ML20245B959

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SALP Rept 50-219/87-99 for Oct 1987 - Jan 1989
ML20245B959
Person / Time
Site: Oyster Creek
Issue date: 04/17/1989
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20245B957 List:
References
50-219-87-99, NUDOCS 8904260403
Download: ML20245B959 (41)


See also: IR 05000219/1987099

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ENCLOSURE 1

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

BOARD REPORT

50-219/87-99

GENERAL PUBLIC UTILITIES NUCLEAR CORPORATION

OYSTER CREEK NUCLEAR GENERATION STATION

ASSESSMENT PERIOD: OCTOBER 1, 1987 - JANUARY 31, 1989

BOARD MEETING DATE: MARCH 14, 1989

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TABLE OF CONTENTS

PAGE

I. Introduction......................................................... 1

I.A Background.................... ................................. 2

I.B Licensee Activities............................................. 2

I.C Direct Inspection and Review Activities......................... 3

II. S u mm a ry o f R e s u l t s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

I I . A O v e ra l l S umma ry . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ...... 5

II.B Facility Performance Analysis Summary........................... 6

II.C Unplanned Shutdowns, Plant Trips, and Forced Outages. . . . . . . . . . . . 7

III. Criteria................ ................ ........................... 8

IV. Performance Analysis................................................. 10

IV.A Plant Operations..................................... ..... 10

IV.B Radiological Controls...... ......... ..................... 14

IV.C Maintenance / Surveillance.............. .................... 18

IV.D . Emergency Preparedness..................................... 22

IV.E Security................ .................................. 24

IV.F Engineering / Technical Support........... .................. 26

IV.G Safety Assessment / Quality Veri fication. . . . . . . . . . . . . . . . . . . . . 29

SUPPORTING DATA AND SUMMARIES

A. Investigations and Allegations Review................................SD/S-1

8. Escalated Enforcement Actions................... ....................SD/S-1

C. Co n fi rmato ry Ac ti on Lette r s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . SD/S-1

D. Li c e n s e e Ev e n t Re p o rt s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . S D/S-1

TABLES

Table I - Enforcement Activity

Table II - Listing of LERs by Functiona'l Area

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I. INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an integrated I

agency effort to collect and evaluate available agency insights, data, and other

information on a plant / site basis in a structured manner in order to assess and

better understand the reasons for a licensee's performance. Unacceptable perform-

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ance is addressed through NRC's enforcement policy and the implementation of this

l policy should not be delayed to await the results of a SALP. Compliance with NRC

rules and regulations satisfies the minimum requirements for continued operation

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of a facility; the degree to which a licensee exceeds regulatory requirements is

a measure of the licensee's commitment to nuclear safety and plant reliability.

The SALP process is used by the NRC to synthesize its observations of and insights

into a licensee's performance and to identify common themes or symptoms. As such,

the NRC needs to recognize and understand the reasons for a licensee's strengths

as well as weaknesses. The SALP process is a means of expressing NRC senior man-

agement's observations and judgements on licensee performance. It should not be

limited to focusing on weaknesses, and it is not intended to identify proposed

resolutions or solutions of problems. The licensee's management is responsible

for ensuring plant safety and establishing effective means to measure, monitor,

and evaluate the quality of all aspects of plant design, hardware, and operation.

The SALP process is intended to further NRC's understanding of (1) how the licen-

see's management guides, directs, evaluates, and provides resources for safe plant

operations, and (2) how these resources are applied and used. As a result, em-

phasis is placed on understanding the reasons for a licensee's performance in

identified functional areas and on sharing this understanding with the licensee

and the public. The SALP process is intended to be sufficiently diagnostic to

provide a rational for allocating NRC resources and to provide meaningful feedback

to the licensee's management.

An NRC SALP Board, composed of the staff members listed below, met on March 14,

1989, to review the observations and data of performance, and to assess licensee

performance in accordance with Chapter NRC-0516, " Systematic Assessment of Licensee

Performance." This guidance and evaluation criteria are summarized in Section III

of this report. The Board's findings and recommendations were forwarded to the

NRC Regional Administrator for approval and issuance.

This report is the NRC's assestment of the licensee's safety performance at Oyster

Creek for the period October 1, 1987 to January 31, 1989.

The SALP Board for Oyster Creek was composed of:

SALP Board

Board Chairman

W. Kane, Director, Division of Reactor Projects (DRP)

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Members

S. Colli"s, Deputy Director, DRP

M. Knapp, Director, Division of Radiation Safety and Safeguards (DRSS) (part time)

T. Martin,. Director, Division of Reactor Safety (DRS).

L._Bettenhausen, Chief, Projects Branch No. 1, DRP

R. Gallo, Chief, Dperations Branch, DRS (part time)

C. Cowgill, Chief,. Reactor Projects Section IA, DRP

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J. Wechselberger,' Senior Operations Engineer, NRR (voting for Senior Resident

Inspector).

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J. Stolz, Director, Project Directorate 1-4, NRR

A. Dromerick, Project Manager, NRR

W.- Johnston, Deputy Director, DRSS'(part time)

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k. Baunack, Project Engineer, DRP i

'0. Lew, Resident Inspector '

E. Collins, Senior Resident Inspector

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I.A Background

Oyster Creek is a GE BWR/2 with a Mark I containment. The Construction Permit'was

issued in December 1964 and commercial operation commenced on December 23, 1969  !

at-1600 Megawatts thermal.

This unit- was delivered to Jersey Central Power and Light Company for operation

as one of the first GE " turnkey" reactor plants. Later, the unit's licensed power

was increased to 1930 Megawatts thermal.

The nuclear steam supply system differs from later model BWRs in that it uses 5

reactor recirculation pumps and the reactor vessel has no internal jet pumps. The

emergency cor* cooling systems consist of two low pressure core spray systems, 2

isolation condensers for heat removal, and an automatic depressurization system. j

I.B Licensee Activities

At the beginning of the assessment period, the plant was shut down in accordance

with a confirmatory action letter. This letter was issued as a result of a safety

limit violation which occurred on September 11, 1987. On November 6, 1987, a let- i

ter permitting restart was issued to the licensee. On November 20, 1987, the In- I

ternational Brotherhood of Electrical Workers initiated a strike against the util-

ity. Management personnel assumed the duties of bargaining unit personnel and

. preparations for plant startup continued. Reactor startup occurred on November

'22, 1987 and the turbine was placed on line on November 24, 1987. The startup and

subsequent plant operation were conducted by supervisory personnel.

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On December. 11, 1987, the strike was settled. Returning workers were trained and

reoriented before resuming normal duties. Plant operation continued at full power

with only minor power reductions for surveillance or maintenance until July 9,

1988 when, following main steam isolation valve (MSIV) surveillance testing, no

steam flow was indicated in the "A" steam line. A shutdown was initiated and the

plant was placed in cold shutdown on July 10, 1988. This terminated'a 229 day

. continuous run.

Subsequent' investigation of the cause of no steam flow in the "A" steam line re-

vealed an.MSIV stem failure. Following MSIV repairs a plant startup commenced on

August 9, 1988, and the generator was placed on the.line on August 12.

