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| {{#Wiki_filter:10CFR50.73 Virginia Electric and Power Company Surry Power Station 5570 Hog Island Road Surry, Virginia 23883 March 19, 1997 U. S. Nuclear Regulatory Commission | | {{#Wiki_filter:10CFR50.73 Virginia Electric and Power Company Surry Power Station 5570 Hog Island Road Surry, Virginia 23883 March 19, 1997 U. S. Nuclear Regulatory Commission Serial No.: 97-166 |
| * Document Control Desk Washington, D. C. 20555 | | * Document Control Desk SPS:VLA Washington, D. C. 20555 Docket No.: 50-280 50-281 License No.: DPR-32 DRP-37 |
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| ==Dear Sirs:== | | ==Dear Sirs:== |
| Serial No.: 97-166 SPS:VLA Docket No.: 50-280 50-281 License No.: DPR-32 DRP-37 Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report (LER)
| | |
| * applicable to Surry Power Station Units 1 and 2. REPORT NUMBER 50-280/50-281 | | Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report (LER) |
| /97-003-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be forwarded to the Management Safety Review Committee for its review. *. Very truly yours, D. A. Christian Station Manager ---* ---------~--9703260334 970319 Enclosure PDR ADOCK 05000280 S. P~,, Commitments contained in this letter: None. cc: Regional Administrator 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323 R. A. Musser NRG Senior Resident Inspector Surry Power Station 2G0112 IIIGIIHIDllllllllllll!mlll | | *applicable to Surry Power Station Units 1 and 2. |
| | REPORT NUMBER 50-280/50-281 /97-003-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be forwarded to the Management Safety Review Committee for its review. |
| | *. Very truly yours, D. A. Christian Station Manager |
| | - --* - - - - -----~-- |
| | 9703260334 970319 Enclosure PDR ADOCK 05000280 S. P~,, |
| | Commitments contained in this letter: None. |
| | cc: Regional Administrator 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323 R. A. Musser NRG Senior Resident Inspector Surry Power Station 2G0112 IIIGIIHIDllllllllllll!mlll |
| * I 7 | | * I 7 |
| * I I !!o I 2 C | | * I I !!o I 2 C |
| * NRC FORM 366 e. NUCLEAR REGULATORY COMMISSION | | * NRC FORM 366 (4-95) |
| *e APPROVED BY 0MB NO. 3150-0104 (4-95) EXPIRES 4/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS. LICENSEE EVENT REPORT (LER) REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INOUSTRY. | | : e. NUCLEAR REGULATORY COMMISSION *e APPROVED BY 0MB NO. 3150-0104 EXPIRES 4/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS. |
| FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (T-6 F33), (See reverse for required number of digits/characters for each block) U.S. MJCLEAR REGULATORY COMMISSION, WASHINGTON, DC. 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MNlAGEMENT N8J BUDGET, WASHINGTON, DC 20503. FACILITY NAME (1) DOCKET NUMBER (2) PAGE(3) SURRY POWER STATION, Unit 1 05000-280 1 OF5 TITLE(4) Loss of Pressurizer Heaters Results in Manual U1 Trip and U2 ESF Actuation ENT DATE (5) LER NUMBER (6) RT DATE (7) OTHER FACILITIES INVOLVED 8) SEQUENTIAL REVISION FACILITY NAME DOCUMENT NUMBER MONTH DAY YEAR YEAR MONTH DAY YEAR Surry Unit 2 osooo~2a1 NUMBER NUMBER 02 19 . 97 97 --003 --0 03 19 97 FACILITY NAME DOCUME_NT NUMBER 05000-OPERATING THiS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11) MODE (9) N 20.2201(b) 20.2203(a)(2)(v) | | REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSEE EVENT REPORT (LER) LICENSING PROCESS AND FED BACK TO INOUSTRY. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (T-6 F33), |
| X 50.73(a)(2)(1) 50.73(a)(2)(viii) | | U.S. MJCLEAR REGULATORY COMMISSION, WASHINGTON, DC. |
| POWER 20.2203(a)(1) 20.2203(a)(3)(i) 50.73(a)(2)(ii) 50.73(a)(2)(x) | | (See reverse for required number of digits/characters for each block) 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MNlAGEMENT N8J BUDGET, WASHINGTON, DC 20503. |
| LEVEL (10) 100 % 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a)(2)(iii) 73.71 20.2203(a)(2)(ii) 20.2203(a)(4) | | FACILITY NAME (1) DOCKET NUMBER (2) PAGE(3) |
| X 50.73(a)(2)(iv) | | SURRY POWER STATION, Unit 1 05000- 280 1 OF5 TITLE(4) |
| OTHER 20.2203(a)(2)(iii) 50.36(c)(1) | | Loss of Pressurizer Heaters Results in Manual U1 Trip and U2 ESF Actuation ENT DATE (5) LER NUMBER (6) RT DATE (7) OTHER FACILITIES INVOLVED 8) |
| I 50.73(a)(2)(v) | | SEQUENTIAL REVISION FACILITY NAME DOCUMENT NUMBER MONTH DAY YEAR YEAR MONTH DAY YEAR NUMBER NUMBER Surry Unit 2 osooo~2a1 19 . FACILITY NAME DOCUME_NT NUMBER 02 97 97 -- 003 -- 0 03 19 97 05000-OPERATING THiS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11) |
| Specify in Abstract below 20.2203(a)(2)(iv) 50.36(c)(2) | | MODE (9) N 20.2201(b) 20.2203(a)(2)(v) X 50.73(a)(2)(1) 50.73(a)(2)(viii) |
| : 50. 73(a)(2)(vii) or in NRC Form 366A LICENSEE CONTACT FOR THIS LER (12) NAME I TIELEPHONE NUMBER (Include Area Coda) D. A. Christian, Station Manager (757) 365-2000 . COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) CAUSE SYSTEM .COMPONENT MANUFACTURER REPORTABLE CAUSE SYSTIEM COMPONENT-MANUF'ACTURER REPORTABLE TONPRDS TONPRDS E AB PMC R305 No B AB ALY B455 No SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY. YEAR I YES . IX I NO SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE).
