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| | issue date = 03/03/1989 | | | issue date = 03/03/1989 |
| | title = LER 89-005-00:on 890204,auto Start of Emergency Diesel Generators 1 & 3 Occurred Upon Loss of Transfer Bus F.Caused by 4,160-volt Supply Circuit Breaker Failure.Circuit Breaker Cleaned & Tested satisfactory.W/890303 Ltr | | | title = LER 89-005-00:on 890204,auto Start of Emergency Diesel Generators 1 & 3 Occurred Upon Loss of Transfer Bus F.Caused by 4,160-volt Supply Circuit Breaker Failure.Circuit Breaker Cleaned & Tested satisfactory.W/890303 Ltr |
| | author name = KANSLER M R | | | author name = Kansler M |
| | author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) | | | author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.) |
| | addressee name = | | | addressee name = |
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| {{#Wiki_filter:POW 28-06-01 NRC Form 366 SJI LICENSEE EVENT REPORT (LER) U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB. NO. 3150-0104 EXPIRES: 8/31/88 FACILITY NAME (11 PAGE (31 Surry Power Station. Unit 1 !DOCKET NUMBER 121 o I s I o I o I o I 'J ,~ In 1 I OF n I c; TITLE l*l Auto Start of #1 and #3 EDGs Upon The Loss Of 'F' Transfer Bus EVENT DATE (5) LER NUMBER (61 REPORT DATE 171 OTHER FACILITIES INVOLVED IBI MONTH DAY YEAR YEAR )l' see~~~~~AL t< | | {{#Wiki_filter:POW 28-06-01 NRC Form 366 - U.S. NUCLEAR REGULATORY COMMISSION 19-SJI APPROVED 0MB. NO. 3150-0104 LICENSEE EVENT REPORT (LER) EXPIRES: 8/31/88 FACILITY NAME (11 DOCKET NUMBER 121 PAGE (31 TITLE l*l Surry Power Station. Unit 1 !o I s I o I o I o I 'J ,~ In 1 OFI n I c; Auto Start of #1 and #3 EDGs Upon The Loss Of 'F' Transfer Bus EVENT DATE (5) LER NUMBER (61 REPORT DATE 171 OTHER FACILITIES INVOLVED IBI MONTH DAY YEAR YEAR )l' see~~~~~AL t< ~~~~~~ MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI 0!2 ol4 89 slg- olols-oloob ol38 l9 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Chock on* or more of th* folloV(ing) (111 OPERATING MODE (91 N 20.402(bl |
| MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI 0!2 ol4 89 slg-olols-oloob ol38 l9 OPERATING MODE (91 N THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Chock on* or more of th* folloV(ing) | | --- 20.405(cl |
| (111 20.402(bl 20.405(cl | | .~ 50,73(al(2JlivJ |
| .~ 50,73(al(2JlivJ | | ,__ 73.71(bl 20.406(el(1 Jlil 50.38(cl(1l |
| -,__ 20.406(el(1 Jlil 50.38(cl(1l 50.73lall21M
| | -- 50.73lall21M 73.71(cl 20.406(al(1 l(IIJ 50.38(cll21 50.73(al(21(viil OTHER (Spacify in Abstract 20.40li(al(1Jlilll 20.406(al(1Jllvl 20.40lilall1 IM 50.73(al(2J(IJ 60.73(all2Jliil 60.73(al(2111ill 50.73(al(21(vilil(AI 50.73(al (21 (vliil (Bl 50.73(all211xl below and in TtJxr. NRC Form 366A) |
| ---,--20.406(al(1 l(IIJ 50.38(cll21 50.73(al(21(viil
| | LICENSEE CONTACT FOR THIS LER (121 NAME TELEPHONE NUMBER AREA CODE M. R. Kansler, Station Manager COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 MANUFAC- MANUFAC-CAUSE SYSTEM COMPONENT TURER TURER D F I A IB IK I R 11 n I n I c; V I I I I I I I X I I L IM 10 IN KI OI 2 I 0 N I I I I I I I SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR EXPECTED SUBMISSION DATE (151 hABSTRACT (Limit to 1400 sptJctJs, i.tJ., approxim*ta/y fiftetJn sing/e-spact1 typ11written lines} (18) |
| ---,__ 20.40li(al(1Jlilll 50.73(al(2J(IJ 50.73(al(21(vilil(AI
| | YES (If yes, complot* EXPECTED SUBMISSION DATE) 1--.l......-------------~..L.---------~-------'--.......,__ |
| --20.406(al(1Jllvl 60.73(all2Jliil 50.73(al (21 (vliil (Bl -,--20.40lilall1 IM 60.73(al(2111ill 50.73(all211xl LICENSEE CONTACT FOR THIS LER (121 73.71(bl 73.71(cl OTHER (Spacify in Abstract below and in TtJxr. NRC Form 366A) NAME TELEPHONE NUMBER AREA CODE M. R. Kansler, Station Manager COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 CAUSE SYSTEM COMPONENT TURER TURER D F I A IB IK I R 11 n I n I c; V I I I I I I I X I I L IM 10 IN KI OI 2 I 0 N I I I I I I I SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR EXPECTED SUBMISSION h DATE (151 YES (If yes, complot* EXPECTED SUBMISSION DATE) ND I I I 1--.l......-------------~..L.---------~-------'--.......,__
| | ND I I I On February 4, 1989, at 2345 hours, with Units 1 and 2 in cold shutdown, the #1 and #3 Emergency Diesel Generators auto-started and loaded onto the lH and 2J emergency busses respectively. This event is reported pursuant to 10 CFR 50.73(a)(2)(iv). The diesels started due to the de-energization of the lH and 2J emergency busses due to the failure of a 4160 volt supply circuit breaker. The running Residual Heat Removal (RHR) pump de-energized during the event. The redundant RHR pump was started approximately three minutes later to supply RHR flow. The failed circuit breaker was cleaned and tested satisfactory. Safety-related 4160 volt supply circuit breaker operator mechanisms will be refurbished. The preventive maintenance program for 4160 volt circuit breakers is being evaluated. |
| ABSTRACT (Limit to 1400 sptJctJs, i.tJ., approxim*ta/y fiftetJn sing/e-spact1 typ11written lines} (18) NRC Farm 366 (9-831 On February 4, 1989, at 2345 hours, with Units 1 and 2 in cold shutdown, the #1 and #3 Emergency Diesel Generators auto-started and loaded onto the lH and 2J emergency busses respectively.