On August 28, 1988, the "B" isolation condenser started " steaming" following a six

day out of service period for maintenance. On September 2, 1988, a plant shutdown

was initiated due to both isolation condensers being declared inoperable. One

isolation condenser was inoperable due to maintenance; the other due to a manual

vent line valve being found in the closed position. The shutdown was terminated

after the vent valve was opened and noncondensibles were calculated to have been-

purged on September 3, 1988.

On September 26, 1988, following a surveillance of the "A" isolation condenser it

also began to " steam". On September 23, following an evaluation of isolation con-

denser' conditions, both condensers were declared inoperable, and a plant shutdown

was initiated. Cold shutdown was achieved on September 30, 1988. Following the

shutdown a decision was made to commence the Cycle 12 Refueling Outage which was

originally scheduled to begin on October 15, 1988. The plant remained shut cown

for the remainder of the SALP period.

On May 1,1988, a new Vice President and Director of Oyster Creek was appointed.

The previous Director of Oyster Creek was appointed Vice President and Director

of a new GPUN division encompassing corporate-wide training and education and

quality assurance programs.

I.C Direct Inspection and Review Activities

Three NRC resident inspectors were assigned to the site. One new tesident was

assigned in January,1988; the third resident was assigned in July 1988. Addition-

ally, two temporary resident inspectors were assigned for a period of six weeks

each. The total inspection time for the assessment period was 8569 hours0.0992 days <br />2.38 hours <br />0.0142 weeks <br />0.00326 months <br /> (resident,

region and headquarters based) with a distribution in the appraisal functional area

as shown with each functional area. This equates to 6427 hours0.0744 days <br />1.785 hours <br />0.0106 weeks <br />0.00245 months <br /> on an annual basis.

Special inspections included the following:

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Special team inspection to assess the safety significance of freezing condi-

tions identified in the reactor building on January 6, 1988 (January 25-29,

1988).

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The annual emergency preparedness exercise was heid on May 11-12, 1988.

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-. ~ Special team inspection to review the circumstances and events leading up to

L a subsystem of the containment spray / emergency service water being returned

to service exceeding operability acceptance' criterion (July 11-15,1988).

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, Regulatory Effectiveness Review conducted July 18-22, 1988.

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. Special team inspection to review licensee's evaluation and response to a main

steam isolation valve broken stem (July 18-22,1988).

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Emergency Operating Procedure inspection conducted September 6-15, 1988.

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Augmented Inspection Team inspection to review the circumstances, events and

licensee response to a situation where both emergency condensers _were inoper-

able (October 5-13,1988).

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Safety System Outage Modification Inspection conducted October 17 through

November 4, 1988 and November 28 through December 16, 1988.

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II. SUMMARY OF RESULTS

II.A Overall Summary

Overall, inconsistent performance was.again noted at the facility. Improvements

were made in the plant material condition, the number of forced outages were

significantly reduced and there were no plant trips. In addition, the number

of operator. errors was reduced. In contrast, however, performance in the areas

of Security and Radiological Controls degraded during the period.

The site and corporate management have undertaken many new initiatives to improve

the performance of the facility both in the area of safety and plant performance.

GPUN maintains a policy for its employees which stresses a high standard of

integrity and procedure adherence and a concept of safety before schedule This

policy is well understood but inconsistently applied at the lower levels of

the organization.

Licensee programs to surface and correct deficiencies are in place but, are not

fully effective. A preliminary safety concern program has evidenced problems

in bringing issues to closure and providing feedback to individuals. Interfaces

between operators and their management have not worked well to resolve identified

deficiencies. Communications problems between the operations department and

support organizations have also been noted.

In the Radiological Controls area, weaknesses were identified that contributed

to a decline in the program's effectiveness. Those weaknesses include ineffective

root cause analysis, incomplete control and planning of radiological operations,

incomplete corrective actions on identified problems, and lax worker attitudes.

The licensee has made significant progress in reducing the maintenance backlog

at the facility and instituted changes to further enhance maintenance effectiveness.

A new training program for maintenance technicians and a shift to a computerized

maintenance control system have been implemented. Rework remains a problem at the

facility and problems were identified associated with implementing the maintenance

control program.

In the area of Technical Support, the licensee has actively responded to

previous SALP concerns. These efforts have resulted in an enhanced root cause

analysis of engineering support and a reduction in the engineering work backlog.

Some examples of insensitivity to emerging and long standing technical problems

still exist. Communications between site and corporate engineering were weak at ,

times and as a result the licensee's engineering resources were sometimes not '

effectively used. The difficulties encountered in correcting some of the long

standing problems are due in part to issues resulting from the age of the plant,

the volume of issues to be resolved, and an ill-defined plant design basis.

Development of a sound design basis for the plant is an essential element i

central to attaining substantial overall improvement in facility performance. l

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In summary, the licensee remains committed to establishing and implementing

programs to support safe, efficient operation of the facility. Full

application and integration of these initiatives is hindered by the age and

design of the facility. These equipment and material issues continue to

challenge personnel performance and stress the licensee's organization.

II.B Facility Performance Analysis Summary

This SALP report incorporates the recent NRC redefinition of the assessment func-

tional areas. Changes include combining the previously separate Maintenance and

Surveillance areas and addition of'the Safety Assessment / Quality Verification area. ,

The Safety Assessment / Quality Verification :ection is largely a synopsis of obser-

vations in other functional areas. Additionally, the Fire Protection, Licensing,

Refueling /0utage, Training, and Assurance of Quality areas have been incorporated

into the remaining functional areas as appropriate.

Rating Rating

Last This

Functional Area Period * Period ** Trend

A. Plant Operations 3 3 Improving

B. Radiological Controls . 3 --

C. Maintenance / Surveillance *** 2/2 2 --

D. Emergency Preparedness 2 2 --

E. Security 1 2 --

F. Engineering / Technical Support 3 2 --

G. Safety Assessment / Quality Verification # 2 --

H. Licensing Activities 2 # --

I. Training & Qualification Effectiveness 2 # --

J. Assurance of Quality 2 # --

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October 16, 1986 to September 30, 1987

    • October 1, 1987 to January 31, 1989

Previously addressed as. separate areas of Maintenance and Surveillance.

  1. Not addressed as a separate area.

NOTE: It is important to note that a major revision of the SALP Manual Chapter

has been made which combined some areas and made changes to the attri-

butes in the functional areas. Therefore, a direct comparison of the

functional area grades cannot be made between the previous SALP and the

current one.

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II.C Unplanned Shutdowns, Plant Trips, and Forced Outages

POWER ROOT FUNCTIONAL i

DATE LEVEL DESCRIPTION CAUSE AREA

7/9/88 40% During testing one MSIV Main Steam N/A

failed to close. The series isolation

MSIV was closed and disabled valve (MSIV)

until the operability of stem had sepa-

the affected valve could be rated from the

established. After several pilot poppet.

attempts, the MSIV appeared Root cause for

to close and open within the the shear fail-

normally expected stroke ure of the MSIV

times. After attempting to stem has not

open both MSIV's, no steam been determined.

flow was indicated in the "A"

steam line. A shutdown of

the reactor was initiated to

determine the cause of no

steam flow in the "A" steam

line header and make appro-

priate repairs.

9/29/88 99% An evaluation of thermal During main- N/A

profiles of the isolation tenance of

condenser piping concluded Isolation Con-

that water was present in denser valve

the steam piping. Due to steam lines

the potential for severe filled with

water hammer upon system water,

initiation, both isolation

condensers were isolated

and declared inoperable

and the reactor was shut

down.