| | POWER 20.2203(a)(1) 20.2203(a)(3)(i) 50.73(a)(2)(ii) 50.73(a)(2)(x) |
| * DATE ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) At 2040 hours on February 19, 1997, with Unit 1 at 100 percent power and Unit 2 at Hot Shutdown, a Technical Specificcttion 3.12.F.2 two hour Limiting Condition of_ Operation was entered due to Reactor Coolant System (RCS) -pressure being less than 2205 psig. An Abnormal Procedure was entered in response to the decreasing RCS pressure.
| | LEVEL (10) 100 % 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a)(2)(iii) 73.71 20.2203(a)(2)(ii) 20.2203(a)(4) X 50.73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c)(1) I 50.73(a)(2)(v) Specify in Abstract below 20.2203(a)(2)(iv) 50.36(c)(2) 50. 73(a)(2)(vii) or in NRC Form 366A LICENSEE CONTACT FOR THIS LER (12) |
| At 2052 hours, a Unit 1 shutdown was commenced. | | NAME I TIELEPHONE NUMBER (Include Area Coda) |
| At 2259 hours, a manual reactor trip was initiated due to a continuing decrease in RCS pressure. | | D. A. Christian, Station Manager (757) 365-2000 . |
| Upon receipt of the reactor trip signal, the Reactor Protection System actuated and functioned as designed, and all control rods inserted into the core. Station operating personnel acted promptly to place the plant in a safe, hot shutdown condition in accordance with the proper procedures. | | COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) |
| The shutdown margin was calculated and the critical safety function status trees were monitored to verify that the unit conditions were acceptable. | | CAUSE SYSTEM .COMPONENT MANUFACTURER REPORTABLE CAUSE SYSTIEM COMPONENT- MANUF'ACTURER REPORTABLE TONPRDS TONPRDS E AB PMC R305 No B AB ALY B455 No SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY. YEAR I YES . |
| Plant response was as expected and the unit stabilized at hot shutdown. | | IX I NO SUBMISSION |
| No conditions adverse to safety resulted from this event and the health and safety of the public were not affected. | | * DATE (If yes, complete EXPECTED SUBMISSION DATE). |
| A detailed Reactor Trip Report and a Root Cause Evaluation is being performed tor this event. The cause of the trip was inability to maintain RCS pressure due to loss of the Group C pressuizer proportional heaters due to failure of the Robicon controller unit. Additional approved recommendatic'"'c: | | ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) |
| from the Root Cause Evaluation will be implemented. | | At 2040 hours on February 19, 1997, with Unit 1 at 100 percent power and Unit 2 at Hot Shutdown, a Technical Specificcttion 3.12.F.2 two hour Limiting Condition of_ Operation was entered due to Reactor Coolant System (RCS) -pressure being less than 2205 psig. An Abnormal Procedure was entered in response to the decreasing RCS pressure. At 2052 hours, a Unit 1 shutdown was commenced. At 2259 hours, a manual reactor trip was initiated due to a continuing decrease in RCS pressure. Upon receipt of the reactor trip signal, the Reactor Protection System actuated and functioned as designed, and all control rods inserted into the core. Station operating personnel acted promptly to place the plant in a safe, hot shutdown condition in accordance with the proper procedures. The shutdown margin was calculated and the critical safety function status trees were monitored to verify that the unit conditions were acceptable. Plant response was as expected and the unit stabilized at hot shutdown. No conditions adverse to safety resulted from this event and the health and safety of the public were not affected. A detailed Reactor Trip Report and a Root Cause Evaluation is being performed tor this event. The cause of the trip was inability to maintain RCS pressure due to loss of the Group C pressuizer proportional heaters due to failure of the Robicon controller unit. Additional approved recommendatic'"'c: from the Root Cause Evaluation will be implemented. This. event is beinQ reported pursuant t6 10 CFR 50.73(a)(2)(iv) and 10 CFR 50.73(a}(2)(i). |
| This. event is beinQ reported pursuant t6 10 CFR 50.73(a)(2)(iv) and 10 CFR 50.73(a}(2)(i). | |
| NRC FORM 366 (4-95) | | NRC FORM 366 (4-95) |
| NRG FORM 366A (4-95) e e U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME (1) Surry Power Station, Unit 1 TEXT (If more space is required, use additional copies of NRG Form 366A) (17) | | |
| | NRG FORM 366A (4-95) e e U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER) |
| | TEXT CONTINUATION FACILITY NAME (1) DOCKET LEA NUMBER (6) PAGE (3) |
| | Surry Power Station, Unit 1 YEAR I SEQUENTIAL NUMBER I ::lEVISION NUMBER 05000- 280 97 -003- 0 20F5 TEXT (If more space is required, use additional copies of NRG Form 366A) (17) |
|
| |
|
| ==1.0 DESCRIPTION== | | ==1.0 DESCRIPTION== |
| | OF THE EVENT At 2040 hours on February 19, 1997, with Unit 1 at 100 percent power and Unit 2 at Hot Shutdown, a Technical Specification (TS) 3.12.F.2 two hour Limiting Condition of Operation was entered due to Reactor Coolant System (RCS) {EIIS-AB} pressure 'being less than 2205 psig. TSs state that pressurizer pressure must be maintained greater than or equal to 2205 psig. If pressure is less than 2205 psig and not restored within two hours, then thermal power shall be reduced to 5 percent rated power within the next four hours. Abnormal Procedure, 1- |
| | - *AP-31.0o, **increasing or Decreasing RCS Pressure, was entered in response to the a |
| | decreasing RCS pressure. At 2052 hours; Unit 1 shutdown was commenced; At 2259 hours, with the unit at approximately 53 percent reactor power, a manual reactor trip was initiated due to the continuing decrease in RCS pressure. Upon receipt of the manual reactor trip, the Reactor Protection System (RPS) functioned as designed and all control rods |
