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* VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT 88-08 APPROVED: ATION MANAGER ' :3809200124 880:::::31 PDR ADOCK 05000280 R PDC -~ POW 34-04 
POW 34-04
< '
.. . .. ' ''f VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT   88-08 APPROVED:   ~ ~~
* SECTION Operating Data Report -Unit No. 1 Operating Data* Report -Unit No. 2 1 Unit Shutdowns and Power Reductions  
ATION MANAGER
-Unit No. 1 Unit Shutdowns and Power Reductions  
    '       :3809200124 880:::::31     -~
-Unit No. 2 Average Daily Unit Power Level -Unit No. 1 Average Daily Unit Power Level -Unit No. 2 Summary of Operating Experience  
PDR ADOCK 05000280 R                 PDC
-Unit No. 1 Summary of Operating Experience  
* 1 SECTION                                                       PAGE Operating Data Report - Unit No. 1                                1 Operating Data* Report - Unit No. 2                               3 Unit Shutdowns and Power Reductions - Unit No. 1                 4 Unit Shutdowns and Power Reductions - Unit No. 2 Average Daily Unit Power Level - Unit No. 1                       6 Average Daily Unit Power Level - Unit No. 2                       7 Summary of Operating Experience - Unit No. 1                     8 Summary of Operating Experience - Unit No. 2                     9 Facility Changes Requiring NRC Approval                         ll:
-Unit No. 2 Facility Changes Requiring NRC Approval Facility Changes That Did Not Require NRC Approval Procedure or Method of Operation Changes that Did Not Require NRC Approval
Facility Changes That Did Not Require NRC Approval               12 Procedure or Method of Operation Changes that Did Not Require NRC Approval                                             15 Procedure or Method of Operation that Did Require NRC Approval   16 Tests and Experiments Requiring NRC Approval                     17 Tests and Experiments That Did Not Require NRC Approval         18 Chemistry Report                                                 19 Fuel Handling - Unit No. 1                                       20 Fuel Handling - Unit No. 2                                       21 Description of Periodic Test Which Were Not Completed Within the Time Limits Specified in Technical Specifications           22
* Procedure or Method of Operation that Did Require NRC Approval Tests and Experiments Requiring NRC Approval Tests and Experiments That Did Not Require NRC Approval Chemistry Report Fuel Handling -Unit No. 1 Fuel Handling -Unit No. 2 Description of Periodic Test Which Were Not Completed Within the Time Limits Specified in Technical Specifications PAGE 1 3 4 6 7 8 9 ll: 12 15 16 17 18 19 20 21 22 PAGE 1 *
 
* OPERA?ING DATA REPORX DOCKE'I NO. 50-280 DATE 09/08/88 . COMPLETED BY L. A. Warren TELEPHONE 804-357-3184 OPERATING STAXUS l. Unit Name: Surry Unit # 1 Notes 2. Reporting Period: August O 1 thru 31. 19 8 8 3. Licensed Thermal Power (MWt): 2441 -..:::..::..=-=------
PAGE 1 OPERA?ING DATA REPORX DOCKE'I NO. 50-280 DATE     09/08/88
: 4. Nameplate Rating (Gross MWe): _.,;8~4.:.:7:..::*:..::5
                                                                                            . COMPLETED BY     L. A. Warren TELEPHONE     804-357-3184 OPERATING STAXUS
___ _.,, __ _ 5. Design Electrical Rating (Net MWe): 788 6. Maximum Dependable Capacity (Gross MWe): ~82:;.,;0;...._
: l. Unit Name:           Surry Unit # 1                                   Notes
__ 7. Maximum Dependable Capacity (Net MWe): 781 8, If Changes Occur in Capacity Ratings (Items Number 3 nirough 7) Since Last Report, Give Reasons: 9. Power Level Io Which Restricted, If Any (Net MWe): 10. Reasons For Restrictions, If Any: This Month Yr.-to*Date 11, Hours In Reporting Period 744.0 5855.0 12. Number of Hours Reactor Was Critical 708.7 3437.0 13, Reactor Reserve Shutdown Hours 0 0 14. Hours Generator On-Line 688.0 3316.6 15, Unit Reserve Shutdown Hours 0 0 16. Gross Thermal Energy Generated (HWB) 1637979.2 7682198.9
: 2. Reporting Period:     August O1 thru 31. 19 8 8 2441
: 17. Gross Electrical Energy Generated (HWB) 544765.0 2573560.0
: 3. Licensed Thermal Power (MWt): -..:::..::..=-=------
: 18. Net Electrical Energy Generated (HWB) 516472. 0 2442986.0
: 4. Nameplate Rating (Gross MWe): _.,;8~4.:.:7:..::*:..::5____.,,_ __
: 19. Unit Service Factor 92.5% 56.7% 20. Unit Available Factor 92.5% 56. 7% 21. Unit Capacity Factor (Using MDC Net) 88.9% 53.4% 22. Unit Capacity Factor (Using DER Net) 88.1% 53% 23. Unit Forced Rate 7.5% 3.9% 24. Shutdown*
: 5. Design Electrical Rating (Net MWe):                       788
Scheduled Over Next 6 Month* (Xype, Date, and Duration of Each), 25. If Shut Down At End Of Report Period Estimated Date of Startups 26. Unit* In Teat Status (Prior to Couaercial Operatioa)1 lH1TIAL CRinCALiff IH1'nAL !L!C'l'llCiff COHHER.CIAL OPERAnON rorecaat Cumulative 137567.0 88160.4 3774. 5 86287.8 3736.2 200402420.3 64948733.0 61598362.0 62.7% 65.4% 57.9% 56 .-8% 17 .2% Achieved (9/77)
: 6. Maximum Dependable Capacity (Gross MWe): ~82:;.,;0;....___
* ** OPERA7ING DA:rA REPOJa OPERATING SL\l'US (JULY) PAGE I CORRECT~ COPY 09/0.8/88 PAGE 2 DC>CREl: NO. 5 0-28 0 DA1'B 8/3/88 COMPLETED BY L. A. warren m.EPHONE 804-357-3184
: 7. Maximum Dependable Capacity (Net MWe):                   781 8, If Changes Occur in Capacity Ratings (Items Number 3 nirough 7) Since Last Report, Give Reasons:
: 1. Unit Name: Surry Unit # 1 Notes 2. Reporting Period: July O 1 thru 31, 1988 3. Licensed Thermal Power (MWt): __,2.._4_4::..:l=-------
: 9. Power Level Io Which Restricted, If Any (Net MWe):
: 10. Reasons For Restrictions, If Any:
This Month         Yr.-to*Date           Cumulative 11,   Hours In Reporting Period                                           744.0             5855.0               137567.0
: 12. Number of Hours Reactor Was Critical                               708.7             3437.0               88160.4 13,   Reactor Reserve Shutdown Hours                                         0                     0               3774. 5
: 14. Hours Generator On-Line                                               688.0             3316.6               86287.8 15,   Unit Reserve Shutdown Hours                                           0                     0               3736.2
: 16. Gross Thermal Energy Generated (HWB)                           1637979.2         7682198.9           200402420.3
: 17. Gross Electrical Energy Generated (HWB)                           544765.0           2573560.0            64948733.0
: 18. Net Electrical Energy Generated (HWB)                           516472. 0         2442986.0            61598362.0
: 19. Unit Service Factor                                                 92.5%               56.7%                 62.7%
: 20. Unit Available Factor                                               92.5%               56. 7%               65.4%
: 21. Unit Capacity Factor (Using MDC Net)                                 88.9%               53.4%                 57.9%
: 22. Unit Capacity Factor (Using DER Net)                                 88.1%               53%                   56 .-8%
: 23. Unit Forced Rate                                                     7.5%                 3.9%               17 .2%
: 24. Shutdown* Scheduled Over Next 6 Month* (Xype, Date, and Duration of Each),
: 25. If Shut Down At End Of Report Period Estimated Date of Startups
: 26. Unit* In Teat Status (Prior to Couaercial Operatioa)1                             rorecaat              Achieved lH1TIAL CRinCALiff IH1'nAL !L!C'l'llCiff COHHER.CIAL OPERAnON (9/77)
 
(JULY)        PAGE I
* OPERA7ING DA:rA REPOJa
                                                                            **              CORRECT~ COPY 09/0.8/88 PAGE 2 DC>CREl: NO. 50-28 0 DA1'B     8/3/88 COMPLETED BY     L. A. warren m.EPHONE       804-357-3184 OPERATING SL\l'US
: 1. Unit Name:           Surry Unit # 1                           Notes
: 2. Reporting Period:   July O1 thru 31, 1988
: 3. Licensed Thermal Power (MWt): __,2.._4_4::..:l=-------
: 4. Nameplate Rating (Gross MWe): _8:..4.:.:7:..:*:.=5"------
: 4. Nameplate Rating (Gross MWe): _8:..4.:.:7:..:*:.=5"------
: s. Design Electrical Rating (Net HWe): 788 6. Maximum Dependable Capacity (Gross HWe): ----'82_0'------
: s. Design Electrical Rating (Net HWe):         788
: 7. Maximum Dependable Capacity (Net HWe): ___ 7_8 __ 1 __ _ a. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: 9. Power Level To Which Restricted, If Any (Net HWe): 10. Reasons For Restrictions, If Any: This Month Yr.-to-Date
: 6. Maximum Dependable Capacity (Gross HWe): ----'82_0'------
: 11. _Hours In Reporting Period D 5111.Q 12. Number of Hours Reactor Was Critical ~lS.Z 2728~3 13. Reactor Reserve Shutdown Hours Q.Q o*o 14. Hours Generator On-Line 33]~0 2628~6 lS. Unit Reserve Shutdown Hours a.a o*o
: 7. Maximum Dependable Capacity (Net HWe): ___7_8__1_ __
* 16. Gross Thermal Energy Generated (HWB) Z2UQ~.5 6Q44219~7
: a. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
: 17. Gross Electrical Energy Generated (HWB) 23~11Q.Q 20287915 18. Net Electrical Energy Generated (HWH) 221QlQ.Q 1926514~0
: 9. Power Level To Which Restricted, If Any (Net HWe):
: 19. Unit Service Factor 51;4% 20. Unit Available Factor 51~4% 21. Unit Capacity Factor (Using MDC Ret) 3B.Q% 48;3% 22. Unit Capacity Factor (Using DER Net) 32~2% jz;a% 23. Unit Forced Rate g;Q'.% 2* 9% 24. Shutdown, Scheduled Over Next 6 Month1 (type, Date, and Duration of !acbh 25. If Shut Down At Ind Of Report Period Estimated Date of Startup* 26. Unit1 In Teat Statu1 (Prior to C011111ercial Operation)a rorecaat CUmulative
: 10. Reasons For Restrictions, If Any:
]36823"0 **.874$.1:7-.
This Month           Yr.-to-Date           CUmulative
3774~5 85599.8 3736.2 198764441.1 64403968.0 61081890.0 . 62.6% 65~3%. 57. 7.% 56".7% 17~2% Achieved (9/77)
: 11. _Hours In Reporting Period                                 Z~~  D             5111.Q               ]36823"0
PAGE 3 *
: 12. Number of Hours Reactor Was Critical                     ~lS.Z               2728~3               **.874$.1:7-.
* OPERATING DATA REPORT DOCKET NO. 50-281 DATE 09/QR/RR COMPLETED BY L. A. warren TELEPHONE 804-357-3184 OPERATING STATUS 1. Unit Name: Surry Unit # 2 Notes 2. Reporting Period: Auqust 01 thru 31, 1988 3, Licensed Thermal Power (HWt): 2441 ......::::.......::.:a...------
: 13. Reactor Reserve Shutdown Hours                                Q.Q                 o*o                 3774~5
: 4.
: 14. Hours Generator On-Line                                   33]~0               2628~6               85599.8 lS. Unit Reserve Shutdown Hours                                   a.a                 o*o                 3736.2
* Nameplate Rating (Gross HWe): 847.S ____ ........., _____ _ 5. Design Electrical Rating (Net HWe): 788 6. Maximum Dependable Capacity (Gross HWe): _8.;;..2::;.0.;;.._
* 16. Gross Thermal Energy Generated (HWB)                 Z2UQ~.5             6Q44219~7           198764441.1
__ 7. Maximum Dependable Capacity (Net HWe): 781 8. If Changes Occur in Capacity Ratings (Items Number 3 l'hrough 7) Since Last Report, Give Reasons: 9. Power Level To Which Restricted, If Any (Net MWe): 10. Reasons For Restrictions, If Any:
: 17. Gross Electrical Energy Generated (HWB)               23~11Q.Q             20287915             64403968.0
* This Month Yr. -to-Date 11, Hours In Reporting Period 744.0 5855.0 12, Number of Hours Reactor Was Critical 744.0 4810.3 13, Reactor Reserve Shutdown Hours ,0 0 14. Hours Generator O~~Line 744.0 4776.7 15. Unit Reserve Shutdown Hours 0 0
: 18. Net Electrical Energy Generated (HWH)                 221QlQ.Q           1926514~0            61081890.0
* 16, Gross Thermal Energy Generated (HWB) 1492661. 9 11193381.0
: 19. Unit Service Factor                                         ~~.~%              51;4%                 . 62.6%
: 17. Gross Electrical Energy Generated (HWH) 443590.0 3649135.0
: 20. Unit Available Factor                                       ~~~5%              51~4%                   65~3%.
: 18. Net Electrical Energy Generated (HWB) 414737.0 3464826.0
: 21. Unit Capacity Factor (Using MDC Ret)                         3B.Q%               48;3%                   57. 7.%
: 19. Unit Service Factor 100% 81.6% 20. Unit Available Factor 100% 81.6% 21. Unit Capacity Factor (Using MDC Net) 71.4% 75.8% 22. Unit Capacity Factor (Using DER Net) 70. 7% 75.1% 23, Unit Forced Rate 0 18.4% 24, Shutdowns Scheduled Over Next 6 Months (?ype, Date, and Duration of Each): Refueling outage, 9/9/88, 68 days . 25, If Shut Down At End Of Report Period Estimated Date of Startupr 26. Units In rest Status (Prior to C011111ercial Operation)r INITIAL CRITICALITY INITIAL ELECTRICI?Y COMMERCIAL OPERAl'ION Forecast Cumulative 134447.0 89476.3 328.1 88075.0 0 206363743.7 67021959.0 63541303.0 65.5% 65.5% 60. 7% 60% 14.6% Achieved (9/77) 
: 22. Unit Capacity Factor (Using DER Net)                         32~2%               jz;a%                   56".7%
-II NO. DATE 11. >-,_ 88-06 8/12/88 s 88.:.07 8/15/88 F , 88-08 8/27 /8_8 IS 88-09 8/29/88 F 1 F: Forced 2 S: Scheduled (9/77) PAGE 4 UNIT SHUIOOWNS AND POWER REDUCTIONS DOCKET NO. _5_0_-_2_80
: 23. Unit Forced Rate                                             g;Q'.%             2* 9%                 17~2%
_____ _ UNIT NAME Surry Unit # DATE 09/08/88 alU'LETED BY L. A. Warren REPORT MONTH ___ A __ U ____ G._u ... s __ T......._l,_9,_88
: 24. Shutdown, Scheduled Over Next 6 Month1 (type, Date, and Duration of !acbh
___ _ TELEPHONE 804-357-3184
: 25. If Shut Down At Ind Of Report Period Estimated Date of Startup*
.., .. C .... a, 0 0 -N 0 C .. ... II C ... u .. .. 0 '1::1 .. II :::, II 0 II a, 0 .. II! .. CD .s::. :::, :::, J: II .. .s::. 0 II! II C :I: UJ JI 0 0 o.o F 1 56 A 3 o.o B 1 0.0 A 1 Reason: A -Equipment Failure (Explain)
: 26. Unit1 In Teat Statu1 (Prior to C011111ercial Operation)a               rorecaat               Achieved (9/77)
B -Maintenance or Test C -Refueling D -Regulatory Restriction LICENSEE EVENT REPORT# E -Operator Training & License Examination F -Administrative G -Operational Error (Explain)
 