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III. CRITERIA

Licensee performance is assessed in selected functional areas, depending upon

whether the facility is in a construction, preoperational, or operational phase.

Functional areas normally represent areas significant to nuclear safety and the

environment. Some functional areas may not be assessed because of little or no

licensee activities or lack of meaningful observations. Special areas may be added

to highlight significant observations.

The following evaluation criteria were used, as applicable, to assess each func-

tional area.

1. Assurance of quality, including management involvement and control;

2. Approach to the identification and resolution of technical issues from a

safety standpoint;

3. Responsiveness to NRC initiatives;

4. Enforcement history;

5. Operational and construction events (including response to, analyses of,

reporting of, and corrective actions for);

6. Staffing (including management); and

7. Effectiveness of training and qualification program.

However, the NRC is not limited to these criteria and others may have been used

where appropriate.

On the basis of the NRC assessment, each functional area evaluated is rated into

to three performance categories. The performance categories used when rating lic-

ensee performance are defined as follows:

Category 1. Licensee management attention and involvement are readily evident and

place emphasis on superior performance of nuclear safety or safeguards activities,

with the resulting performance substantially exceeding regulatory requirements.

Licensee resources are ample and effectively used so that a high level of plant

and personnel performance is being achieved. Reduced NRC attention may be appro-

priate.

Category 2. Licensee management attention to and involvement in the performance

of nuclear safety or safeguards activities are good. The licensee has attained

a level of performance above that needed to meet regulatory requirements. Licensee

resources are adequate and reasonably allocated so that good plant and personnel

performance is being achieved. NRC attention may be maintained at normal levels.

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Category 3. Licensee management attention to and involvement in the performance

of nuclear safety or safeguards activities are not sufficient. The licensee's

performance does not significantly exceed that needed to meet minimal regulatory

requirements. Licensee resources appear to be strained or not effectively used.

NRC attention should be increased above normal levels.

The SALP Board may assess a functional area to compare the licensee's performance

during the last quarter of the assessment period to that during the entire period

in order to. determine the recent trend. The SALP trend categories are as follows:

Improving: Licensee performance was determined to be improving near the close of

the assessment period.

Declining: Licensee performance was determined to be declining near the close of

the assessment period and the licensee had not taken meaningful steps to address

this pattern.

A trend'is assigned only when, in the opinion of the SALP Board, the trend is sig-

nificant enough to be' considered indicative of a. likely change in the performance

category in the near future. For example, a classification of " Category 2, Im-

proving" indicates the ' clear potential for " Category 1" performance in the next

SALP period.

It should be noted that Category 3 performance, the lowest category, represents

acceptable, although~ minimally adequate, safety performance. If at any time the

NRC concluded that a licensee was not achieving an adequate level of safety per-

formance, it would then be incumbent upon NRC to take prompt appropriate action

in the interest-of public health and safety. Such matters would be dealt with

independently from, and on a more urgent schedule than, the SALP process.

It should also be noted that the industry continues to be subject to rising per-

formance expectations. NRC expects licensees to use industry-wide and plant-speci-

fic operating ' experience actively in order to effect performance improvement. Thus,

a licensee s safety performance would be expected to show improvement over the

8

years in order to maintain consistent SALP ratings.

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IV. PERFORMANCE ANALYSIS

.IV.A Plant Operations (2840 Hrs., 33%)

IV.A.1 Analysis

The previous SALP rating in this area was Category 3. Improvements were noted in

onshift decisionmaking, emphasis on shift teamwork, control room professional en-

vironment and operator action to control water level transients. Special NRC in-

spection findings were generally positive; concluding that a competent organization

with strong management and effective programs were in place. However, the special

inspections also observed a lack of promulgation of management goals to lower level

personnel to ensure understanding of risk importance and a more inquisitive ap-

proach to non-routine plant conditions. Positive observations were contrasted with

safety significant events indicating inconsistencies in program application and

personnel performance. Additional assessment concluded that equipment challenges

<added to a decrease in the operators performance. Procedural . conflicts fostering

a graded approach to compliance, schedule pressure and housekeeping problems, all

contributed to a conclusion of overall inconsistent operational performance.

During the current SALP cycle, senior operations management was changed and the

new managers encouraged an increased emphasis in identifying problems for resolu-

tion. Improved periodic meetings were held with shift management to develop a bet-

ter understanding of problems and to unify operations management. Senior site

management has continued to emphasize cooperation and teamwork through periodic

meetings of all key site management personnel to resolve problems and increase

communication among divisional representatives at the facility. Other positive

attributes include major evolutions by operational plans specifying organizational

responsibility, restart certifications, senior corporate management review of re-

start readiness, and implementation of the INPO sponsored HPES process. Senior

site management took a major step in reenforcing the concept of safety before

schedule, when, with the direct involvement of the site director, refueling errors

were dramatically decreased. Refueling activities were delayed to facilitate ex-

tensive training sessions for operators, core engineers, and operations management

to discuss the " error-free" refueling plan, refueling operations and the concept

of safety before schedule. The reactor refueling was subsequently conducted with-

out error.

The plant continuously operated for 229 days. This was due in part from increased

attention to plant equipment problems. This is in direct contrast to the past when

numerous reactor scrams and unplanned shutdowns have impacted plant performance.

Recently the plant implemented a modification to help control reactor water level

following post plant trips; this been an identified problem in previous SALP re-

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ports. Other positive indicators of current plant performance are the reduction

in temporary procedure changes exceeding the 14 day technical specification appro-

val limit, increased personnel in operator training programs and periodic meet-

ings between the site director and the QA organization to effect resolution of

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quality issues. In addition, the licensee has established an Operations Coordina-

tions office to alleviate some of the administrative burden from the shift super- l

visor during outages. This is perceived as positive; however, early in the outage, '

shift supervisors were at times concerned about effective communication regarding

outage activities.

Operators have shown improvement by a professional attitude toward their duties

and proper control room decorum; however, some distractions are still noted.

One particular bright spot has been the determination of a few operators to

identify and report potential significant equipment and system problems and to

correct long standing facility problems. Operators and operations personnel in

general are responsive to inspector concerns and are open in their communications.

Conditions are not conducive to promoting cooperation and teamwork between

operators and operations middle management. Likewise, lack of support to the

operators by operations middle management was noted. This was evidenced by

certain equipment being allowed to remain out of service for long periods, as

in the case of the reactor building heating and ventilation problems that lead

to freezing in the reactor building despite operator complaints, and isolation

condenser steam line temperature anomalies not being addressed. Operations

management did not adequately respond to QA findings associated with the contain-

ment spray / emergency service water system, and this eventually led to a plant

problem. Also, the acceptance by operations management of modified systems for

operation without a formal turnover of the completed modification has resulted

in system operation without complete documentation.

A strike occurred immediately before returning the plant to power operation in the

fall of 1987. The NRC determined that the licensee's strike plans were comprehen-

sive and appropriate to address the situation. Management personnel assigned to

perform operator duties during this time were thorough and knowledgeable in plant

operation and startup activities. Management plans to transfer operation of the

plant to union personnel after the strike were also considered highly effective.

The licensee has initiated a number of programs to improve worker attitudes and

increase productivity since the conclusion of the strike.

