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| {{#Wiki_filter:*-,-.... -,__, ** ~-* ***.** _ * *----** . *l '--4->-*-...:C" ** -.~ ............ | | {{#Wiki_filter:*- , -. . . . -,__, ** ~ - * ~ ***.** _ * *--- -** . *l '--4->-*-...:C" ** - . ~ ............ __ ., __ ._ ... _ *.** _, __ * - * - ~ - - - - - - ' * . . . _.- - ~ - - - - * * - - * - * - - - - - - ~ - - - - - - - - ... * * * - - - ~ - * " * - - - * - - ~ *** -- |
| __ ., __ ._ ... _ *.** _, __ *-*-~------' * ... _.--~----**--* | | POW 28-06-01 NRC Form 3611 U.S. NUCLEAR REGULATORY COMMISSION 19-83) |
| -*------~-------- | | APPROVED 0MB NO. 3160-0104 EXPIRES: 8/31 /88 LICENSEE EVENT REPORT (LERI FACILITY NAME 11) DOCKET NUMBER 12) I PAuE 131 TITLE C*I Surrv Power Statton. Unit 1 !0 15 I O IO I O I'J I A I n 1 loF n I ~ |
| ... ***---~-*"*-- | | Individual Rod Position Indicators Inoperable Due to Dirtv Contacts in a DC Power Suoolv EVENT DATE 15) LER NUMBER (6) REPORT DA'fE (7) OTHER FACILITIES INVOLVED (8) |
| -*--~ *** --POW 28-06-01 NRC Form 3611 19-83) LICENSEE EVENT REPORT (LERI U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3160-0104 EXPIRES: 8/31 /88 Surrv Power Statton. Unit 1 !DOCKET NUMBER 12) I PAuE 131 0 15 I O IO I O I 'J I A I n 1 loF n I FACILITY NAME 11) TITLE C*I Individual Rod Position Indicators Inoperable Due to Dirtv Contacts in a DC Power Suoolv EVENT DATE 15) LER NUMBER (6) REPORT DA'fE (7) OTHER FACILITIES INVOLVED (8) MONTH DAY YEAR YEAR .tt tr MONTH DAY YEAR FACILITY NAMES DOCKET NUMBER(S) o I 1 1 I 7 8-17 a I 1 --ol 1 1 s -o Io ol s 1 I 7 s I 7 OPERATING MODE (9) THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Chsck ons or mars of the fol/ovying) | | MONTH DAY YEAR YEAR .tt SE~~~~~~AL tr ~E~~~~ MONTH DAY YEAR FACILITY NAMES DOCKET NUMBER(S) oI 1 1 I 7 8-17 a I1 - - ol 1 1s - oIo ol s 1 I 7 sI 7 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Chsck ons or mars of the fol/ovying) (11 I OPERATING MODE (9) |
| (11 I N 50.73lalC2J(iv) | | N I1 I O .O - |
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| 2D.'°2(bl 20.'°5(c)
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| | POWER Lf~~L r 20.'°5lalC1 JIil 20.'°51all1lliil |
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| &0.73(1112) lvllll(BJ 51!.73(alC2llxl OTHER (S1>>clfy in Ab1tnct -/HJ/ow *nd In Toxt, NRC Form 366A) -20.'°5(all1 llivl &0.73(alC2l(il) | | 50.73CalC2lM 50.73(alC2l(vll) 73.71(*1 OTHER (S1>>clfy in Ab1tnct |
| --2D.'°51al11 lM &0.73C.l(2l(lli)
| | /HJ/ow *nd In Toxt, NRC Form 366A) rt*i= - |
| ! LICENSEE CONTACT FOR THIS LER 112) NAME .... TELEPHONE NUMBER AREA CODE D. L. Benson, *station Manager 8 I O I 4 3 15 I 7 I -13 11 I 8 f CAUSE SYSTEM COMPONENT I I I I I I I I COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 TURER I I I I I I Rrco~;:g~E lililllilllililil!li!ilililil!lililllilllilil!lll!l!l
| | ~ |
| ~AUSE SYSTEM I t COMPONENT MANUFAC* TURER I I I I I I I I I I I I SUPPLEMENTAL REPORT EXPECTED (1'1 MONTH DAY YEAR EXPECTED SUBMISSION DATE 115) . f YES (If yos, comp/or* EXPECTED SUBMISSION DA TEI I ABSTRACT (Limit to 1400 1poco1, I.e., opproxim*t*ly fiftaen 1ingle-1poc*
| | 20.'°5Call1 llilil &0.731*ll2JCIJ 50.73(alC2lCvllllCAJ 20.'°5(all1 llivl 2D.'°51al11 lM - ! |
| rypewrltran lines/ 1161 NRC Form 3118 9-83 On July 17, 1987 at 1440 hours with Unit 1 at 100% power, the Unit 1 Individual Rod Position Indicators (IRPI) {EIIS-ZI} | | &0.73(alC2l(il) |
| for shutdown banks A and Band control banks A, B, and c indicated 28 steps below the control rod group demand counter position {EIIS-CTR}. | | &0.73C.l(2l(lli) |
| Control Bank D indicated 26 steps below its control rod group demand counter position. | | LICENSEE CONTACT FOR THIS LER 112) |