H -Other (Explain) 3 .. E~ C II ,n II II C II .. '1::1 0 '1::1 CAUSE & CORRECTIVE ACTION to II 0 11. 0 :; a E 0 PREVEN'I RECURRFJ( CE 0 0 Unit reduced to 89% power 730MW to maintair condensate polishing
PAGE 3 OPERATING DATA REPORT DOCKET NO. 50-281 DATE    09/QR/RR COMPLETED BY    L. A. warren TELEPHONE    804-357-3184 OPERATING STATUS
~p less than 50 psid. Unit reactor trip and safety injection due tc a failed CLS relay during Ini;trument Departmen1 testing. , Unit reduced to 68% 560MW to permit repain to main generator H2 cooling system. Unit reduced to 78% 650MW to repair isolated phase bus duct grounding straps. Method: 4 1 -Manual 2 -Manual Scram. 3 -Automatic Scram. 4 -Other (Explain)
: 1. Unit Name:          Surry Unit # 2                                  Notes 2.
Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (I.Ell) File (NUREG 0161) 5 Exhibit 1 -s.-Source 
3, 4.
-1D NO. DA:rE a. >, I-88-12 8/06/88 s 88-13 8/08/88 s 88-14 8/17/88 s 8/18/88 I 88-15 s 88-16 8/20/88 s 88-17 8/26/88 s 88-18 8/31/88 s 1 F: Forced 2 S: Scheduled
5.
.(9/77) UNIT SHUTDOWNS AND POWER REDUCTIONS REPffiT MONTH AUGUST 1988 "' .. C ... CD 0 .. 0 -N 0 C .. LICENSEE C ... .. C ... u E :r II in .. .. 0 'tJ .. 1D II II C II Ill :J m 0 .. II EVENT .. 'tJ 0 'tJ .. 0 1D .r: .. 0 a. 0 :c II :J ~o :J .. .r: REPORT# E 0 C -II en C 0 :a 0 0 C 0.0 B 1 0.0 B 1 0.0 B 1 o.o B 1 0.0 B 1 0.0 B 1 0.0 B 1 Reason: 3 Method: A -Equipment Failure (Explain)
Reporting Period:  Auqust 01 thru 31, 1988
B -Maintenance or Test 1 -Manual 2 -Manual Scram. PAGE 5 DOCKET NO. __ s_o-_2_8_1
* Nameplate Rating (Gross HWe):
_____ _ UNITNAME __ ~s~u~r~rv~u~oi~t
2441 Design Electrical Rating (Net HWe):
....... U_2.;._ ____ _ DATE 09/08/88 -----------------
847.S Licensed Thermal Power (HWt): ......::::.......::.:a...------
COMPLETED BY L. A. Warren TELEPoo~:::so:4:-:3:s1:-~3:1s~4::::~:=
788
CAUSE & CORRECTIVE ACTION TO PREVENT RECURRENCE Unit reduced to 73% SOOMW to clean waterboxes and perform waterbox tube cleaning.
: 6. Maximum Dependable Capacity (Gross HWe): _8.;;..2::;.0.;;..__ _
Unit reduced to 73% 5151\1W to repair waterbox tube leak. Unit reduced to 69.5% 510MW to clean water boxes. Unit reduced to 75% 555MW to perform 2-PT-29~ 1 turbine valve freedom test. Unit reduced to 71% 505MW to clean water boxes. Unit reduced to 71.5% 520MW to clea water boxes. Unit reduced to 62% 440MW to clean water boxes. 4 C -Refueling D -Regulatory Restriction 3 -Automatic Scram. 4 -Other (Explain)
: 7. Maximum Dependable Capacity (Net HWe):               781
Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG 0161) E -Operator Training & License Examination . F -Administrative G -Operational Error (Explain)
: 8. If Changes Occur in Capacity Ratings (Items Number 3 l'hrough 7) Since Last Report, Give Reasons:
H -Other (Explain) s Exhibit 1 -Same Source MONTH *
: 9. Power Level To Which Restricted, If Any (Net MWe):
* PAGE 6 AVERAGE DAILY UNIT POWER LEVEL AUGUST 1988 DAY AVERAGE DAILY POWER LEVEL (MWe-Net) 1 760 2 759 '3 756 4 733 '5 739 6 762 7 760 8 759 9 762 10 761 11 760 12 711 1 '3 757 14 758 1 '5 754 16 0 INSTRUCTIONS DOCKET NO, 50-280 ---,.,...._-~-..--
: 10. Reasons For Restrictions, If Any:
UNI? Surry Unit # 1 DArE 9/8/88 COMPLETED BY L. A. Warren . ?ELEPHONE 804-357-3184 DAY AVERAGE DAILY POWER LEVEL (MWe-Net) 17 333 18 717 19 762 20 764 21 764 22 765 2 '3 767 24 765 25 764 26 764 27 718 28 765 29 745 '30 766 31 769 On this format, list the average daily unit power level in MWe-Net for ~ach day in the reporting month, Compute to the nearest whole megawatt.
* This Month        Yr. -to-Date          Cumulative 11,  Hours In Reporting Period                                          744.0              5855.0            134447.0 12,  Number of Hours Reactor Was Critical                              744.0              4810.3              89476.3 13,  Reactor Reserve Shutdown Hours                                      ,0                    0                328.1
(9/77) 
: 14. Hours Generator O~~Line                                            744.0             4776.7              88075.0
*
: 15. Unit Reserve Shutdown Hours                                           0                   0                   0
* PAGE 7 .. AVERAGE DAILY UNIX POWER LEVEL MONTH AJJGJJST J 988 DAY AVERAGE DAILY POWER LEVEL 1 2 '3 4 5 6 7 8 9 10 11 12 l'3 14 15 16 INSTRUCTIONS (MWe-Net) 625 620 616 611 511 592 560 512 577 571 567 567 566 569 570 DOCKE'.r NO. 50-281 ~:----,,.,,.....,,......,,.--
* 16,   Gross Thermal Energy Generated (HWB)                         1492661. 9         11193381.0         206363743.7
UNIT Surry Unit # 2 DATE 9/8/88 COHPLE'IED BY L. A. Warren !ELEPHONE 804-357-3184 DAY AVERAGE DAILY POWER LEVEL (MWe-Net) 17 18 19 20 538 21 521 22 530 23 533 24 567 25 547 26 533 27 544 28 529 29 528 '30 514 31 496 On this format, list the average daily unit power level in MWe-Net for ~ach day in the reporting month. Compute to the nearest whole megawatt.
: 17. Gross Electrical Energy Generated (HWH)                       443590.0           3649135.0          67021959.0
_(9/77)
: 18. Net Electrical Energy Generated (HWB)                         414737.0           3464826.0          63541303.0
* *
: 19. Unit Service Factor                                               100%                 81.6%               65.5%
: 20. Unit Available Factor                                             100%                 81.6%               65.5%
: 21. Unit Capacity Factor (Using MDC Net)                               71.4%               75.8%               60. 7%
: 22. Unit Capacity Factor (Using DER Net)                               70. 7%               75.1%               60%
23,   Unit Forced Rate                                                     0                 18.4%               14.6%
24,   Shutdowns Scheduled Over Next 6 Months (?ype, Date, and Duration of Each):
Refueling outage, 9/9/88, 68 days                                   .
25,   If Shut Down At End Of Report Period Estimated Date of Startupr
: 26. Units In rest Status (Prior to C011111ercial Operation)r                     Forecast              Achieved INITIAL CRITICALITY INITIAL ELECTRICI?Y COMMERCIAL OPERAl'ION (9/77)
 
PAGE 4 UNIT SHUIOOWNS AND POWER REDUCTIONS                                      DOCKET NO. _5_0_-_2_80_ _ _ _ __
UNIT NAME    Surry Unit #
DATE    09/08/88 alU'LETED BY      L. A. Warren REPORT MONTH ___A__U
____G._u...s__T......._l,_9,_88____                      TELEPHONE    804-357-3184 C                  ....0  a,     0
                    -           0          N C      ..
LICENSEE                                    C II    C          ... u                          E~                        II ,n II                    0    '1::1                                    II    II NO.     DATE      11.
a, 0
J:
                                      ~
II CD II II!
0
                                                  .s::.
II
                                                        .s::.
II II II!
C EVENT REPORT#
II
:; a
                                                                                                  '1::1 0
0 C
: 11. 0 E  0 II 0 '1::1             CAUSE & CORRECTIVE ACTION to PREVEN'I RECURRFJ( CE 0                  :I:   UJ JI                                                  0 0
0 88-06    8/12/88          s        o.o        F              1                                                              Unit reduced to 89% power 730MW to maintair condensate polishing ~p less than 50 psid.
88.:.07  8/15/88        ,F         56         A             3                                                               Unit reactor trip and safety injection due tc a failed CLS relay during Ini;trument Departmen1 testing.                                  ,
88-08    8/27 /8_8      IS          o.o       B             1                                                               Unit reduced to 68% 560MW to permit repain to main generator H2 cooling system.
88-09    8/29/88        F          0.0       A             1                                                               Unit reduced to 78% 650MW to repair isolated phase bus duct grounding straps.
1                        2                                                          3                                              4 F: Forced              Reason:                                                          Method:                                    Exhibit G - Instructions S: Scheduled          A - Equipment Failure (Explain)                                   1 - Manual                                for Preparation of Data B - Maintenance or Test                                           2 - Manual Scram.                          Entry Sheets for Licensee C - Refueling                                                     3 - Automatic Scram.                      Event Report (I.Ell) File D - Regulatory Restriction                                       4 - Other (Explain)                        (NUREG 0161)
E - Operator Training & License Examination 5
F - Administrative                                                                                           Exhibit 1 -  s.-  Source G - Operational Error (Explain)
(9/77)                      H - Other (Explain)
 