During this SALP period, operator license examinations were successfully admini-

stered to five SR0 and 3 R0 candidates. It was noted that control room staffing

consisted of only a five shift rotation.

Operations have improved in specific areas, which may be attributed to self initi-

ated actions as well as significant input from internal license and regulatory

organizations. Although the plant operated continuously for 229 days, power re-

ductions were required to repair plant equipment problems. Some long standing

equipment problems still persist. These include intermediate range monitors,

control rod drive hydraulic control units, safety relief valve acoustic monitors

and thermocouple and various secondary equipment problems.

NRC observations indicate that, although daily planning meetings effectively com-

municate plant and maintenance status, there are interface problems at the working

level between the Operations Department and support organizations. Examples of

conditions that resulted from this are: worker contamination from poorly planned

post maintenance testing of the offgas system, the loss of secondary containment

during isolation condenser maintenance, overlapping stack gas monitor tagouts which

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resulted in making the monitor inoperable and the removing of a station battery

and the opposite train diesel from service simultaneously, thus, making both

diesels unable to respond in the event of a loss of offsite power.

Operations understanding of the technical specifications and the design basis and

evaluating plant conditions against these requirements is a weakness. Examples

include operations attempt to startup the plant in an action statement with an

inoperable offgas sample pump and three control rods made inoperable due to in-

adequate operator response to low gas pressure alarms.

Station procedures are generally good, but have been key contributors to two major

events during this SALP period. Placing the isolation condensers in a questionable

condition and potentially exceeding a limiting condition for operation with the

containment spray / emergency service water system were direct results of poor pro-

cedures. In the first case, a long standing procedure deficiency became evident

and in the second, a poor modification process resulted in the procedure problems.

Also, during the freezing reactor building temperature inspection, inadequate pro-

cedure reviews were discovered. In this case, the system procedure had been re-

vised 13 times over a 20 year period without detecting that the control room reac-

tor building temperature gauge referred to in the procedure was never installed.

Other examples include operator confusion from the conflictir g instructions for

equalizing pressure across the MSIVs and minimum battery room air temperature pro-

vided by different procedures, and an unspecified action in response to a refueling

cavity seal leak alarm.

Operator errors have decreased since the last SALP, and, overall, improvement in

this area has been seen. However, there were some errors during the plant opera-

tion. During reactor defueling numerous operational errors occurred that resulted

in the direct involvement of the Site Director to bring about a positive change.

There was one instance of a lack of command and control during the MSIV stem fail-

ure in which a half trip was not inserted promptly. Also, logging of some events

was not timely such as the isolation condenser initiation which was not logged or

reported until some time after it occurred.

During this SALP period, a special inspection was performed of the Emergency

Operating Procedures (EOPs). This inspection concluded that the E0Ps were tech-

nically sound, that the operators understood their fundamental technical principles,

and that the operators were able to execute the E0Ps. The overall quality of the

emergency operating procedures is considered to be a strength. The team did ob-  !

serve an unfamiliarity with the " hands-on" use of the procedures and flow charts.

This unfamiliarity is considered a training deficiency.

Operator attitude was a concern identified during the E0P inspection as well as i

during defueling. The E0P inspection identified an attitude of overconfidence as

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well as a tendency to minimize the significance of the E0Ps. Likewise, in response

to the number of errors which occurred during the defueling, operators displayed

an attitude that this performance was no different than that of the previous years.

Management did take corrective action to improve refueling performance.

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__ _ _ _ _ . _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ . _ _ _ _ . _ _ _ _

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13

In conclusion, operations has shown improvement, including a reduction in operator

errors. Senior site management has made efforts to build cooperation and teamwork.

Operations middle management has not aggressively supported operators by correcting i'

identified S concerns, addressing operator questions and concerns, and improving

middle management and operator cooperation and teamwork. Plant material condition

continues to improve as evidenced by a long operational period. The initiative

shown by several operators to correct long standing facility problems is encourag-

ing. Procedure weaknesses still exist and contributed to plant events.

IV.A.2 Conclusion

Category 3, Improving.

IV.A.3 Recommendation

None.

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. _ _ _ _ _ _ _ _ _ _ _ _

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14

IV.B Radiological Controls (560 Hrs., 6.5%)

IV.B.1 Analysis

Previous SALP-

The last SALP rated this area as Category 2. Weaknesses noted included: incomplete

pre-job briefing of workers; ineffective root cause analyses following radiological

incidents; lack of emphasis and followup of quality control functions performed

by Radiological Engineering; and poor ALARA effort and ineffective goal setting

and goal tracking. Strengths included an adequate staff with good qualifications,

good facilities ard equipment, training, posting, and access control.

Current SALP

Four special .nspections were conducted in this area during the current SALP period,

in addition co the routine reviews by the resident inspectors.

Overall, the licensee's radiological control program remains adequate. However,

continuing weaknesses were identified that contributed to a noticeable degradation

in program effectiveness. These weaknesses include (1) deterioration of control

and planning of radiological operations, (2) incomplete corrective action on iden-

tified problems, (3) continued examples of ineffective root cause analysis, and

(4) a lack of aggressive action to reduce collective worker exposure.

Control and planning of radiological work is generally adequate, but instances of

. poor performance were noted. Appropriate actions to address deteriorating radio-

logical conditions were not taken in some cases. As an example, a control rod

manipulator was used to facilitate the removal of control rod drives from the

reactor. This resulted in an increase in the rate at which the drives were removed

and sent to the drive maintenance and rebuild area. However, the effects of this

increased rate on radiological conditions in that area were not adequately consi-

dered. As the backlog of control rod drives in the rebuild area became excessive,

the area became highly contaminated. The contamination subsequently spread outside

the rebuild area to other areas of the reactor building. The problem was compounded

by the lack of experience and incomplete training of the workers in the rebuild

area. Although the workers had been put through mockup training, the pace of the

training was rapid, and many were not trained on the actual work performed in the

rebuild area.

Although the licensee continues to demonstrate an ability to identify problems,

the corrective action program was at times ineffective in achieving desired im-

provements and preventing recurrence. The following are examples of this problem.

--

Improper priority assignments to radiological control problems were observed.

For example, high radiation area doors which were required to be locked were

found unlocked due to their poor mechanical condition. Although corrective

action was proposed, it was not cr lated because of the low assigned job

priority and subsequent cancellation of the work orders. This resulted in

continued instances where high radiation area access control was compromised.

- _ _ _ _ _ . _ _

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'--

Investigation following the occurrence of radiological incidents is prompt,

but the depth of review conducted is frequently limited in scope and effec-

tiveness. As an example, disturbances in the ventilation flow pathways in

the Augmented Offgas system building produced airborne contamination in the

building. Following a nunber of personnel contaminations, the licensee com-

mitted to sampling the air for radioactive gas in case of such incidents.

However, the sampling is still not being done in a systematic and controlled

manner. The lack of timely performance of air samples was identified during

the previous SALP period. In the past this weakness could have led to situ-

ations where the licensee was not able to adequately assess the exposure that

workers were receiving from airborne contamination. The licensee was not

responsive and did not acknowledge the concern, and this weakness still re-

mains. Another identified weakness has been the failure to perform appro-

priate surveys in areas with non-uniform radiation fields. This program

weakness recurs despite licensee's corrective actions implemented to date.

