE (15)
ABSTRACT      (Limit to  1400 spaces,   i.e., approximately     15 single-spaced typemritten lines)     (16)
On November                10, 1993, at approximately 0848 EST, with the reactor at approximately 974 reactor power, the ability to control the >>A<< main feedwater regulating valve was lost. This resulted in steam generator level transients. At 0850 EST, the reactor tripped on Lo Lo level (</=
174) in the <<A>> steam generator.                                     The Control Room operators performed the actions of procedures E-0 and ES-0.1.
The      underlying cause was determined to be disconnection of the <<A<< main feedwater regulating valve positioner feedback linkage arm from the valve actuator linkage rod, due to disengagement of the connecting screw and nut. (This event is NUREG-1220 (B) cause code.)
Corrective action was to install a new screw and nut. Corrective action to preclude repetition is outlined in Section V (B).
HRC FORH    366  (5-92)


RCFORH366A5-92)U.SIN)CLEARREGULATORY (XIIISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBY(NRINO.3150-0104 EXPIRES5/31/95ESTIHATEDBURDEHPERRESPOHSETOCOHPLYWITHTHISIHFORHATIOH COLLECTIOH REGUEST:50.0NRS.FORWARDCOHHENTSREGARDIHGBURDENESTIHATETOTHEINFORHATION ANDRECORDSHANAGEHENT BRANCN(HNBB7714),U.S.NUCLEARREGULATORY COHHISSIOH, WASHINGTON, DC20555-0001 ANDTOTHEPAPERWORK REDUCTION PROJECT(3140-0104)
RC FORH  366A                                U.S IN)CLEAR REGULATORY (XIII SSI  ON              APPROVED BY (NRI NO. 3150-0104 5-92)                                                                                                  EXPIRES  5/31/95 EST IHATED BURDEH    PER  RESPOHSE  TO  COHPLY  WITH THIS IHFORHATIOH COLLECTIOH REGUEST: 50.0 NRS.
~OFFICEOFHANAGEHENT ANDBUDGETWASHINGTON DC20503.FACILITYIWK1R.E.GinnaNuclearPowerPlantDOCKETHINBER205000244YEAR93LERHWBER6SEQUENTIAL REVISIONPAGE3pp2OF11--006-EXT(Ifmorespaceisrequired, useadditional copiesofNRCForm366A)(17)I.PRE-EVENT PLANTCONDITIONS Theplantwasatapproximately 97%steadystatereactorpower.Themonthlysurveillance testofthe"A"auxiliary feedwater (AFW)pumpwasinprogress, usingprocedure PT-16M-A(Auxiliary Feedwater Pump"A"-Monthly).
FORWARD  COHHENTS REGARD IHG BURDEN EST IHATE TO LICENSEE EVENT REPORT (LER)                                          THE  INFORHATION AND RECORDS HANAGEHENT BRANCN TEXT CONTINUATION                                          (HNBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOH, WASHINGTON, DC 20555-0001       AND TO THE PAPERWORK REDUCTION     PROJECT     (3140-0104) ~   OFFICE    OF HANAGEHENT AND BUDGET      WASHINGTON    DC 20503.
II.DESCRIPTION OFEVENTA.DATESANDAPPROXIMATE TIMESOFMAJOROCCURRENCES:
FACILITY  IWK  1                      DOCKET HINBER    2              LER HWBER    6                  PAGE  3 YEAR      SEQUENTIAL      REVISION R.E. Ginna Nuclear Power Plant                                05000244              93    -- 006               pp        2 OF 11 EXT (If more  space  is required, use additional copies of  NRC Form 366A)     (17)
oNovember10,1993,0850EST:Eventdateandtime.oNovember10,1993,0850EST:Discovery dateandtime.oNovember10,1993,0850EST:ControlRoomoperators verifybothreactortripbreakersopen,andallcontrolandshutdownrodsinserted.
I.       PRE-EVENT PLANT CONDITIONS The plant was at approximately 97% steady state reactor power.
oNovember10,1993,0851EST:ControlRoomoperators manuallystopbothmainfeedwater pumpstolimitareactorcoolantsystemcooldown.
The monthly surveillance test of the "A" auxiliary feedwater (AFW) pump was in progress, using procedure PT-16M-A (Auxiliary Feedwater Pump "A" Monthly).
oNovember10,1993,0852EST:ControlRoomoperators manuallyclosebothmainsteamisolation valvestolimitareactorcoolantsystemcooldown.
II.     DESCRIPTION OF EVENT A. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
oNovember10,1993,1045EST:Plantstabilized athotshutdowncondition.
o        November 10, 1993, 0850 EST: Event date and                                      time.
NRCFORH366A(5-92) 1 NRCFORN366A(5-92)U.SNUCLEARREGULATORY CQWISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBY(NBNO.3150-0104 EXPIRES5/31/95ESTIHATED BURDENPERRESPONSETOCDHPLYWITHTHISINFORHATIOH COLLECTIOH REQUEST:50.0HRS.FORWARDCONNENTSREGARDING BURDENESTINATETOTHEIHFORHATIOH AHDRECORDSHAHAGEHEHT BRANCH(HNBB7714),U.S.NUCLEARREGULATORY COHHISSIOH, WASHIHGTOH, DC20555-0001 ANDTOTHEPAPERWORK REDUCTION PROJECT(3140-0104),
o        November 10, 1993, 0850 EST:                     Discovery date and time.
OFFICEOFNANAGEHENT ANDBUDGETWASHINGTON DC20503.FACILITYNANE1R.E.GinnaNuclearPowerPlantDOCKETNINBER2YEAR0500024493LERNINBER6SEQUENTIAL
o        November 10, 1993, 0850 EST:                       Control Room operators verify both reactor trip breakers                            open, and          all control and shutdown rods              inserted.
-006-REVISION00PAGE33OF11TEXT(Ifmorespeceisrequired, useadditional copiesofNRCForm366A)(17)B.EVENT:OnNovember10,1993,surveillance testprocedure PT-16M-Awasinitiated, atapproximately 0835EST.Aspartofthistest,the>>A>>AFWpumpwasstarted.Controlofthemainfeedwater regulating valve(MFRV)andbypassfeedwater regulating valveforthe>>Asteamgenerator (S/G)wasshiftedtothe"Manual"mode,andtheControlRoomoperatorslightlyclosedthe>>A>>MFRV.The>>A>>MFRVinitially startedclosing,andthenappearedtodriftopen,basedonindications ofincreased feedwater flowtothe>>A>>S/G.DespitetheeffortsoftheControlRoomoperators toclosethe>>A>>MFRV,the>>A>>MFRVcontinued todriftopen.TheAdvancedDigitalFeedwater ControlSystem(ADFCS)responded asdesigned, andshiftedallfeedwater regulating valves(forbothS/Gs)to"Manual".
o        November 10, 1993, 0851 EST:                       Control          Room    operators manually stop both main feedwater pumps to                                    limit a reactor coolant system cooldown.
TheControlRoomoperators terminated PT-16M-Aandturnedoffthe>>A>>AFWpump.>>A>>S/Glevelcontinued toincrease, untilitreachedthehighleveloverridesetpointof674.The>>A>>MFRVclosedasdesignedat674level.Allfeedwater flowwasnowdirectedtothe>>B>>S/G.The>>B>>S/Glevelalsoreachedthe674highleveloverridesetpoint, andthe>>B>>MFRVclosed.TheMFRVsreopenedasdesignedwhenS/Glevelsdecreased tolessthan674.Duetothepositioner feedbacklinkagefailure,theControlRoomoperators hadlosttheabilitytocontrol>>A>>S/Glevel.The>>A>>S/Gleveldecreased to<174,resulting inareactortriponS/GLoLolevel,at0850EST.HRCFORN366A(5.92)  
o        November 10, 1993, 0852 EST: Control Room operators manually close both main steam isolation valves to limit a reactor coolant system cooldown.
o        November 10, 1993, 1045 EST: Plant stabilized at hot shutdown condition.
NRC FORH  366A  (5-92)