| | NRC Farm 366 (9-831 |
| This event is reported pursuant to 10 CFR 50.73(a)(2)(iv). | |
| The diesels started due to the de-energization of the lH and 2J emergency busses due to the failure of a 4160 volt supply circuit breaker. The running Residual Heat Removal (RHR) pump de-energized during the event. The redundant RHR pump was started approximately three minutes later to supply RHR flow. The failed circuit breaker was cleaned and tested satisfactory. | |
| Safety-related 4160 volt supply circuit breaker operator mechanisms will be refurbished. | |
| The preventive maintenance program for 4160 volt circuit breakers is being evaluated. | |
| NRC Form 36r.A 19-.<?3) *\ FACILITY NAME (1) LICENSE-ENT REPORT (LERI TEXT CONTINU-ON DOCKET NUMBER (2) .!:'OW :.::'.8 06-01 U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMS NO. 3150-0104 EXPIRES: 8/31 /88 LER NUMBER (61 PAGE (3) Surrv Power Station, Unit 1 TEXT /ff mom ,pace is n,quimd, u/111 additioMI NRC Form 366A 's/ (17) NRC FORM 366A 19-83i 1.0 Description of the Event On February 4, 1989 at 2345 hours, with Units 1 and 2 in cold shutdown, operators were removing the 'C' Reserve Station Service Transformer (RSST) {EIIS-XPT} | |
| from service in preparation for a special test. To power the electrical busses supplied from the 'C' RSST, operators closed the applicable circuit breakers {EIIS-BKR}
| |
| to establish backfeed from the main transformer and the station service transformer (Figure 1). In accordance with the governing procedure, the backfeed lineup was established and the 'C ' RSST output breaker (15Fl -Figure 1) was opened. When 15Fl was opened the lH and 2J emergency busses and the lC and 2C station service busses de-energized.
| |
| Upon de-energization of the above busses, circuit breakers 15C2, 25Cl, 25C2, 15H8, and 25J8 tripped open on undervoltage.
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| The running residual heat removal (RHR) {EIIS-BP}
| |
| pump and component cooling (CC) water pump {EIIS-P} on Unit two tripped. The #1 and #3 Emergency Diesel Generators (EDGs) {EIIS-DG}
| |
| auto-started and loaded onto the dead lH and 2J emergency busses, respectively.
| |
| The EDGs restored power to the components powered from these emergency busses with the exception of the RHR and cc system pumps for which the "stub bus" supply breaker must be manually reset. Other problems that were associated with the event are as follows: -The backup service air compressor
| |
| {EIIS-CMP}
| |
| failed to auto start when power was lost to the running service air compressor.
| |
| Station instrument air was being supplied from service air. Instrument air header pressure consequently decreased causing the auxiliary ventilation system to realign to its safety injection configuration.
| |
| -The memory and setpoints for the process vent and ventilation vent radiation monitors were lost when power was lost to these instruments.
| |
| -The sample pumps for both units' containment particulate and gas radiation monitors tripped when power was lost to the 1 and 2 'C' station service busses. *U.S. GPO. 1988-520-58~
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| llOtl7l1 NRC Form 366A 19-<'3) LICENSEE-NT REPORT (LERI TEXT CONTINUA.N POW 28-06-01 U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104
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| *, a-;;rnlrnw:i'e"T,ii-------------...,-;=;-;;;--::::-;:::::;:;:-;::;-----,--------=EX.::..Pl~RE::S:..:::
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| 8~/3~1188:__.:_
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| ___ 1 I FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3) Surry Power Station, Unit 1 0 1 5 1°1°1°12la lo al 9 o lo Is ol o ol 3oF ols TEXT /If man, space is requiffJd, u.,, additional NRC Form 366A 's/ (17) NRC FORM 388A (9-83) This event is being reported as an unplanned actuation of engineered safety features (EDG starts and auxiliary ventilation realignment).