--

One of the principal reasons for the failure of corrective actions is that

investigations conducted by the licensee following an incident do not identify

root causes.but-instead concentrate on immediate and sometimes superficial

factors. The critiques rarely address problems that result from poor super-

visory practices or poor planning, and tend to concentrate on errors committed

by the worker and by first line supervisors. In the control rod rebuild room

incident mentioned above, important and key contributing factors were not

considered in the critique, including failure to anticipate a potential over-

load of the work area, a lack of clear and adequate procedures to control the

work, and poorly trained technicians with little or no experience in covering

this type of work. In another incident, a technician and his supervisor

removed some temporary shielding in accordance with instructions from radio-

logical engineering causing an increase in the dose rate in the area and un-

knowingly created conditions that classified the area as a locked high radi-

ation area-. The critique of the incident failed to point out that, among the

root causes of the incident were improper surveys in a non-uniform radiation

field, incomplete supervisory shift briefings, and problems with the tagging

and tracking system for temporary shielding.

--

Engineering evaluation in response to NRC concerns has generally been thorough

and professional when the problem in question was internal to the Radiological

Controls organization on site. This is contrasted by situations in which the

evaluations had to be performed by some departments other than Radiological

Controls which were poor in quality, excessively brief and unsubstantiated,

and reluctantly given. One example was in connection with the licensee's

request to permit occupancy of the upper levels of the drywell during fuel

movements. In response to an NRC concern regarding radiological safety in

the upper elevations in case of a fuel drop accident, the licensee proposed

a fence, but did not supply adequate supporting calculations on fence strength.

Subsequent calculations were brief, with no stated assumptions. Also, as part

of this evaluation, the licensee proposed mechanical stops to limit the range

of horizontal movement of the refueling bridge. However, the stops were not

installed because of an oversight, and defueling proceeded without these stops

until detected by licensed operators while testing the fuel handling bridge.

__________ _ _ _ _ _ _ _ _ __ ._ 3

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Lack of aggressive action to reduce collective worker exposure can be found in

examples of a lax attitude towards adherence to radiological controls procedures.

For example, personnel, including maintenance and quality assurance, have been

observed on several occasions entering posted contamination areas and ignoring

entry requirements,.such as the use of proper protective clothing. One individual

repeated this infringement of the rules immediately after his attention was drawn

to that fact.

Performance in the area of ALARA remained consistent with that observed during

the previous assessment period. The cumulative exposure for the current outage

to date is over 1500 man-rem despite an outage goal of 900 man-rem. This goal is

still high in comparison to the national average due to a high in plant source term,

plant design and the scope of work in the outage. Compared with previous outages,

more efforts to reduce exposure were taken during this outage, however, a lack of

progress in long range source term reduction was evident. Source term reduction

initiatives included decontamination of many areas of the plant and several highly

contaminated systems and the use.of shielding in the drywell. Job planning, how-

ever, still needs improvement. An exposure reduction plan has recently been de-

veloped by the licensee in an effort to identify the areas in which exposure re-

duction methods can be effectively used. According to this plan, implementation

of-the recommended measures should produce a realistic two year rolling average

during 1990-1992 of 470 man-rem. Some items recommended in the plan were imple-

mented during the current outage, but to date, no specific timetable was published

to implement the major recommendations in the plan to achieve the desired collec-

tive dose reduction and to achieve parity with the rest of the industry. ,

Radiological Effluent Monitoring and Control

One inspection of the licensee's radioactive effluent control program was conducted

near the end of the assessment period. The licensee has in place an effective pro-

gram for controlling radioactive effluent releases from the site. The licensee

is meeting Technical Specification requirements with respect to radioactive ef-

fluent sampling, analysis, surveillance-, and reporting requirements. The required

reports are complete and thorough. A noted strength of the licensee's radioactive  ;

effluent control program is the attempt to minimize the release of liquid radio- i

active effluents from the site. During the third quarter of 1987 and for the j

period January 1,1988 - May 31,1988 no liquid effluent releases were made from

the site.

Quality assurance audits of the gaseous and liquid radioactive effluent areas were l

thorough and of sufficient technical depth to adequately assess program capabili-

ties and performance. In addition, Operational QA surveillance activities were

of excellent technical depth and were conducted by an individual with appropriate

technical expertise.

Chemistry Control

The area of chemical measurement has improved during this assessment period. In-

itially several analytical results (chloride, sulfate, silica, iron, and boron)

were in disagreement with the criteria used for comparison. These results were

_ _ - _ _ _ _ - - - _ - _ _ _ _ - _. -

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possibly due to high laboratory room temperature, high reagent water temperature,

and an inadequate pipet calibration technique. With special attention to control

of these problems, all analyzed results were in agreement with the standards.

Currently, the licensee is upgrading the room temperature control system which is

indication of the management attention to the chemical measurement program.

Training was of high quality as reflected by the technical depth and also for ap-

placability in the chemistry laboratory. Quality assurance audits of the chemistry

program were thorough and of sufficient technical depth to adequately assess pro-

gram performance.

In summary, the licensee's effluent controls program remains effective and labora-

tory chemistry control improved. Nonetheless, a number of problems persisted during

this period which reflect a decrease in the Radiological Controls program effec-

tiveness. Job planning and control were weak in some areas; incident evaluation

and corrective action were incomplete and did not always identify the root cause

of a problem. ALARA planning suffered from the lack of aggressive source term

reduction and resulted in elevated collective exposure.

IV.B.2 Conclusion

Category 3.

IV.B.3 Recommendation

Licensee: Perform prompt self-assessment of third party review to assure problems

are fully identified and corrective action plan developed.

NRC: Follow up self-assessment with review and appraisal.

i

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18

IV.C Maintenance / Surveillance (2653 Hrs., 31%)

IV.C.1 Analysis

The previous SALP rated both areas of maintenance and surveillance as Category 2.

Inlthe area of Surveillance / Inservice Testing, strong administrative control and

strong procedures were noted. Concerns were expressed regarding a lack of aggres-

siveness in root cause analysis of some surveillance . identified problems, and that

communications between plant departments required improvement. In Maintenance,

plant impacting reliability and maintenance associated equipment problems indicated

a need for improvement in the overall quality of work performed, and a need for

improvement in communications between groups. Also noted were significant steps

taken by the licensee to improve overall performance including: personnel changes,

a critical self-assessment, establishment of ccmmittees to review problems, im-

provements in post-maintenance testing, and efforts to reduce work backlog.

During this SALP period, the-licensee has demonstrated responsiveness to NRC con-

cerns and resolve to improve'the performance of plant maintenance. The maintenance

program at Oyster Creek remains generally effective and the licensee has imple-

mented several major initiatives to build.a more effective maintenance program.

The Oyster Creek surveillance program continues to be effective, characterized by

strong administrative controls.

Two areas that remain weak are maintenance rework and surveillance which fre-

quently fail. Examples of rework have occurred, including valve leaks at control

rod drive hydraulic control units, main steam isolation valve (MSIV) work, inter-

Emediate range neutron monitors, and recirculation pump speed control. In each case,

corrective maintenance was performed, which failed to correct the deficiency. In

addition, surveillance test repeat failures have been main steam isolation valve

slow closure test stroke times too long, snubber and hanger deficiencies, anc'

reactor pressure switches out of tolerance. In some cases, equipment age is a

factor in these recurring deficiencies and the licensee has implemented major

modifications to improve or upgrade equipment. In other cases, however, rework

items are a result of ineffective root cause determination and rework identifica-

tion and correction program.