PAGE 5 UNIT SHUTDOWNS AND POWER REDUCTIONS                        DOCKET NO. _ _ s_o-_2_8_1_ _ _ _ __
UNITNAME __~s~u~r~rv~u~oi~t.......
U_2.;.______
DATE    09/08/88 REPffiT MONTH  AUGUST 1988 COMPLETED BY  -----------------
L. A. Warren TELEPoo~:::so:4:-:3:s1:-~3:1s~4::::~:=
CD  0 C        N        0  C  ..
0
                                                    ... u          LICENSEE      E :r C
C                                                  II in 1D                   0      'tJ                              II  II NO.     DA:rE     a.
Ill
:J 0
m 1D 0
                                                .r:
                                                    .. 1D II
                                                        ~
EVENT        ..
                                                                                      'tJ 0
C  II 0 'tJ
: a. 0 CAUSE & CORRECTIVE ACTION TO I-C
:J
:c
                                        ~
II
                                                ~
II
:J
                                                    .r:
en  C
:a 0
REPORT#      ~o          E 0
0 0                          PREVENT RECURRENCE C
88-12    8/06/88       s         0.0      B        1                                                Unit reduced to 73% SOOMW to clean waterboxes and perform waterbox tube cleaning.
88-13    8/08/88       s           0.0      B        1                                                 Unit reduced to 73% 5151\1W to repair waterbox tube leak.
88-14    8/17/88      s          0.0     B        1                                                Unit reduced      to    69.5%    510MW        to    clean water boxes.
88-15    8/18/88 I
s          o.o      B        1                                                Unit reduced to 75% 555MW to                        perform 2-PT-29~ 1 turbine valve freedom test.
88-16    8/20/88      s          0.0      B        1                                                Unit reduced        to    71%    505MW        to      clean water boxes.
88-17    8/26/88      s          0.0     B        1                                                Unit reduced      to    71.5%    520MW        to    clea water boxes.
88-18    8/31/88      s          0.0     B        1                                                Unit reduced        to    62%    440MW          to    clean water boxes.
1                      2                                                    3                                4 F: Forced            Reason:                                                   Method:                       Exhibit G - Instructions S: Scheduled        A - Equipment Failure (Explain)                          1 - Manual                    for Preparation of Data B - Maintenance or Test                                  2 - Manual Scram.             Entry Sheets for Licensee C - Refueling                                            3 - Automatic Scram.           Event Report (LER) File D - Regulatory Restriction                                4 - Other (Explain)             (NUREG 0161)
E - Operator Training & License Examination .
F - Administrative s  Exhibit 1 - Same Source G - Operational Error (Explain)
.(9/77)                  H - Other (Explain)
 
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO,    50-280
                                                          ---,.,...._-~-..--
PAGE 6 UNI?    Surry Unit # 1 DArE    9/8/88 COMPLETED BY    L. A. Warren
                                        . ?ELEPHONE    804-357-3184 MONTH AUGUST 1988 DAY  AVERAGE DAILY POWER LEVEL                  DAY    AVERAGE DAILY POWER LEVEL (MWe-Net)                                            (MWe-Net) 1                  760                          17                    333 2                  759                          18                    717
      '3                756                          19                    762 4                 733                          20                    764
      '5                739                          21                    764 6                  762                          22                    765 7                  760                          2 '3                  767 8                  759                          24                    765 9                  762                          25                    764 10                  761                          26                    764 11                  760                          27                    718 12                  711                          28                    765 1 '3                757                          29                    745 14                  758                          '30                  766 1 '5               754                          31                    769 16                    0 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for ~ach day in the reporting month, Compute to the nearest whole megawatt.
(9/77)
 
PAGE 7 AVERAGE DAILY UNIX POWER LEVEL DOCKE'.r NO. 50-281
                                                            ~:----,,.,,.....,,......,,.--
UNIT   Surry Unit # 2 DATE 9/8/88 COHPLE'IED BY    L. A. Warren
                                          !ELEPHONE      804-357-3184 MONTH AJJGJJST J988 DAY   AVERAGE DAILY POWER LEVEL                   DAY AVERAGE DAILY POWER LEVEL (MWe-Net)                                                    (MWe-Net) 1                   625                          17 2                                                 18
        '3                 620                          19 4                   616                          20                              538 5                   611                          21                              521 6                   511                          22                              530 7                   592                          23                              533 8                   560                          24                              567 9                   512                          25                              547 10                   577                            26                              533 11                   571                            27                              544 12                   567                            28                              529 l'3                 567                            29                              528 14                   566                            '30                            514 15                  569                            31                              496 16                 570 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for ~ach day in the reporting month. Compute to the nearest whole megawatt.
_(9/77)
 
PAGE 8


==SUMMARY==
==SUMMARY==
OF OPERATING EXPERIENCE MONTH/YEAR
OF OPERATING EXPERIENCE MONTH/YEAR _ _A_U-'-G;..-U_S_T""""l"-'9....c;8_8_
__ A_U-'-G;..-U_S_T""""l"-'9....c;8_8_
Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
PAGE 8 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
UNIT ONE 08-01-88   0000       This reporting period begins with the unit at 100% 810 MW.
UNIT ONE 08-01-88 0000 08-12-88 0505 0529 1530 1600 2115 2252 08-15-88 0927 08-16-88 2049 08-17-88 1733 2011 2333 08-18-88 0500 08-27-88 0045 0211 0500 0643 08-29-88 1325 1342 1506 This reporting period begins with the unit at 100% 810 MW. Commenced power reduction at 150 MW /hr to maintain condensate polishing differential pressure less than 50 psid. Holding power at 92% 735 MW. Commenced power reduction at 150 MW /hr to maintain condensate polishing differential pressure.
08-12-88  0505      Commenced power reduction at 150 MW /hr to maintain condensate polishing differential pressure less than 50 psid.
Holding power at 89% 730 MW. Commenced power increase at 150 MW /hr. Unit at 100% 805 MW. Unit reactor trip and safety injection due to a failed CLS relay. Reactor Critical.
0529      Holding power at 92% 735 MW.
Unit on line. Holding power at 58% 810 MWs. Commenced power increase at 5%/hr. Unit at 100% 805 MW. Commenced power reduction at 150 MW /hr to permit repairs to main generator Hz cooling system. Holding power at 68% 560 MW. Commenced power increease at 150 MW /hr. Unit at 100% 805 MW. Commenced power reduction at 5%/min. to repair isolated phase bus duct grounding straps. Holding power at 78% 650 MW. Commenced power increase at 5%/hr.
1530      Commenced power reduction at 150 MW /hr to maintain condensate polishing differential pressure.
*
1600      Holding power at 89% 730 MW.
* PAGE 9
2115      Commenced power increase at 150 MW /hr.
2252      Unit at 100% 805 MW.
08-15-88  0927      Unit reactor trip and safety injection due to a failed CLS relay.
08-16-88  2049      Reactor Critical.
08-17-88  1733      Unit on line.
2011      Holding power at 58% 810 MWs.
2333      Commenced power increase at 5%/hr.
08-18-88  0500      Unit at 100% 805 MW.
08-27-88  0045      Commenced power reduction at 150 MW /hr to permit repairs to main generator Hz cooling system.
0211      Holding power at 68% 560 MW.
0500      Commenced power increease at 150 MW /hr.
0643      Unit at 100% 805 MW.
08-29-88  1325      Commenced power reduction at 5%/min. to repair isolated phase bus duct grounding straps.
1342      Holding power at 78% 650 MW.
1506      Commenced power increase at 5%/hr.


==SUMMARY==
==SUMMARY==
OF OPERATING EXPERIENCE MONTH/YEAR AUGUST 1988 ---------Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
OF OPERATING EXPERIENCE
UNIT ONE (cont'd) 08-29-88 1840 08-31-88 2400 UNIT TWO 08-01-88 0000 08-06-88 0500 0545 1100 1600 08-07-88 0445 0513 08-08-88 0703 0703 08-09-88 0130 1600 1838 2400 08-17-88 2101 2225 Unit at 100% 805 MW. This reporting period ends with the unit at 100% 805 MW. This reporting period begins with the unit at 89% 655 MW due to 3B feedwater heater being out of service. Commenced power reduction at 150 MW /hr to permit cleaning water boxes. Holding power at 79.5% 580 MW. Commenced power reduction at 3%/hr to support waterbox tube cleaning.
* PAGE 9 MONTH/YEAR         AUGUST 1988 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
Holding power at 73% 500 MW. Commenced power increase at 150 MW /hr. Holding power at 90% 665 MW. Commenced power reduction at 150 MW /hr to support waterbox maintenance.
UNIT ONE       (cont'd) 08-29-88 1840         Unit at 100% 805 MW.
Holding power at 79% 600 MW. Commenced power reduction at 0.5%/hr to maintain condenser backpressure less than 5 psid. Holding power at 73% 515 MW. Commenced power increase at 3%/hr. Holding power at 88% 640 MW. Commenced power reduction at 150 MW /hr to clean water boxes. Holding power at 69.5% 510 MW.
08-31-88  2400        This reporting period ends with the unit at 100% 805 MW.
*
UNIT TWO 08-01-88  0000        This reporting period begins with the unit at 89% 655 MW due to 3B feedwater heater being out of service.
* PAGE 10
08-06-88  0500        Commenced power reduction at 150 MW /hr to permit cleaning water boxes.
0545        Holding power at 79.5% 580 MW.
1100        Commenced power reduction at 3%/hr to support waterbox tube cleaning.
1600        Holding power at 73% 500 MW.
08-07-88  0445        Commenced power increase at 150 MW /hr.
0513        Holding power at 90% 665 MW.
08-08-88  0703        Commenced power reduction at 150 MW /hr to support waterbox maintenance.
0703        Holding power at 79% 600 MW.
08-09-88  0130        Commenced power reduction at 0.5%/hr to maintain condenser backpressure less than 5 psid.
1600        Holding power at 73% 515 MW.
1838        Commenced power increase at 3%/hr.
2400        Holding power at 88% 640 MW.
08-17-88  2101        Commenced power reduction at 150 MW /hr to clean water boxes.
2225        Holding power at 69.5% 510 MW.


==SUMMARY==
==SUMMARY==
OF OPERATING EXPERIENCE MONTH/YEAR
OF OPERATING EXPERIENCE
__ A_U_G_u_s_T_l
* PAGE 10 MONTH/YEAR __A_U_G_u_s_T_l_98_8_ __
_98_8 __ _ Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
UNIT TWO 08-18-88 0500 (Cont'd) Commenced power increase at 3%/hr. 0800 Holding power at 85% 630 MW. 2243 Commenced power reduction at 150 MW/hr to perform 2-PT-29.1.
UNIT TWO         (Cont'd) 08-18-88   0500       Commenced power increase at 3%/hr.
2313 Holding power at 75% 555 MW. 0 8-19-8 8 12 4 7 Commenced power increase at 3%/hr. 1600 Holding power at 84% 600 MW. 08-20-88 2232 Commenced power reduction at 150 MW /hr to clean waterboxes.
0800       Holding power at 85% 630 MW.
08-21-88 0000-2400 Varied unit power and load between 82% 600 MW to 71% 505 MW 08-22-88 0521 0800 08-26-88 1825 1903 2100 2345 08-31-88 1910 2007 2252 08-31-88 2400 too support waterbox cleaning.
2243       Commenced power reduction at 150 MW/hr to perform 2-PT-29.1.
Commenced power increase at 3%/hr from 71 % 505 MW. Holding power at 79% 590 MW. Commenced power reduction at 150 *MW/hr to permit cleaning water boxes. Holding power at 71.5% 520 MW. Commenced power increase at 3%/hr. Holding power at 78.5% 590 MW. Commence power reduction at 150 MW /hr to clean waterboxes.
2313       Holding power at 75% 555 MW.
Holding power at 62% 440 MW. Commenced power increase at 8%/hr. This reporting period ends with the unit at 70% 490 MW due to 3B feedwater being out of service, 1 C 1 waterbox removed from service for cleaning and EOL coastdown in progress.
08-19-8 8 12 47      Commenced power increase at 3%/hr.
*
1600       Holding power at 84% 600 MW.
* F AGILITY CHANGES REQUIRING NRC APPROVAL MONTH/YEAR AUGUST 1988 NONE DURING THIS PERIOD PAGE 11 DC 84-69 DC 86-15 DC 87-32 PAGE 12 *
08-20-88   2232       Commenced power reduction at 150 MW /hr to clean waterboxes.
* FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR AUGUST 1988 ---------PRESSURIZER SAFETY VALVE LOOP-SEAL INSULATION OVENS UNIT l This design change installed metal reflective thermal insulation boxes which will enclose the safety valves loop seal piping. This is to maintain the loop seal water temperature at approximately 400&deg;F. This temperature will allow part of the water to flash to steam after passing through the safety valves. The reduced density of the watersteam mixture will cause reduced fluid transient loads for the piping and supports.  
08-21-88   0000-2400 Varied unit power and load between 82% 600 MW to 71% 505 MW too support waterbox cleaning.
08-22-88   0521       Commenced power increase at 3%/hr from 71 % 505 MW.
0800        Holding power at 79% 590 MW.
08-26-88  1825        Commenced power reduction at 150 *MW/hr to permit cleaning water boxes.
1903        Holding power at 71.5% 520 MW.
2100        Commenced power increase at 3%/hr.
2345        Holding power at 78.5% 590 MW.
08-31-88  1910        Commence power reduction at 150 MW /hr to clean waterboxes.
2007        Holding power at 62% 440 MW.
2252        Commenced power increase at 8%/hr.
08-31-88  2400        This reporting period ends with the unit at 70% 490 MW due to 3B feedwater being out of service, 1C 1 waterbox removed from service for cleaning and EOL coastdown in progress.
 