| | {EIIS-AA-ROD} inse_rted into the, core as indicated by the rod bottom lighUndication and by all Individual Rod.Position Indicators (IRPls) indicating less than 10 steps. A shutdown margin c~lcul~tion verified adequate shutdown margin. |
| | * All three Auxiliary Feedwater Pumps (AFW) {EIIS-BA*P} automatically started as designed on lo~ low steam generator {EIIS-AB-SG} levels following the trip. ** |
| | The RCS pressure and temperature stabilized at no load Tavg following the trip. No primary safety or power operated relief valves were actuated during the event. No secondary safety relief valves or power operated relief valves {EIIS-RV} actuated during the transient. All electrical busses transferred properly following the trip and all emergency diesel generators were operable. However, Reactor Coolant Pump A (RCP) {EIIS-AB-P} tripped during .the Station Service Bus transfer to the Reserve Station Service Transformers due to unexpected actuation of the speed sensing relays. RCP C was secured by the operating* team in accordance with procedures to prevent fu-rther RCS pressure decrease. ,Pressurizier Spray Valve B {EIIS-AB-V} had been previously isolated due to leakby. No safety injection occurred. |
| | Since Unit 2 was in Hot Shutdown at the time of the trip, automatic load shedding was enabled, and the load shed affected station service electrical loads tripped as designed. At the time of the load shed sequence, the Unit 2, Main Feed Pump A (MFP) {EIIS-SJ} was in service, and the Unit 2 MFP B was tagged out for repairs. Unit 2 MFP Atripped on lo~d shed as designed. This resulted in a loss of both MFPs on Unit 2 and resulted in an automatic start of both Unit 2 Motor Driven Auxiliary Feedwater P:.imps. |
| | * At 2328 hours on 2/19/97, a one hour Non-Emergency report was made to the NRC in accordance with 10 CFR 50.72(b)(1 )(i)(A) for initiation of any plant shutdown required by TS. |
| | This report also included the notification of the Unit 1 RPS actuation following the manual reactor trip. In ac..;ordance with 10 CFR 50.72(br(2)(ii), a separate four hour report was made at 0149 hours due to the automatic AFW actuation on Unit 2. |
| | * NRG FOFM 366A (4*95) |
| | |
| | NRC FORM 366A (4-95) e eu.s. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER) |
| | TEXT CONTINUATION FACILITY NAME (1) DOCKET LEA NUMBER (6) PAGE (3) |
| | Surry Power Station, Unit 1 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 05000- 280 97 -003- 0 30F5 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) |
| | There were no radiation releases due to this event, nor were there any personnel injuries or contamination events. |
| | This event is being reported pursuant to 10 CFR 50.73(a)(2)(iv) for a condition that resulted in automatic actuation of the RPS for Unit 1 and automatic actuation of an Engineering Safety Feature (ESF) for Unit 1 and Unit 2. This event is also being reported pursuant to 10 CFR 50.73(a)(2)(i) due to completion of a TS required shutdown for Unit 1. |
| | 2.0 SAFETY CONSEQUENCES AND IMPLICATIONS Upor receipt of the _reactor trip signal, the RPS actuated and functioned as designed, and al.I control rods inserted into the core. Station operating personnel acted promptly to place the |
| | .unit in a safe, hot shutdown, condition in accordance with t_he proper procedures. The Shift Technical Advisor calculated .the shutdown margin* and monitored the critical safety function status* trees to verify that the unit conditions were acceptable. Plant response was as expected and the unit stabilized at. hot shutdown. There were no radiation releases due to . |
| | * this event, nor were there any personnel injuries. or contamination events.: . No cond_itiohs adverse to safety resulted from this event and the health and safety of the public .were not affected. .. . .. |
| | .3.0 CAUSE The cause of the trip was inability to maintain RCS pressure due to loss of the Group C pressurizer proportional heaters. This loss of the proportional pressurizer heaters was due to age related failures of a Robicon controller unit circuit card. |
| | 4.0 IMMEDIATE CORRECTIVE ACTION(S) |
| | Following the reactor trip at 2259 hours on February 19, 1997, control room operators initiated the appropriate emergency operating procedures. The reactor trip breakers were verified open and control rods were verified inserted into the core. |
| | The Shift Technical Advisor calculated the shutdown margin and monitored the critical safety function status trees to verify that the unit conditions were acceptable. * |
| | * Management conducted a post trip review meeting with the operating staff at 0100 hours on February 20, 1997. |
| | NRG FORM :;ssA (4*95) |
|
| |
|
| OF THE EVENT DOCKET 05000-280 LEA NUMBER (6) YEAR I SEQUENTIAL I ::lEVISION NUMBER NUMBER 97 -003-0 PAGE (3) 20F5 At 2040 hours on February 19, 1997, with Unit 1 at 100 percent power and Unit 2 at Hot Shutdown, a Technical Specification (TS) 3.12.F.2 two hour Limiting Condition of Operation was entered due to Reactor Coolant System (RCS) {EIIS-AB}
| | l NRC FORM 366A (4-95) e e.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LEA) |
| pressure 'being less than 2205 psig. TSs state that pressurizer pressure must be maintained greater than or equal to 2205 psig. If pressure is less than 2205 psig and not restored within two hours, then thermal power shall be reduced to 5 percent rated power within the next four hours. Abnormal Procedure, 1--*AP-31.0o, **increasing or Decreasing RCS Pressure, was entered in response to the decreasing RCS pressure.