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| ===2.0 Safety=== | | .!:'OW :.::'.8 06-01 NRC Form 36r.A U.S. NUCLEAR REGULATORY COMMISSION 19-.<?3) |
| Consequences and Implications The consequences of this event were minimal because the EDGs auto-started and loaded as designed to | | LICENSE-ENT REPORT (LERI TEXT CONTINU-ON APPROVED OMS NO. 3150-0104 EXPIRES: 8/31 /88 |
| * provide power to the affected emergency busses. Although RHR flow to Unit 2 was lost when the 2J bus de-energized, the redundant pump was started approximately three minutes later to provide the required RHR flow. The RCS temperature increased less than two degrees Fahrenheit due to the loss of the running RHR pump; therefore, the health and safety of the public were not affected by the event. 3.0 Cause The cause of the event was the failure of 4160 volt circuit breaker 25C2 (Figure 1). Breaker 25C2 indicated fully closed, but its main contacts had stopped approximately two inches from full closure. Since 25C2 was not closed (but indicated closed), busses lH, 2J, lC, and 2C de-energized when breaker 15Fl was opened. The failure of 25C2 was due to an accumulation of dust and dirt in its closing mechanism. | | *\ FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (61 PAGE (3) |
| The preventive maintenance procedure used to clean the bre.aker did not include steps for cleaning the closing mechanism. | | Surrv Power Station, Unit 1 TEXT /ff mom ,pace is n,quimd, u/111 additioMI NRC Form 366A 's/ (17) 1.0 Description of the Event On February 4, 1989 at 2345 hours, with Units 1 and 2 in cold shutdown, operators were removing the 'C' Reserve Station Service Transformer (RSST) {EIIS-XPT} |
| | from service in preparation for a special test. To power the electrical busses supplied from the 'C' RSST, operators closed the applicable circuit breakers |
| | {EIIS-BKR} to establish backfeed from the main transformer and the station service transformer (Figure 1). In accordance with the governing procedure, the backfeed lineup was established and the 'C ' RSST output breaker (15Fl - Figure 1) was opened. When 15Fl was opened the lH and 2J emergency busses and the lC and 2C station service busses de-energized. Upon de-energization of the above busses, circuit breakers 15C2, 25Cl, 25C2, 15H8, and 25J8 tripped open on undervoltage. The running residual heat removal (RHR) |
| | {EIIS-BP} pump and component cooling (CC) water pump |
| | {EIIS-P} on Unit two tripped. The #1 and #3 Emergency Diesel Generators (EDGs) {EIIS-DG} auto-started and loaded onto the dead lH and 2J emergency busses, respectively. The EDGs restored power to the components powered from these emergency busses with the exception of the RHR and cc system pumps for which the "stub bus" supply breaker must be manually reset. |
| | Other problems that were associated with the event are as follows: |
| | - The backup service air compressor {EIIS-CMP} |
| | failed to auto start when power was lost to the running service air compressor. Station instrument air was being supplied from service air. Instrument air header pressure consequently decreased causing the auxiliary ventilation system to realign to its safety injection configuration. |
| | - The memory and setpoints for the process vent and ventilation vent radiation monitors were lost when power was lost to these instruments. |
| | - The sample pumps for both units' containment particulate and gas radiation monitors tripped when power was lost to the 1 and 2 'C' station service busses. |
| | *U.S. GPO. 1988-520-58~ llOtl7l1 NRC FORM 366A 19-83i |
| | |
| | POW 28-06-01 NRC Form 366A 19-<'3) U.S. NUCLEAR REGULATORY COMMISSION LICENSEE-NT REPORT (LERI TEXT CONTINUA.N APPROVED 0MB NO. 3150-0104 |
| | *, a - ; ; r n l r n w : i ' e " T , i i - - - - - - - - - - - - - . . . , - ; = ; - ; ; ; - - : : : : - ; : : : : : ; : ; : - ; : : ; - - - - - , - - - - - - - - = E X . : : . . P l ~ R E : : S : . . : : : |
| | I FACILITY NAME (1) DOCKET NUMBER (2) |
| | LER NUMBER (6) 8~/3~1188:__.:__ _ _ |
| | PAGE (3) 1 Surry Power Station, Unit 1 0 TEXT /If man, space is requiffJd, u.,, additional NRC Form 366A 's/ (17) 15 1°1°1°12la lo al 9 o lo Is ol o ol 3oF ols This event is being reported as an unplanned actuation of engineered safety features (EDG starts and auxiliary ventilation realignment). |
| | 2.0 Safety Consequences and Implications The consequences of this event were minimal because the EDGs auto-started and loaded as designed to |
| | * provide power to the affected emergency busses. |