PAGE 11 F AGILITY CHANGES REQUIRING NRC APPROVAL MONTH/YEAR   AUGUST 1988 NONE DURING THIS PERIOD
 
PAGE 12 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR
                                            - - - -1988
                                      - -AUGUST    ---
DC 84-69    PRESSURIZER SAFETY VALVE LOOP-SEAL INSULATION OVENS UNIT l This design change installed metal reflective thermal insulation boxes which will enclose the safety valves loop seal piping. This is to maintain the loop seal water temperature at approximately 400&deg;F. This temperature will allow part of the water to flash to steam after passing through the safety valves. The reduced density of the watersteam mixture will cause reduced fluid transient loads for the piping and supports.


==SUMMARY==
==SUMMARY==
OF SAFETY ANALYSIS The installation of the boxes will not affect the operation of the pressurizer or the safety valves. The boxes will reduce fluid transient loads to ensure the piping and supports are qualified for the design basis transients once the supports have been modified.
OF SAFETY ANALYSIS The installation of the boxes will not affect the operation of the pressurizer or the safety valves. The boxes will reduce fluid transient loads to ensure the piping and supports are qualified for the design basis transients once the supports have been modified. The boxes do not affect any safety related system or component and does not impact any Technical Specification.
The boxes do not affect any safety related system or component and does not impact any Technical Specification.
DC 86-15    LEVEL INSTRUMENTATION TO PREVENT LOSS OF SHUTDOWN COOLING                                                   UNIT l This design change installed a permanent standpipe arrangement to replace the temporary polyhose arrangement installed during each outage.
LEVEL INSTRUMENTATION TO PREVENT LOSS OF SHUTDOWN COOLING UNIT l This design change installed a permanent standpipe arrangement to replace the temporary polyhose arrangement installed during each outage. Local level indication, control room indication and a control room low level alarm are provided for reactor coolant level during outage periods.  
Local level indication, control room indication and a control room low level alarm are provided for reactor coolant level during outage periods.


==SUMMARY==
==SUMMARY==
OF SAFETY ANALYSIS The system will be placed into service only during cold shutdown conditions.
OF SAFETY ANALYSIS The system will be placed into service only during cold shutdown conditions. At all other times the system is isolated from other systems.
At all other times the system is isolated from other systems. The portion of the system up to and including the second isolation valve is designed to reactor coolant design pressure and temperature.
The portion of the system up to and including the second isolation valve is designed to reactor coolant design pressure and temperature. This system does not affect safety related equipment or the operation of the safety related systems.
This system does not affect safety related equipment or the operation of the safety related systems. WEED 9007 RTD REPLACEMENT UNIT l This modification replaced the eighteen (18) narrow range RTDs with RTDs which have adequately demonstrated environmental qualification as set forth by NUREG 0588 Category 1.  
DC 87-32    WEED 9007 RTD REPLACEMENT                                           UNIT l This modification replaced the eighteen (18) narrow range RTDs with RTDs which have adequately demonstrated environmental qualification as set forth by NUREG 0588 Category 1.


==SUMMARY==
==SUMMARY==
OF SAFETY ANALYSIS The replacement RTDs are essentially one for one replacements of an enhanced design and will not affect any of the operations or ability of equipment important to safety to perform their safety functions.
OF SAFETY ANALYSIS The replacement RTDs are essentially one for one replacements of an enhanced design and will not affect any of the operations or ability of equipment important to safety to perform their safety functions.
PAGE 13 FACIIJT.ANGES THAT DID NOT REQUIR.RC APPROVAL MONTH/YEAR AUGUST 1988 AC S2-88-0615 ADMINISTRATIVE CONTROL 08/04/88 This change provides administrative control while closing MOV-SW-205B or MOV-SW-205D in order to accomplish maintenance on the associated valve. Since the valves (MOV-SW-205B and 205D) will remain operable and will be manually opened prior to auto or manual start of the recirculation spray (RS) pumps, the change will not affect the operation of the RS system. Therefore, no unreviewed safety question is created. AC S2-88-0805 ADMINISTRATIVE CONTROL 08/05/88 FS 88-40 TM S2-88-60 This change maintained recirculation spray (RS) heat exchangers service water discharge valves 2-SW-MOV-205B  
 
& D closed under administrative control to prevent service water ingress to the recirculation spray heat exchangers from the discharge tunnel to prevent biofouling of the RS heat exchangers.
PAGE 13 FACIIJT.ANGES THAT DID NOT REQUIR.RC APPROVAL MONTH/YEAR         AUGUST 1988 AC S2-88-0615 ADMINISTRATIVE CONTROL                                           08/04/88 This change provides administrative control while closing MOV-SW-205B or MOV-SW-205D in order to accomplish maintenance on the associated valve.
Since the valves (MOV-SW-205B and 205D) will remain operable and will be manually opened prior to auto or manual start of the RS pumps, the change will not affect the operation of the RS system. Therefore, no unreviewed safety question is created. FSAR CHANGE REQUEST 08/09/88 Design Change 77-09 modified the usable volume of Unit 1 and Unit 2 R WSTs. The modification affected LC Os for safety injection and* containment spray systems. The 10 CFR 50.59 review resulted in no unreviewed safety question since DC 77-09 did not alter the basic design function of the affected systems. TEMPORARY MODIFICATION 08-19-88 This modification allowed the lead from terminal board 58C-2 to 2AST 1 to be lifted and prevent the mechanical anti-motoring trip from operating.
Since the valves (MOV-SW-205B and 205D) will remain operable and will be manually opened prior to auto or manual start of the recirculation spray (RS) pumps, the change will not affect the operation of the RS system. Therefore, no unreviewed safety question is created.
AC S2-88-0805 ADMINISTRATIVE CONTROL                                           08/05/88 This change maintained recirculation spray (RS) heat exchangers service water discharge valves 2-SW-MOV-205B & D closed under administrative control to prevent service water ingress to the recirculation spray heat exchangers from the discharge tunnel to prevent biofouling of the RS heat exchangers.
Since the valves (MOV-SW-205B and 205D) will remain operable and will be manually opened prior to auto or manual start of the RS pumps, the change will not affect the operation of the RS system. Therefore, no unreviewed safety question is created.
FS 88-40      FSAR CHANGE REQUEST                                               08/09/88 Design Change 77-09 modified the usable volume of Unit 1 and Unit 2 R WSTs. The modification affected LC Os for safety injection and*
containment spray systems.
The 10 CFR 50.59 review resulted in no unreviewed safety question since DC 77-09 did not alter the basic design function of the affected systems.
TM S2-88-60  TEMPORARY MODIFICATION                                           08-19-88 This modification allowed the lead from terminal board 58C-2 to 2AST 1 to be lifted and prevent the mechanical anti-motoring trip from operating.
Removal of the mechanical anti-motoring trip will not have an adverse effect on the turbine overspeed or loss of electrical load analysis.
Removal of the mechanical anti-motoring trip will not have an adverse effect on the turbine overspeed or loss of electrical load analysis.
Therefore, there is no unreviewed safety question.
Therefore, there is no unreviewed safety question.
TM Sl-88-132 TEMPORARY MODIFICATION 08/20/88 A jumper was installed from the sample connection of the VCT gas space to the sample connection of the gas stripper surge tank at the sample sink. Venting the VCT via the sampling system will not increase the probability of an accident nor increase the consequences of an accident.
TM Sl-88-132 TEMPORARY MODIFICATION                                           08/20/88 A jumper was installed from the sample connection of the VCT gas space to the sample connection of the gas stripper surge tank at the sample sink.
Protection to the system is provided by relief valves in the system. Hose and fittings are rated in excess of operating pressures for the systems. Therefore, no unreviewed safety question is created.
Venting the VCT via the sampling system will not increase the probability of an accident nor increase the consequences of an accident. Protection to the system is provided by relief valves in the system. Hose and fittings are rated in excess of operating pressures for the systems. Therefore, no unreviewed safety question is created.
A PAGE 14 FACIUT.ANGES THAT DID NOT REQUIRlaRC APPROVAL AC Sl-88-810 AC S2-88-8 IO MONTH/YEAR AUGUST 1988 ADMINISTRATIVE CONTROL 08/20/88 While the charging pump component cooling (CC) pump's drain valve is open to feed and bleed the system to increase chromate concentration, an operator will be stationed at the drain valve to close it immediately should the head tank level drop .s_ 30%. Feeding and bleeding the charging pump CC system by opening the charging pump CC pump's drain valve will not affect the operability of the charging system. It will enhance corrosion control by the addition of chromates.
 
Therefore, this administrative control does not constitute an unreviewed safety question.
A                 PAGE 14 FACIUT.ANGES THAT DID NOT REQUIRlaRC APPROVAL MONTH/YEAR        AUGUST 1988 AC Sl-88-810 ADMINISTRATIVE CONTROL                                          08/20/88 AC S2-88-8 IO While the charging pump component cooling (CC) pump's drain valve is open to feed and bleed the system to increase chromate concentration, an operator will be stationed at the drain valve to close it immediately should the head tank level drop .s_ 30%.
AC Sl-88-0820 ADMINISTRATIVE CONTROL 08/20/88 This change maintained recirculation spray (RS) heat exchanger (HX) service water (SW) discharge valve (1-SW-MOV-lOSA) closed under administrative control to prevent SW ingress into the RS HX from the discharge tunnel to prevent biofouling of the RS HX. Since valve 1-SW-MOV-lOSA will remain operable (as per EWR 88-326) and will be opened prior to auto or manual start of the RS pumps, the change will not affect the operation of the RS system. Therefore, no unreviewed safety question is created. AC Sl-88-0821 ADMINISTRATIVE CONTROL 08/21/88 This change allowed manual control over the 'C' RSST tap changer with constant communication with the control room due to failure in the automatic control. Manual control of the 'C' reserve station service transformer tap changer is required due to a failure in the automatic system. Manual control ensure voltages on the emergency buses will remain in spec and will reduce the chance of loss of off site power to 1 H and 2J emergency buses. Manual operation will maintain voltages within the intent of GDC 17. AC Sl-88-0823 ADMINISTRATIVE CONTROL 08/23/88 The dike at the emergency switchgear room was temporarily removed and a flood watch was placed at the door and at the turbine building pit areas. The dike was reinstalled in the event of a flood. The removal of this dike will not adversely affect any safety related equipment or create an unreviewed safety question.
Feeding and bleeding the charging pump CC system by opening the charging pump CC pump's drain valve will not affect the operability of the charging system. It will enhance corrosion control by the addition of chromates. Therefore, this administrative control does not constitute an unreviewed safety question.
l-TOP-2027 OCEDURE OR METHOD OF OP AT DID NOT REQUIRE NRG APP MONTH/YEAR AUGUST 1988 TEMPORARY OPERATING PROCEDURE PAGE 15 08/01/88 This change provided a means for flushing the primary drains transfer tanks (PDTT) discharge lines to the primary drains tanks (PDT) and to inspect PDTT pumps discharge check valves to clear/identify blockage in PDTT discharge lines. An unreviewed safety question does not exist because the probability and consequences of a liquid waste release are unaffected.
AC Sl-88-0820 ADMINISTRATIVE CONTROL                                           08/20/88 This change maintained recirculation spray (RS) heat exchanger (HX) service water (SW) discharge valve (1-SW-MOV-lOSA) closed under administrative control to prevent SW ingress into the RS HX from the discharge tunnel to prevent biofouling of the RS HX.
All liquid waste released from the check valves will be contained and directed to floor drains and the containment sump. Flush water will also be directed to the PDT and will be contained.
Since valve 1-SW-MOV-lOSA will remain operable (as per EWR 88-326) and will be opened prior to auto or manual start of the RS pumps, the change will not affect the operation of the RS system. Therefore, no unreviewed safety question is created.
Any uncontrolled release will be stopped by closing l-DG-74. This valve can also be immediately shut if containment isolation is necessary.
AC Sl-88-0821 ADMINISTRATIVE CONTROL                                           08/21/88 This change allowed manual control over the 'C' RSST tap changer with constant communication with the control room due to failure in the automatic control.
JUSTIFICATION FOR CONTINUED OPERATION 08/11/88 This Justification for Continued Operation documents plant operation with three out of four Radiation Monitoring Pumps operable on Service Water Discharge Lines from Recirculation Spray Heat Exchangers (RSHX). The reviewed condition does not affect the function of the RS system. Significant increases in exposure or releases will not occur because a backup radiation monitor exists and under the postulated failure of the RSHX, the heat exchanger can be
Manual control of the 'C' reserve station service transformer tap changer is required due to a failure in the automatic system. Manual control ensure voltages on the emergency buses will remain in spec and will reduce the chance of loss of offsite power to 1H and 2J emergency buses. Manual operation will maintain voltages within the intent of GDC 17.
* isolated without reducing the required heat removal via the RS system. Therefore, an unreviewed safety question does not exist.
AC Sl-88-0823 ADMINISTRATIVE CONTROL                                           08/23/88 The dike at the emergency switchgear room was temporarily removed and a flood watch was placed at the door and at the turbine building pit areas. The dike was reinstalled in the event of a flood.
*
The removal of this dike will not adversely affect any safety related equipment or create an unreviewed safety question.
* PROCEDURE OR METHOD OF OPERATION THAT DID REQUIRE NRC APPROVAL MONTH/YEAR AUGUST 1988 --------NONE DURING THIS PERIOD PAGE 16 
 