During an unplanned outage, July 1988, the licensee repaired a temperature problem

on a reactor feed pump, speed control on the recirculation pump, safety relief

valve thermocouple, intermediate range neutron monitors, and a hydraulic control

unit. In each case the problem reoccurred during the subsequent startup. The

licensee has programmatic controls in place to address rework, but these have not

been used. The licensee has taken several additional steps to uddress this area.

This includes a Human Performance Evaluation Program to aid in root cause identi-

fication, the establishment of a goal of no restart errors as a result of 12R work

and a formalized administrative control procedure for post maintenance testing.

The effectiveness of these measures to address rework concerns has not been as-

sessed.

- .. .. .

_ _ _ _ _ _ . _ -

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19

The licensee has significantly reduced its maintenance backlog and committed to

achieving 100% equipment operability. As a result of this effort, the licensee

is performing a greater quantity and more complex work during plant operation.

The licensee made errors in coordinating some activities which resulted in equip-

ment inoperability. Examples of this problem are a major bus outage and overlap-

ping maintenance resulting in loss of stack gas sample flow. In these cases, there

was a lack of understanding of the effect of the maintenance activity on plant

equipment. This resulted, in part, from a lack of communication between work force

and plant operations. The licensee has recognized the need for better communica-

tion between departments and strengthened the Plan of the Day status meeting and

has added other daily planning meetings. Generally, these meetings are effective

at surfacing plant problems and identifying who is responsible for corrective

action.

In addition to the coordination of major maintenance efforts, work control has

shown some weaknesses. Examples include: snubber repair in progress and the snub-

bers not being declared inoperable, inadvertently boring into the drywell shell,

secondary containment boundary work degrading containment integrity, and diesel

generator overhaul and testing. These examples demonstrate the need to continue

to reinforce that work activities must be planned, approved and effectively con-

trolled by the written work documents.

The licensee has undertaken several major initiatives to improve maintenance. The

first was a reorganization of the maintenance division. This fundamentally changed

the functional structure from one of " area" supervisors to one of " work discipline"

supervisors. In addition, the licensee has implemented changes to the work man-

agement system to computerize and simplify the job order generation process. The

effectiveness of this change has not been assessed, however, during implementation

of the new computerized system, some inadequate work control occurred. Also, a

Short Form Job Order was revised to change the scope to implement a modification

to a plant cooling water system, and it was not treated as a modification.

Another licensee initiative is increased training for workers and development of

a craft training facility. The licensee has also effectively used mockups for

major maintenance tasks such as the feedwater line freeze seal and torus to drywell

vacuum breaker repairs.

The licensee preventive maintenance program remains generally effective. It is

a specific area of focus of licensee attention to implement measures to better

identify specific preventive maintenance needs and more effectively track and pre-

dict equipment failures. These licensee initiatives are aimed at addressing long

term equipment performance and includes the Life of System Maintenance Program

(reliability centered maintenance). This has been implemented in a limited manner

on the service and instrument air system.

The licensee continues to implement a strong surveillance test program. Some areas

that require more attention are valve control during surveillance testing, accept-

ance of out of specification results, and that the test program include appropriate

_ _ _ _ _ - _ - _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ -_ _

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I

plant equipment (e.g., air accumulators and underground electrical cables). Sur-

veillance test valve control is also assessed in the Operations area. In addition,

NRC inspection noted a minor weakness in Measuring and Test Equipment (M&TE) con-

trol.

In general, the quality and accuracy of the maintenance and surveillance procedures

are good. The licensee is active in identifying and correcting weaknesses as they

arise. One specific area of observed weakness in surveillance testing is valve

position control. Situations have occurred where the same individual performed

the line up and the verification, procedural direction as to "as-left" positions

were not clear, and procedural direction for valve positions was in error. Two

of these situations resulted in equipment being misaligned and led to erroneous

surveillance test data on the containment spray heat exchangers and inability to

vent the isolation condensers. These valve dispositions have occurred, in part,

due to the incompleteness of incorporating plant modifications into surveillance

test procedures; and in part due to a lack of specific direction for valve positions.

The licensee is generally effective at identifying and addressing test discrepan-

cies and establishing acceptance criteria, however, several examples of inadequate

acceptance of test results have been seen. Out of specification results have been

accepted without explanation (MSIV closure), acceptance criteria have been changed

without a safety review (containment spray heat exchangers AP), IST out of speci-

fication problems without appropriate action (liquid poison), and questionable

baseline data methodology (emergency service water). While generally effective,

licensee performance shows the need for increased attention in the area of estab-

lishing acceptance criteria, and effectively evaluating test results.

The licensee has recognized the need for improvement in jumper control and also

the need to evaluate and improve the testability of systems. On a system by system

basis, the licensee is evaluating permanent design changes to improve testability.

This outage, a modification was implemented on the core spray system to eliminate

the need to lift leads and use jumpers. The licensee initiative to improve the

testability of systems demonstrates their commitment to improve long term surveil-

lance performance.

In conclusion, the licensee has in place generally effective maintenance and sur-

veillance test programs. Significant progress has been made in reducing mainten-

ance backlogs and a strong surveillance test program is being maintained. While

some areas of weaknesses have been seen in both areas, the licensee is responsive

to NRC concerns. Improvements have been seen in the areas of interdepartmental

communications and the plant material condition. Some areas where weaknesses have

been identified are: the identification and evaluation of maintenance rework items

and surveillance repeat failures and the administrative control of the work man-

agement system. Overall performance in the areas of maintenance and surveillance

has improved.

IV.C.2 Conclusion

Category 2.

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.

IV.C.3

'

Recommendation

Licensee: Provide NRC with schedule for implementation of reliability centered

maintenance control.

NRC: None.

_ ______ ____________-_- . _ _

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22  !

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IV.D Emergency preparedness (249 Hrs., 3%)

1

IV.D.1 Analysis

During the previous assessment period, licensee performance in this area was rated

Category 2. This rating was principally based upon observations of performance

during the full participation exercise. Although overall performance was satis-

factory, several recurrent weaknesses were identified. In addition, concerns were

identified relative to slow staff response to an actual pager call-out from an

Unusual Event.

During the current assessment period, a full participation exercise was observed

and three routine safety inspections were conducted. The licensee issued a new

corporate Emergency Plan for both GPU Nuclear sites. Because of the significance

of the changes, the Plan was submitted for NRC review prior to implementation.

During the review it was identified that the Plan did not reflect the guidance of

NRC Information Notice 83-28 concerning protective actions for a General Emergency.

Acceptable changes weta made to the Plan and it was subsequently implemented and i

distributed. '

A full participation exercise was conducted on May 11, 1988. The exercise scenario

was written to involve a security threat. The licensee's overall response was  ;

satisfactory, and, in some areas, performance was excellent. These areas included

control of a hazardous material spill, communication with the bomb disposal team,

and relocation of command and control from the Emergency Command Center to the

Technical Support Center. Several weaknesses were identified. The principal con-

cerns were in the areas of contamination control, adequacy of support to the Ener-

gency Support Director by the Technical Support Coordinator, and a question of

authority for the Operations Support Center. The number of weaknesses identified

is consistent with previous exercises. Overall exercise performance has been

adequate with approximately the same number of weaknesses identified from exercise

to exercise. This trend is apparently due to a lack of effectiveness of EP train-

ing.