| | Although RHR flow to Unit 2 was lost when the 2J bus de-energized, the redundant pump was started approximately three minutes later to provide the required RHR flow. The RCS temperature increased less than two degrees Fahrenheit due to the loss of the running RHR pump; therefore, the health and safety of the public were not affected by the event. |
| | 3.0 Cause The cause of the event was the failure of 4160 volt circuit breaker 25C2 (Figure 1). Breaker 25C2 indicated fully closed, but its main contacts had stopped approximately two inches from full closure. |
| | Since 25C2 was not closed (but indicated closed), |
| | busses lH, 2J, lC, and 2C de-energized when breaker 15Fl was opened. |
| | The failure of 25C2 was due to an accumulation of dust and dirt in its closing mechanism. The preventive maintenance procedure used to clean the bre.aker did not include steps for cleaning the closing mechanism. |
| The backup service air compressor failed to start due to a low oil pressure signal. The cause of the low oil pressure signal is being investigated. | | The backup service air compressor failed to start due to a low oil pressure signal. The cause of the low oil pressure signal is being investigated. |
| The auxiliary ventilation system realigned to its safety injection configuration as designed on low air pressure. | | The auxiliary ventilation system realigned to its safety injection configuration as designed on low air pressure. |
| The loss of memory and setpoints to the process vent and ventilation vent radiation monitors was due to the failure of the instruments' backup battery supply. The cause of the backup battery supply failure is under investigation. | | The loss of memory and setpoints to the process vent and ventilation vent radiation monitors was due to the failure of the instruments' backup battery supply. |
| *u.s. GPO, 1988-520-589,00070 NRC Form 360::A 19-83) FACILITY NAME (1) LICENSE~ENT REPORT (LER) TEXT CONTINU-ON DOCKET NUMBER (2) U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31 /88 LER NUMBER (6) PAGE (3) Surry Power Station, Unit 1 o Is Io Io I o I 2 la lo a I 9 olo Is o I o o I q oF o Is' TEXT (ff more space is required, Ullil additiafllJ! | | The cause of the backup battery supply failure is under investigation. |
| NRC Fonn Jti6A 's) (17) NRC FORM 366A 19-83) 4.0 Immediate Corrective Actions Approximately three minutes after the Unit two 'B' RHR pump had tripped, operators started the 'A' pump to provide RHR flow in accordance with the appropriate abnormal procedure. | | NRC FORM 388A *u.s. GPO, 1988-520-589,00070 (9-83) |
| The reactor coolant system (RCS) {EIIS-AB} | | |
| temperature had increased by less than two degrees Fahrenheit to approximately 96 degrees F. At 2349 hours operators reclosed the "stub bus" supply breaker to the Unit 2 J bus RHR and cc pumps. At 2356 hours operators reclosed the "stub bus" supply breaker for the Unit 1 H bus RHR and CC pumps. By 0016 hours (2-5-89) breakers 15Fl, 15Cl, and 25Cl had been reclosed restoring power to both units' 'C' station service busses, and normal power was restored to the affected emergency busses. 5.0 Additional Corrective Action(s) | | NRC Form 360::A 19-83) U.S. NUCLEAR REGULATORY COMMISSION LICENSE~ENT REPORT (LER) TEXT CONTINU-ON APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31 /88 FACILITY NAME (1) |
| | DOCKET NUMBER (2) |
| | LER NUMBER (6) PAGE (3) |
| | Surry Power Station, Unit 1 o Is Io Io I o I 2 la lo a I 9 olo Is o I o o Iq oF o Is' TEXT (ff more space is required, Ullil additiafllJ! NRC Fonn Jti6A 's) (17) 4.0 Immediate Corrective Actions Approximately three minutes after the Unit two 'B' RHR pump had tripped, operators started the 'A' pump to provide RHR flow in accordance with the appropriate abnormal procedure. The reactor coolant system (RCS) |
| | {EIIS-AB} temperature had increased by less than two degrees Fahrenheit to approximately 96 degrees F. At 2349 hours operators reclosed the "stub bus" supply breaker to the Unit 2 J bus RHR and cc pumps. At 2356 hours operators reclosed the "stub bus" supply breaker for the Unit 1 H bus RHR and CC pumps. By 0016 hours (2-5-89) breakers 15Fl, 15Cl, and 25Cl had been reclosed restoring power to both units' 'C' station service busses, and normal power was restored to the affected emergency busses. |
| | 5.0 Additional Corrective Action(s) |
| The 25C2 breaker was cleaned and tested satisfactorily. | | The 25C2 breaker was cleaned and tested satisfactorily. |
| Operators reset the low oil pressure trip on the backup service air compressor and it was started satisfactorily. | | Operators reset the low oil pressure trip on the backup service air compressor and it was started satisfactorily. |