| | TEXT CONTINUATION FACILITY NAME (1) DOCKET LEA NUMBER (6) PAGE (3) |
| At 2052 hours; a Unit 1 shutdown was commenced; At 2259 hours, with the unit at approximately 53 percent reactor power, a manual reactor trip was initiated due to the continuing decrease in RCS pressure.
| | Surry Power Station, Unit 1 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 05000- 280 97 -003- 0 40F 5 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) 5.0 ADDITIONAL CORRECTIVE ACTION($) |
| Upon receipt of the manual reactor trip, the Reactor Protection System (RPS) functioned as designed and all control rods {EIIS-AA-ROD}
| | A Root Cause Evaluation was initiated to investigate the Pressurizer Heater C control circuitry failure. The Robicon controller module was sent to the vendor. The investigation by the vendor revealed age related failures of capacitors, zenor diodes, and resistors in a controller circuit card. The components were replaced, and the controller module was calibrated. . The Robicon controller module was re-installed and satisfactory post maintenance tests returned the proportional heaters to service. |
| inse_rted into the, core as indicated by the rod bottom lighUndication and by all Individual Rod.Position Indicators (IRPls) indicating less than 10 steps. A shutdown margin c~lcul~tion verified adequate shutdown margin.
| | Upon completion of repairs to the pressurizer heaters and the Post Trip review, Unit 1 was taken critical at 0724 hours and on iine at 1342 hours on February 22, 1997. Unit 1 was |
| * All three Auxiliary Feedwater Pumps (AFW) {EIIS-BA*P}
| | . returned to 100% reactor power at 1353 hours on February 23, 1997. |
| automatically started as designed on lo~ low steam generator
| | It was determined that the trip of the RCP A was due to the failure of Pro-Star speed sensing relays {EIIS-AB-RLY} due to a manufacturing deficiency. The relay was replaced: Software problems in the computations being performed by the Pro-Star relays were discovered following the Unit 1 trip. The specific causes and corrective actions will be implemented by the corrective action program. |
| {EIIS-AB-SG}
| | As part of the Root Cause Evaluation, the equipment problems which occurred were evaluated in accordance with the Maintenance Rule and it was determined that two Maintenance Rule Functional Failures occurred. The first was the Robicon heater controller failure and the second was the failure of the speed sensing relays. These are being addressed in ac.cordance with maintenance rule program requirements. |
| levels following the trip. *
| | 6.0 ACTIONS TO PREVENT RECURRENCE / |
| * The RCS pressure and temperature stabilized at no load Tavg following the trip. No primary safety or power operated relief valves were actuated during the event. No secondary safety relief valves or power operated relief valves {EIIS-RV}
| | A detailed Reactor Trip Report and a Root Cause Evaluation is being performed for this* |
| actuated during the transient.
| | event. The Pro-Star relay and the Robicon controller failures are being evaluated. Additional approved recommendations from the Root Cause Evaluation will be implemented in accordance with the corrective action program. |
| All electrical busses transferred properly following the trip and all emergency diesel generators were operable.
| | An evaluation of preventive maintenance on the* Robicon controllers is being conducted. |
| However, Reactor Coolant Pump A (RCP) {EIIS-AB-P}
| | 7.0 SIMILAR EVENTS None NRC FORM 366A (4-95) |
| tripped during .the Station Service Bus transfer to the Reserve Station Service Transformers due to unexpected actuation of the speed sensing relays. RCP C was secured by the operating*
| | |
| team in accordance with procedures to prevent fu-rther RCS pressure decrease. , Pressurizier Spray Valve B {EIIS-AB-V}
| | * !FNRG FORM 366A (4-95) e eU.S. NUCLEAR REGULATORY COMMISSION |
| had been previously isolated due to leakby. No safety injection occurred.
| | . LICENSEE EVENT REPORT (LER) |
| Since Unit 2 was in Hot Shutdown at the time of the trip, automatic load shedding was enabled, and the load shed affected station service electrical loads tripped as designed.
| | . TEXT CONTINUATION FACILITY NAME (1) DOCKET LEA NUMBER (6) PAGE (3) |
| At the time of the load shed sequence, the Unit 2, Main Feed Pump A (MFP) {EIIS-SJ}
| | Surry Power Station, Unit 1 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 05000- 280 97 -003- 0 50F5 TEXT (If more space is required, use additional copies of NRC Form 366A} (17) 8.0 MANUFACTURER Robicon Controller Unit: |
| was in service, and the Unit 2 MFP B was tagged out for repairs. Unit 2 MFP Atripped on lo~d shed as designed.