NRCFORH366A(5-92)U.S.NICLEARREGULATORY C(SIIISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBY(SIINO-3150-0104 EXPIRES5/31/95ESTIHATED BURDENPERRESPONSETOCOHPLYMITHTHISIHFORHATIOH COLLECTION REQUEST:50.0HRS~FORNARDCOHHENTSREGARDING BURDENESTIHATETOTHEIHFORHATIOH ANDRECORDSHANAGEHEHT BRAHCH(HHBB7714),U.S.NUCLEARREGULATORY COHHISSIOH, MASHINGTON, DC20555-0001 ANDTOTHEPAPERlJORK REDUCTION PROJECT(3150.0104),
1 NRC FORN 366A                              U.S NUCLEAR REGULATORY CQWISS ION              APPROVED BY  (NB NO. 3150-0104 (5-92)                                                                                            EXPIRES  5/31/95 ESTIHATED BURDEN PER RESPONSE TO CDHPLY WITH THIS INFORHATIOH COLLECTIOH REQUEST: 50.0 HRS.
OFFICEOFHANAGEHENT ANDBUDGETNASHINGTON DC20503.FACILITYHAHE1R.E.GinnaNuclearPowerPlantDOCKETNWBER2YEAR0500024493LERNEER6SEQUENTIAL--006-REVISION00PAGE34OF11TEXT(lfmorespaceisrequired, useadditional copiesofHRCForm366A)(17)TheControlRoomoperators performed theimmediate actionsofEmergency Operating Procedure E-0(ReactorTriporSafetyInjection),
FORWARD CONNENTS REGARDING BURDEN ESTINATE TO LICENSEE EVENT REPORT (LER)                                    THE IHFORHATIOH AHD RECORDS HAHAGEHEHT BRANCH TEXT CONTINUATION                                      (HNBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOH, WASHIHGTOH, DC 20555-0001       AND TO THE PAPERWORK REDUCTION     PROJECT     (3140-0104),   OFFICE    OF NANAGEHENT AND BUDGET      WASHINGTON  DC  20503.
andtransitioned
FACILITY NANE  1                      DOCKET NINBER  2              LER NINBER    6                PAGE  3 YEAR SEQUENTIAL      REVISION R.E. Ginna Nuclear Power Plant                            05000244            93    006                 00      3 OF      11 TEXT (If more spece  is required, use additional copies of NRC Form 366A)   (17)
.toEmergency Operating Procedure ES-0.1(ReactorTripResponse) whenitwasverifiedthatbothreactortripbreakerswereopen,allcontrolandshutdownrodswereinserted, andsafetyinjection wasnotactuatedorrequired.
B. EVENT:
Duringperformance ofE-O,theControlRoomoperators notedthecontinuing RCScooldownandincreasing S/Glevels,andreferredtoFunctional Restoration procedure FR-H.3(Response toSteamGenerator HighLevel).Theoperators verifiedthattheAFWpumpshadstarted,asdesigned, ontheLoLoS/Glevel.UsingtheguidanceofFR-H.3,theymanuallystoppedbothmainfeedwater pumps.Inaddition, bothmainsteamisolation valves(MSIVs)weremanuallyclosedbytheControlRoomoperators.
On    November 10, 1993,              surveillance test procedure PT-16M-A was initiated,               at approximately 0835 EST. As part of this test, the >>A>> AFW pump was started.
Theseactionsmitigated theRCScooldown.
Control of the main feedwater regulating valve (MFRV) and bypass feedwater regulating valve for the >>A steam generator (S/G) was shifted to the "Manual" mode, and the Control Room operator slightly closed the >>A>> MFRV.
Theplantwassubsequently stabilized inhotshutdown, usingprocedure 0-2.2(PlantShutdownFromHotShutdowntoColdShutdown) atapproximately 1045EST.C.INOPERABLE STRUCTURES, COMPONENTS, ORSYSTEMSTHATCONTRIBUTED TOTHEEVENT:NoneD.OTHERSYSTEMSORSECONDARY FUNCTIONS AFFECTED:
The >>A>> MFRV initially started closing, and then appeared to drift open, based on indications of increased feedwater flow to the >>A>> S/G.
NoneNRCFORH366A(5-92)  
Despite the efforts of the Control Room operators to close the >>A>> MFRV, the >>A>> MFRV continued to drift open. The Advanced Digital Feedwater Control System (ADFCS) responded as designed, and shifted all feedwater regulating valves (for both S/Gs) to "Manual". The Control Room operators terminated PT-16M-A and turned off the >>A>> AFW pump. >>A>> S/G level continued to increase, until it reached the high level override setpoint of 674. The >>A>> MFRV closed as designed at 674 level. All feedwater flow was now directed to the >>B>> S/G. The >>B>> S/G level also reached the 674 high level override setpoint, and the
                >>B>> MFRV        closed.
The MFRVs reopened              as designed when S/G levels decreased to less than 674. Due to the positioner feedback linkage failure, the Control Room operators had    lost the ability to control                    >>A>> S/G level.                 The >>A>>
S/G    level    decreased        to  <  174,     resulting          in  a  reactor trip on S/G Lo Lo level, at 0850 EST.
HRC FORN 366A (5.92)


NRCFORN366A(5-92)U.S.WCLEARREGUUlTORY CQHISSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBYWNO.3150-0104 EXPIRES5/31/95ESTINATEDBURDEHPERRESPOHSETOCOHPLYNITHTHISIHFORHATI OHCOLLECTIONREQUEST:50.0HRS.FORllARDCONHENTSREGARDING BURDENESTINATETOTHEINFORHATIONAHDRECORDSHANAGEKENT BRANCH(HHBB7714),U.S~NUCLEARREGULATORY CONNISSIOH, llASHINGTON, DC20555-0001 ANDTOTHEPAPERIKNK REDUCTION PROJECT(3110-0104),
NRC FORH 366A                              U.S. NICLEAR REGULATORY C(SIIISSION              APPROVED BY  (SII NO- 3150-0104 (5-92)                                                                                             EXPIRES  5/31/95 ESTIHATED BURDEN    PER  RESPONSE  TO  COHPLY    MITH THIS IHFORHATIOH COLLECTION REQUEST: 50.0          HRS ~
OFFICEOFHANAGENENT ANDBUDGETIIASNINGTOH DC20503.FACILITYHANE1R.E.GinnaNuclearPowerPlantDOCKETNINBER20500024493-006--00LERHWSER6YEARSEQUENTIAL REVISIONPAGE35OF11TEXT(Ifmorespaceisrequired, useadditional copiesofNRCForm366A)(17)E.METHODOFDISCOVERY:
FORNARD  COHHENTS  REGARDING BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER)                                      THE IHFORHATIOH AND RECORDS HANAGEHEHT BRAHCH TEXT CONTINUATION                                        (HHBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOH, MASHINGTON, DC 20555-0001      AND TO THE PAPERlJORK REDUCTION    PROJECT    (3150.0104),    OFFICE    OF HANAGEHENT AND BUDGET NASHINGTON DC 20503.
Thiseventwasimmediately apparentduetothelossofabilitytocontrolfeedwater flowtothe"A"S/G.Thereactortripwasimmediately apparentduetoalarmsandindications intheControlRoom.F.OPERATORACTION:Afterthereactortrip,theControlRoomoperators performed theactionsofEmergency Operating Procedures E-0(ReactorTriporSafetyInjection) andES-0.1(ReactorTripResponse).
FACILITY HAHE  1                      DOCKET NWBER    2              LER NEER    6                PAGE  3 YEAR SEQUENT IAL      REVISION R.E. Ginna Nuclear Power Plant                            05000244                                                    4 OF 11 93    -- 006              00 TEXT (lf more space  is required, use additional copies of HRC Form 366A)    (17)
Themainfeedwater pumpsweremanuallystoppedandtheMSIVsweremanuallyclosedtolimitfurtherRCScooldown.
The    Control Room operators performed the immediate actions of Emergency Operating Procedure E-0 (Reactor Trip or Safety Injection), and transitioned .to Emergency Operating Procedure ES-0.1 (Reactor Trip Response) when            it  was verified that both reactor trip breakers were open, all control and shutdown rods were inserted, and safety injection was not actuated or required. During performance of E-O, the Control Room operators noted the continuing RCS cooldown and increasing S/G levels, and referred to Functional Restoration procedure FR-H.3 (Response to Steam Generator High Level). The operators verified that the AFW pumps had started, as designed, on the Lo Lo S/G level. Using the guidance of FR-H.3, they manually stopped both main feedwater pumps. In addition, both main steam isolation valves (MSIVs) were manually closed by the Control Room operators. These actions mitigated the RCS cooldown.
Theplantwasstabilized athotshutdown.
The plant was subsequently stabilized in hot shutdown, using procedure 0-2.2 (Plant Shutdown From Hot Shutdown to Cold Shutdown) at approximately 1045 EST.
Subsequently, theControlRoomoperators notifiedhighersupervision andtheNuclearRegulatory Commission per10CFR50.72, Non-Emergency, 4HourNotification atapproximately 1030EST.G.SAFETYSYSTEMRESPONSES:
C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:
NoneIII.CAUSEOFEVENTA.IMMEDIATE CAUSE:Thereactortripwasdueto"A"S/GLoLolevel(</=174).B.INTERMEDIATE CAUSE:The"A"S/GLoLolevel(</=174)wasduetodecreased feedwater flowtothe"A"S/G,causedbylossofabilitytocontrolthe"A"MFRV.NRCFORN366A(5-92) 0 NRCFORH366A(5-92)U.SIRKLEARREGULATORY C(IIIISSI(HI LICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBY(SRIHO.3150-0104 EXPIRES5/31/95ESTIHATED BURDENPERRESPONSETOCOHPLYlllTHTHISINFORHATION COLLECTIOH REQUEST:50.0NRS.FORIIARDCOHHENTSREGARDING BURDENESTIHATETOTHEINFORHATIOH ANDRECORDSHANAGEHENT BRANCH(HNBB7714),U.S.NUCLEARREGULATORY COHHISSIOH, llASHIHGTOH, DC20555-0001 ANDTOTHEPAPERNORK REDUCTION PROJECT(3140-0104),
None D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
OFFICEOFHANAGEHENT ANDBUDGETHASHINGTON OC20503.FACILITYIWK1R.E.GinnaNuclearPowerPlantDOCKETMMBER205000244YEAR93LERABER6SEQUENTIAL
None NRC FORH 366A (5-92)
--006-REVISIOH00PAGE36OF11TEXT(Ifmorespaceisrequired, useadditional copiesofNRCForm366A)(17)C.ROOTCAUSE:Theunderlying causeofthelossofability.tocontrolthe"A"MFRVwasthedisconnection ofthepositioner feedbacklinkagearmfromthevalveactuatorlinkagerodonthe"A"MFRV,duetodisengagement oftheconnecting screwandnut.(ThiseventisNUREG-1220 (B)causecode,Design,Manufacturing, Construction/
 