| The IRPis were declared inoperable in accordance with Technical Specifications 3.12.E. The IRPis were returned to service at 1524 hours. Instrument Technicians determined that the DC power supply contacts to the Rod Position Indication Cabinet were dirty. The contacts for the DC power supply were cleaned, and the IRPI indication*returned to the proper position. | | - &0.73(1112) lvllll(BJ 51!.73(alC2llxl NAME .... TELEPHONE NUMBER AREA CODE D. L. Benson, *station Manager 8 I OI 4 3 15 I 7 I - 13 11 I 8 f COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 MANUFAC- MANUFAC* |
| ' ~-8708210058 870817 PDR ADDCK 05000280 S. PDR I I NRC Form 368A (9-831 FACILITY NAME (1) e e LICENSEE EVENT REPORT (LERI TEXT CONTINUATION POW 28-06-01 U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31 /88 DOCKET NUMIIER (2) LER NUMBER (61 PAGE (31 Surry Power Station, Unit 1 0 15 IO IO IO I 218 IO 8 17 -011 I 5 -0 I O 01 :i OF O I 3 NRC FORM 3661l (11-831 1. 0 Description of the Event On. July 17, 1987. at 1440 hours with. Unit 1 at 100% power, the Unit 1 Individual Rod Position Indicators (IRPI) {EIIS-ZI} | | CAUSE SYSTEM COMPONENT SYSTEM COMPONENT TURER TURER Rrco~;:g~E lililllilllililil!li!ilililil!lililllilllilil!lll!l!l ~AUSE I I I I I I I I I I I I I I I I I I I I I t I I I I I I SUPPLEMENTAL REPORT EXPECTED (1'1 MONTH DAY YEAR EXPECTED SUBMISSION |
| for shutdown banks A and B and control banks A, B, and C indicated 28 steps below the control rod group demand counter position {EIIS-CTR}. | | .f YES (If yos, comp/or* EXPECTED SUBMISSION DA TEI DATE 115) |
| Control Bank D indicated 26 steps below its control rod group demand counter position. | | I I I ABSTRACT (Limit to 1400 1poco1, I.e., opproxim*t*ly fiftaen 1ingle-1poc* rypewrltran lines/ 1161 On July 17, 1987 at 1440 hours with Unit 1 at 100% power, the Unit 1 Individual Rod Position Indicators (IRPI) |
| The IRPis were declared inoperable in accordance with Technical Specifications 3 *. 12. E. The IRPis were returned to service at 1524 hours. 2.0 Safety Consequences and Implications IRPI provides control rod position indication in the Main Control Room. The Control Rod Demand Counters which indicate control rod po_sition as demanded by the Rod Control System, remained operable during the time that IRPis were not operable. | | {EIIS-ZI} for shutdown banks A and Band control banks A, B, and c indicated 28 steps below the control rod group demand counter position {EIIS-CTR}. Control Bank D indicated 26 steps below its control rod group demand counter position. |
| Inoperable IRPis will not affect the operation of the Control Rod Assemblies | | The IRPis were declared inoperable in accordance with Technical Specifications 3.12.E. The IRPis were returned to service at 1524 hours. |
| {EIIS-ROD} | | Instrument Technicians determined that the DC power supply contacts to the Rod Position Indication Cabinet were dirty. |
| and all rods were capable of being dropped if required. | | The contacts for the DC power supply were cleaned, and the IRPI indication*returned to the proper position. |
| Therefore, this event did not constitute an unreviewed safety question and the health and safety of the public were not affected. | | ' ~- |
| 3.0 Cause Instrument Technicians determined that the DC power supply contacts to the Rod Position Indication Cabinet were dirty. 4.0 Inunediate Corrective Actions The contacts for the DC power supply were cleaned, and the IRPI indication returned to the proper position. | | 8708210058 870817 PDR ADDCK 05000280 S. PDR NRC Form 3118 9-83 |
| : 5. 0 Additional Corr.ective* | | |
| Actions None. | | POW 28-06-01 e e U.S. NUCLEAR REGULATORY COMMISSION NRC Form 368A (9-831 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31 /88 FACILITY NAME (1) DOCKET NUMIIER (2) LER NUMBER (61 PAGE (31 Surry Power Station, Unit 1 0 15 IO IO IO I 218 IO 8 17 - 011 I5 - 0 I O 01 :i OF OI 3 |
| * U.S.GPO: 1986*0*624-538/455 | | : 1. 0 Description of the Event On. July 17, 1987. at 1440 hours with. Unit 1 at 100% power, the Unit 1 Individual Rod Position Indicators (IRPI) {EIIS-ZI} for shutdown banks A and B and control banks A, B, and C indicated 28 steps below the control rod group demand counter position |