*
PAGE 15 OCEDURE OR METHOD OF OP AT DID NOT REQUIRE NRG APP MONTH/YEAR           AUGUST 1988 l-TOP-2027 TEMPORARY OPERATING PROCEDURE                                 08/01/88 This change provided a means for flushing the primary drains transfer tanks (PDTT) discharge lines to the primary drains tanks (PDT) and to inspect PDTT pumps discharge check valves to clear/identify blockage in PDTT discharge lines.
* PAGE 17 TESTS AND EXPERIMENTS REQUIRING NRC APPROVAL MONTH/YEAR AUGUST 1988 ----------
An unreviewed safety question does not exist because the probability and consequences of a liquid waste release are unaffected. All liquid waste released from the check valves will be contained and directed to floor drains and the containment sump. Flush water will also be directed to the PDT and will be contained. Any uncontrolled release will be stopped by closing l-DG-74. This valve can also be immediately shut if containment isolation is necessary.
NONE DURING THIS PERIOD
JUSTIFICATION FOR CONTINUED OPERATION                       08/11/88 This Justification for Continued Operation documents plant operation with three out of four Radiation Monitoring Pumps operable on Service Water Discharge Lines from Recirculation Spray Heat Exchangers (RSHX).
*
The reviewed condition does not affect the function of the RS system. Significant increases in exposure or releases will not occur because a backup radiation monitor exists and under the postulated failure of the RSHX, the heat exchanger can be
* PAGE 18 TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR AUGUST 1988 -----------
* isolated without reducing the required heat removal via the RS system. Therefore, an unreviewed safety question does not exist.
NONE DURING THIS PERIOD
 
* VIRGINIA POWER SURRY POWER STATION
PROCEDURE OR METHOD OF OPERATION THAT DID REQUIRE NRC APPROVAL PAGE 16 MONTH/YEAR
* CHEMISTRY REPORT 19 88 -----------
              - -AUGUST
AUGUST PAGE 19 PRIMARY COOLANT UNIT NO. 1 UNIT NO. 2 ANALYSIS -MAX. Gross Radioact., l!Ci/ml 8.88E-l Suspended Solids, PPm o.o Gross Tritium, &#xb5;Ci/ml 2.23E-l '
                  - - -1988 NONE DURING THIS PERIOD
* 131 Iodine , &#xb5;Ci/ml 3.73E-3 1 131 1 1 1 *n 0.16 Hydrogen, cc/b. 31.9 Lithium, ppm 2.35 Boron-10, ppm* 267.0 Oxygen, (DO), 01>m <0.005 Chloride, ppm 0.010 pH@ 25 degree Celsius 6.50
 
TESTS AND EXPERIMENTS REQUIRING NRC APPROVAL PAGE 17 MONTH/YEAR     AUGUST 1988 NONE DURING THIS PERIOD
 
            *
* PAGE 18 TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR     AUGUST 1988 NONE DURING THIS PERIOD
 
                        *-----------   VIRGINIA POWER                             PAGE 19 SURRY POWER STATION
* CHEMISTRY REPORT AUGUST                19 88 PRIMARY COOLANT                       UNIT NO. 1                     UNIT NO. 2
      - ANALYSIS MAX.         MIN. AVG.        MAX.        MIN.    . AVG.
Gross Radioact., l!Ci/ml         8.88E-l    l.18E-l  6.87E-l  2.00E-1 9.17E-2      1. 55E-l Suspended Solids, PPm           o.o        o.o      o.o      o.o          o.o      o.o Gross Tritium, &#xb5;Ci/ml           2.23E-l     l.51E-l  1. 93E-l  6.47E-:i 3.78E-2      5.29E-2
* 131                     3.73E-3    4.57E-4  2.54E-3    2. 04E:.L 6.23E-5    1. 30E-4 Iodine       , &#xb5;Ci/ml 1
131 1 1 1 *n                 0.16       0.09      0 .12    0. 15        0.05    0.09 Hydrogen, cc/b.                 31.9       25.5      27.8      131. O      26.1      29.0 Lithium, ppm                     2.35       2.06      2.21      0.47        0.29    0.37 Boron-10, ppm*                   267.0       184.0    202.9      0.764      ~0.196    0.439 Oxygen, (DO),       01>m       <0.005      <0.005    <0.005    <0.005
                                                                          --k0.005  <0.005 0.010      0.003    0.007    <0.010    kO~OOl    <0.002 Chloride, ppm pH@ 25 degree Celsius           6.50       6.27      6.41      8.68        7.44    8 .11
* Boron-10
* Boron-10
* Total Boron X 0.196 REMARKS: MIN. l.18E-l o.o l.51E-l 4.57E-4 0.09 25.5 2.06 184.0 <0.005 0.003 6.27 AVG. MAX. MIN. . AVG. 6.87E-l 2.00E-1 9.17E-2 1. 55E-l o.o o.o o.o o.o 1. 93E-l 6.47E-:i 3.78E-2 5.29E-2 2.54E-3 2. 04E:.L 6.23E-5 1. 30E-4 0 .12 0. 15 0.05 0.09 27.8 131. O 26.1 29.0 2.21 0.47 0.29 0.37 202.9 0.764 ~0.196 0.439 <0.005 <0.005 k0.005 <0.005 --0.007 <0.010 kO~OOl <0.002 --6.41 8.68 7.44 8 .11 UNIT I: Started month at 100%. Ramped down to 96% on 8-4 because of condensate polishing differential pressure and were back to 100% on 8-6. On 8-12, 0500 started to ramp down to 90% again due to condensate polishing differential pressure but were back to 100% by 2252. On 8-15 at 0927, a reactor trip occurred and the unit stayed in hot shutdown until the reactor was cr1tical on 8-16 at 2049. The unit was at 100% on 8-18 at 0500. On 8-27, started at 0025 to ramp down to 68% to repair a hydrogen cooler and was back to 100% by 0643. On 8-29, started at 1300 to ramp down to 79% due to fire in main generator leads and was back to 100% by 1855 and ended the month at 100%. Lithium was added 8-8 at 2010, 180g; 8-12 at 1025, 420g; 8-15 at 1830, 480g; 8-18 at 0515, 502g; 8-19 at 1300, 389g; 8-27 at 1100, 400g; for a total of 2371 grams of LiOH. UNIT 2: Started the month at 89%an~ coasting to refueling.
* Total Boron X 0.196 REMARKS:
On 8-6 at 0545, ramped back to 73% to clean waterboxes and returned to 90% on 8-7 at 0840. On 8-8, ramped down to 72% to clean waterboxes and returned to 88% on 8-10 at 0035. On 8-18, ramped down to 73% to perform PT-29.1 and clean waterboxes and returned to 84% on 8-19. On 8-21 at 2204, ramped down to 71% to clean waterboxes and returned to 79% on 8-22 and end of month at 76%. The B Debora tor was in service from 8-7 at 2015 to 8-9 at 0035; from 8-26 at 2255 to 8-27 at 0925. Lithium was added 8-11 at 1330, 180g; 8-22 at 1250; 145g; 8-25 at 1115, 225g; 8-27 at 1100, 178g; for a total of 728 grams of LiOH.
UNIT I:       Started month at 100%. Ramped down to 96% on 8-4 because of condensate polishing differential pressure and were back to 100% on 8-6. On 8-12, 0500 started to ramp down to 90% again due to condensate polishing differential pressure but were back to 100% by 2252. On 8-15 at 0927, a reactor trip occurred and the unit stayed in hot shutdown until the reactor was cr1tical on 8-16 at 2049. The unit was at 100% on 8-18 at 0500. On 8-27, started at 0025 to ramp down to 68% to repair a hydrogen cooler and was back to 100% by 0643. On 8-29, started at 1300 to ramp down to 79% due to fire in main generator leads and was back to 100% by 1855 and ended the month at 100%.
--------~--~-------
Lithium was added 8-8 at 2010, 180g; 8-12 at 1025, 420g; 8-15 at 1830, 480g; 8-18 at 0515, 502g; 8-19 at 1300, 389g; 8-27 at 1100, 400g; for a total of 2371 grams of LiOH.
PAGE 20 *
UNIT 2:       Started the month at 89%an~ coasting to refueling. On 8-6 at 0545, ramped back to 73% to clean waterboxes and returned to 90% on 8-7 at 0840. On 8-8, ramped down to 72% to clean waterboxes and returned to 88% on 8-10 at 0035. On 8-18, ramped down to 73% to perform PT-29.1 and clean waterboxes and returned to 84% on 8-19.
* GNSI CASTOR V/21 #500-11-008 (ISFSI) UNIT 1 FUEL HANDLING DATE August 1988 NEW OR DATE NUMBER OF NEW OR SPENT SPENT FUEL SHIPPED OR ASSEMBLIES ASSEMBLY ANSI INITIAL FUEL SHIPPING SHIPMENT II RECEIVED PER SHIPMENT fl II ENRICHMENT CASK ACTIVITY LEVEL CV/21 500-11-008 08126188 NIA C50 --3.12% NIA CV/21 500-11-008 08126188 NIA C51 -3.12% N/A -
On 8-21 at 2204, ramped down to 71% to clean waterboxes and returned to 79% on 8-22 and end of month at 76%. The B Debora tor was in service from 8-7 at 2015 to 8-9 at 0035; from 8-26 at 2255 to 8-27 at 0925. Lithium was added 8-11 at 1330, 180g; 8-22 at 1250; 145g; 8-25 at 1115, 225g; 8-27 at 1100, 178g; for a total of 728 grams of LiOH.
PAGE 21 .NSI CASTOR V/21 1500-11-008  
 
