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Category:Letter
MONTHYEARIR 05000277/20244012024-10-17017 October 2024 Security Baseline Inspection Report 05000277/2024401 and 05000278/2024401 (Cover Letter Only) RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24284A2842024-10-10010 October 2024 (Wcgs), Revision of One Form That Implements the Radiological Emergency Response Plan (RERP) ML24281A1012024-10-0707 October 2024 Senior Reactor and Reactor Operator Initial License Examinations ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification ML24221A2582024-09-0606 September 2024 Response to Request for Re-Engagement Regarding the Subsequent License Renewal Environmental Review for Peach Bottom Atomic Power Station, Units 2 and 3 05000277/LER-2024-003, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum2024-09-0505 September 2024 Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum IR 05000277/20240022024-09-0404 September 2024 Reissued Integrated Inspection Report 05000277/2024002 and 05000278/2024002 IR 05000277/20240052024-08-29029 August 2024 Updated Inspection Plan for Peach Bottom Atomic Power Station, Units 2 and 3 (Report 05000277/2024005 and 05000278/2024005) IR 05000277/20240102024-08-23023 August 2024 Fire Protection Team Inspection Report 05000277/2024010 and 05000278/2024010 ML24235A0342024-08-23023 August 2024 U.S. Nuclear Regulatory Commission’S Analysis of Constellation Energy Generation’S Decommissioning Funding Status Report ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 ML24227A5492024-08-14014 August 2024 Integrated Inspection Report 05000277/2024002 and 05000278/2024002 IR 05000482/20240052024-08-14014 August 2024 Updated Inspection Plan for Wolf Creek Generating Station (Report 05000482/2024005) ML24225A1692024-08-12012 August 2024 10 CFR 50.46 Annual Report ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24214A3232024-08-0101 August 2024 Response to Request for Additional Information - Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification ML24206A1252024-07-24024 July 2024 Revision of Three Procedures and Two Forms That Implement the Radiological Emergency Response Plan (RERP) ML24191A0612024-07-0606 July 2024 Independent Spent Fuel Storage Installation (ISFSI) - Annual Radioactive Effluent Release Report ML24178A3672024-06-26026 June 2024 Correction to 2023 Annual Radioactive Effluent Release Report – Report 47 ML24178A4142024-06-26026 June 2024 Revision of One Procedure and One Form That Implement the Radiological Emergency Response Plan (RERP) ML24177A1512024-06-24024 June 2024 Post Accident Monitoring Instrumentation Report ML24166A1172024-06-20020 June 2024 Regulatory Audit Summary Regarding Proposed Alternative Schedule to Complete Decommissioning Beyond 60 Years RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations IR 05000277/20243012024-06-13013 June 2024 Initial Operator Licensing Examination Report 05000277/2024301 and 05000278/2024301 RS-24-058, Regarding Subsequent License Renewal Environmental Review2024-06-0505 June 2024 Regarding Subsequent License Renewal Environmental Review ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities ML24150A2722024-05-29029 May 2024 Annual Radiological Environmental Operating Report 81, January 1, 2023 Through December 31, 2023 ML24150A0032024-05-28028 May 2024 Request for Exemptions from 10 CFR 50.82(a)(8)(i)(A) and 10 CFR 50.75(h)(1)(iv) and Proposed Amendment to the Decommissioning Trust Agreement ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report IR 05000277/20240012024-05-13013 May 2024 Integrated Inspection Report 05000277/2024001 and 05000278/2024001 ML24134A1792024-05-13013 May 2024 Supplemental Information in Support of Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations IR 05000277/20245012024-05-0808 May 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000277/2024501 and 05000278/2024501 RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24121A1832024-04-30030 April 2024 Pre-Submittal Meeting Presentation Material Peach Bottom ECCS Compensated Level System Replacement Project ML24118A0032024-04-27027 April 2024 2023 Annual Radioactive Effluent Release Report - Report 47 ML24120A2762024-04-23023 April 2024 Independent Spent Fuel Storage Installation (ISFSI) Facility - Annual Radioactive Effluent Release Report 66 January 1, 2023 Through December 31, 2023 CNL-24-033, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-04-17017 April 2024 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24107A2462024-04-15015 April 2024 Submittal of Changes to Technical Specifications Bases ML24103A2042024-04-12012 April 2024 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24102A0472024-04-11011 April 2024 Operator Licensing Examination Approval 05000277/LER-2024-002, Uncoordinated DC Circuits Cause Unanalyzed Condition2024-04-0808 April 2024 Uncoordinated DC Circuits Cause Unanalyzed Condition RS-24-002, Constellation Energy Generation, LLC - Annual Property Insurance Status Report2024-04-0101 April 2024 Constellation Energy Generation, LLC - Annual Property Insurance Status Report RS-24-023, Report on Status of Decommissioning Funding.2024-03-22022 March 2024 Report on Status of Decommissioning Funding. 