| | Manufacturer - Robicon Model - Series 413 Pro-Star Relays: |
| This resulted in a loss of both MFPs on Unit 2 and resulted in an automatic start of both Unit 2 Motor Driven Auxiliary Feedwater P:.imps.
| | Manufacturer - ABB Model with 1.6 version software NRG FORM 366A (4-95)}} |
| * At 2328 hours on 2/19/97, a one hour Non-Emergency report was made to the NRC in accordance with 1 O CFR 50.72(b)(1
| |
| )(i)(A) for initiation of any plant shutdown required by TS. This report also included the notification of the Unit 1 RPS actuation following the manual reactor trip. In ac..;ordance with 10 CFR 50.72(br(2)(ii), a separate four hour report was made at 0149 hours due to the automatic AFW actuation on Unit 2.
| |
| * NRG FOFM 366A (4*95)
| |
| NRC FORM 366A (4-95) e eu.s. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET LEA NUMBER (6) FACILITY NAME (1) Surry Power Station, Unit 1 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER 05000-280 97 -003-0 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) PAGE (3) 30F5 There were no radiation releases due to this event, nor were there any personnel injuries or contamination events. This event is being reported pursuant to 10 CFR 50.73(a)(2)(iv) for a condition that resulted in automatic actuation of the RPS for Unit 1 and automatic actuation of an Engineering Safety Feature (ESF) for Unit 1 and Unit 2. This event is also being reported pursuant to 10 CFR 50.73(a)(2)(i) due to completion of a TS required shutdown for Unit 1. 2.0 SAFETY CONSEQUENCES AND IMPLICATIONS Upor receipt of the _reactor trip signal, the RPS actuated and functioned as designed, and al.I control rods inserted into the core. Station operating personnel acted promptly to place the .unit in a safe, hot shutdown, condition in accordance with t_he proper procedures. | |
| The Shift Technical Advisor calculated .the shutdown margin* and monitored the critical safety function status* trees to verify that the unit conditions were acceptable.
| |
| Plant response was as expected and the unit stabilized at. hot shutdown.
| |
| There were no radiation releases due to .
| |
| * this event, nor were there any personnel injuries.
| |
| or contamination events.: . No cond_itiohs adverse to safety resulted from this event and the health and safety of the public .were not affected. . . . .. . 3.0 CAUSE The cause of the trip was inability to maintain RCS pressure due to loss of the Group C pressurizer proportional heaters. This loss of the proportional pressurizer heaters was due to age related failures of a Robicon controller unit circuit card. 4.0 IMMEDIATE CORRECTIVE ACTION(S)
| |
| Following the reactor trip at 2259 hours on February 19, 1997, control room operators initiated the appropriate emergency operating procedures.
| |
| The reactor trip breakers were verified open and control rods were verified inserted into the core. The Shift Technical Advisor calculated the shutdown margin and monitored the critical safety function status trees to verify that the unit conditions were acceptable.
| |
| *
| |
| * Management conducted a post trip review meeting with the operating staff at 0100 hours on February 20, 1997. NRG FORM :;ssA (4*95)
| |
| NRC FORM 366A (4-95) e e.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LEA) TEXT CONTINUATION FACILITY NAME (1) Surry Power Station, Unit 1 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) 5.0 ADDITIONAL CORRECTIVE ACTION($)
| |
| DOCKET 05000-280 LEA NUMBER (6) PAGE (3) YEAR I SEQUENTIAL I REVISION NUMBER NUMBER 97 -003-0 40F 5 A Root Cause Evaluation was initiated to investigate the Pressurizer Heater C control circuitry failure. The Robicon controller module was sent to the vendor. The investigation by the vendor revealed age related failures of capacitors, zenor diodes, and resistors in a controller circuit card. The components were replaced, and the controller module was calibrated. . The Robicon controller module was re-installed and satisfactory post maintenance tests returned the proportional heaters to service. Upon completion of repairs to the pressurizer heaters and the Post Trip review, Unit 1 was taken critical at 0724 hours and on iine at 1342 hours on February 22, 1997. Unit 1 was . returned to 100% reactor power at 1353 hours on February 23, 1997. It was determined that the trip of the RCP A was due to the failure of Pro-Star speed sensing relays {EIIS-AB-RLY}
| |
| due to a manufacturing deficiency. | |
| The relay was replaced: | |
| Software problems in the computations being performed by the Pro-Star relays were discovered following the Unit 1 trip. The specific causes and corrective actions will be implemented by the corrective action program. As part of the Root Cause Evaluation, the equipment problems which occurred were evaluated in accordance with the Maintenance Rule and it was determined that two Maintenance Rule Functional Failures occurred. | |
| The first was the Robicon heater controller failure and the second was the failure of the speed sensing relays. These are being addressed in ac.cordance with maintenance rule program requirements. | |
| 6.0 ACTIONS TO PREVENT RECURRENCE | |
| / A detailed Reactor Trip Report and a Root Cause Evaluation is being performed for this* event. The Pro-Star relay and the Robicon controller failures are being evaluated.