During the first routine safety inspection, concerns were identified in two areas.

The first involved training: lists of staff participating in drills and exercises

were not maintained; and the Training Dep, tment's computerized database for

tracking EP training was not up to date. The second was in the area of dose as-

sessment and monitoring: the dose calculation model includes an excessively large

default iodine component which could result in overly conservative protective

action recommendations; and the volume of air samples collected by field teams is

so large that the collection filter may saturate making the results unreliable.

During the se'cond routine safety inspc:: tion, the inspectors determined that the

licensee was responsive to many NRC concerns. The Emergency Dose Calculational

Manual has been revised and many but not all calculational conservatism have been

removed. However, the concern regarding the default iodine component in the dose

model and the suitability of field sampling equipment and methodology to collect

iodine still had not been adequately addressed. This raises a concern regarding

_ _ - - _ _ _ _ _ _ _ - _ _ . . _ _ _ - - __ .

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23

the licensee's approach to resolution of technical issues. The licensee demon-

strated satisfactory response and personnel call-out to an actual Unusual Event

during the inspection. Several improvements have been made to emergency response

facilities and equipment. The licensee has renovated the Emergency Operations

Facility, installed a remote siren verification system, replaced the auto-dialer

call-in system by a computer based system, established a back-up Operational Sup-

port Center and is completing installation of a second siren activation system.

Staffing is adequate both for emergency preparedness maintenance and in numbers

of trained emergency response personnel.

Efforts to improve the emergency preparedness program are evidenced by the fact

that Emergency Preparedness staff routinely handles 43 ongoing activities and at

the time of the inspection was involved in 12 special projects. Some of these

activities include 26 improv9 ment actions in areas that have been completed or were

in progress at the time of the inspection.

Oyster Creek Directors have become involved regularly in emergency preparedness

training with the result that the need to reschedule training has almost vanished.

The Training Department has also introduced several innovative approaches and a

computerized data base is in place which tracks emergency preparedness training.

The site and field team air samplers are being replaced by a system which will col-

lect a sample without risk of saturation. Stack and turbine offgas monitoring

systems are being upgraded, and an Evacuation Time Estimate update study is being

undertaken. One issue which still requires licensee action is the training of

Technical Support Center engineers in accident analysis other than Core Damage

Assessment.

In summary, the licensee has committed adequate resources to emergency preparedness

and has demonstrated adequate response to GPU and NRC identified concerns. The

Director for the Environmental and Radiological Controls Division expends about

twenty percent of his time on EP issues. Technical issues have been and are being

resolved. Site management has become routinely involved in emergency preparedness

activities and training has also responded to needs for improvement. There are

no offsite problems. The persistent number of exercise weaknesses identified re-  ;

mains a concern. Finally, the licensee has not yet resolved NRC concerns regarding  ;

an overly conservative dose assessment model or the lack of training of TSC engi-

neers in severe accident analysis.

IV.D.2 Conclusion

Category 2.

IV.D.3 Recommendation

None.

- _ _ _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ .

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IV.E Security (134 Hrs., 1.5's)

I V . E .1 ~ Analysis

Two special and one routine physical security inspection were conducted by region-

based physical security inspectors. Routine inspections by resident inspectors

were conducted throughout the assessment period. An NRC Regulatory Effectiveness

Review was conducted in July 1988.

During the previous assessment period, the licensee's performance in this area was

Category 1. This rating was based upon continued implementation of the licensee's

self-assessment program, its enforcement history, a strong training and qualifica-

' tion program and the implementation of security equipment upgrades.

Dt..ng this assessment period, the licensee's security systems were reviewed during

a Regulatory Effectiveness Review (RER), and program implementation was evaluated

during a routine and two special region-based physical security inspections. Con-

tinuing inspections by the NRC resident inspectors were conducted during the period.

In the two previous SALP reports, two longstanding regulatory issues were identi-

fied as being addressed by the licensee. Both of these issues were resolved during

this period; however, resolution of one enhancement of the perimeter intrusion

detection system required several schedule extensions, and the other, a control

room issue, was initially found to be unacceptable by the NRC and another proposal

was submitted, which was found to be acceptable. Considering the nature and com-

plexity of the issues, the licensee demonstrated an adequate response to the NRC's

l concern, albeit, timeliness could have been better.

Corporate security management continued to be actively involved in all site secur-

ity program matters. This involvement included visits to the site by the corporate

staff to provide assistance, program appraisals and direct support in the budgeting

and planning processes affecting program modifications and upgrades. Security

personnel are also actively involved in the Region I Nuclear Security Association

and other industry groups engaged in nuclear plant security matters. This demon-

strates program support from upper 1.r ~ anagement.

The licensee continued the use of self-inspection techniques to provide oversight

of security program implementation and measurement of personnel performance. A

well developed training and qualification program and on-the-job performance

evaluations contributed to minimize personnel errors by members of the security

organization during routine operations. However, during outages, maintenance pro-

I jects resulted in the degradation of vital barriers, without prior notification

of the security department, on several occasions. Additionally, on one occasion,

operations personnel did not notify security personnel that a protected area bar-

rier had been degraded. Because security was not notified of these degraded bar-

riers, compensatory measures were not implemented for extended periods. Also,

during the current outage, members of the security force had to work a significant

amount of overtime to support the outage work. This may have contributed to a j

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25

reduction in the alertness of security force members since on two separate occa-

sions security force members who were controlling access to vital areas allowed

individuals whose access authorizations had expired to enter the vital areas.

These cases did not result in major degradation in security, but they did have the

potential to do so. Management had planned to augment the security force with

fifteen temporary contract watchmen to support the outage work, however, only five

were able to successfully pass licensee screening and training requirements.

The licensee submitted two security event reports in accordance with 10 CFR 73.71

during this assessment period. In addition, on two occasions, the NRC identified

events that should have been reported but were not. A contributing factor in the

failure to make the required reports was a misinterpretation of 10 CFR 73, Appendix

G.

The RER, which was conducted in July 1988, reviewed the licensee's ability to meet

the general performance requirements of 10 CFR Part 73. The RER report identified

strengths in some areas and contained recommendations for upgrades in other areas.

The licensee is reviewing the report and has not yet responded.

During this assessment period the licensee submitted four revisions to the Security

Plans in accordance with provisions of 10 CFR 50.54(p). Two of the revisions were

reviewed and found to be acceptable and two revisions are currently under review

by the NRC. The licensee also submitted revisions to the Security Plan in response

to the 10 CFR 73.55 Miscellaneous Amendments and Search Requirements. The revisions

contained commitments which meet the objectives of the rule change and were found

to be acceptable. The licensee responses to requests were not timely but were,

in general, technically sound.

{ In summary, the licensee continues to maintain an effective, performance-oriented

1 security program. Management attention to and support of the program are evident

in most aspects of the program implementation. However, weaknesses were observed

in the management efforts expended to maintain security awareness among other site

personnel to maintain adequate security staffing during extended outages, and

to understand NRC's reporting requirements for security events led to an overall

decline in performance during the period.