NRC FORN  366A                                  U.S. WCLEAR REGUUlTORY CQHISS ION              APPROVED BY  W NO. 3150-0104 (5-92)                                                                                                EXPIRES  5/31/95 EST INATED BURDEH    PER  RESPOHSE  TO  COHPLY    NITH THIS IHFORHATIOH COLLECT ION REQUEST:       50.0  HRS.
FORllARD CONHENTS REGARDING BURDEN EST INATE TO LICENSEE EVENT REPORT (LER)                                        THE INFORHATION AHD RECORDS HANAGEKENT BRANCH TEXT CONTINUATION                                        (HHBB 7714), U.S ~ NUCLEAR REGULATORY CONNISSIOH, llASHINGTON, DC 20555-0001     AND TO THE PAPERIKNK REDUCTION     PROJECT     (3110-0104),     OFFICE    OF HANAGENENT AND BUDGET IIASNINGTOH DC 20503.
FACILITY HANE    1                      DOCKET NINBER  2              LER HWSER    6                  PAGE  3 YEAR    SEQUENTIAL      REVISION R.E. Ginna Nuclear Power Plant                                05000244            93    006--               00        5 OF 11 TEXT  (If more  space  is required,   use  additional copies of NRC Form 366A) (17)
E. METHOD OF DISCOVERY:
This event was immediately apparent due to the loss of ability to control feedwater flow to the "A" S/G. The reactor trip was immediately apparent due to alarms and indications in the Control Room.
F. OPERATOR ACTION:
After the reactor trip, the Control Room operators performed the actions of Emergency Operating Procedures E-0 (Reactor Trip or Safety Injection) and ES-0.1 (Reactor Trip Response).                     The main feedwater pumps were manually stopped and the MSIVs were manually closed to limit further RCS cooldown. The plant was stabilized at hot shutdown. Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Commission per 10CFR50.72, Non-Emergency, 4 Hour Notification at approximately 1030 EST.
G. SAFETY SYSTEM RESPONSES:
None III.     CAUSE OF EVENT A. IMMEDIATE CAUSE:
The    reactor        trip was      due    to "A"     S/G Lo Lo        level
(</= 174)       .
B. INTERMEDIATE CAUSE:
The "A" S/G Lo Lo                  level (</= 174) was due to decreased feedwater flow to the "A" S/G, caused by loss of ability to control the "A" MFRV.
NRC FORN  366A  (5-92)
 
0 NRC FORH 366A                              U.S  IRKLEAR REGULATORY C(IIIISSI(HI             APPROVED BY (SRI HO. 3150-0104 (5-92)                                                                                              EXPIRES  5/31/95 ESTIHATED BURDEN    PER  RESPONSE  TO  COHPLY    lllTH THIS INFORHATION COLLECTIOH REQUEST: 50.0 NRS.
FORIIARD COHHENTS REGARDING BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER)                                      THE INFORHATIOH AND RECORDS HANAGEHENT BRANCH TEXT CONTINUATION                                        (HNBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOH, llASHIHGTOH, DC 20555-0001     AND TO THE PAPERNORK REDUCTION     PROJECT   (3140-0104),   OFFICE      OF HANAGEHENT AND BUDGET HASHINGTON OC 20503.
FACILITY IWK    1                      DOCKET MMBER    2              LER  ABER 6                    PAGE  3 YEAR SEQUENTIAL      REVISIOH R.E. Ginna Nuclear Power Plant                            05000244                                                  6 OF 11 93    -- 006             00 TEXT (If more space  is required, use additional copies of NRC Form 366A)   (17)
C. ROOT CAUSE:
The underlying cause                of the loss of ability .to control the "A" MFRV was the                disconnection of the positioner feedback linkage arm                from the valve actuator linkage rod on the "A" MFRV,               due to disengagement of the connecting screw and                nut. (This event is NUREG-1220 (B)   cause code, Design, Manufacturing, Construction/
Installation).
Installation).
IV.ANALYSISOFEVENTThiseventisreportable inaccordance with10CFR50.73,LicenseeEventReportSystem,item(a)(2)(iv),whichrequiresareportof,"anyeventorcondition thatresultedinmanualorautomatic actuation ofanyengineered safetyfeature(ESF)including thereactorprotection system(RPS)".The"A"S/GLoLolevelreactortripwasanautomatic actuation oftheRPS.TheclosuresoftheMFRVsat674S/Glevelswerealsoautomatic actuations ofanESFcomponent.
IV.     ANALYSIS OF EVENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (iv), which requires a report of, "any event or condition that resulted in manual or automatic actuation of any engineered safety feature (ESF) including the reactor protection system (RPS)".                                           The "A" S/G Lo Lo level reactor trip was an automatic actuation of the RPS.       The closures of the MFRVs at 674 S/G levels were also automatic actuations of an ESF component.
Anassessment wasperformed considering boththesafetyconsequences andimplications ofthiseventwiththefollowing resultsandconclusions:
An assessment          was performed          considering both the safety consequences and implications                      of this event with the following results and conclusions:
Therewerenosafetyconsequences orimplications attributed tothereactortripbecause:oThetworeactortripbreakersopenedasrequired.
There were no safety consequences                        or implications attributed to the reactor trip because:
oAllcontrolandshutdownrodsinsertedasdesigned.
o    The two      reactor trip breakers opened as required.
oTheplantwasstabilized athotshutdown.
o    All control and shutdown rods inserted as designed.
HRCFORH366A(5-92)
o    The plant was stabilized at hot shutdown.
I NRCFORH366A(5-92)USWCLEARREGULATORY CQIIISSIOHLICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBYQ%lHO.3150-0104 EXPIRES5/31/95ESTIHATED BURDENPERRESPOHSETOCOHPLYllITHTHISINFORHATION COLLECTIOH REQUEST:50.0HRS.FORllARDCOHHEHTSREGARDIHG BURDENESTIHATETOTHEIHFORHATION ANDRECORDSHANAGEHENT BRANCH(HNBB7714),U.S.NUCLEARREGULATORY CDHHISSIOHi llASHINGTOH, DC20555-0001 AHDTOTHEPAPERlJORK REDUCTION PROJECT(3150.0104),
HRC FORH 366A (5-92)
OFFICEOFHAHAGEHENT ANDBUDGETllASHINGTON DC20503.FACILITYHAHER.E.GinnaNuclearPowerPlantDOCKETNWBER2YEAR0500024493LERNNBER6SEQUENTIAL--006-REVISION00PAGE37OF11TEXT(Ifmorespaceisrequired, useadditional copiesofHRCForm366A)(17)TheGinnaUpdatedFinalSafetyAnalysisReport(UFSAR)transient, asdescribed inChapter15.2.6,"LossofNormalFeedwater",
 
describes acondition wherethereactortripsonLoLoS/Glevel.ThisUFSARtransient wasreviewedandcomparedtotheplantresponseforthisevent.TheUFSARtransient isacompletelossofMainFeedwater (MFW)atfullpower,withonlyoneAFWpumpavailable one(1)minuteafterthelossofMFW,andsecondary steamrelief(i.e.decayheatremoval)throughthesafetyvalvesonly.Theprotection againstalossofMFWincludesthereactortriponLoLoS/GlevelandthestartoftheAFWpumps.Theseprotection featuresoperatedasdesigned.
I NRC FORH 366A                              U S  WCLEAR REGULATORY  CQIIISSI OH            APPROVED BY Q%l HO. 3150-0104 (5-92)                                                                                             EXPIRES  5/31/95 ESTIHATED BURDEN PER RESPOHSE TO COHPLY llITH THIS INFORHATION COLLECTIOH REQUEST: 50.0 HRS.
Basedontheaboveevaluation, theplanttransient ofNovember10,1993isboundedbytheUFSARSafetyAnalysisassumptions.
FORllARD COHHEHTS REGARDIHG BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER)                                    THE IHFORHATION AND RECORDS HANAGEHENT BRANCH TEXT CONTINUATION                                      (HNBB 7714), U.S. NUCLEAR REGULATORY CDHHISSIOHi llASHINGTOH, DC 20555-0001     AHD TO THE PAPERlJORK REDUCTION     PROJECT     (3150.0104),   OFFICE  OF HAHAGEHENT AND BUDGET llASHINGTON DC 20503.
Therewerenooperational orsafetyconsequences orimplications attributed totheclosureoftheMFRVsat674S/Glevelbecause:0oThevalveclosuresignalsoccurredat.therequiredS/Glevel.Theplantwasquicklystabilized tomitigateanyconsequences oftheevent.oAsthevalvesclosedasdesigned, theassumptions oftheUFSARforsteamlinebreakweremet.Technical Specifications (TS)werereviewedinrespecttotheposttripreviewdata.Thefollowing are-theresultsofthatreview:HRCFORH366A(5-92)  
FACILITY HAHE                          DOCKET NWBER    2              LER NNBER    6                PAGE  3 SEQUENT IAL      REVISION YEAR R.E. Ginna Nuclear Power Plant                            05000244                                                  7 OF 11 93    -- 006               00 TEXT (If more space  is required, use additional copies of HRC Form 366A)   (17)
The Ginna Updated Final Safety Analysis Report (UFSAR) transient, as described in Chapter 15.2.6, "Loss of Normal Feedwater", describes a condition where the reactor trips on Lo Lo S/G level. This UFSAR transient was reviewed and compared to the plant response for this event. The UFSAR transient is a complete loss of Main Feedwater (MFW) at full power, with only one AFW pump available one (1) minute after the loss of MFW, and secondary steam relief (i.e. decay heat removal) through the safety valves only. The protection against a loss of MFW includes the reactor trip on Lo Lo S/G level and the start of the AFW pumps. These protection features operated as designed.
Based on the above evaluation, the plant transient of November 10, 1993 is bounded by the UFSAR Safety Analysis assumptions.
There were no operational or safety consequences                                      or implications attributed to the closure of the MFRVs at 674 S/G level because:
0    The valve closure signals occurred at. the required S/G level.
o    The plant was quickly stabilized to mitigate any consequences of the event.
o    As the valves closed as designed, the assumptions of the UFSAR      for  steam      line break        were met.
Technical Specifications (TS) were reviewed in respect to the post trip review data. The following are- the results of that review:
HRC FORH 366A  (5-92)
 