* . (ISFSI) UNIT 2 FUEL HANDLING DATE August 1988 NEW OR DATE NUMBER OF NEW OR SPENT SPENT FUEL SHIPPED OR ASSEMBLIES ASSEMBLY ANSI INITIAL FUEL SHIPPING SHIPMENT()
PAGE 20 GNSI CASTOR V/21 #500-11-008 (ISFSI)
RECEIVED PER SHIPMENT () 11 ENRICHMENT CASK ACTIVITY LEVEL CV/21 500-11-008 08/26/88 N/A P24 -3.11 N/A CV/21 500-11-008 08/26/88 N/A P05 -3.11 N/A CV/21 500-11-008 08/26/88 N/A P09 -3.11 N/A C'J /21 500-11-008 08/26/88 N/A P23 -3.11 N/A CV/21 500-11-008 08/26/88 N/A P04 -* 3.11 N/A CV/21 500-11-008
UNIT     1                           FUEL HANDLING               DATE August 1988 NEW OR       DATE     NUMBER OF                                       NEW OR SPENT SPENT FUEL   SHIPPED OR ASSEMBLIES     ASSEMBLY   ANSI     INITIAL     FUEL SHIPPING SHIPMENT II   RECEIVED PER SHIPMENT       fl       II     ENRICHMENT   CASK ACTIVITY LEVEL CV/21 500-11-008   08126188     NIA             C50       --   3.12%         NIA CV/21 500-11-008   08126188     NIA             C51       -     3.12%         N/A
* 08/26/88 N/A P07 -3.11 N/A CV/21 500-11-008 08/26/88 N/A P02 -3.11 N/A CV/21 500-11-008 08/26/88 N/A P06 -3.11 N/A CV/21 500-11-008 08/26/88 N/A PI4 -3.11 N/A CV/21 500-11-008 08/26/88 N/A PI7 -3.11 N/A CV/21 500-11-008 08/26/88 N/A POI -3.11 N/A CV/21 500-11-008 08/26/88 N/A P03 -3.11 N/A CV/21 500-11-008 08/26/88 N/A P27 -3.11 N/A CV/21 500-11-008 08126188 NIA PIO -3.11 NIA CV/21 500-11-008 08126/88 NIA P28 -3.11 NIA CV/21 500-11-008 08l?fll88 NIA P08 -3.11 N/A CV/21 500-11-onR ORl?.fl/88 NIA Pl2 -3.11 NIA CV/21 -500-11-008 08/26188 NIA P22 -3.11 NIA CV/21 500-11-008 08/26188 NIA P29 --3.11 N/A
 
.. PAGE 22 *
PAGE 21
* DESCRIPTION OF PERIODIC TEST WHICH WERE NOT COMPLETED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR AUGUST 1988 ----------
                              .NSI CASTOR V/21 1500-11-008 *
NONE DURING THIS PERIOD
                                    .         (ISFSI)
----------------' . . \ * * . .../ VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 September 14, 1988 U.S. Nuclear Regulatory Commission Attention:
UNIT     2                                 FUEL HANDLING             DATE August 1988 NEW OR         DATE           NUMBER OF                                   NEW OR SPENT SPENT FUEL     SHIPPED OR       ASSEMBLIES     ASSEMBLY ANSI INITIAL     FUEL SHIPPING SHIPMENT()     RECEIVED       PER SHIPMENT         ()     11 ENRICHMENT   CASK ACTIVITY LEVEL CV/21 500-11-008       08/26/88           N/A             P24 -       3.11           N/A CV/21 500-11-008       08/26/88           N/A             P05 -       3.11           N/A CV/21 500-11-008       08/26/88           N/A             P09 -       3.11           N/A C'J /21 500-11-008       08/26/88           N/A             P23 -       3.11           N/A CV/21 500-11-008       08/26/88           N/A             P04 -*       3.11           N/A CV/21 500-11-008
Document Control Desk Washington, D. C. 20555 Gentlemen:
* 08/26/88           N/A             P07 -       3.11           N/A CV/21 500-11-008       08/26/88           N/A             P02 -       3.11           N/A CV/21 500-11-008       08/26/88           N/A             P06 -       3.11           N/A CV/21 500-11-008       08/26/88           N/A             PI4 -       3.11           N/A CV/21 500-11-008       08/26/88           N/A             PI7 -       3.11           N/A CV/21 500-11-008       08/26/88           N/A             POI -       3.11           N/A CV/21 500-11-008       08/26/88           N/A             P03 -       3.11           N/A CV/21 500-11-008       08/26/88           N/A             P27   -       3.11           N/A CV/21 500-11-008       08126188           NIA             PIO   -       3.11           NIA CV/21 500-11-008       08126/88           NIA             P28   -       3.11           NIA CV/21 500-11-008       08l?fll88         NIA             P08 -       3.11           N/A CV/21 500-11-onR       ORl?.fl/88         NIA             Pl2   -       3.11           NIA CV/21                                                                                 -
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Serial No. NO/RPC:vlh Docket Nos. License Nos. 88-627 50-280 50-281 DPR-32 DPR-37 Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of August 1988. W. R. Cartwright Vice President  
500-11-008       08/26188           NIA             P22   -       3.11           NIA CV/21 500-11-008       08/26188           NIA             P29   --     3.11           N/A
-Nuclear Enclosure cc: U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N. W. Suite 2900 Atlanta, Georgia 30323 Mr. W. E. Holland NRC Senior Resident Inspector Surry Power Station}}
 
PAGE 22 DESCRIPTION OF PERIODIC TEST WHICH WERE NOT COMPLETED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR           AUGUST 1988 NONE DURING THIS PERIOD
 
..../
      . '. \
VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 September 14, 1988 U.S. Nuclear Regulatory Commission                       Serial No. 88-627 Attention: Document Control Desk                         NO/RPC:vlh Washington, D. C. 20555                                   Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37 Gentlemen:
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of August 1988.
W. R. Cartwright Vice President - Nuclear Enclosure cc:       U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N. W.
Suite 2900 Atlanta, Georgia 30323 Mr. W. E. Holland NRC Senior Resident Inspector Surry Power Station}}

Latest revision as of 23:39, 2 February 2020

Monthly Operating Repts for Aug 1988 for Surry Power Station.W/880914 Ltr
ML18152A289
Person / Time
Site: Surry  Dominion icon.png
Issue date: 08/31/1988
From: Cartwright W, Warren L
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
88-627, NUDOCS 8809200124
Download: ML18152A289 (25)


Text

..

POW 34-04

.. . .. ' f VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT 88-08 APPROVED: ~ ~~

ATION MANAGER

' :3809200124 880:::::31 -~

PDR ADOCK 05000280 R PDC

  • 1 SECTION PAGE Operating Data Report - Unit No. 1 1 Operating Data* Report - Unit No. 2 3 Unit Shutdowns and Power Reductions - Unit No. 1 4 Unit Shutdowns and Power Reductions - Unit No. 2 Average Daily Unit Power Level - Unit No. 1 6 Average Daily Unit Power Level - Unit No. 2 7 Summary of Operating Experience - Unit No. 1 8 Summary of Operating Experience - Unit No. 2 9 Facility Changes Requiring NRC Approval ll:

Facility Changes That Did Not Require NRC Approval 12 Procedure or Method of Operation Changes that Did Not Require NRC Approval 15 Procedure or Method of Operation that Did Require NRC Approval 16 Tests and Experiments Requiring NRC Approval 17 Tests and Experiments That Did Not Require NRC Approval 18 Chemistry Report 19 Fuel Handling - Unit No. 1 20 Fuel Handling - Unit No. 2 21 Description of Periodic Test Which Were Not Completed Within the Time Limits Specified in Technical Specifications 22

PAGE 1 OPERA?ING DATA REPORX DOCKE'I NO. 50-280 DATE 09/08/88

. COMPLETED BY L. A. Warren TELEPHONE 804-357-3184 OPERATING STAXUS

l. Unit Name: Surry Unit # 1 Notes
2. Reporting Period: August O1 thru 31. 19 8 8 2441
3. Licensed Thermal Power (MWt): -..:::..::..=-=------
4. Nameplate Rating (Gross MWe): _.,;8~4.:.:7:..::*:..::5____.,,_ __
5. Design Electrical Rating (Net MWe): 788
6. Maximum Dependable Capacity (Gross MWe): ~82:;.,;0;....___
7. Maximum Dependable Capacity (Net MWe): 781 8, If Changes Occur in Capacity Ratings (Items Number 3 nirough 7) Since Last Report, Give Reasons:
9. Power Level Io Which Restricted, If Any (Net MWe):
10. Reasons For Restrictions, If Any:

This Month Yr.-to*Date Cumulative 11, Hours In Reporting Period 744.0 5855.0 137567.0

12. Number of Hours Reactor Was Critical 708.7 3437.0 88160.4 13, Reactor Reserve Shutdown Hours 0 0 3774. 5
14. Hours Generator On-Line 688.0 3316.6 86287.8 15, Unit Reserve Shutdown Hours 0 0 3736.2
16. Gross Thermal Energy Generated (HWB) 1637979.2 7682198.9 200402420.3
17. Gross Electrical Energy Generated (HWB) 544765.0 2573560.0 64948733.0
18. Net Electrical Energy Generated (HWB) 516472. 0 2442986.0 61598362.0
19. Unit Service Factor 92.5% 56.7% 62.7%
20. Unit Available Factor 92.5% 56. 7% 65.4%
21. Unit Capacity Factor (Using MDC Net) 88.9% 53.4% 57.9%
22. Unit Capacity Factor (Using DER Net) 88.1% 53% 56 .-8%
23. Unit Forced Rate 7.5% 3.9% 17 .2%
24. Shutdown* Scheduled Over Next 6 Month* (Xype, Date, and Duration of Each),
25. If Shut Down At End Of Report Period Estimated Date of Startups
26. Unit* In Teat Status (Prior to Couaercial Operatioa)1 rorecaat Achieved lH1TIAL CRinCALiff IH1'nAL !L!C'l'llCiff COHHER.CIAL OPERAnON (9/77)

(JULY) PAGE I

  • OPERA7ING DA:rA REPOJa
    • CORRECT~ COPY 09/0.8/88 PAGE 2 DC>CREl: NO. 50-28 0 DA1'B 8/3/88 COMPLETED BY L. A. warren m.EPHONE 804-357-3184 OPERATING SL\l'US
1. Unit Name: Surry Unit # 1 Notes
2. Reporting Period: July O1 thru 31, 1988
3. Licensed Thermal Power (MWt): __,2.._4_4::..:l=-------
4. Nameplate Rating (Gross MWe): _8:..4.:.:7:..:*:.=5"------
s. Design Electrical Rating (Net HWe): 788
6. Maximum Dependable Capacity (Gross HWe): ----'82_0'------
7. Maximum Dependable Capacity (Net HWe): ___7_8__1_ __
a. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
9. Power Level To Which Restricted, If Any (Net HWe):
10. Reasons For Restrictions, If Any:

This Month Yr.-to-Date CUmulative

11. _Hours In Reporting Period Z~~ D 5111.Q ]36823"0
12. Number of Hours Reactor Was Critical ~lS.Z 2728~3 **.874$.1:7-.
13. Reactor Reserve Shutdown Hours Q.Q o*o 3774~5
14. Hours Generator On-Line 33]~0 2628~6 85599.8 lS. Unit Reserve Shutdown Hours a.a o*o 3736.2
  • 16. Gross Thermal Energy Generated (HWB) Z2UQ~.5 6Q44219~7 198764441.1
17. Gross Electrical Energy Generated (HWB) 23~11Q.Q 20287915 64403968.0
18. Net Electrical Energy Generated (HWH) 221QlQ.Q 1926514~0 61081890.0
19. Unit Service Factor ~~.~% 51;4% . 62.6%
20. Unit Available Factor ~~~5% 51~4% 65~3%.
21. Unit Capacity Factor (Using MDC Ret) 3B.Q% 48;3% 57. 7.%
22. Unit Capacity Factor (Using DER Net) 32~2% jz;a% 56".7%
23. Unit Forced Rate g;Q'.% 2* 9% 17~2%
24. Shutdown, Scheduled Over Next 6 Month1 (type, Date, and Duration of !acbh
25. If Shut Down At Ind Of Report Period Estimated Date of Startup*
26. Unit1 In Teat Statu1 (Prior to C011111ercial Operation)a rorecaat Achieved (9/77)

PAGE 3 OPERATING DATA REPORT DOCKET NO. 50-281 DATE 09/QR/RR COMPLETED BY L. A. warren TELEPHONE 804-357-3184 OPERATING STATUS

1. Unit Name: Surry Unit # 2 Notes 2.

3, 4.

5.