| |
| Additional approved recommendations from the Root Cause Evaluation will be implemented in accordance with the corrective action program. An evaluation of preventive maintenance on the* Robicon controllers is being conducted. | |
| 7.0 SIMILAR EVENTS None NRC FORM 366A (4-95) l | |
| * !F e eU.S. NUCLEAR REGULATORY COMMISSION NRG FORM 366A (4-95) .. LICENSEE EVENT REPORT (LER) . TEXT CONTINUATION FACILITY NAME (1) DOCKET LEA NUMBER (6) PAGE (3) Surry Power Station, Unit 1 YEAR I SEQUENTIAL I REVISION NUMBER NUMBER 05000-280 97 -003-0 50F5 TEXT (If more space is required, use additional copies of NRC Form 366A} (17) 8.0 MANUFACTURER Robicon Controller Unit: Manufacturer | |
| -Robicon Model -Series 413 Pro-Star Relays: Manufacturer | |
| -ABB Model with 1 .6 version software -NRG FORM 366A (4-95)}} | |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket ML18153A2201998-02-0606 February 1998 LER 98-001-00:on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was submitted.W/980206 Ltr ML18153A2071998-01-13013 January 1998 LER 97-012-01:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors ML18153A2101998-01-13013 January 1998 LER 97-009-01:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status ML18153A1911997-11-26026 November 1997 LER 97-011-00:on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket ML18153A2201998-02-0606 February 1998 LER 98-001-00:on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was submitted.W/980206 Ltr ML18153A2071998-01-13013 January 1998 LER 97-012-01:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors ML18153A2101998-01-13013 January 1998 LER 97-009-01:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status ML18153A1911997-11-26026 November 1997 LER 97-011-00:on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage. ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With 990115 Ltr ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un. ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With 981214 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With 981111 Ltr ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With 981012 Ltr ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2.W/980807 Ltr ML18152B7621998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Surry Power Station,Units 1 & 2.W/980707 Ltr ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML18153A3141998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Surry Power Station,Units 1 & 2.W/980610 ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B8161998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Surry Power Station Units 1 & 2.W/980508 Ltr ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML20217P9941998-04-0707 April 1998 Safety Evaluation Granting Licensee Third 10-yr Inservice Insp Program Relief Requests SR-018 - Sr-024 ML18153A2951998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sps,Units 1 & 2.W/ 980408 Ltr ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket 1999-09-30
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10CFR50.73 Virginia Electric and Power Company Surry Power Station 5570 Hog Island Road Surry, Virginia 23883 March 19, 1997 U. S. Nuclear Regulatory Commission Serial No.: 97-166
- Document Control Desk SPS:VLA Washington, D. C. 20555 Docket No.: 50-280 50-281 License No.: DPR-32 DRP-37
Dear Sirs:
Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report (LER)
- applicable to Surry Power Station Units 1 and 2.
REPORT NUMBER 50-280/50-281 /97-003-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be forwarded to the Management Safety Review Committee for its review.
- . Very truly yours, D. A. Christian Station Manager
- --* - - - - -----~--
9703260334 970319 Enclosure PDR ADOCK 05000280 S. P~,,
Commitments contained in this letter: None.
cc: Regional Administrator 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323 R. A. Musser NRG Senior Resident Inspector Surry Power Station 2G0112 IIIGIIHIDllllllllllll!mlll
- e. NUCLEAR REGULATORY COMMISSION *e APPROVED BY 0MB NO. 3150-0104 EXPIRES 4/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS.
REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSEE EVENT REPORT (LER) LICENSING PROCESS AND FED BACK TO INOUSTRY. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (T-6 F33),
U.S. MJCLEAR REGULATORY COMMISSION, WASHINGTON, DC.
(See reverse for required number of digits/characters for each block) 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MNlAGEMENT N8J BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) PAGE(3)
SURRY POWER STATION, Unit 1 05000- 280 1 OF5 TITLE(4)
Loss of Pressurizer Heaters Results in Manual U1 Trip and U2 ESF Actuation ENT DATE (5) LER NUMBER (6) RT DATE (7) OTHER FACILITIES INVOLVED 8)
SEQUENTIAL REVISION FACILITY NAME DOCUMENT NUMBER MONTH DAY YEAR YEAR MONTH DAY YEAR NUMBER NUMBER Surry Unit 2 osooo~2a1 19 . FACILITY NAME DOCUME_NT NUMBER 02 97 97 -- 003 -- 0 03 19 97 05000-OPERATING THiS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11)
MODE (9) N 20.2201(b) 20.2203(a)(2)(v) X 50.73(a)(2)(1) 50.73(a)(2)(viii)
POWER 20.2203(a)(1) 20.2203(a)(3)(i) 50.73(a)(2)(ii) 50.73(a)(2)(x)
LEVEL (10) 100 % 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a)(2)(iii) 73.71 20.2203(a)(2)(ii) 20.2203(a)(4) X 50.73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c)(1) I 50.73(a)(2)(v) Specify in Abstract below 20.2203(a)(2)(iv) 50.36(c)(2) 50. 73(a)(2)(vii) or in NRC Form 366A LICENSEE CONTACT FOR THIS LER (12)
NAME I TIELEPHONE NUMBER (Include Area Coda)
D. A. Christian, Station Manager (757) 365-2000 .
COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM .COMPONENT MANUFACTURER REPORTABLE CAUSE SYSTIEM COMPONENT- MANUF'ACTURER REPORTABLE TONPRDS TONPRDS E AB PMC R305 No B AB ALY B455 No SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY. YEAR I YES .
IX I NO SUBMISSION
- DATE (If yes, complete EXPECTED SUBMISSION DATE).