NRC FORN  366A                                U.S. IRICLEAR REGUIATORY CQNIISSION              APPROVED BY INHI NO. 3150-0104 (5-92)                                                                                                EXPIRES  5/31/95 ESTIHATED BURDEH PER RESPONSE To COHPLY MITH THIs IHFORHATIDH coLLEcTIoN REQUEBT: 50.0 HRS.
FORllARD COHHEHTS REGARDIHG BURDEN ESTIHATE To LICENSEE EVENT REPORT (LER)                                        THE INFORHATIOH AHD RECORDS HANAGEHEHT BRANCH TEXT CONTINUATION                                          (HNBB 7714), U.S. NUCLEAR REGULATORY CONHISSION, NASHINGTOH, Dc 20555-0001      AHD To THE PAPERlJORK REDUCTION    PROJECT    (3140-0104),    OFFICE  OF NAHAGENENT AHD BUDGET llASHIHGTOH Dc 20503.
FACILITY NANE  1                        DOCKET NNBER    2              LER  NWER    6                  PAGE  3
                                                                                      'YEAR    SEQUENTIAL      REVISIOH R.E. Ginna Nuclear Power Plant                                05000244            93    006--                00        8 OF 11 TEXT  (If more space  is required,  use additionat copies of  NRC Form 366A)  (17) o      Following the reactor trip, PRZR water level decreased to below 04, due          to a moderate RCS cooldown. This cooldown occurred during the post trip recovery period. This cooldown was bounded by the plant accident analysis, and did not exceed the TS limit of 100 degrees F per hour. Additional mitigation was provided by closing the MSIVs and stopping the main feedwater pumps. TS 3.1.1.5 states, in part, that when the RCS temperature is at or above 350 degrees F, the pressurizer water level will be maintained between 124 and 874 of level span to be considered operable.                                        TS 3.1.1.5 also states, in part, that                  if  the pressurizer is inoperable due to water level, restore the pressurizer to operable status within six (6) hours or have the reactor below an RCS temperature of 350 degrees F and the RHR system in operation within an additional six (6) hours. Pressurizer water level recovered to greater than 124 level within ten (10) minutes, well before the six (6) hour action statement.
o    Both S/G levels decreased to less than 04 following the reactor trip. This is an expected observed transient. TS 4.3.5.5 states that in order to demonstrate that a reactor coolant loop is operable, the S/G water level shall be >/=
164. Thus, both coolant loops were inoperable, even though both loops were still in operation and performing their intended function of decay heat removal. Both S/Gs were available as a heat sink, and sufficient AFH flow was maintained for adequate steam release from both S/Gs. TS 3.1.1.1(c) states, in part, that except for special tests, when the RCS temperature is at or above 350 degrees F with the reactor power less than or equal to 130 MWT (8.54), at least one reactor coolant loop and its associated S/G and reactor coolant pump shall be in operation. Both reactor coolant loops were in operation, but the S/Gs were inoperable due to level indication. Both loops were returned to operable status. "A" S/G level was restored to > 164 within one (1) minute, and "B" S/G level was restored to > 164 in approximately ten (10) seconds.
HRC FORH  366A (5 92)


NRCFORN366A(5-92)U.S.IRICLEARREGUIATORY CQNIISSION LICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBYINHINO.3150-0104 EXPIRES5/31/95ESTIHATED BURDEHPERRESPONSEToCOHPLYMITHTHIsIHFORHATIDH coLLEcTIoN REQUEBT:50.0HRS.FORllARDCOHHEHTSREGARDIHG BURDENESTIHATEToTHEINFORHATIOH AHDRECORDSHANAGEHEHT BRANCH(HNBB7714),U.S.NUCLEARREGULATORY CONHISSION, NASHINGTOH, Dc20555-0001 AHDToTHEPAPERlJORK REDUCTION PROJECT(3140-0104),
HRC FORH 366A                              U.S   IN)CLEAR REGULATORY CQBIISSIQI              APPROVED BY  MB HO. 3150-0104 5-92)                                                                                                EXPIRES  5/31/95 EST INATED BURDEN PER RESPONSE      TO CONPLY MITH THIS INFORNATI OH COLLECTION REQUEST 50 ~ 0 HRS.
OFFICEOFNAHAGENENT AHDBUDGETllASHIHGTOH Dc20503.FACILITYNANE1R.E.GinnaNuclearPowerPlantDOCKETNNBER205000244LERNWER6'YEARSEQUENTIAL REVISIOH93-006--00PAGE38OF11TEXT(Ifmorespaceisrequired, useadditionat copiesofNRCForm366A)(17)oFollowing thereactortrip,PRZRwaterleveldecreased tobelow04,duetoamoderateRCScooldown.
FORNARD COHHEHl'S REGARD IHG BURDEH EST I HATE TO LICENSEE EVENT REPORT (LER)                                        THE IHFORHATI OH AHD RECORDS NANAGENEHT BRANCH TEXT CONTINUATION                                        (HHBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOH, HASHIHGTOH, DC 20555-0001       AND TO THE PAPERNORK REDUCTION     PROJECT     (3140 0104),   OFFICE  OF NANAGENEHT AHD BUDGET llASNIHGTON DC 20503.
Thiscooldownoccurredduringtheposttriprecoveryperiod.Thiscooldownwasboundedbytheplantaccidentanalysis, anddidnotexceedtheTSlimitof100degreesFperhour.Additional mitigation wasprovidedbyclosingtheMSIVsandstoppingthemainfeedwater pumps.TS3.1.1.5states,inpart,thatwhentheRCStemperature isatorabove350degreesF,thepressurizer waterlevelwillbemaintained between124and874oflevelspantobeconsidered operable.
FACI LITY RANE  1                        DOCKET HlMBER  2              LER HINBER    6                PAGE  3 YEAR SEQUENTIAL      REVISION R.E. Ginna Nuclear Power Plant                                05000244            93    -- 006               pp      9 OF 11 TEXT (If more space  is required, use additional copies  oi NRC Form 366A) (17) o    Condensate Storage Tank (CST),level decreased to less than 22,500 gallons of water, due to a malfunction of the condensate makeup and reject valves. The malfunction caused the CSTs to          fill    the main condenser hotwell. TS 3.4.3 states, in part, that with the RCS temperature at or above 350 degrees F, one or more CSTs with a minimum of 22,500 gallons of water, shall be operable as a source of auxiliary feedwater. With the CSTs inoperable, within four (4) hours either restore the CSTs to operable status, or be in at least hot shutdown within the following six (6) hours and at an RCS temperature less than 350 degrees F within the following six (6) hours. The reactor was already at hot shutdown, and the CSTs were restored to operable status within approximately fifty statement.
TS3.1.1.5alsostates,inpart,thatifthepressurizer isinoperable duetowaterlevel,restorethepressurizer tooperablestatuswithinsix(6)hoursorhavethereactorbelowanRCStemperature of350degreesFandtheRHRsysteminoperation withinanadditional six(6)hours.Pressurizer waterlevelrecovered togreaterthan124levelwithinten(10)minutes,wellbeforethesix(6)houractionstatement.
(50) minutes, well before the twelve (12) hour action Based on the above and a review of post trip data and past plant transients,             it    can be concluded that the plant operated as designed and that there were no unreviewed safety questions and that the public's health and safety was assured at all times.                                                                    f V.       CORRECTIVE ACTION A. ACTION TAKEN              TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
oBothS/Glevelsdecreased tolessthan04following thereactortrip.Thisisanexpectedobservedtransient.
o      The "A" MFRV Bailey positioner was replaced.                                          (Refer to LER 92-006, Rev. 1, Docket No. 50-244.)                                   The newly installed positioner was reattached to the valve actuator linkage rod using a vendor-recommended screw with an elastic stop nut.
TS4.3.5.5statesthatinordertodemonstrate thatareactorcoolantloopisoperable, theS/Gwaterlevelshallbe>/=164.Thus,bothcoolantloopswereinoperable, eventhoughbothloopswerestillinoperation andperforming theirintendedfunctionofdecayheatremoval.BothS/Gswereavailable asaheatsink,andsufficient AFHflowwasmaintained foradequatesteamreleasefrombothS/Gs.TS3.1.1.1(c) states,inpart,thatexceptforspecialtests,whentheRCStemperature isatorabove350degreesFwiththereactorpowerlessthanorequalto130MWT(8.54),atleastonereactorcoolantloopanditsassociated S/Gandreactorcoolantpumpshallbeinoperation.
HRC FORH 366A (5-92)
Bothreactorcoolantloopswereinoperation, buttheS/Gswereinoperable duetolevelindication.
Bothloopswerereturnedtooperablestatus."A"S/Glevelwasrestoredto>164withinone(1)minute,and"B"S/Glevelwasrestoredto>164inapproximately ten(10)seconds.HRCFORH366A(592)  