| ... .... *-----*----- | | {EIIS-CTR}. Control Bank D indicated 26 steps below its control rod group demand counter position. |
| .. *--*-* *---*-***-* | | The IRPis were declared inoperable in accordance with Technical Specifications 3 *. 12. E. The IRPis were returned to service at 1524 hours. |
| ----~---~-----****-*-*** | | 2.0 Safety Consequences and Implications IRPI provides control rod position indication in the Main Control Room. The Control Rod Demand Counters which indicate control rod po_sition as demanded by the Rod Control System, remained operable during the time that IRPis were not operable. |
| *--------~-*~~- | | Inoperable IRPis will not affect the operation of the Control Rod Assemblies {EIIS-ROD} and all rods were capable of being dropped if required. Therefore, this event did not constitute an unreviewed safety question and the health and safety of the public were not affected. |
| ........:,..___ | | 3.0 Cause Instrument Technicians determined that the DC power supply contacts to the Rod Position Indication Cabinet were dirty. |
| .. ---.__... ___ ,_ ___ *..... e* e POW 28-06-01 NRC Form 31111A (9-831 LICENSEE EVENT REPORT ILER) TEXT CONTINUATION U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31 /BB FACILITY NAME 11 l DOCKET NUMBER 121 LER NUMBER (6) PAGE (31 Surry Power Station, Unit 1 o 15 Io Io Io , 2 I 8 ,o 8 ,1 -0 , 115 -0 IO O 1 3 OF 013 TEXT f/f tntn _..ii,.,,.,..,, -NditioMI NRC l'oml .&,l'*l 1171 NRC FOAM 3HA (ll-831 6.0 Actlons Taken to Prevent Recurrence None. 7.0 Similar Events *None. 8.0. Manufacturer/Model Number Westinghouse/T"17Pe E2786. ' \ '*
| | 4.0 Inunediate Corrective Actions The contacts for the DC power supply were cleaned, and the IRPI indication returned to the proper position. |
| * U.S.GPO: 198B*0*624*538/455
| | : 5. 0 Additional Corr.ective* Actions None. |
| .e August 17, 1987 U.S. Nuclear Regulatory Commission Docmnent Control Desk 016 Phillips Building. | | NRC FORM 3661l |
| Washington, D.C. 20555 Gentlemen:
| | * U.S.GPO: 1986*0*624-538/455 (11-831 |
| : e. VIRGINIA ELECTRIC AND POWER COMPAtl!Y Surry Power Station P. 0. Box 316 Surry, Virginie 23883 Serial No. : 87-017 Docket'Bo.:
| | |
| 50-280 Licensee Bo.: DPR-32 Pursuant to Surry Power Station Technical.Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report for Surry Unit 1. | | ... .... *-----*-----..*--*-* *---*-***-* --- -~---~-----****-*-*** *--------~-*~~- ........:,..___ ~ .__... ,_ *..... |
| * REPORT NUMBER 87-015-00 This report has been reviewed by the Station Nuclear_ Safety and Operating Committee and will be reviewed by Safety Evaluation and Control * . Very truly yours, David*L. Benson Station Manager Enclosure cc:. Dr. J. Belson Grace Regional Administrator Suite 2900 101 Marietta Street, BW Atlanta, Georgia 30323}} | | e* e POW 28-06-01 NRC Form 31111A U.S. NUCLEAR REGULATORY COMMISSION (9-831 LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31 /BB FACILITY NAME 11 l DOCKET NUMBER 121 LER NUMBER (6) PAGE (31 Surry Power Station, Unit 1 o 15 Io Io Io , 2 I 8 ,o 8 ,1 - 0 , 115 - 0 IO O1 3 OF 013 TEXT f/f tntn _..ii,.,,.,..,, - NditioMI NRC l'oml .&,l'*l 1171 6.0 Actlons Taken to Prevent Recurrence None. |
| | 7.0 Similar Events |
| | *None. |
| | 8.0. Manufacturer/Model Number Westinghouse/T"17Pe E2786. |
| | ' \ |
| | NRC FOAM 3HA (ll-831 |
| | * U.S.GPO: 198B*0*624*538/455 |
| | |
| | .e e. |
| | VIRGINIA ELECTRIC AND POWER COMPAtl!Y Surry Power Station P. 0. Box 316 Surry, Virginie 23883 August 17, 1987 U.S. Nuclear Regulatory Commission Serial No. : 87-017 Docmnent Control Desk Docket'Bo.: 50-280 016 Phillips Building. Licensee Bo.: DPR-32 Washington, D.C. 20555 Gentlemen: |
| | Pursuant to Surry Power Station Technical.Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report for Surry Unit 1. |