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
At 2040 hours0.0236 days <br />0.567 hours <br />0.00337 weeks <br />7.7622e-4 months <br /> on February 19, 1997, with Unit 1 at 100 percent power and Unit 2 at Hot Shutdown, a Technical Specificcttion 3.12.F.2 two hour Limiting Condition of_ Operation was entered due to Reactor Coolant System (RCS) -pressure being less than 2205 psig. An Abnormal Procedure was entered in response to the decreasing RCS pressure. At 2052 hours0.0238 days <br />0.57 hours <br />0.00339 weeks <br />7.80786e-4 months <br />, a Unit 1 shutdown was commenced. At 2259 hours0.0261 days <br />0.628 hours <br />0.00374 weeks <br />8.595495e-4 months <br />, a manual reactor trip was initiated due to a continuing decrease in RCS pressure. Upon receipt of the reactor trip signal, the Reactor Protection System actuated and functioned as designed, and all control rods inserted into the core. Station operating personnel acted promptly to place the plant in a safe, hot shutdown condition in accordance with the proper procedures. The shutdown margin was calculated and the critical safety function status trees were monitored to verify that the unit conditions were acceptable. Plant response was as expected and the unit stabilized at hot shutdown. No conditions adverse to safety resulted from this event and the health and safety of the public were not affected. A detailed Reactor Trip Report and a Root Cause Evaluation is being performed tor this event. The cause of the trip was inability to maintain RCS pressure due to loss of the Group C pressuizer proportional heaters due to failure of the Robicon controller unit. Additional approved recommendatic'"'c: from the Root Cause Evaluation will be implemented. This. event is beinQ reported pursuant t6 10 CFR 50.73(a)(2)(iv) and 10 CFR 50.73(a}(2)(i).
NRC FORM 366 (4-95)
NRG FORM 366A (4-95) e e U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET LEA NUMBER (6) PAGE (3)
Surry Power Station, Unit 1 YEAR I SEQUENTIAL NUMBER I ::lEVISION NUMBER 05000- 280 97 -003- 0 20F5 TEXT (If more space is required, use additional copies of NRG Form 366A) (17)
1.0 DESCRIPTION
OF THE EVENT At 2040 hours0.0236 days <br />0.567 hours <br />0.00337 weeks <br />7.7622e-4 months <br /> on February 19, 1997, with Unit 1 at 100 percent power and Unit 2 at Hot Shutdown, a Technical Specification (TS) 3.12.F.2 two hour Limiting Condition of Operation was entered due to Reactor Coolant System (RCS) {EIIS-AB} pressure 'being less than 2205 psig. TSs state that pressurizer pressure must be maintained greater than or equal to 2205 psig. If pressure is less than 2205 psig and not restored within two hours, then thermal power shall be reduced to 5 percent rated power within the next four hours. Abnormal Procedure, 1-
- *AP-31.0o, **increasing or Decreasing RCS Pressure, was entered in response to the a
decreasing RCS pressure. At 2052 hours0.0238 days <br />0.57 hours <br />0.00339 weeks <br />7.80786e-4 months <br />; Unit 1 shutdown was commenced; At 2259 hours0.0261 days <br />0.628 hours <br />0.00374 weeks <br />8.595495e-4 months <br />, with the unit at approximately 53 percent reactor power, a manual reactor trip was initiated due to the continuing decrease in RCS pressure. Upon receipt of the manual reactor trip, the Reactor Protection System (RPS) functioned as designed and all control rods
{EIIS-AA-ROD} inse_rted into the, core as indicated by the rod bottom lighUndication and by all Individual Rod.Position Indicators (IRPls) indicating less than 10 steps. A shutdown margin c~lcul~tion verified adequate shutdown margin.
The RCS pressure and temperature stabilized at no load Tavg following the trip. No primary safety or power operated relief valves were actuated during the event. No secondary safety relief valves or power operated relief valves {EIIS-RV} actuated during the transient. All electrical busses transferred properly following the trip and all emergency diesel generators were operable. However, Reactor Coolant Pump A (RCP) {EIIS-AB-P} tripped during .the Station Service Bus transfer to the Reserve Station Service Transformers due to unexpected actuation of the speed sensing relays. RCP C was secured by the operating* team in accordance with procedures to prevent fu-rther RCS pressure decrease. ,Pressurizier Spray Valve B {EIIS-AB-V} had been previously isolated due to leakby. No safety injection occurred.
Since Unit 2 was in Hot Shutdown at the time of the trip, automatic load shedding was enabled, and the load shed affected station service electrical loads tripped as designed. At the time of the load shed sequence, the Unit 2, Main Feed Pump A (MFP) {EIIS-SJ} was in service, and the Unit 2 MFP B was tagged out for repairs. Unit 2 MFP Atripped on lo~d shed as designed. This resulted in a loss of both MFPs on Unit 2 and resulted in an automatic start of both Unit 2 Motor Driven Auxiliary Feedwater P:.imps.
- At 2328 hours0.0269 days <br />0.647 hours <br />0.00385 weeks <br />8.85804e-4 months <br /> on 2/19/97, a one hour Non-Emergency report was made to the NRC in accordance with 10 CFR 50.72(b)(1 )(i)(A) for initiation of any plant shutdown required by TS.
This report also included the notification of the Unit 1 RPS actuation following the manual reactor trip. In ac..;ordance with 10 CFR 50.72(br(2)(ii), a separate four hour report was made at 0149 hours0.00172 days <br />0.0414 hours <br />2.463624e-4 weeks <br />5.66945e-5 months <br /> due to the automatic AFW actuation on Unit 2.