| Operators realigned the auxiliary ventilation system to its normal configuration after instrument air pressure had been returned to normal. The sample pump for each unit's containment particulate and gas radiation monitor was restarted. | | Operators realigned the auxiliary ventilation system to its normal configuration after instrument air pressure had been returned to normal. |
| | The sample pump for each unit's containment particulate and gas radiation monitor was restarted. |
| Instument technicians restored the setpoints to the process vent and ventilation vent radiation monitors. | | Instument technicians restored the setpoints to the process vent and ventilation vent radiation monitors. |
| 6.0 Action(s) | | 6.0 Action(s) Taken to Prevent Recurrence Prior to the restart of either unit, safety related 4160 volt feeder breaker operator mechanisms will be refurbished. The preventive maintenance program for 4160 volt breakers is being evaluated. |
| Taken to Prevent Recurrence Prior to the restart of either unit, safety related 4160 volt feeder breaker operator mechanisms will be refurbished. | | NRC FORM 366A 19-83) |
| The preventive maintenance program for 4160 volt breakers is being evaluated. | | *u.s. GPO: 1988-520-58':) Ll0070 |
| *u.s. GPO: 1988-520-58':) | | |
| Ll0070 NRC Form 366A 19-oJI FACILITY NAME (1) LICENSE.ENT REPORT (LERI TEXT CONTINU-ON DOCKET NUMBER (21 U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31 /88 LER NUMBER (6) PAGE (31 YEAR rrr SEQUENTIAL
| | NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION 19-oJI LICENSE.ENT REPORT (LERI TEXT CONTINU-ON APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31 /88 FACILITY NAME (1) DOCKET NUMBER (21 LER NUMBER (6) PAGE (31 YEAR rrr SEQUENTIAL NUMBER |
| [ft REVISION NUMBER NUMBER Surry Power Station, Unit 1 01s101010121s10 slg-olols-olo ols°Fols TEXT /If mom space is required, U5" additional NRC Form 366A's) (171 Troubleshooting on the process vent and ventilation vent radiation monitors' battery backup system will be performed to identify the failure mode. The cause of the oil pressure signal in the backup service air compressor is being investigated. | | [ft REVISION NUMBER Surry Power Station, Unit 1 01s101010121s10 slg-olols-olo ols°Fols TEXT /If mom space is required, U5" additional NRC Form 366A's) (171 Troubleshooting on the process vent and ventilation vent radiation monitors' battery backup system will be performed to identify the failure mode. |
| Instructions will be added to the Abnormal Procedures for loss of station service bus voltage to direct operators to restart the containment particulate and gas radiation monitor sample pumps after power is restored if power is lost to the 'C' station service bus. 7.0 Similar Events None 8.0 Manufacturer/Model Numbers Circuit Breaker 25C2 Process Vent and Ventilation Vent Radiation Monitors Service Air Compressor ITE Circuit Breaker Company Model SHK-350 Kaman Sciences Corporation Model KMG-HRN & HRH Atlas Copco Model ZT 3 A NRC FORM 3BBA (9-831 *u.s. GPO, 1988-520-589100070 | | The cause of the oil pressure signal in the backup service air compressor is being investigated. |
| * e FIGURE 1 e Surry Power Station Docket # 05000280 LER # 1-89-005 SIMPLIFIED ELECTRICAL SCHEMATIC BACKFEED LINEUP GRID UNIT 2 GENERATOR___.
| | Instructions will be added to the Abnormal Procedures for loss of station service bus voltage to direct operators to restart the containment particulate and gas radiation monitor sample pumps after power is restored if power is lost to the 'C' station service bus. |
| OUTPUT --_. BREAKERS MOAB (CLOSED) ...--'-L_, 500 KV M!'~~--~ XFRMR~ 'C' GRID 15C2 15C1 UNIT 1 'C' STATION SERVICE BUS 25J8 25J3 2J EMERG8'JCY BUS RESERVE STATION SERVICE 1RNSFRMR 25C1 25C2 UNIT 2 'C' STATION SERVICE BUS 15H8 15H3 1H EMERGENCY BUS D OPEN CIRCUIT BREAKER I CLOSED CIRCUIT BREAKER -----ii | | 7.0 Similar Events None 8.0 Manufacturer/Model Numbers Circuit Breaker 25C2 ITE Circuit Breaker Company Model SHK-350 Process Vent and Kaman Sciences Corporation Ventilation Vent Model KMG-HRN & HRH Radiation Monitors Service Air Compressor Atlas Copco Model ZT 3 A NRC FORM 3BBA |
| * 22 KV 22 KV *4160 V GENERATOR DISCONNECT
| | *u.s. GPO, 1988-520-589100070 (9-831 |
| \ e VIRGl!'4IA ELECTRIC ANO .POWER COMPANY Surry P_, Station March 3, 1989 U.S. Nuclear Regulatory Commission Docmnent Control Desk 016 Phillips Building Washington, D.C. 20555 Gentlemen: | | |
| P. 0. Box 316 Surry, Virginia 23883 Serial No.: Docket Nos. : License No: 89-006 50-280 DPR-32 Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report for Unit 1. REPORT NUMBER 89-005-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be reviewed by Safety Evaluation and Control. Very truly yours, Enclosure I I cc: Regional Administrator Suite 2900 101 Marietta Street, NW Atlanta, Georgia 30323 ,f&r\-z,.