HRCFORH366A5-92)U.SIN)CLEARREGULATORY CQBIISSIQI LICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBYMBHO.3150-0104 EXPIRES5/31/95ESTINATEDBURDENPERRESPONSETOCONPLYMITHTHISINFORNATIOHCOLLECTION REQUEST50~0HRS.FORNARDCOHHEHl'S REGARDIHGBURDEHESTIHATETOTHEIHFORHATIOHAHDRECORDSNANAGENEHT BRANCH(HHBB7714),U.S.NUCLEARREGULATORY COHHISSIOH, HASHIHGTOH, DC20555-0001 ANDTOTHEPAPERNORK REDUCTION PROJECT(31400104),OFFICEOFNANAGENEHT AHDBUDGETllASNIHGTON DC20503.FACILITYRANE1R.E.GinnaNuclearPowerPlantDOCKETHlMBER205000244LERHINBER6YEARSEQUENTIAL 93--006-REVISIONPAGE3pp9OF11TEXT(Ifmorespaceisrequired, useadditional copiesoiNRCForm366A)(17)oCondensate StorageTank(CST),level decreased tolessthan22,500gallonsofwater,duetoamalfunction ofthecondensate makeupandrejectvalves.Themalfunction causedtheCSTstofillthemaincondenser hotwell.TS3.4.3states,inpart,thatwiththeRCStemperature atorabove350degreesF,oneormoreCSTswithaminimumof22,500gallonsofwater,shallbeoperableasasourceofauxiliary feedwater.
0 HRC FORH 366A                              U.S  INCLEAR REGULATORY CRIBS ION                APPROVED BY (HN HO. 3150-0104 (5-92)                                                                                             EXPIRES  5/31/95 ESTIHATED BURDEN    PER  RESPOHSE  TO  COHPLY    WITH THIS INFORHATIOH COLLECTIOH REQUEST:         50.0  HRS.
WiththeCSTsinoperable, withinfour(4)hourseitherrestoretheCSTstooperablestatus,orbeinatleasthotshutdownwithinthefollowing six(6)hoursandatanRCStemperature lessthan350degreesFwithinthefollowing six(6)hours.Thereactorwasalreadyathotshutdown, andtheCSTswererestoredtooperablestatuswithinapproximately fifty(50)minutes,wellbeforethetwelve(12)houractionstatement.
FORWARD  COHHEHTS  REGARDIHG    BURDEN  ESTIHATE TO LICENSEE EVENT REPORT (LER)                                      THE  INFORHATIOH AND RECORDS HANAGEHEHT BRANCH TEXT CONTINUATION                                        (HHBB 7714), U.S. NUCLEAR REGULATORY COHHISSION, WASHINGTON, DC 20555-0001       AHD TO THE PAPERWORK REDUCT10H     PROJECT     (31/0-0104),     OFFICE    OF HANAGEHEHT AHD BUDGET      WASHINGTON    OC  20503.
Basedontheaboveandareviewofposttripdataandpastplanttransients, itcanbeconcluded thattheplantoperatedasdesignedandthattherewerenounreviewed safetyquestions andthatthepublic'shealthandsafetywasassuredatalltimes.fV.CORRECTIVE ACTIONA.ACTIONTAKENTORETURNAFFECTEDSYSTEMSTOPRE-EVENT NORMALSTATUS:oThe"A"MFRVBaileypositioner wasreplaced.
FACILITY HAHE  1                      DOCKET HNBER  2              LER HWBER    6                  PAGE    3 SEQUENTIAL      REVISION YEAR R.E. Ginna Nuclear Power Plant                              05000244            93    -- 006               00      10 OF 11 TEXT (lf more space  is required, use additional copies of  NRC Form 366A) (1)')
(RefertoLER92-006,Rev.1,DocketNo.50-244.)Thenewlyinstalled positioner wasreattached tothevalveactuatorlinkagerodusingavendor-recommended screwwithanelasticstopnut.HRCFORH366A(5-92) 0 HRCFORH366A(5-92)U.SINCLEARREGULATORY CRIBSIONLICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBY(HNHO.3150-0104 EXPIRES5/31/95ESTIHATED BURDENPERRESPOHSETOCOHPLYWITHTHISINFORHATIOH COLLECTIOH REQUEST:50.0HRS.FORWARDCOHHEHTSREGARDIHG BURDENESTIHATETOTHEINFORHATIOH ANDRECORDSHANAGEHEHT BRANCH(HHBB7714),U.S.NUCLEARREGULATORY COHHISSION, WASHINGTON, DC20555-0001 AHDTOTHEPAPERWORK REDUCT10H PROJECT(31/0-0104),
o      The >>B>> MFRV          positioner        was    inspected, and rework of the positioner        was    performed.           This included installation of a vendor-recommended screw with an elastic stop nut.
OFFICEOFHANAGEHEHT AHDBUDGETWASHINGTON OC20503.FACILITYHAHE1R.E.GinnaNuclearPowerPlantDOCKETHNBER20500024493--006-LERHWBER6YEARSEQUENTIAL REVISION00PAGE310OF11TEXT(lfmorespaceisrequired, useadditional copiesofNRCForm366A)(1)')oThe>>B>>MFRVpositioner wasinspected, andreworkofthepositioner wasperformed.
o      The >>A>> and >>B>> MFRVs were repacked.                               (Refer to LER 92-006, Rev. 1, Docket No. 50-244.)
Thisincludedinstallation ofavendor-recommended screwwithanelasticstopnut.oThe>>A>>and>>B>>MFRVswererepacked.
o      Linkage connections              for other accessible valves with Bailey      positioners        were      inspected to ensure satisfactory integrity of the connections.
(RefertoLER92-006,Rev.1,DocketNo.50-244.)oLinkageconnections forotheraccessible valveswithBaileypositioners wereinspected toensuresatisfactory integrity oftheconnections.
o      The malfunction of the condensate makeup and reject valves was caused by a fitting leak which was associated with the common demand signal shared by both valves. The fitting was tightened, and both valves were verified to respond correctly to control main condenser hotwell level.
oThemalfunction ofthecondensate makeupandrejectvalveswascausedbyafittingleakwhichwasassociated withthecommondemandsignalsharedbybothvalves.Thefittingwastightened, andbothvalveswereverifiedtorespondcorrectly tocontrolmaincondenser hotwelllevel.B.ACTIONTAKENORPLANNEDTOPREVENTRECURRENCE:
B. ACTION TAKEN            OR PLANNED TO PREVENT RECURRENCE:
oApplicable procedures willbeupgradedtoensureBaileyvendormanualinformation concerning feedbacklinkagearm:connections isaddressed.
o      Applicable procedures will be upgraded to ensure Bailey vendor manual information concerning feedback linkage arm:
00Trainingwillbeconducted toenhancetheknowledge ofappropriate personnel onthegeneraltopicoffasteners, andstressing linkagearmconnections, specifically.
connections         is  addressed.
Reworkofpositioner feedbacklinkagearmconnections, forallothervalveswithBaileypositioners, willbeaccomplished.
0      Training will be conducted to enhance the knowledge of appropriate personnel on the general topic of fasteners, and stressing linkage arm connections, specifically.
Thiswillincludeinstallation ofvendor-recommended screwsandelasticstopnuts.NRCFORH366A(592)  
0      Rework of positioner feedback linkage arm connections, for all other valves with Bailey positioners, will be accomplished.             This will include installation of vendor-recommended screws and elastic stop nuts.
NRC FORH 366A (5 92)


HRCFORH366A(5-92)U.SWCLEARREGULATORY CQBIISSIOH LICENSEEEVENTREPORT(LER)TEXTCONTINUATION APPROVEDBYQBIHO.3150-0104 EXPIRES5/31/95ESTIHATED BURDENPERRESPONSETOCOMPLYUITHTHISINFORHATIOH COLLECTION REQUEST:50.0HRS.FORNARDCOHMEHTSREGARDING BURDENESTIMATETOTHEIHFORHATION ANDRECORDSHANAGEMENT BRANCH(HNBB7714),U.S.NUCLEARREGULATORY COHHISSION, llASHINGTON, DC20555-0001 AHDTOTHEPAPERNORK REDUCTIOH PROJECT(3140-0104),
HRC FORH  366A                              U.S  WCLEAR REGULATORY CQBIISSIOH             APPROVED BY  QBI HO. 3150-0104 (5-92)                                                                                              EXPIRES  5/31/95 ESTIHATED BURDEN PER RESPONSE TO COMPLY UITH THIS INFORHATIOH COLLECTION REQUEST: 50.0 HRS.
OFFICEOFHANAGEHENT ANDBUDGETUASHINGTON DC20503.FACILITYNAIK1R.E.GinnaNuclearPowerPlantDOCKETHQSER20500024493-006-00LERHINBER6YEARSEOUENTIALREVISIONPAGE311OF11TEXT(Ifmorespaceisrequired, useadditional copiesofHRCForm366A)(17)VI.ADDITIONAL INFORMATION A.FAILEDCOMPONENTS:
FORNARD COHMEHTS REGARDING BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER)                                    THE IHFORHATION AND RECORDS HANAGEMENT BRANCH (HNBB 7714), U.S. NUCLEAR REGULATORY COHHISSION, TEXT CONTINUATION                                      llASHINGTON, DC 20555-0001     AHD TO THE PAPERNORK REDUCTIOH   PROJECT     (3140-0104),   OFFICE  OF HANAGEHENT AND BUDGET UASHINGTON DC 20503.
Thefailedcomponent wasthe"A"MFRVpositioner feedbacklinkagearmconnection.
FACILITY NAIK  1                      DOCKET HQSER  2              LER HINBER  6                PAGE  3 SEOUENT IAL    REVISION YEAR R.E. Ginna Nuclear Power Plant                              05000244            93    006               00      11 OF 11 TEXT (If more  space is required, use additional copies of HRC  Form 366A) (17)
ThisassemblyisaBaileypneumatic positioner, modelAV112100,manufac-turedbyBaileyControlsInc.B.PREVIOUSLERsONSIMILAREVENTS:AsimilarLEReventhistorical searchwasconducted withthefollowing results:Nodocumentation ofsimilarLEReventswiththesamerootcauseatGinnaNuclearPowerPlantcouldbeidentified.
VI.       ADDITIONAL INFORMATION A. FAILED          COMPONENTS:
However,LERs88-005,90-'007,and90-010weresimilareventswithdifferent rootcauses.C.SPECIALCOMMENTS:
The    failed      component was the "A" MFRV positioner feedback        linkage      arm connection.             This assembly is a Bailey      pneumatic        positioner,         model    AV 112100, manufac-tured by Bailey Controls Inc.
LER92-006,Rev.1,identified threecorrective actionsrelatedtoMFRVs:replacethe"A"MFRVactuatorwitharebuiltactuator, replacethe"A"MFRVpositioner, andrepackbothMFRVs.Twoofthesecorrective actionswereaccomplished inresponsetothisevent(LER93-006).Post-maintenance testingofMFRVs,andsubsequent satisfactory operation ofbothMFRVs,havedemonstrated thatreplacement ofthe"A"MFRVactuatorisnolongerrequired.
B. PREVIOUS LERs ON SIMILAR EVENTS:
HRCFORM366A(5-92)}}
A  similar      LER  event    historical          search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Nuclear Power Plant could be identified. However, LERs 88-005, 90-'007, and 90-010 were similar events with different root causes.
C. SPECIAL COMMENTS:
LER    92-006, Rev. 1,           identified three corrective actions related to          MFRVs:     replace      the "A" MFRV actuator with a rebuilt      actuator,       replace      the "A" MFRV positioner, and repack      both    MFRVs.       Two    of  these corrective actions were accomplished in response to this event (LER 93-006). Post-maintenance testing of MFRVs, and subsequent satisfactory operation of both MFRVs, have demonstrated that replacement of the "A" MFRV actuator is no longer required.
HRC FORM  366A  (5-92)}}