05000277/LER-2024-001, Submittal of LER 2024-001-00 for Peach Bottom Atomic Power Station (PBAPS) Unit 2, Automatic Reactor Scram Due to an Invalid Generator Lockout2024-03-21021 March 2024 Submittal of LER 2024-001-00 for Peach Bottom Atomic Power Station (PBAPS) Unit 2, Automatic Reactor Scram Due to an Invalid Generator Lockout IR 05000277/20244022024-03-12012 March 2024 Cybersecurity Inspection Report 05000277/2024402 and 05000278/2024402 (Cover Letter Only) 2024-09-06
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000277/LER-2024-003, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum2024-09-0505 September 2024 Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum 05000277/LER-2024-002, Uncoordinated DC Circuits Cause Unanalyzed Condition2024-04-0808 April 2024 Uncoordinated DC Circuits Cause Unanalyzed Condition ML24081A1212024-03-21021 March 2024 Automatic Reactor Scram Due to an Invalid Generator Lockout ML21196A4852021-07-16016 July 2021 LER 2-2021-002-00 for Peach Bottom Atomic Power Station, Unit 2, Safety Relief Valve Inoperability Due to Nitrogen Leakage from Braided Hose Wear 05000278/LER-2017-0012017-12-20020 December 2017 Reactor Pressure Boundary Leakage Due to Weld Failure in One-Inch Diameter Instrument Line, LER 17-001-00 for Peach Bottom Atomic Power Station (PBAPS), Unit 3 Regarding Reactor Pressure Boundary Leakage Due to Weld Failure in One-Inch Diameter Instrument Line 05000277/LER-2017-0012017-03-0808 March 2017 Emergency Diesel Generator Exhaust Stacks Nonconforming Design for Tornado Missile Protection, LER 17-001-00 for Peach Bottom Atomic Power Station (PBAPS), Unit 2 Regarding Emergency Diesel Generator Exhaust Stacks Nonconforming Design for Tornado Missile Protection 05000278/LER-2016-0012016-11-22022 November 2016 Leak in High Pressure Coolant Injection Drain Pipe Results in a Loss of Safety Function, LER 16-001-00 for Peach Bottom, Unit 3, Regarding Leak in High Pressure Coolant Injection Drain Pipe Results in a Loss of Safety Function 05000277/LER-2016-0012016-11-11011 November 2016 Leak in High Pressure Service Water Pipe Results in Condition Prohibited by Technical Specifications, LER 16-001-00 for Peach Bottom, Unit 2, Regarding Leak in High Pressure Service Water Pipe Results in Condition Prohibited by Technical Specifications 05000278/LER-2015-0012016-02-26026 February 2016 Loss of High Pressure Coolant Injection System Function as a Result of Failed Flow Controller Signal Converter, LER 15-001-00 for Peach Bottom, Unit 3, Regarding Loss of High Pressure Coolant Injection System Function as a Result of Failed Flow Controller Signal Converter ML13058A0432013-02-22022 February 2013 Submittal of Independent Spent Fuel Storage Installation (ISFSI) Cask Event Report ML1007702362010-03-12012 March 2010 60-Day Security Event Report 2-10-S01 ML0927401622009-09-30030 September 2009 LER 09-S01-00 for Peach Bottom, Units 2 & 3 Regarding Unescorted Access Granted to Contract Worker Who Did Not Provide Complete Work History Information ML1015505682009-07-10010 July 2009 Event Notification for Peach Bottom on Elevated Tritium Levels Found in On-Site Well ML0434503772004-12-10010 December 2004 LER-04-S01-00 for Peach Bottom Atomic Power Station (PBAPS) Unit 2 and Unit 3, 60 Day Security Event Report 2-04-S01 ML19095A7391976-12-0505 December 1976 Reporting Abnormal Occurrence No. 50-278-74-33 at Peach Bottom Atomic Power Station for Failure of Main Steam Line High Flow Switch dPIS-3-2-116C to Trip During Surveillance Test 2024-09-05
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LER-2024-003, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum |
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10 CFR 50.73 CCN: 24-45
September 05, 2024
U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001
Peach Bottom Atomic Power Station (PBAPS) Unit 2 Subsequent Renewed Facility Operating License No. DPR-44 NRC Docket No. 50-277
Subject: Licensee Event Report (LER) 2024-003-00 Automatic Reactor Scram Following Main Turbine Trip due to Degraded Condenser Vacuum
Reference: ENS 57221
The subject report is being submitted in accordance with 50.73(a)(2)(iv)(A) for actuation of the Reactor Protection System and Containment Isolation signals.
There are no commitments contained in this letter. If you have any questions, please contact the Peach Bottom Regulatory Assurance Engineer, Ms. Amy Huber at (267) 533-7247.