| | e FIGURE 1 e Surry Power Station Docket # 05000280 LER # 1-89-005 SIMPLIFIED ELECTRICAL SCHEMATIC BACKFEED LINEUP GRID MOAB (CLOSED) |
| I \}} | | UNIT 2 GENERATOR___. |
| | OUTPUT --_. ...-- '-L_, 500 KV BREAKERS M!'~~--~ |
| | XFRMR~ |
| | GRID |
| | 'C' -----ii |
| | * 22 KV RESERVE STATION SERVICE 22 KV GENERATOR 1RNSFRMR DISCONNECT 15C2 15C1 25C1 25C2 *4160 V UNIT 1 UNIT 2 |
| | 'C' STATION 'C' STATION SERVICE BUS SERVICE BUS 25J8 15H8 25J3 15H3 2J 1H EMERG8'JCY EMERGENCY BUS BUS D OPEN CIRCUIT BREAKER I CLOSED CIRCUIT BREAKER |
| | |
| | \ |
| | e VIRGl!'4IA ELECTRIC ANO .POWER COMPANY Surry P_, Station P. 0. Box 316 Surry, Virginia 23883 March 3, 1989 U.S. Nuclear Regulatory Commission Serial No.: 89-006 Docmnent Control Desk Docket Nos. : 50-280 016 Phillips Building License No: DPR-32 Washington, D.C. 20555 Gentlemen: |
| | Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report for Unit 1. |
| | REPORT NUMBER 89-005-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be reviewed by Safety Evaluation and Control. |
| | I Very truly yours, I Enclosure cc: Regional Administrator Suite 2900 101 Marietta Street, NW Atlanta, Georgia 30323 |
| | ,f&r\-z,. |
| | I \}} |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket ML18153A2201998-02-0606 February 1998 LER 98-001-00:on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was submitted.W/980206 Ltr ML18153A2071998-01-13013 January 1998 LER 97-012-01:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors ML18153A2101998-01-13013 January 1998 LER 97-009-01:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status ML18153A1911997-11-26026 November 1997 LER 97-011-00:on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket ML18153A2201998-02-0606 February 1998 LER 98-001-00:on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was submitted.W/980206 Ltr ML18153A2071998-01-13013 January 1998 LER 97-012-01:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors ML18153A2101998-01-13013 January 1998 LER 97-009-01:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status ML18153A1911997-11-26026 November 1997 LER 97-011-00:on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage. ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With 990115 Ltr ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un. ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With 981214 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With 981111 Ltr ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With 981012 Ltr ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2.W/980807 Ltr ML18152B7621998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Surry Power Station,Units 1 & 2.W/980707 Ltr ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML18153A3141998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Surry Power Station,Units 1 & 2.W/980610 ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B8161998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Surry Power Station Units 1 & 2.W/980508 Ltr ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML20217P9941998-04-0707 April 1998 Safety Evaluation Granting Licensee Third 10-yr Inservice Insp Program Relief Requests SR-018 - Sr-024 ML18153A2951998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sps,Units 1 & 2.W/ 980408 Ltr ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket 1999-09-30
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POW 28-06-01 NRC Form 366 - U.S. NUCLEAR REGULATORY COMMISSION 19-SJI APPROVED 0MB. NO. 3150-0104 LICENSEE EVENT REPORT (LER) EXPIRES: 8/31/88 FACILITY NAME (11 DOCKET NUMBER 121 PAGE (31 TITLE l*l Surry Power Station. Unit 1 !o I s I o I o I o I 'J ,~ In 1 OFI n I c; Auto Start of #1 and #3 EDGs Upon The Loss Of 'F' Transfer Bus EVENT DATE (5) LER NUMBER (61 REPORT DATE 171 OTHER FACILITIES INVOLVED IBI MONTH DAY YEAR YEAR )l' see~~~~~AL t< ~~~~~~ MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI 0!2 ol4 89 slg- olols-oloob ol38 l9 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Chock on* or more of th* folloV(ing) (111 OPERATING MODE (91 N 20.402(bl
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-- 50.73lall21M 73.71(cl 20.406(al(1 l(IIJ 50.38(cll21 50.73(al(21(viil OTHER (Spacify in Abstract 20.40li(al(1Jlilll 20.406(al(1Jllvl 20.40lilall1 IM 50.73(al(2J(IJ 60.73(all2Jliil 60.73(al(2111ill 50.73(al(21(vilil(AI 50.73(al (21 (vliil (Bl 50.73(all211xl below and in TtJxr. NRC Form 366A)
LICENSEE CONTACT FOR THIS LER (121 NAME TELEPHONE NUMBER AREA CODE M. R. Kansler, Station Manager COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (131 MANUFAC- MANUFAC-CAUSE SYSTEM COMPONENT TURER TURER D F I A IB IK I R 11 n I n I c; V I I I I I I I X I I L IM 10 IN KI OI 2 I 0 N I I I I I I I SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR EXPECTED SUBMISSION DATE (151 hABSTRACT (Limit to 1400 sptJctJs, i.tJ., approxim*ta/y fiftetJn sing/e-spact1 typ11written lines} (18)
YES (If yes, complot* EXPECTED SUBMISSION DATE) 1--.l......-------------~..L.---------~-------'--.......,__
ND I I I On February 4, 1989, at 2345 hours0.0271 days <br />0.651 hours <br />0.00388 weeks <br />8.922725e-4 months <br />, with Units 1 and 2 in cold shutdown, the #1 and #3 Emergency Diesel Generators auto-started and loaded onto the lH and 2J emergency busses respectively. This event is reported pursuant to 10 CFR 50.73(a)(2)(iv). The diesels started due to the de-energization of the lH and 2J emergency busses due to the failure of a 4160 volt supply circuit breaker. The running Residual Heat Removal (RHR) pump de-energized during the event. The redundant RHR pump was started approximately three minutes later to supply RHR flow. The failed circuit breaker was cleaned and tested satisfactory. Safety-related 4160 volt supply circuit breaker operator mechanisms will be refurbished. The preventive maintenance program for 4160 volt circuit breakers is being evaluated.