Reporting Period: Auqust 01 thru 31, 1988

  • Nameplate Rating (Gross HWe):

2441 Design Electrical Rating (Net HWe):

847.S Licensed Thermal Power (HWt): ......::::.......::.:a...------

788

6. Maximum Dependable Capacity (Gross HWe): _8.;;..2::;.0.;;..__ _
7. Maximum Dependable Capacity (Net HWe): 781
8. If Changes Occur in Capacity Ratings (Items Number 3 l'hrough 7) Since Last Report, Give Reasons:
9. Power Level To Which Restricted, If Any (Net MWe):
10. Reasons For Restrictions, If Any:
  • This Month Yr. -to-Date Cumulative 11, Hours In Reporting Period 744.0 5855.0 134447.0 12, Number of Hours Reactor Was Critical 744.0 4810.3 89476.3 13, Reactor Reserve Shutdown Hours ,0 0 328.1
14. Hours Generator O~~Line 744.0 4776.7 88075.0
15. Unit Reserve Shutdown Hours 0 0 0
  • 16, Gross Thermal Energy Generated (HWB) 1492661. 9 11193381.0 206363743.7
17. Gross Electrical Energy Generated (HWH) 443590.0 3649135.0 67021959.0
18. Net Electrical Energy Generated (HWB) 414737.0 3464826.0 63541303.0
19. Unit Service Factor 100% 81.6% 65.5%
20. Unit Available Factor 100% 81.6% 65.5%
21. Unit Capacity Factor (Using MDC Net) 71.4% 75.8% 60. 7%
22. Unit Capacity Factor (Using DER Net) 70. 7% 75.1% 60%

23, Unit Forced Rate 0 18.4% 14.6%

24, Shutdowns Scheduled Over Next 6 Months (?ype, Date, and Duration of Each):

Refueling outage, 9/9/88, 68 days .

25, If Shut Down At End Of Report Period Estimated Date of Startupr

26. Units In rest Status (Prior to C011111ercial Operation)r Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICI?Y COMMERCIAL OPERAl'ION (9/77)

PAGE 4 UNIT SHUIOOWNS AND POWER REDUCTIONS DOCKET NO. _5_0_-_2_80_ _ _ _ __

UNIT NAME Surry Unit #

DATE 09/08/88 alU'LETED BY L. A. Warren REPORT MONTH ___A__U

____G._u...s__T......._l,_9,_88____ TELEPHONE 804-357-3184 C ....0 a, 0

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LICENSEE C II C ... u E~ II ,n II 0 '1::1 II II NO. DATE 11.

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11. 0 E 0 II 0 '1::1 CAUSE & CORRECTIVE ACTION to PREVEN'I RECURRFJ( CE 0 :I: UJ JI 0 0

0 88-06 8/12/88 s o.o F 1 Unit reduced to 89% power 730MW to maintair condensate polishing ~p less than 50 psid.

88.:.07 8/15/88 ,F 56 A 3 Unit reactor trip and safety injection due tc a failed CLS relay during Ini;trument Departmen1 testing. ,

88-08 8/27 /8_8 IS o.o B 1 Unit reduced to 68% 560MW to permit repain to main generator H2 cooling system.

88-09 8/29/88 F 0.0 A 1 Unit reduced to 78% 650MW to repair isolated phase bus duct grounding straps.

1 2 3 4 F: Forced Reason: Method: Exhibit G - Instructions S: Scheduled A - Equipment Failure (Explain) 1 - Manual for Preparation of Data B - Maintenance or Test 2 - Manual Scram. Entry Sheets for Licensee C - Refueling 3 - Automatic Scram. Event Report (I.Ell) File D - Regulatory Restriction 4 - Other (Explain) (NUREG 0161)

E - Operator Training & License Examination 5

F - Administrative Exhibit 1 - s.- Source G - Operational Error (Explain)

(9/77) H - Other (Explain)

PAGE 5 UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. _ _ s_o-_2_8_1_ _ _ _ __

UNITNAME __~s~u~r~rv~u~oi~t.......

U_2.;.______

DATE 09/08/88 REPffiT MONTH AUGUST 1988 COMPLETED BY -----------------

L. A. Warren TELEPoo~:::so:4:-:3:s1:-~3:1s~4::::~:=

CD 0 C N 0 C ..

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88-12 8/06/88 s 0.0 B 1 Unit reduced to 73% SOOMW to clean waterboxes and perform waterbox tube cleaning.

88-13 8/08/88 s 0.0 B 1 Unit reduced to 73% 5151\1W to repair waterbox tube leak.

88-14 8/17/88 s 0.0 B 1 Unit reduced to 69.5% 510MW to clean water boxes.

88-15 8/18/88 I

s o.o B 1 Unit reduced to 75% 555MW to perform 2-PT-29~ 1 turbine valve freedom test.

88-16 8/20/88 s 0.0 B 1 Unit reduced to 71% 505MW to clean water boxes.

88-17 8/26/88 s 0.0 B 1 Unit reduced to 71.5% 520MW to clea water boxes.

88-18 8/31/88 s 0.0 B 1 Unit reduced to 62% 440MW to clean water boxes.

1 2 3 4 F: Forced Reason: Method: Exhibit G - Instructions S: Scheduled A - Equipment Failure (Explain) 1 - Manual for Preparation of Data B - Maintenance or Test 2 - Manual Scram. Entry Sheets for Licensee C - Refueling 3 - Automatic Scram. Event Report (LER) File D - Regulatory Restriction 4 - Other (Explain) (NUREG 0161)

E - Operator Training & License Examination .

F - Administrative s Exhibit 1 - Same Source G - Operational Error (Explain)

.(9/77) H - Other (Explain)

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO, 50-280

---,.,...._-~-..--

PAGE 6 UNI? Surry Unit # 1 DArE 9/8/88 COMPLETED BY L. A. Warren

. ?ELEPHONE 804-357-3184 MONTH AUGUST 1988 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 760 17 333 2 759 18 717

'3 756 19 762 4 733 20 764

'5 739 21 764 6 762 22 765 7 760 2 '3 767 8 759 24 765 9 762 25 764 10 761 26 764 11 760 27 718 12 711 28 765 1 '3 757 29 745 14 758 '30 766 1 '5 754 31 769 16 0 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for ~ach day in the reporting month, Compute to the nearest whole megawatt.

(9/77)

PAGE 7 AVERAGE DAILY UNIX POWER LEVEL DOCKE'.r NO. 50-281

~:----,,.,,.....,,......,,.--

UNIT Surry Unit # 2 DATE 9/8/88 COHPLE'IED BY L. A. Warren

!ELEPHONE 804-357-3184 MONTH AJJGJJST J988 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) (MWe-Net) 1 625 17 2 18

'3 620 19 4 616 20 538 5 611 21 521 6 511 22 530 7 592 23 533 8 560 24 567 9 512 25 547 10 577 26 533 11 571 27 544 12 567 28 529 l'3 567 29 528 14 566 '30 514 15 569 31 496 16 570 INSTRUCTIONS On this format, list the average daily unit power level in MWe-Net for ~ach day in the reporting month. Compute to the nearest whole megawatt.

_(9/77)

PAGE 8

SUMMARY

OF OPERATING EXPERIENCE MONTH/YEAR _ _A_U-'-G;..-U_S_T""""l"-'9....c;8_8_

Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.

UNIT ONE 08-01-88 0000 This reporting period begins with the unit at 100% 810 MW.

08-12-88 0505 Commenced power reduction at 150 MW /hr to maintain condensate polishing differential pressure less than 50 psid.

0529 Holding power at 92% 735 MW.

1530 Commenced power reduction at 150 MW /hr to maintain condensate polishing differential pressure.

1600 Holding power at 89% 730 MW.

2115 Commenced power increase at 150 MW /hr.

2252 Unit at 100% 805 MW.

08-15-88 0927 Unit reactor trip and safety injection due to a failed CLS relay.

08-16-88 2049 Reactor Critical.

08-17-88 1733 Unit on line.

2011 Holding power at 58% 810 MWs.

2333 Commenced power increase at 5%/hr.

08-18-88 0500 Unit at 100% 805 MW.

08-27-88 0045 Commenced power reduction at 150 MW /hr to permit repairs to main generator Hz cooling system.

0211 Holding power at 68% 560 MW.

0500 Commenced power increease at 150 MW /hr.

0643 Unit at 100% 805 MW.

08-29-88 1325 Commenced power reduction at 5%/min. to repair isolated phase bus duct grounding straps.

1342 Holding power at 78% 650 MW.

1506 Commenced power increase at 5%/hr.

SUMMARY

OF OPERATING EXPERIENCE

  • PAGE 9 MONTH/YEAR AUGUST 1988 Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.

UNIT ONE (cont'd) 08-29-88 1840 Unit at 100% 805 MW.

08-31-88 2400 This reporting period ends with the unit at 100% 805 MW.

UNIT TWO 08-01-88 0000 This reporting period begins with the unit at 89% 655 MW due to 3B feedwater heater being out of service.

08-06-88 0500 Commenced power reduction at 150 MW /hr to permit cleaning water boxes.

0545 Holding power at 79.5% 580 MW.

1100 Commenced power reduction at 3%/hr to support waterbox tube cleaning.

1600 Holding power at 73% 500 MW.

08-07-88 0445 Commenced power increase at 150 MW /hr.

0513 Holding power at 90% 665 MW.

08-08-88 0703 Commenced power reduction at 150 MW /hr to support waterbox maintenance.

0703 Holding power at 79% 600 MW.

08-09-88 0130 Commenced power reduction at 0.5%/hr to maintain condenser backpressure less than 5 psid.

1600 Holding power at 73% 515 MW.

1838 Commenced power increase at 3%/hr.

2400 Holding power at 88% 640 MW.

08-17-88 2101 Commenced power reduction at 150 MW /hr to clean water boxes.

2225 Holding power at 69.5% 510 MW.

SUMMARY

OF OPERATING EXPERIENCE

  • PAGE 10 MONTH/YEAR __A_U_G_u_s_T_l_98_8_ __

Listed below in chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.

UNIT TWO (Cont'd) 08-18-88 0500 Commenced power increase at 3%/hr.

0800 Holding power at 85% 630 MW.

2243 Commenced power reduction at 150 MW/hr to perform 2-PT-29.1.

2313 Holding power at 75% 555 MW.

08-19-8 8 12 47 Commenced power increase at 3%/hr.

1600 Holding power at 84% 600 MW.

08-20-88 2232 Commenced power reduction at 150 MW /hr to clean waterboxes.

08-21-88 0000-2400 Varied unit power and load between 82% 600 MW to 71% 505 MW too support waterbox cleaning.

08-22-88 0521 Commenced power increase at 3%/hr from 71 % 505 MW.

0800 Holding power at 79% 590 MW.

08-26-88 1825 Commenced power reduction at 150 *MW/hr to permit cleaning water boxes.

1903 Holding power at 71.5% 520 MW.

2100 Commenced power increase at 3%/hr.

2345 Holding power at 78.5% 590 MW.

08-31-88 1910 Commence power reduction at 150 MW /hr to clean waterboxes.

2007 Holding power at 62% 440 MW.

2252 Commenced power increase at 8%/hr.

08-31-88 2400 This reporting period ends with the unit at 70% 490 MW due to 3B feedwater being out of service, 1C 1 waterbox removed from service for cleaning and EOL coastdown in progress.

PAGE 11 F AGILITY CHANGES REQUIRING NRC APPROVAL MONTH/YEAR AUGUST 1988 NONE DURING THIS PERIOD

PAGE 12 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR

- - - -1988

- -AUGUST ---

DC 84-69 PRESSURIZER SAFETY VALVE LOOP-SEAL INSULATION OVENS UNIT l This design change installed metal reflective thermal insulation boxes which will enclose the safety valves loop seal piping. This is to maintain the loop seal water temperature at approximately 400°F. This temperature will allow part of the water to flash to steam after passing through the safety valves. The reduced density of the watersteam mixture will cause reduced fluid transient loads for the piping and supports.

SUMMARY

OF SAFETY ANALYSIS The installation of the boxes will not affect the operation of the pressurizer or the safety valves. The boxes will reduce fluid transient loads to ensure the piping and supports are qualified for the design basis transients once the supports have been modified. The boxes do not affect any safety related system or component and does not impact any Technical Specification.

DC 86-15 LEVEL INSTRUMENTATION TO PREVENT LOSS OF SHUTDOWN COOLING UNIT l This design change installed a permanent standpipe arrangement to replace the temporary polyhose arrangement installed during each outage.

Local level indication, control room indication and a control room low level alarm are provided for reactor coolant level during outage periods.

SUMMARY

OF SAFETY ANALYSIS The system will be placed into service only during cold shutdown conditions. At all other times the system is isolated from other systems.

The portion of the system up to and including the second isolation valve is designed to reactor coolant design pressure and temperature. This system does not affect safety related equipment or the operation of the safety related systems.

DC 87-32 WEED 9007 RTD REPLACEMENT UNIT l This modification replaced the eighteen (18) narrow range RTDs with RTDs which have adequately demonstrated environmental qualification as set forth by NUREG 0588 Category 1.

SUMMARY

OF SAFETY ANALYSIS The replacement RTDs are essentially one for one replacements of an enhanced design and will not affect any of the operations or ability of equipment important to safety to perform their safety functions.