Latest revision as of 09:35, 4 February 2020

LER 93-006-00:on 931110,feedwater Transient Occurred,Due to Loss of Ability to Control Feedwater Regulating Valve.Caused by low-low SG Level Reactor Trip.New Screw & Nut Installed in Linkage arm.W/931210 Ltr
ML17263A499
Person / Time
Site: Ginna Constellation icon.png
Issue date: 12/10/1993
From: Mecredy R, St Martin J
ROCHESTER GAS & ELECTRIC CORP.
To: Andrea Johnson
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM), Office of Nuclear Reactor Regulation
References
LER-93-006, LER-93-6, NUDOCS 9312270027
Download: ML17263A499 (26)


Text

ACCELERATED DEMONS~TION SYSTEM DISTRIBUTION REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9312270027 DOC.DATE: 93/12/10 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION ST.MARTIN,J.T. Rochester Gas & Electric Corp.

MECREDY,R.C. Rochester Gas & Electric Corp.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 93-006-00:on 931110,feedwater transient occured,due to ability controll feedwater regulating valve. Caused by LO LO steam genorator level reactor trip. New screw & nut installed D in leakage arm.w/931210 ltr.

DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR i ENCL T1TLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.

/ SIZE:

NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72). 05000244 A RECIPIENT COPIES RECIPIENT D COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PDl-3 LA 1 1 PD1-3 PD 1 1 D JOHNSON,A 1 1 INTERNAL: AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRIL/RPEB 1 1 NRR/DRSS/PRPB 2 2 NRR--DSSA PLB 1 1 NRR/DSSA/SRXB 1 1 EG IEE 02 1 1 RES/DSIR/EIB 1 1 RGN-1~ PIE 01 1 1 EXTERNAL EG&G BRYCE I J ~ H 2 2 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MURPHYIG A ~ 1 1 NSIC POORE,W. 1 1 NUDOCS FULL TXT 1 1 D

D D

NOTE TO ALL "RIDS" RECIPIENTS:

S PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 28 ENCL 28

E Neo

<g(~VifiFNT If'iflÃJilif s

I ml ~ 0 w/ ',.r " eoec is 'fiIitiiiiffffillliiiiiii 'ssnsc ROCHESTER GAS AND ELECTRIC CORPORATION ~ *"

89 EAST AVENUE, ROCHESTER N. Y. 14649.0001 ROBERT C. MECREDY TELEPHONE Vice Piesfdent AREA CODE 7 1B 546 2700 Olnnn Nuclear Psoducsion December 10, 1993 U.S. Nuclear Regulatory Commission Attn: Allen R. Johnson Project Directorate I-3 Document Control Desk Washington, DC 20555

Subject:

LER 93-006, Feedwater Transient, Due to Loss of Ability to Control Feedwater Regulating Valve, Causes a Lo Lo Steam Generator Level Reactor Trip R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (iv), which requires a report of, "any event or condition that resulted in a manual or automatic actuation of any engineered safety feature (ESF), including the reactor protection system (RPS)", the attached Licensee Event Report LER 93-006 is hereby submitted.

This 'event has in no way affected the public',s health and safety.

Very truly yours, Robert C. Me edy xc: U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 4j.OOa9 9312270027 931210 PDR ADOCK 05000244 S PDR y~

p

~ rt. l al

~

i i*

MRC FORH 366 U s. IH)cLEAR REGULATDRY ccsallssioN APPROVED BY (NB NO 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY MITH THIS INFORHATIOH COLLECTION REQUEST: 50.0 HRS.

LXCENSEE EVENT REPORT (LER) FORMARD COHHEHTS REGARDIHG BURDEN ESTINATE TO THE INFORNATION AND RECORDS HANAGEHENT BRAHCH (HHBB 7714), U.S. NUCLEAR REGULATORY COHHISSIDM, (See reverse for required number of digits/characters for each block) WASHINGTON, DC 20555-0001 AND TO THE PAPERUORK REDUCTION PROJECT (3140.0104), OFFICE OF HAMAGEHENT AMD BUDGET llASHINGTOM DC 20503.

FAclLITY Nba (1) R. E ~ Ginna Nuclear Power Plant DOCKET IRNBER (2) PAGE (3) 05000244 1 OF 11 TITLE (4) Feeckater Transient, Due to Loss of Ability to Control Fee>hater Regulating Valve, Causes a Lo Lo Steam Generator Level Reactor Trip EVENT DATE 5 LER NMBER 6 REPORT DATE 7 OTHER FACILITIES INVOLVED 8 SEQUENTIAL REVISIOH FACILITY NAHE DOCKET NUNBER HOHTH DAY YEAR YEAR HOHTH DAY YEAR NUHBER NUMBER 10 93 93 006 00 12 10 93 FACILITY HAHE DOCKET HUHBER OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREHENTS OF 10 CFR: Check one or mor e 11 H(X)E (9)

N 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b)

PQKR 20.405(a )(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c) 097 LEVEL (10) 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) OTHER 20.405(a)(1)(iii) 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) (Specify in 20.405(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) Abstract and in Text, below 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) MRC Form 366A LICENSEE CONTACT FOR THIS LER 12 NAHE John T. St. Hartin - Director, Operating Experience TELEPHONE HUNGER (Include Area Code)

(315) 524-4446 GNPLETE ONE LINE FOR EACH GNRNEMT FAILURE DESCRIBED IN THIS REPORT 13 REPORTABLE REPORTABLE CAUSE SYSTEH COMPONENT HAMUFACTURER CAUSE SYSTEH COMPONENT HAHUFACTURER TO HPRDS TO MPRDS B JB LCV B042 SUPPLEMENTAL REPORT EXPECTED 14 EXPECTED HOMTH OAY YEAR

'YES SUBHISSION (If yes, complete EXPECTED SUBHISSIOM DATE) ~ DATE (15)

ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typemritten lines) (16)

On November 10, 1993, at approximately 0848 EST, with the reactor at approximately 974 reactor power, the ability to control the >>A<< main feedwater regulating valve was lost. This resulted in steam generator level transients. At 0850 EST, the reactor tripped on Lo Lo level (</=

174) in the <<A>> steam generator. The Control Room operators performed the actions of procedures E-0 and ES-0.1.

The underlying cause was determined to be disconnection of the <<A<< main feedwater regulating valve positioner feedback linkage arm from the valve actuator linkage rod, due to disengagement of the connecting screw and nut. (This event is NUREG-1220 (B) cause code.)

Corrective action was to install a new screw and nut. Corrective action to preclude repetition is outlined in Section V (B).

HRC FORH 366 (5-92)

RC FORH 366A U.S IN)CLEAR REGULATORY (XIII SSI ON APPROVED BY (NRI NO. 3150-0104 5-92) EXPIRES 5/31/95 EST IHATED BURDEH PER RESPOHSE TO COHPLY WITH THIS IHFORHATIOH COLLECTIOH REGUEST: 50.0 NRS.

FORWARD COHHENTS REGARD IHG BURDEN EST IHATE TO LICENSEE EVENT REPORT (LER) THE INFORHATION AND RECORDS HANAGEHENT BRANCN TEXT CONTINUATION (HNBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOH, WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (3140-0104) ~ OFFICE OF HANAGEHENT AND BUDGET WASHINGTON DC 20503.

FACILITY IWK 1 DOCKET HINBER 2 LER HWBER 6 PAGE 3 YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 93 -- 006 pp 2 OF 11 EXT (If more space is required, use additional copies of NRC Form 366A) (17)

I. PRE-EVENT PLANT CONDITIONS The plant was at approximately 97% steady state reactor power.

The monthly surveillance test of the "A" auxiliary feedwater (AFW) pump was in progress, using procedure PT-16M-A (Auxiliary Feedwater Pump "A" Monthly).

II. DESCRIPTION OF EVENT A. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:

o November 10, 1993, 0850 EST: Event date and time.

o November 10, 1993, 0850 EST: Discovery date and time.

o November 10, 1993, 0850 EST: Control Room operators verify both reactor trip breakers open, and all control and shutdown rods inserted.

o November 10, 1993, 0851 EST: Control Room operators manually stop both main feedwater pumps to limit a reactor coolant system cooldown.

o November 10, 1993, 0852 EST: Control Room operators manually close both main steam isolation valves to limit a reactor coolant system cooldown.

o November 10, 1993, 1045 EST: Plant stabilized at hot shutdown condition.