| | * REPORT NUMBER 87-015-00 This report has been reviewed by the Station Nuclear_ Safety and Operating Committee and will be reviewed by Safety Evaluation and Control * |
| | .Very truly yours, David*L. Benson Station Manager Enclosure cc:. Dr. J. Belson Grace Regional Administrator Suite 2900 101 Marietta Street, BW Atlanta, Georgia 30323}} |
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Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket ML18153A2201998-02-0606 February 1998 LER 98-001-00:on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was submitted.W/980206 Ltr ML18153A2071998-01-13013 January 1998 LER 97-012-01:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors ML18153A2101998-01-13013 January 1998 LER 97-009-01:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status ML18153A1911997-11-26026 November 1997 LER 97-011-00:on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage. ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With 990115 Ltr ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un. ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With 981214 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With 981111 Ltr ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With 981012 Ltr ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2.W/980807 Ltr ML18152B7621998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Surry Power Station,Units 1 & 2.W/980707 Ltr ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML18153A3141998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Surry Power Station,Units 1 & 2.W/980610 ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B8161998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Surry Power Station Units 1 & 2.W/980508 Ltr ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML20217P9941998-04-0707 April 1998 Safety Evaluation Granting Licensee Third 10-yr Inservice Insp Program Relief Requests SR-018 - Sr-024 ML18153A2951998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sps,Units 1 & 2.W/ 980408 Ltr ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket 1999-09-30
[Table view] |
Text
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POW 28-06-01 NRC Form 3611 U.S. NUCLEAR REGULATORY COMMISSION 19-83)
APPROVED 0MB NO. 3160-0104 EXPIRES: 8/31 /88 LICENSEE EVENT REPORT (LERI FACILITY NAME 11) DOCKET NUMBER 12) I PAuE 131 TITLE C*I Surrv Power Statton. Unit 1 !0 15 I O IO I O I'J I A I n 1 loF n I ~
Individual Rod Position Indicators Inoperable Due to Dirtv Contacts in a DC Power Suoolv EVENT DATE 15) LER NUMBER (6) REPORT DA'fE (7) OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR .tt SE~~~~~~AL tr ~E~~~~ MONTH DAY YEAR FACILITY NAMES DOCKET NUMBER(S) oI 1 1 I 7 8-17 a I1 - - ol 1 1s - oIo ol s 1 I 7 sI 7 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Chsck ons or mars of the fol/ovying) (11 I OPERATING MODE (9)
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LICENSEE CONTACT FOR THIS LER 112)
- &0.73(1112) lvllll(BJ 51!.73(alC2llxl NAME .... TELEPHONE NUMBER AREA CODE D. L. Benson, *station Manager 8 I OI 4 3 15 I 7 I - 13 11 I 8 f COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 MANUFAC- MANUFAC*
CAUSE SYSTEM COMPONENT SYSTEM COMPONENT TURER TURER Rrco~;:g~E lililllilllililil!li!ilililil!lililllilllilil!lll!l!l ~AUSE I I I I I I I I I I I I I I I I I I I I I t I I I I I I SUPPLEMENTAL REPORT EXPECTED (1'1 MONTH DAY YEAR EXPECTED SUBMISSION
.f YES (If yos, comp/or* EXPECTED SUBMISSION DA TEI DATE 115)
I I I ABSTRACT (Limit to 1400 1poco1, I.e., opproxim*t*ly fiftaen 1ingle-1poc* rypewrltran lines/ 1161 On July 17, 1987 at 1440 hours0.0167 days <br />0.4 hours <br />0.00238 weeks <br />5.4792e-4 months <br /> with Unit 1 at 100% power, the Unit 1 Individual Rod Position Indicators (IRPI)
{EIIS-ZI} for shutdown banks A and Band control banks A, B, and c indicated 28 steps below the control rod group demand counter position {EIIS-CTR}. Control Bank D indicated 26 steps below its control rod group demand counter position.