NRC FORM 366A (4-95) e eu.s. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET LEA NUMBER (6) PAGE (3)
Surry Power Station, Unit 1 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 05000- 280 97 -003- 0 30F5 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
There were no radiation releases due to this event, nor were there any personnel injuries or contamination events.
This event is being reported pursuant to 10 CFR 50.73(a)(2)(iv) for a condition that resulted in automatic actuation of the RPS for Unit 1 and automatic actuation of an Engineering Safety Feature (ESF) for Unit 1 and Unit 2. This event is also being reported pursuant to 10 CFR 50.73(a)(2)(i) due to completion of a TS required shutdown for Unit 1.
2.0 SAFETY CONSEQUENCES AND IMPLICATIONS Upor receipt of the _reactor trip signal, the RPS actuated and functioned as designed, and al.I control rods inserted into the core. Station operating personnel acted promptly to place the
.unit in a safe, hot shutdown, condition in accordance with t_he proper procedures. The Shift Technical Advisor calculated .the shutdown margin* and monitored the critical safety function status* trees to verify that the unit conditions were acceptable. Plant response was as expected and the unit stabilized at. hot shutdown. There were no radiation releases due to .
- this event, nor were there any personnel injuries. or contamination events.: . No cond_itiohs adverse to safety resulted from this event and the health and safety of the public .were not affected. .. . ..
.3.0 CAUSE The cause of the trip was inability to maintain RCS pressure due to loss of the Group C pressurizer proportional heaters. This loss of the proportional pressurizer heaters was due to age related failures of a Robicon controller unit circuit card.
4.0 IMMEDIATE CORRECTIVE ACTION(S)
Following the reactor trip at 2259 hours0.0261 days <br />0.628 hours <br />0.00374 weeks <br />8.595495e-4 months <br /> on February 19, 1997, control room operators initiated the appropriate emergency operating procedures. The reactor trip breakers were verified open and control rods were verified inserted into the core.
The Shift Technical Advisor calculated the shutdown margin and monitored the critical safety function status trees to verify that the unit conditions were acceptable. *
- Management conducted a post trip review meeting with the operating staff at 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on February 20, 1997.
NRG FORM :;ssA (4*95)
l NRC FORM 366A (4-95) e e.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LEA)
TEXT CONTINUATION FACILITY NAME (1) DOCKET LEA NUMBER (6) PAGE (3)
Surry Power Station, Unit 1 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 05000- 280 97 -003- 0 40F 5 TEXT (If more space is required, use additional copies of NRC Form 366A) (17) 5.0 ADDITIONAL CORRECTIVE ACTION($)
A Root Cause Evaluation was initiated to investigate the Pressurizer Heater C control circuitry failure. The Robicon controller module was sent to the vendor. The investigation by the vendor revealed age related failures of capacitors, zenor diodes, and resistors in a controller circuit card. The components were replaced, and the controller module was calibrated. . The Robicon controller module was re-installed and satisfactory post maintenance tests returned the proportional heaters to service.
Upon completion of repairs to the pressurizer heaters and the Post Trip review, Unit 1 was taken critical at 0724 hours0.00838 days <br />0.201 hours <br />0.0012 weeks <br />2.75482e-4 months <br /> and on iine at 1342 hours0.0155 days <br />0.373 hours <br />0.00222 weeks <br />5.10631e-4 months <br /> on February 22, 1997. Unit 1 was
. returned to 100% reactor power at 1353 hours0.0157 days <br />0.376 hours <br />0.00224 weeks <br />5.148165e-4 months <br /> on February 23, 1997.
It was determined that the trip of the RCP A was due to the failure of Pro-Star speed sensing relays {EIIS-AB-RLY} due to a manufacturing deficiency. The relay was replaced: Software problems in the computations being performed by the Pro-Star relays were discovered following the Unit 1 trip. The specific causes and corrective actions will be implemented by the corrective action program.
As part of the Root Cause Evaluation, the equipment problems which occurred were evaluated in accordance with the Maintenance Rule and it was determined that two Maintenance Rule Functional Failures occurred. The first was the Robicon heater controller failure and the second was the failure of the speed sensing relays. These are being addressed in ac.cordance with maintenance rule program requirements.
6.0 ACTIONS TO PREVENT RECURRENCE /
A detailed Reactor Trip Report and a Root Cause Evaluation is being performed for this*
event. The Pro-Star relay and the Robicon controller failures are being evaluated. Additional approved recommendations from the Root Cause Evaluation will be implemented in accordance with the corrective action program.
An evaluation of preventive maintenance on the* Robicon controllers is being conducted.
7.0 SIMILAR EVENTS None NRC FORM 366A (4-95)
- !FNRG FORM 366A (4-95) e eU.S. NUCLEAR REGULATORY COMMISSION
. LICENSEE EVENT REPORT (LER)
. TEXT CONTINUATION FACILITY NAME (1) DOCKET LEA NUMBER (6) PAGE (3)
Surry Power Station, Unit 1 YEAR I SEQUENTIAL NUMBER I REVISION NUMBER 05000- 280 97 -003- 0 50F5 TEXT (If more space is required, use additional copies of NRC Form 366A} (17) 8.0 MANUFACTURER Robicon Controller Unit:
Manufacturer - Robicon Model - Series 413 Pro-Star Relays:
Manufacturer - ABB Model with 1.6 version software NRG FORM 366A (4-95)