NRC FORH 366A (5-92)

1 NRC FORN 366A U.S NUCLEAR REGULATORY CQWISS ION APPROVED BY (NB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO CDHPLY WITH THIS INFORHATIOH COLLECTIOH REQUEST: 50.0 HRS.

FORWARD CONNENTS REGARDING BURDEN ESTINATE TO LICENSEE EVENT REPORT (LER) THE IHFORHATIOH AHD RECORDS HAHAGEHEHT BRANCH TEXT CONTINUATION (HNBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOH, WASHIHGTOH, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (3140-0104), OFFICE OF NANAGEHENT AND BUDGET WASHINGTON DC 20503.

FACILITY NANE 1 DOCKET NINBER 2 LER NINBER 6 PAGE 3 YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 93 006 00 3 OF 11 TEXT (If more spece is required, use additional copies of NRC Form 366A) (17)

B. EVENT:

On November 10, 1993, surveillance test procedure PT-16M-A was initiated, at approximately 0835 EST. As part of this test, the >>A>> AFW pump was started.

Control of the main feedwater regulating valve (MFRV) and bypass feedwater regulating valve for the >>A steam generator (S/G) was shifted to the "Manual" mode, and the Control Room operator slightly closed the >>A>> MFRV.

The >>A>> MFRV initially started closing, and then appeared to drift open, based on indications of increased feedwater flow to the >>A>> S/G.

Despite the efforts of the Control Room operators to close the >>A>> MFRV, the >>A>> MFRV continued to drift open. The Advanced Digital Feedwater Control System (ADFCS) responded as designed, and shifted all feedwater regulating valves (for both S/Gs) to "Manual". The Control Room operators terminated PT-16M-A and turned off the >>A>> AFW pump. >>A>> S/G level continued to increase, until it reached the high level override setpoint of 674. The >>A>> MFRV closed as designed at 674 level. All feedwater flow was now directed to the >>B>> S/G. The >>B>> S/G level also reached the 674 high level override setpoint, and the

>>B>> MFRV closed.

The MFRVs reopened as designed when S/G levels decreased to less than 674. Due to the positioner feedback linkage failure, the Control Room operators had lost the ability to control >>A>> S/G level. The >>A>>

S/G level decreased to < 174, resulting in a reactor trip on S/G Lo Lo level, at 0850 EST.

HRC FORN 366A (5.92)

NRC FORH 366A U.S. NICLEAR REGULATORY C(SIIISSION APPROVED BY (SII NO- 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY MITH THIS IHFORHATIOH COLLECTION REQUEST: 50.0 HRS ~

FORNARD COHHENTS REGARDING BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE IHFORHATIOH AND RECORDS HANAGEHEHT BRAHCH TEXT CONTINUATION (HHBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOH, MASHINGTON, DC 20555-0001 AND TO THE PAPERlJORK REDUCTION PROJECT (3150.0104), OFFICE OF HANAGEHENT AND BUDGET NASHINGTON DC 20503.

FACILITY HAHE 1 DOCKET NWBER 2 LER NEER 6 PAGE 3 YEAR SEQUENT IAL REVISION R.E. Ginna Nuclear Power Plant 05000244 4 OF 11 93 -- 006 00 TEXT (lf more space is required, use additional copies of HRC Form 366A) (17)

The Control Room operators performed the immediate actions of Emergency Operating Procedure E-0 (Reactor Trip or Safety Injection), and transitioned .to Emergency Operating Procedure ES-0.1 (Reactor Trip Response) when it was verified that both reactor trip breakers were open, all control and shutdown rods were inserted, and safety injection was not actuated or required. During performance of E-O, the Control Room operators noted the continuing RCS cooldown and increasing S/G levels, and referred to Functional Restoration procedure FR-H.3 (Response to Steam Generator High Level). The operators verified that the AFW pumps had started, as designed, on the Lo Lo S/G level. Using the guidance of FR-H.3, they manually stopped both main feedwater pumps. In addition, both main steam isolation valves (MSIVs) were manually closed by the Control Room operators. These actions mitigated the RCS cooldown.

The plant was subsequently stabilized in hot shutdown, using procedure 0-2.2 (Plant Shutdown From Hot Shutdown to Cold Shutdown) at approximately 1045 EST.

C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:

None D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:

None NRC FORH 366A (5-92)

NRC FORN 366A U.S. WCLEAR REGUUlTORY CQHISS ION APPROVED BY W NO. 3150-0104 (5-92) EXPIRES 5/31/95 EST INATED BURDEH PER RESPOHSE TO COHPLY NITH THIS IHFORHATIOH COLLECT ION REQUEST: 50.0 HRS.

FORllARD CONHENTS REGARDING BURDEN EST INATE TO LICENSEE EVENT REPORT (LER) THE INFORHATION AHD RECORDS HANAGEKENT BRANCH TEXT CONTINUATION (HHBB 7714), U.S ~ NUCLEAR REGULATORY CONNISSIOH, llASHINGTON, DC 20555-0001 AND TO THE PAPERIKNK REDUCTION PROJECT (3110-0104), OFFICE OF HANAGENENT AND BUDGET IIASNINGTOH DC 20503.

FACILITY HANE 1 DOCKET NINBER 2 LER HWSER 6 PAGE 3 YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 93 006-- 00 5 OF 11 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)

E. METHOD OF DISCOVERY:

This event was immediately apparent due to the loss of ability to control feedwater flow to the "A" S/G. The reactor trip was immediately apparent due to alarms and indications in the Control Room.

F. OPERATOR ACTION:

After the reactor trip, the Control Room operators performed the actions of Emergency Operating Procedures E-0 (Reactor Trip or Safety Injection) and ES-0.1 (Reactor Trip Response). The main feedwater pumps were manually stopped and the MSIVs were manually closed to limit further RCS cooldown. The plant was stabilized at hot shutdown. Subsequently, the Control Room operators notified higher supervision and the Nuclear Regulatory Commission per 10CFR50.72, Non-Emergency, 4 Hour Notification at approximately 1030 EST.

G. SAFETY SYSTEM RESPONSES:

None III. CAUSE OF EVENT A. IMMEDIATE CAUSE:

The reactor trip was due to "A" S/G Lo Lo level

(</= 174) .

B. INTERMEDIATE CAUSE:

The "A" S/G Lo Lo level (</= 174) was due to decreased feedwater flow to the "A" S/G, caused by loss of ability to control the "A" MFRV.

NRC FORN 366A (5-92)

0 NRC FORH 366A U.S IRKLEAR REGULATORY C(IIIISSI(HI APPROVED BY (SRI HO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY lllTH THIS INFORHATION COLLECTIOH REQUEST: 50.0 NRS.

FORIIARD COHHENTS REGARDING BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE INFORHATIOH AND RECORDS HANAGEHENT BRANCH TEXT CONTINUATION (HNBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOH, llASHIHGTOH, DC 20555-0001 AND TO THE PAPERNORK REDUCTION PROJECT (3140-0104), OFFICE OF HANAGEHENT AND BUDGET HASHINGTON OC 20503.

FACILITY IWK 1 DOCKET MMBER 2 LER ABER 6 PAGE 3 YEAR SEQUENTIAL REVISIOH R.E. Ginna Nuclear Power Plant 05000244 6 OF 11 93 -- 006 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)

C. ROOT CAUSE:

The underlying cause of the loss of ability .to control the "A" MFRV was the disconnection of the positioner feedback linkage arm from the valve actuator linkage rod on the "A" MFRV, due to disengagement of the connecting screw and nut. (This event is NUREG-1220 (B) cause code, Design, Manufacturing, Construction/

Installation).

IV. ANALYSIS OF EVENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (iv), which requires a report of, "any event or condition that resulted in manual or automatic actuation of any engineered safety feature (ESF) including the reactor protection system (RPS)". The "A" S/G Lo Lo level reactor trip was an automatic actuation of the RPS. The closures of the MFRVs at 674 S/G levels were also automatic actuations of an ESF component.

An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:

There were no safety consequences or implications attributed to the reactor trip because:

o The two reactor trip breakers opened as required.

o All control and shutdown rods inserted as designed.

o The plant was stabilized at hot shutdown.

HRC FORH 366A (5-92)

I NRC FORH 366A U S WCLEAR REGULATORY CQIIISSI OH APPROVED BY Q%l HO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPOHSE TO COHPLY llITH THIS INFORHATION COLLECTIOH REQUEST: 50.0 HRS.

FORllARD COHHEHTS REGARDIHG BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE IHFORHATION AND RECORDS HANAGEHENT BRANCH TEXT CONTINUATION (HNBB 7714), U.S. NUCLEAR REGULATORY CDHHISSIOHi llASHINGTOH, DC 20555-0001 AHD TO THE PAPERlJORK REDUCTION PROJECT (3150.0104), OFFICE OF HAHAGEHENT AND BUDGET llASHINGTON DC 20503.

FACILITY HAHE DOCKET NWBER 2 LER NNBER 6 PAGE 3 SEQUENT IAL REVISION YEAR R.E. Ginna Nuclear Power Plant 05000244 7 OF 11 93 -- 006 00 TEXT (If more space is required, use additional copies of HRC Form 366A) (17)

The Ginna Updated Final Safety Analysis Report (UFSAR) transient, as described in Chapter 15.2.6, "Loss of Normal Feedwater", describes a condition where the reactor trips on Lo Lo S/G level. This UFSAR transient was reviewed and compared to the plant response for this event. The UFSAR transient is a complete loss of Main Feedwater (MFW) at full power, with only one AFW pump available one (1) minute after the loss of MFW, and secondary steam relief (i.e. decay heat removal) through the safety valves only. The protection against a loss of MFW includes the reactor trip on Lo Lo S/G level and the start of the AFW pumps. These protection features operated as designed.