NRC Farm 366 (9-831
.!:'OW :.::'.8 06-01 NRC Form 36r.A U.S. NUCLEAR REGULATORY COMMISSION 19-.<?3)
LICENSE-ENT REPORT (LERI TEXT CONTINU-ON APPROVED OMS NO. 3150-0104 EXPIRES: 8/31 /88
- \ FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (61 PAGE (3)
Surrv Power Station, Unit 1 TEXT /ff mom ,pace is n,quimd, u/111 additioMI NRC Form 366A 's/ (17) 1.0 Description of the Event On February 4, 1989 at 2345 hours0.0271 days <br />0.651 hours <br />0.00388 weeks <br />8.922725e-4 months <br />, with Units 1 and 2 in cold shutdown, operators were removing the 'C' Reserve Station Service Transformer (RSST) {EIIS-XPT}
from service in preparation for a special test. To power the electrical busses supplied from the 'C' RSST, operators closed the applicable circuit breakers
{EIIS-BKR} to establish backfeed from the main transformer and the station service transformer (Figure 1). In accordance with the governing procedure, the backfeed lineup was established and the 'C ' RSST output breaker (15Fl - Figure 1) was opened. When 15Fl was opened the lH and 2J emergency busses and the lC and 2C station service busses de-energized. Upon de-energization of the above busses, circuit breakers 15C2, 25Cl, 25C2, 15H8, and 25J8 tripped open on undervoltage. The running residual heat removal (RHR)
{EIIS-BP} pump and component cooling (CC) water pump
{EIIS-P} on Unit two tripped. The #1 and #3 Emergency Diesel Generators (EDGs) {EIIS-DG} auto-started and loaded onto the dead lH and 2J emergency busses, respectively. The EDGs restored power to the components powered from these emergency busses with the exception of the RHR and cc system pumps for which the "stub bus" supply breaker must be manually reset.
Other problems that were associated with the event are as follows:
- The backup service air compressor {EIIS-CMP}
failed to auto start when power was lost to the running service air compressor. Station instrument air was being supplied from service air. Instrument air header pressure consequently decreased causing the auxiliary ventilation system to realign to its safety injection configuration.
- The memory and setpoints for the process vent and ventilation vent radiation monitors were lost when power was lost to these instruments.
- The sample pumps for both units' containment particulate and gas radiation monitors tripped when power was lost to the 1 and 2 'C' station service busses.
POW 28-06-01 NRC Form 366A 19-<'3) U.S. NUCLEAR REGULATORY COMMISSION LICENSEE-NT REPORT (LERI TEXT CONTINUA.N APPROVED 0MB NO. 3150-0104
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I FACILITY NAME (1) DOCKET NUMBER (2)
LER NUMBER (6) 8~/3~1188:__.:__ _ _
PAGE (3) 1 Surry Power Station, Unit 1 0 TEXT /If man, space is requiffJd, u.,, additional NRC Form 366A 's/ (17) 15 1°1°1°12la lo al 9 o lo Is ol o ol 3oF ols This event is being reported as an unplanned actuation of engineered safety features (EDG starts and auxiliary ventilation realignment).
2.0 Safety Consequences and Implications The consequences of this event were minimal because the EDGs auto-started and loaded as designed to
- provide power to the affected emergency busses.
Although RHR flow to Unit 2 was lost when the 2J bus de-energized, the redundant pump was started approximately three minutes later to provide the required RHR flow. The RCS temperature increased less than two degrees Fahrenheit due to the loss of the running RHR pump; therefore, the health and safety of the public were not affected by the event.
3.0 Cause The cause of the event was the failure of 4160 volt circuit breaker 25C2 (Figure 1). Breaker 25C2 indicated fully closed, but its main contacts had stopped approximately two inches from full closure.
Since 25C2 was not closed (but indicated closed),
busses lH, 2J, lC, and 2C de-energized when breaker 15Fl was opened.
The failure of 25C2 was due to an accumulation of dust and dirt in its closing mechanism. The preventive maintenance procedure used to clean the bre.aker did not include steps for cleaning the closing mechanism.
The backup service air compressor failed to start due to a low oil pressure signal. The cause of the low oil pressure signal is being investigated.
The auxiliary ventilation system realigned to its safety injection configuration as designed on low air pressure.
The loss of memory and setpoints to the process vent and ventilation vent radiation monitors was due to the failure of the instruments' backup battery supply.
The cause of the backup battery supply failure is under investigation.