PAGE 13 FACIIJT.ANGES THAT DID NOT REQUIR.RC APPROVAL MONTH/YEAR AUGUST 1988 AC S2-88-0615 ADMINISTRATIVE CONTROL 08/04/88 This change provides administrative control while closing MOV-SW-205B or MOV-SW-205D in order to accomplish maintenance on the associated valve.

Since the valves (MOV-SW-205B and 205D) will remain operable and will be manually opened prior to auto or manual start of the recirculation spray (RS) pumps, the change will not affect the operation of the RS system. Therefore, no unreviewed safety question is created.

AC S2-88-0805 ADMINISTRATIVE CONTROL 08/05/88 This change maintained recirculation spray (RS) heat exchangers service water discharge valves 2-SW-MOV-205B & D closed under administrative control to prevent service water ingress to the recirculation spray heat exchangers from the discharge tunnel to prevent biofouling of the RS heat exchangers.

Since the valves (MOV-SW-205B and 205D) will remain operable and will be manually opened prior to auto or manual start of the RS pumps, the change will not affect the operation of the RS system. Therefore, no unreviewed safety question is created.

FS 88-40 FSAR CHANGE REQUEST 08/09/88 Design Change 77-09 modified the usable volume of Unit 1 and Unit 2 R WSTs. The modification affected LC Os for safety injection and*

containment spray systems.

The 10 CFR 50.59 review resulted in no unreviewed safety question since DC 77-09 did not alter the basic design function of the affected systems.

TM S2-88-60 TEMPORARY MODIFICATION 08-19-88 This modification allowed the lead from terminal board 58C-2 to 2AST 1 to be lifted and prevent the mechanical anti-motoring trip from operating.

Removal of the mechanical anti-motoring trip will not have an adverse effect on the turbine overspeed or loss of electrical load analysis.

Therefore, there is no unreviewed safety question.

TM Sl-88-132 TEMPORARY MODIFICATION 08/20/88 A jumper was installed from the sample connection of the VCT gas space to the sample connection of the gas stripper surge tank at the sample sink.

Venting the VCT via the sampling system will not increase the probability of an accident nor increase the consequences of an accident. Protection to the system is provided by relief valves in the system. Hose and fittings are rated in excess of operating pressures for the systems. Therefore, no unreviewed safety question is created.

A PAGE 14 FACIUT.ANGES THAT DID NOT REQUIRlaRC APPROVAL MONTH/YEAR AUGUST 1988 AC Sl-88-810 ADMINISTRATIVE CONTROL 08/20/88 AC S2-88-8 IO While the charging pump component cooling (CC) pump's drain valve is open to feed and bleed the system to increase chromate concentration, an operator will be stationed at the drain valve to close it immediately should the head tank level drop .s_ 30%.

Feeding and bleeding the charging pump CC system by opening the charging pump CC pump's drain valve will not affect the operability of the charging system. It will enhance corrosion control by the addition of chromates. Therefore, this administrative control does not constitute an unreviewed safety question.

AC Sl-88-0820 ADMINISTRATIVE CONTROL 08/20/88 This change maintained recirculation spray (RS) heat exchanger (HX) service water (SW) discharge valve (1-SW-MOV-lOSA) closed under administrative control to prevent SW ingress into the RS HX from the discharge tunnel to prevent biofouling of the RS HX.

Since valve 1-SW-MOV-lOSA will remain operable (as per EWR 88-326) and will be opened prior to auto or manual start of the RS pumps, the change will not affect the operation of the RS system. Therefore, no unreviewed safety question is created.

AC Sl-88-0821 ADMINISTRATIVE CONTROL 08/21/88 This change allowed manual control over the 'C' RSST tap changer with constant communication with the control room due to failure in the automatic control.

Manual control of the 'C' reserve station service transformer tap changer is required due to a failure in the automatic system. Manual control ensure voltages on the emergency buses will remain in spec and will reduce the chance of loss of offsite power to 1H and 2J emergency buses. Manual operation will maintain voltages within the intent of GDC 17.

AC Sl-88-0823 ADMINISTRATIVE CONTROL 08/23/88 The dike at the emergency switchgear room was temporarily removed and a flood watch was placed at the door and at the turbine building pit areas. The dike was reinstalled in the event of a flood.

The removal of this dike will not adversely affect any safety related equipment or create an unreviewed safety question.

PAGE 15 OCEDURE OR METHOD OF OP AT DID NOT REQUIRE NRG APP MONTH/YEAR AUGUST 1988 l-TOP-2027 TEMPORARY OPERATING PROCEDURE 08/01/88 This change provided a means for flushing the primary drains transfer tanks (PDTT) discharge lines to the primary drains tanks (PDT) and to inspect PDTT pumps discharge check valves to clear/identify blockage in PDTT discharge lines.

An unreviewed safety question does not exist because the probability and consequences of a liquid waste release are unaffected. All liquid waste released from the check valves will be contained and directed to floor drains and the containment sump. Flush water will also be directed to the PDT and will be contained. Any uncontrolled release will be stopped by closing l-DG-74. This valve can also be immediately shut if containment isolation is necessary.

JUSTIFICATION FOR CONTINUED OPERATION 08/11/88 This Justification for Continued Operation documents plant operation with three out of four Radiation Monitoring Pumps operable on Service Water Discharge Lines from Recirculation Spray Heat Exchangers (RSHX).

The reviewed condition does not affect the function of the RS system. Significant increases in exposure or releases will not occur because a backup radiation monitor exists and under the postulated failure of the RSHX, the heat exchanger can be

  • isolated without reducing the required heat removal via the RS system. Therefore, an unreviewed safety question does not exist.

PROCEDURE OR METHOD OF OPERATION THAT DID REQUIRE NRC APPROVAL PAGE 16 MONTH/YEAR

- -AUGUST

- - -1988 NONE DURING THIS PERIOD

TESTS AND EXPERIMENTS REQUIRING NRC APPROVAL PAGE 17 MONTH/YEAR AUGUST 1988 NONE DURING THIS PERIOD

  • PAGE 18 TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR AUGUST 1988 NONE DURING THIS PERIOD
  • ----------- VIRGINIA POWER PAGE 19 SURRY POWER STATION
  • CHEMISTRY REPORT AUGUST 19 88 PRIMARY COOLANT UNIT NO. 1 UNIT NO. 2

- ANALYSIS MAX. MIN. AVG. MAX. MIN. . AVG.

Gross Radioact., l!Ci/ml 8.88E-l l.18E-l 6.87E-l 2.00E-1 9.17E-2 1. 55E-l Suspended Solids, PPm o.o o.o o.o o.o o.o o.o Gross Tritium, µCi/ml 2.23E-l l.51E-l 1. 93E-l 6.47E-:i 3.78E-2 5.29E-2

  • 131 3.73E-3 4.57E-4 2.54E-3 2. 04E:.L 6.23E-5 1. 30E-4 Iodine , µCi/ml 1

131 1 1 1 *n 0.16 0.09 0 .12 0. 15 0.05 0.09 Hydrogen, cc/b. 31.9 25.5 27.8 131. O 26.1 29.0 Lithium, ppm 2.35 2.06 2.21 0.47 0.29 0.37 Boron-10, ppm* 267.0 184.0 202.9 0.764 ~0.196 0.439 Oxygen, (DO), 01>m <0.005 <0.005 <0.005 <0.005

--k0.005 <0.005 0.010 0.003 0.007 <0.010 kO~OOl <0.002 Chloride, ppm pH@ 25 degree Celsius 6.50 6.27 6.41 8.68 7.44 8 .11

  • Boron-10
  • Total Boron X 0.196 REMARKS:

UNIT I: Started month at 100%. Ramped down to 96% on 8-4 because of condensate polishing differential pressure and were back to 100% on 8-6. On 8-12, 0500 started to ramp down to 90% again due to condensate polishing differential pressure but were back to 100% by 2252. On 8-15 at 0927, a reactor trip occurred and the unit stayed in hot shutdown until the reactor was cr1tical on 8-16 at 2049. The unit was at 100% on 8-18 at 0500. On 8-27, started at 0025 to ramp down to 68% to repair a hydrogen cooler and was back to 100% by 0643. On 8-29, started at 1300 to ramp down to 79% due to fire in main generator leads and was back to 100% by 1855 and ended the month at 100%.

Lithium was added 8-8 at 2010, 180g; 8-12 at 1025, 420g; 8-15 at 1830, 480g; 8-18 at 0515, 502g; 8-19 at 1300, 389g; 8-27 at 1100, 400g; for a total of 2371 grams of LiOH.

UNIT 2: Started the month at 89%an~ coasting to refueling. On 8-6 at 0545, ramped back to 73% to clean waterboxes and returned to 90% on 8-7 at 0840. On 8-8, ramped down to 72% to clean waterboxes and returned to 88% on 8-10 at 0035. On 8-18, ramped down to 73% to perform PT-29.1 and clean waterboxes and returned to 84% on 8-19.

On 8-21 at 2204, ramped down to 71% to clean waterboxes and returned to 79% on 8-22 and end of month at 76%. The B Debora tor was in service from 8-7 at 2015 to 8-9 at 0035; from 8-26 at 2255 to 8-27 at 0925. Lithium was added 8-11 at 1330, 180g; 8-22 at 1250; 145g; 8-25 at 1115, 225g; 8-27 at 1100, 178g; for a total of 728 grams of LiOH.

PAGE 20 GNSI CASTOR V/21 #500-11-008 (ISFSI)

UNIT 1 FUEL HANDLING DATE August 1988 NEW OR DATE NUMBER OF NEW OR SPENT SPENT FUEL SHIPPED OR ASSEMBLIES ASSEMBLY ANSI INITIAL FUEL SHIPPING SHIPMENT II RECEIVED PER SHIPMENT fl II ENRICHMENT CASK ACTIVITY LEVEL CV/21 500-11-008 08126188 NIA C50 -- 3.12% NIA CV/21 500-11-008 08126188 NIA C51 - 3.12% N/A

PAGE 21

.NSI CASTOR V/21 1500-11-008 *

. (ISFSI)

UNIT 2 FUEL HANDLING DATE August 1988 NEW OR DATE NUMBER OF NEW OR SPENT SPENT FUEL SHIPPED OR ASSEMBLIES ASSEMBLY ANSI INITIAL FUEL SHIPPING SHIPMENT() RECEIVED PER SHIPMENT () 11 ENRICHMENT CASK ACTIVITY LEVEL CV/21 500-11-008 08/26/88 N/A P24 - 3.11 N/A CV/21 500-11-008 08/26/88 N/A P05 - 3.11 N/A CV/21 500-11-008 08/26/88 N/A P09 - 3.11 N/A C'J /21 500-11-008 08/26/88 N/A P23 - 3.11 N/A CV/21 500-11-008 08/26/88 N/A P04 -* 3.11 N/A CV/21 500-11-008

  • 08/26/88 N/A P07 - 3.11 N/A CV/21 500-11-008 08/26/88 N/A P02 - 3.11 N/A CV/21 500-11-008 08/26/88 N/A P06 - 3.11 N/A CV/21 500-11-008 08/26/88 N/A PI4 - 3.11 N/A CV/21 500-11-008 08/26/88 N/A PI7 - 3.11 N/A CV/21 500-11-008 08/26/88 N/A POI - 3.11 N/A CV/21 500-11-008 08/26/88 N/A P03 - 3.11 N/A CV/21 500-11-008 08/26/88 N/A P27 - 3.11 N/A CV/21 500-11-008 08126188 NIA PIO - 3.11 NIA CV/21 500-11-008 08126/88 NIA P28 - 3.11 NIA CV/21 500-11-008 08l?fll88 NIA P08 - 3.11 N/A CV/21 500-11-onR ORl?.fl/88 NIA Pl2 - 3.11 NIA CV/21 -

500-11-008 08/26188 NIA P22 - 3.11 NIA CV/21 500-11-008 08/26188 NIA P29 -- 3.11 N/A

PAGE 22 DESCRIPTION OF PERIODIC TEST WHICH WERE NOT COMPLETED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR AUGUST 1988 NONE DURING THIS PERIOD

..../

. '. \

VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 September 14, 1988 U.S. Nuclear Regulatory Commission Serial No.88-627 Attention: Document Control Desk NO/RPC:vlh Washington, D. C. 20555 Docket Nos. 50-280 50-281 License Nos. DPR-32 DPR-37 Gentlemen:

VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of August 1988.

W. R. Cartwright Vice President - Nuclear Enclosure cc: U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N. W.

Suite 2900 Atlanta, Georgia 30323 Mr. W. E. Holland NRC Senior Resident Inspector Surry Power Station