Based on the above evaluation, the plant transient of November 10, 1993 is bounded by the UFSAR Safety Analysis assumptions.

There were no operational or safety consequences or implications attributed to the closure of the MFRVs at 674 S/G level because:

0 The valve closure signals occurred at. the required S/G level.

o The plant was quickly stabilized to mitigate any consequences of the event.

o As the valves closed as designed, the assumptions of the UFSAR for steam line break were met.

Technical Specifications (TS) were reviewed in respect to the post trip review data. The following are- the results of that review:

HRC FORH 366A (5-92)

NRC FORN 366A U.S. IRICLEAR REGUIATORY CQNIISSION APPROVED BY INHI NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEH PER RESPONSE To COHPLY MITH THIs IHFORHATIDH coLLEcTIoN REQUEBT: 50.0 HRS.

FORllARD COHHEHTS REGARDIHG BURDEN ESTIHATE To LICENSEE EVENT REPORT (LER) THE INFORHATIOH AHD RECORDS HANAGEHEHT BRANCH TEXT CONTINUATION (HNBB 7714), U.S. NUCLEAR REGULATORY CONHISSION, NASHINGTOH, Dc 20555-0001 AHD To THE PAPERlJORK REDUCTION PROJECT (3140-0104), OFFICE OF NAHAGENENT AHD BUDGET llASHIHGTOH Dc 20503.

FACILITY NANE 1 DOCKET NNBER 2 LER NWER 6 PAGE 3

'YEAR SEQUENTIAL REVISIOH R.E. Ginna Nuclear Power Plant 05000244 93 006-- 00 8 OF 11 TEXT (If more space is required, use additionat copies of NRC Form 366A) (17) o Following the reactor trip, PRZR water level decreased to below 04, due to a moderate RCS cooldown. This cooldown occurred during the post trip recovery period. This cooldown was bounded by the plant accident analysis, and did not exceed the TS limit of 100 degrees F per hour. Additional mitigation was provided by closing the MSIVs and stopping the main feedwater pumps. TS 3.1.1.5 states, in part, that when the RCS temperature is at or above 350 degrees F, the pressurizer water level will be maintained between 124 and 874 of level span to be considered operable. TS 3.1.1.5 also states, in part, that if the pressurizer is inoperable due to water level, restore the pressurizer to operable status within six (6) hours or have the reactor below an RCS temperature of 350 degrees F and the RHR system in operation within an additional six (6) hours. Pressurizer water level recovered to greater than 124 level within ten (10) minutes, well before the six (6) hour action statement.

o Both S/G levels decreased to less than 04 following the reactor trip. This is an expected observed transient. TS 4.3.5.5 states that in order to demonstrate that a reactor coolant loop is operable, the S/G water level shall be >/=

164. Thus, both coolant loops were inoperable, even though both loops were still in operation and performing their intended function of decay heat removal. Both S/Gs were available as a heat sink, and sufficient AFH flow was maintained for adequate steam release from both S/Gs. TS 3.1.1.1(c) states, in part, that except for special tests, when the RCS temperature is at or above 350 degrees F with the reactor power less than or equal to 130 MWT (8.54), at least one reactor coolant loop and its associated S/G and reactor coolant pump shall be in operation. Both reactor coolant loops were in operation, but the S/Gs were inoperable due to level indication. Both loops were returned to operable status. "A" S/G level was restored to > 164 within one (1) minute, and "B" S/G level was restored to > 164 in approximately ten (10) seconds.

HRC FORH 366A (5 92)

HRC FORH 366A U.S IN)CLEAR REGULATORY CQBIISSIQI APPROVED BY MB HO. 3150-0104 5-92) EXPIRES 5/31/95 EST INATED BURDEN PER RESPONSE TO CONPLY MITH THIS INFORNATI OH COLLECTION REQUEST 50 ~ 0 HRS.

FORNARD COHHEHl'S REGARD IHG BURDEH EST I HATE TO LICENSEE EVENT REPORT (LER) THE IHFORHATI OH AHD RECORDS NANAGENEHT BRANCH TEXT CONTINUATION (HHBB 7714), U.S. NUCLEAR REGULATORY COHHISSIOH, HASHIHGTOH, DC 20555-0001 AND TO THE PAPERNORK REDUCTION PROJECT (3140 0104), OFFICE OF NANAGENEHT AHD BUDGET llASNIHGTON DC 20503.

FACI LITY RANE 1 DOCKET HlMBER 2 LER HINBER 6 PAGE 3 YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 93 -- 006 pp 9 OF 11 TEXT (If more space is required, use additional copies oi NRC Form 366A) (17) o Condensate Storage Tank (CST),level decreased to less than 22,500 gallons of water, due to a malfunction of the condensate makeup and reject valves. The malfunction caused the CSTs to fill the main condenser hotwell. TS 3.4.3 states, in part, that with the RCS temperature at or above 350 degrees F, one or more CSTs with a minimum of 22,500 gallons of water, shall be operable as a source of auxiliary feedwater. With the CSTs inoperable, within four (4) hours either restore the CSTs to operable status, or be in at least hot shutdown within the following six (6) hours and at an RCS temperature less than 350 degrees F within the following six (6) hours. The reactor was already at hot shutdown, and the CSTs were restored to operable status within approximately fifty statement.

(50) minutes, well before the twelve (12) hour action Based on the above and a review of post trip data and past plant transients, it can be concluded that the plant operated as designed and that there were no unreviewed safety questions and that the public's health and safety was assured at all times. f V. CORRECTIVE ACTION A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:

o The "A" MFRV Bailey positioner was replaced. (Refer to LER 92-006, Rev. 1, Docket No. 50-244.) The newly installed positioner was reattached to the valve actuator linkage rod using a vendor-recommended screw with an elastic stop nut.

HRC FORH 366A (5-92)

0 HRC FORH 366A U.S INCLEAR REGULATORY CRIBS ION APPROVED BY (HN HO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPOHSE TO COHPLY WITH THIS INFORHATIOH COLLECTIOH REQUEST: 50.0 HRS.

FORWARD COHHEHTS REGARDIHG BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE INFORHATIOH AND RECORDS HANAGEHEHT BRANCH TEXT CONTINUATION (HHBB 7714), U.S. NUCLEAR REGULATORY COHHISSION, WASHINGTON, DC 20555-0001 AHD TO THE PAPERWORK REDUCT10H PROJECT (31/0-0104), OFFICE OF HANAGEHEHT AHD BUDGET WASHINGTON OC 20503.

FACILITY HAHE 1 DOCKET HNBER 2 LER HWBER 6 PAGE 3 SEQUENTIAL REVISION YEAR R.E. Ginna Nuclear Power Plant 05000244 93 -- 006 00 10 OF 11 TEXT (lf more space is required, use additional copies of NRC Form 366A) (1)')

o The >>B>> MFRV positioner was inspected, and rework of the positioner was performed. This included installation of a vendor-recommended screw with an elastic stop nut.

o The >>A>> and >>B>> MFRVs were repacked. (Refer to LER 92-006, Rev. 1, Docket No. 50-244.)

o Linkage connections for other accessible valves with Bailey positioners were inspected to ensure satisfactory integrity of the connections.

o The malfunction of the condensate makeup and reject valves was caused by a fitting leak which was associated with the common demand signal shared by both valves. The fitting was tightened, and both valves were verified to respond correctly to control main condenser hotwell level.

B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:

o Applicable procedures will be upgraded to ensure Bailey vendor manual information concerning feedback linkage arm:

connections is addressed.

0 Training will be conducted to enhance the knowledge of appropriate personnel on the general topic of fasteners, and stressing linkage arm connections, specifically.

0 Rework of positioner feedback linkage arm connections, for all other valves with Bailey positioners, will be accomplished. This will include installation of vendor-recommended screws and elastic stop nuts.

NRC FORH 366A (5 92)

HRC FORH 366A U.S WCLEAR REGULATORY CQBIISSIOH APPROVED BY QBI HO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COMPLY UITH THIS INFORHATIOH COLLECTION REQUEST: 50.0 HRS.

FORNARD COHMEHTS REGARDING BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE IHFORHATION AND RECORDS HANAGEMENT BRANCH (HNBB 7714), U.S. NUCLEAR REGULATORY COHHISSION, TEXT CONTINUATION llASHINGTON, DC 20555-0001 AHD TO THE PAPERNORK REDUCTIOH PROJECT (3140-0104), OFFICE OF HANAGEHENT AND BUDGET UASHINGTON DC 20503.

FACILITY NAIK 1 DOCKET HQSER 2 LER HINBER 6 PAGE 3 SEOUENT IAL REVISION YEAR R.E. Ginna Nuclear Power Plant 05000244 93 006 00 11 OF 11 TEXT (If more space is required, use additional copies of HRC Form 366A) (17)

VI. ADDITIONAL INFORMATION A. FAILED COMPONENTS:

The failed component was the "A" MFRV positioner feedback linkage arm connection. This assembly is a Bailey pneumatic positioner, model AV 112100, manufac-tured by Bailey Controls Inc.

B. PREVIOUS LERs ON SIMILAR EVENTS:

A similar LER event historical search was conducted with the following results: No documentation of similar LER events with the same root cause at Ginna Nuclear Power Plant could be identified. However, LERs88-005, 90-'007, and 90-010 were similar events with different root causes.

C. SPECIAL COMMENTS:

LER 92-006, Rev. 1, identified three corrective actions related to MFRVs: replace the "A" MFRV actuator with a rebuilt actuator, replace the "A" MFRV positioner, and repack both MFRVs. Two of these corrective actions were accomplished in response to this event (LER 93-006). Post-maintenance testing of MFRVs, and subsequent satisfactory operation of both MFRVs, have demonstrated that replacement of the "A" MFRV actuator is no longer required.

HRC FORM 366A (5-92)