Respectfully,
Ryan C. Stiltner Plant Manager Peach Bottom Atomic Power Station
Enclosure
cc: USNRC, Administrator, Region I USNRC, Senior Resident Inspector W. DeHaas, Commonwealth of Pennsylvania S. Seaman, State of Maryland B. Watkins, PSE&G, Financial Controls and Co-Owner Affairs
Abstract
While conducting power ascension following a maintenance outage, Peach Bottom Unit 2 began experiencing increasing condensate pump discharge chlorides because of a condenser tube leak. A condenser water box was isolated to facilitate repairs, but due to high river temperatures combined with elev ated offgas inleakage, the water box isolation resulted in degrading condenser vacuum. Attempts to restore vacuum were unsuccessful and ultimately required a trip of the main turbine.
Because the Reactor Protection System (RPS) input for Turbine Stop Valve (TSV) and Turbine Control Valve fast (TCV) closure was armed, the turbine valve closure generated a scram signal. Group II and III Primary Containment Isolation Valves isolated because reactor water level reached the isolation setpoint. Reactor water level was maintained with feedwater and pressure was maintained with bypass valves. The scram occurred without complication and all systems responded as expected. Unit 3 was not impacted by this event.
This event is reportable under 10CFR50.73(a)(2)(iv)(A) due to manual or automatic isolation of systems listed in 10CFR50.73(a)(2)(iv)(B) including RPS and containment isolation signals. An ENS notification was made within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of the event, reference ENS 57221.
Plant Operating Conditions Before the Event
Prior to the event, on July 10, 2024, Peach Bottom Unit 2 was in Mode 1 conducting power ascension following a maintenance outage. It was identified that condensate pump discharge chloride conductivity was increasing, indicative of a condenser (EIIS: SG) tube leak. To facilitate investigation and repair of leaking tubes, a condenser waterbox was isolated with the reactor at approximately 62% power. Waterbox isolation combined with seasonally high river temperatures and elevated offgas (EIIS: WF) inleakage from a degraded valve in the offgas system resulted in degrading condenser vacuum. Although the waterbox was returned to service, condenser vacuum continued to degrade. The operating crew reduced power per station procedures, but condenser vacuum reached the threshold requiring a manual trip of the main turbine (EIIS: TA).
Event Description
The turbine was manually tripped on July 10, 2024 at 07:28 with the reactor at 25.6% power, which is within the physical capability of bypass valves (EIIS: SO). This is below the power level at which the Reactor Protection System (RPS) input for Turbine Stop Valve (TSV) and Turbine Control Valve (TCV) fast closure (EIIS: TA) is required to be armed per Technical Specifications, but due to conservative instrument setpoints, the input was still armed and the closure of the valves generated a scram signal. The scram occurred without complication. The Reactor Pressure Vessel (RPV) low level setpoint was reached, resulting in isolation of Group II and III Primary Containment Isolation System (PCIS) (EIIS: JM) valves as expected. Water level in the RPV was restored and maintained with Feedwater (EIIS: SJ) and pressure was maintained with bypass valves.
This event is reportable under 10CFR50.73(a)(2)(iv)(A) due to manual or automatic isolation of systems listed in 10CFR50.73(a)(2)(iv)(B) including RPS and containment isolation signals. An ENS notification was made within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of the event, reference ENS 57221.
Safety Consequences
The reactor Scram occurred as designed and resulted in no safety consequences. All safety systems responded as expected. Use of emergency core cooling systems for level and pressure control was not required. Unit 3 was not impacted by this event.
Cause and Corrective Actions
The cause of the scram was RPS input from TSV and TC V fast closure due to a manual trip of the Main turbine. Procedures directed tripping the turbine if steam flow was within bypass valve capability but did not warn that the RPS logic may be armed. Actions have been taken to revise procedures from tripping the turbine if within bypass valve capability to if it is known that the Main TCV/TSV closure is bypassed on A or B RPS.
Additionally, the cause of the degraded condenser vacuum condition was investigated. The root cause of this condition is that the station did not recognize and evaluate the cumulative effect of increased offgas air inleakage and isolation of a condenser waterbox with high river temperatures, culminating in a rapid lowering of main condenser vacuum. As a contributor, station models were unable to accurately predict the impact of elevated offgas inleakage on condenser performance. The corrective actions focus on enhancing the station governance for isolating a waterbox.
Previous Similar Events
In February 2004, Peach Bottom manually scrammed due to decreasing condenser vacuum. The cause of the loss of vacuum was inleakage of non-condensable gases from a crack in a feed pump turbine expansion joint.
Ref. LER 2004-002-00, dated 4/30/2004.
In August 2022, Peach Bottom experienced condenser vacuum degradation during a load drop in support of condenser cleaning activities, after isolating condenser wate r boxes. In this case, conditions were stabilized without requiring a trip of the main turbine or a reactor scram. Increased offgas flow was not a factor in this event.