The IRPis were declared inoperable in accordance with Technical Specifications 3.12.E. The IRPis were returned to service at 1524 hours0.0176 days <br />0.423 hours <br />0.00252 weeks <br />5.79882e-4 months <br />.
Instrument Technicians determined that the DC power supply contacts to the Rod Position Indication Cabinet were dirty.
The contacts for the DC power supply were cleaned, and the IRPI indication*returned to the proper position.
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8708210058 870817 PDR ADDCK 05000280 S. PDR NRC Form 3118 9-83
POW 28-06-01 e e U.S. NUCLEAR REGULATORY COMMISSION NRC Form 368A (9-831 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31 /88 FACILITY NAME (1) DOCKET NUMIIER (2) LER NUMBER (61 PAGE (31 Surry Power Station, Unit 1 0 15 IO IO IO I 218 IO 8 17 - 011 I5 - 0 I O 01 :i OF OI 3
- 1. 0 Description of the Event On. July 17, 1987. at 1440 hours0.0167 days <br />0.4 hours <br />0.00238 weeks <br />5.4792e-4 months <br /> with. Unit 1 at 100% power, the Unit 1 Individual Rod Position Indicators (IRPI) {EIIS-ZI} for shutdown banks A and B and control banks A, B, and C indicated 28 steps below the control rod group demand counter position
{EIIS-CTR}. Control Bank D indicated 26 steps below its control rod group demand counter position.
The IRPis were declared inoperable in accordance with Technical Specifications 3 *. 12. E. The IRPis were returned to service at 1524 hours0.0176 days <br />0.423 hours <br />0.00252 weeks <br />5.79882e-4 months <br />.
2.0 Safety Consequences and Implications IRPI provides control rod position indication in the Main Control Room. The Control Rod Demand Counters which indicate control rod po_sition as demanded by the Rod Control System, remained operable during the time that IRPis were not operable.
Inoperable IRPis will not affect the operation of the Control Rod Assemblies {EIIS-ROD} and all rods were capable of being dropped if required. Therefore, this event did not constitute an unreviewed safety question and the health and safety of the public were not affected.
3.0 Cause Instrument Technicians determined that the DC power supply contacts to the Rod Position Indication Cabinet were dirty.
4.0 Inunediate Corrective Actions The contacts for the DC power supply were cleaned, and the IRPI indication returned to the proper position.
- 5. 0 Additional Corr.ective* Actions None.
NRC FORM 3661l
- U.S.GPO: 1986*0*624-538/455 (11-831
... .... *-----*-----..*--*-* *---*-***-* --- -~---~-----****-*-*** *--------~-*~~- ........:,..___ ~ .__... ,_ *.....
e* e POW 28-06-01 NRC Form 31111A U.S. NUCLEAR REGULATORY COMMISSION (9-831 LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31 /BB FACILITY NAME 11 l DOCKET NUMBER 121 LER NUMBER (6) PAGE (31 Surry Power Station, Unit 1 o 15 Io Io Io , 2 I 8 ,o 8 ,1 - 0 , 115 - 0 IO O1 3 OF 013 TEXT f/f tntn _..ii,.,,.,..,, - NditioMI NRC l'oml .&,l'*l 1171 6.0 Actlons Taken to Prevent Recurrence None.
7.0 Similar Events
8.0. Manufacturer/Model Number Westinghouse/T"17Pe E2786.
' \
NRC FOAM 3HA (ll-831
- U.S.GPO: 198B*0*624*538/455
.e e.
VIRGINIA ELECTRIC AND POWER COMPAtl!Y Surry Power Station P. 0. Box 316 Surry, Virginie 23883 August 17, 1987 U.S. Nuclear Regulatory Commission Serial No. : 87-017 Docmnent Control Desk Docket'Bo.: 50-280 016 Phillips Building. Licensee Bo.: DPR-32 Washington, D.C. 20555 Gentlemen:
Pursuant to Surry Power Station Technical.Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report for Surry Unit 1.
- REPORT NUMBER 87-015-00 This report has been reviewed by the Station Nuclear_ Safety and Operating Committee and will be reviewed by Safety Evaluation and Control *
.Very truly yours, David*L. Benson Station Manager Enclosure cc:. Dr. J. Belson Grace Regional Administrator Suite 2900 101 Marietta Street, BW Atlanta, Georgia 30323