NRC FORM 388A *u.s. GPO, 1988-520-589,00070 (9-83)
NRC Form 360::A 19-83) U.S. NUCLEAR REGULATORY COMMISSION LICENSE~ENT REPORT (LER) TEXT CONTINU-ON APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31 /88 FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6) PAGE (3)
Surry Power Station, Unit 1 o Is Io Io I o I 2 la lo a I 9 olo Is o I o o Iq oF o Is' TEXT (ff more space is required, Ullil additiafllJ! NRC Fonn Jti6A 's) (17) 4.0 Immediate Corrective Actions Approximately three minutes after the Unit two 'B' RHR pump had tripped, operators started the 'A' pump to provide RHR flow in accordance with the appropriate abnormal procedure. The reactor coolant system (RCS)
{EIIS-AB} temperature had increased by less than two degrees Fahrenheit to approximately 96 degrees F. At 2349 hours0.0272 days <br />0.653 hours <br />0.00388 weeks <br />8.937945e-4 months <br /> operators reclosed the "stub bus" supply breaker to the Unit 2 J bus RHR and cc pumps. At 2356 hours0.0273 days <br />0.654 hours <br />0.0039 weeks <br />8.96458e-4 months <br /> operators reclosed the "stub bus" supply breaker for the Unit 1 H bus RHR and CC pumps. By 0016 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> (2-5-89) breakers 15Fl, 15Cl, and 25Cl had been reclosed restoring power to both units' 'C' station service busses, and normal power was restored to the affected emergency busses.
5.0 Additional Corrective Action(s)
The 25C2 breaker was cleaned and tested satisfactorily.
Operators reset the low oil pressure trip on the backup service air compressor and it was started satisfactorily.
Operators realigned the auxiliary ventilation system to its normal configuration after instrument air pressure had been returned to normal.
The sample pump for each unit's containment particulate and gas radiation monitor was restarted.
Instument technicians restored the setpoints to the process vent and ventilation vent radiation monitors.
6.0 Action(s) Taken to Prevent Recurrence Prior to the restart of either unit, safety related 4160 volt feeder breaker operator mechanisms will be refurbished. The preventive maintenance program for 4160 volt breakers is being evaluated.
NRC FORM 366A 19-83)
- u.s. GPO: 1988-520-58':) Ll0070
NRC Form 366A U.S. NUCLEAR REGULATORY COMMISSION 19-oJI LICENSE.ENT REPORT (LERI TEXT CONTINU-ON APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31 /88 FACILITY NAME (1) DOCKET NUMBER (21 LER NUMBER (6) PAGE (31 YEAR rrr SEQUENTIAL NUMBER
[ft REVISION NUMBER Surry Power Station, Unit 1 01s101010121s10 slg-olols-olo ols°Fols TEXT /If mom space is required, U5" additional NRC Form 366A's) (171 Troubleshooting on the process vent and ventilation vent radiation monitors' battery backup system will be performed to identify the failure mode.
The cause of the oil pressure signal in the backup service air compressor is being investigated.
Instructions will be added to the Abnormal Procedures for loss of station service bus voltage to direct operators to restart the containment particulate and gas radiation monitor sample pumps after power is restored if power is lost to the 'C' station service bus.
7.0 Similar Events None 8.0 Manufacturer/Model Numbers Circuit Breaker 25C2 ITE Circuit Breaker Company Model SHK-350 Process Vent and Kaman Sciences Corporation Ventilation Vent Model KMG-HRN & HRH Radiation Monitors Service Air Compressor Atlas Copco Model ZT 3 A NRC FORM 3BBA
- u.s. GPO, 1988-520-589100070 (9-831
e FIGURE 1 e Surry Power Station Docket # 05000280 LER # 1-89-005 SIMPLIFIED ELECTRICAL SCHEMATIC BACKFEED LINEUP GRID MOAB (CLOSED)
UNIT 2 GENERATOR___.
OUTPUT --_. ...-- '-L_, 500 KV BREAKERS M!'~~--~
XFRMR~
GRID
'C' -----ii
- 22 KV RESERVE STATION SERVICE 22 KV GENERATOR 1RNSFRMR DISCONNECT 15C2 15C1 25C1 25C2 *4160 V UNIT 1 UNIT 2
'C' STATION 'C' STATION SERVICE BUS SERVICE BUS 25J8 15H8 25J3 15H3 2J 1H EMERG8'JCY EMERGENCY BUS BUS D OPEN CIRCUIT BREAKER I CLOSED CIRCUIT BREAKER
\
e VIRGl!'4IA ELECTRIC ANO .POWER COMPANY Surry P_, Station P. 0. Box 316 Surry, Virginia 23883 March 3, 1989 U.S. Nuclear Regulatory Commission Serial No.: 89-006 Docmnent Control Desk Docket Nos. : 50-280 016 Phillips Building License No: DPR-32 Washington, D.C. 20555 Gentlemen:
Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report for Unit 1.
REPORT NUMBER 89-005-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be reviewed by Safety Evaluation and Control.
I Very truly yours, I Enclosure cc: Regional Administrator Suite 2900 101 Marietta Street, NW Atlanta, Georgia 30323
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