IV.E.2 Conclusion

Category 2.

IV.E.3 Recommendation

None.

w_____-_____-_______ _

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26

IV.F Engineering / Technical Support (1716 Hrs., 20%)

IV.F.1 Analysis

During the previous assessment period, licensee performance in this area was rated

Category 3. This rating was principally based on multiple examples of inadequate

root cause analysis, ineffective problem solution once the root cause was identi-

fied, poor technical reviews, long outstanding unresolved problems, delays in im-

plementation of NRC requirements, failure to meet commitments, communication prob-

lems, weakness in vendor control, and the fact that little change has been noted

over the period of time covered by the past three SALPs. The previous SALP board

also noted continued inconsistent performance during the assessment period. The

licensee was encouraged to expedite completion of the technical support self as-

sessment (TSSA) (which was started by the licensee in response to a recommendation !

by the SALP Board in 1986) and initiation of an associated corrective action plan. ,

1

During this SALP period, the quality of engineering support activities continued

to be inconsistent. Early in the SALP period, the licensee was actively engaged

in addressing the weaknesses and concerns identified ir, previous SALP Reports. i

These initiatives slowed down significantly during the assessment period due to

events that required the licensee's immediate attention and resources. Thus, the

licensee failed to complete the TSSA and initiate corrective action as recommended

by the previous SALP Board.

The licensee has taken several positive steps to enhance the effectiveness of the

Corporate Technical Function Division. Programs were developed and established

to incorporate safety perspective in engineering work prioritization, to trend and

analyze technical information, to enhance the quality of root cause analyses, to

improve engineering configuration management, design basis documents and as-built

drawings, to conduct Safety System Functional Inspections and to provide formalized

training to improve the quality and timeliness of safety reviews and plant modifi-

cations, Architect Engineers (AE) were placed on retainer and effectively used

to supplement the licensee's staff, providing the licensee with a wide spectrum

of engineering resources at short notice.

As a result of the above efforts, the following improvements were noted in the

support provided by the corporate Technical Function Division staff. Unlike pre-

vious outages, the corporate staff was able to complete practically all engineering

work prior to the commencement of the recently completed 12 R outage. The engi-

neering work back log was substantially reduced during this assessment period.

Prompt, conservative and comprehensive corrective actions for ISI and Appendix R

issues were developed and provided to the site. The engineering support provided

to resolve the isolation condenser steaming issue and the associated AIT concerns

was thorough, well coordinated, of good quality and was provided in a timely manner.

The licensee's efforts to address NRC Bulletins 79-02 and 79-14 were also extensive l

and of good quality. However, it must be noted that it took the licensee almost

ten years to complete this task.

.

. _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _

_ _ _ . _ _ . . . _ - - _ - - - - - - - - - - - - - - - - - - ' - - - -

-$ $4

I

i . l

.

27

In spite of the above improvements in capability and performance, several instances

- of inadequate engineering and technical support were noted. Examples of these ,

problems are discussed later in this section. Since similar problems were not 4

observed when site and corporate resources were both focused on the same technical

issues, it appears that the licensee still does not have an effective mechanism

to determine when site and corporate coordination is necessary or to always engage

and employ appropriate combinations of licensee resources to resolve site engi-

neering problems.

Efforts are being made to improve communication between engineering and operations

organizations. Corporate policy is being revised to encourage rotational assign-

ments for engineers between corporate and sites. However, instances of inadequate

communications between site and corporate personnel continue. For example, the

engineering personnel did not adequately inform the operations personnel about a

potential diesel generator bus over loading condition. Specific operator actions

are required to avoid over loading of this bus. The necessary operator training

or direction was not established as operations personnel were not aware of the

required operator actions. Instances in which plant changes were implemented

without involving the established modification process, site engineers or corporate

engineers include: the replacement of a reactor coolant system sampling valve with

another valve that was three times heavier, the removal of a resin column under

a work request and not under the configuration control requirements, and the change

out of an IRM range switch without the system engineer involvement. As stated

previously, when corporate and site technical personnel worked together, good de-

signs and engineering resolution were normally produced.

Instances of lack of inquisitiveness to understand technical issues and to identify

root causes of problems continue. For example, upon identification by the NRC of

the anomalous steam line temperature during the first isolation condenser steaming

event, the licensee performed a literature search for explanation. This literature

search yielded no explanation and no further evaluation was conducted by the lic-

ensee until the second isolation condenser developed a similar condition. Simi-

larly, the licensee identified several significant weaknesses in the activities

related to NRC Bulletin 79-02 and 79-14 during last SALP period; however, the lic-

ensee decided to take no actions until concerns were raised by the NRC inspectors.

As discussed further in the safety a:sessment/ quality verification section, the

licensee's initial resolution of the Preliminary Safety Concern (PSC) involving

the inoperability of the automatic depressurization system was another clear ex-

ample of shallow analysis of a newly identified problem.

Concerns for the adequacy of engineering resource commitments to the resolution

of long standing problems remains. Examples of these problems include: the erratic

operation and failure of the intermediate range monitors; degradation of the emer-

gency service water system discharge butterfly valve due to throttling; inadequate

emergency service water pump performance; and erratic performance of acoustic moni-

tors.

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .

- - _ _ - _ _ - _ _ _ _ _ _ _ _ _

P l

<

. . i

4.

.

28 i

As' stated in the Safety Assessment / Quality Verification section of this report, i

the safety review process was generally good and the quality of the reviews

improved. However, the licensee does not -always appropriately document the.

basis'for conclusions. For example, when the licensee's re-analysis of the

torus-attached piping indicated that the calculated stresses might be above

allowables, the licensee determined the matter was not reportable to the NRC.

When questioned by the NRC, the licensee maintained that there was no safety

significance to this issue as the analysis was overly conservative, but had no

documented analysis to back up that position. Subsequently, the licensee

completed a state-of-the-art- analysis and was able to demonstrate that the

stresses in question were within allowables.

The accuracy, quality and availability of plant engineering drawings remain a

problem. Although the SS0MI found drawings representing recent modifications to

be good and to generally reflect as-built conditions, routine NRC inspections and

discussion with operators determined that older drawings are frequently inaccurate,

unreadable.or not easily locatable. Problems precipitated by these deficiencies

are illustrated in the following examples: (1) inadequate as-built drawings con-

tributed 'to the stack gas monitor being made inoperable during the performance of

maintenance; (2) relanding of a loose wire in the control room resulted in a plant

response different from that expected, based on a review of plant drawing, and

(3) an operator was unable to identify the source of power to the reactor building

to torus vacuum relief valve since the appropriate drawings were not readily

available.

In summary, the licensee responded positively to the concerns identified in

previous SALP reports. They initiated measures to enhance the effectiveness

of the corporate engineering division, improved the quality of root cause

analysis and engineering support,'and reduced engineering work back log.

However, examples of inadequate engineering solutions, insensitivity to technical

problems, failure to meet commitments, lack of reliable design basis documents

and failure to resolve long standing technical deficiencies continue to exist.

The licensee's engineering resources are not as effectively used at this site

as at TMI, although both are supported by the same corporate staff. The

difficulty in correcting the recurring and long standing problems at this site

may be explained by the volume of the issues; the latter, in large part, is

precipitated by the vintage and age of the plant. It may also be explained by

the lingering coordination problems and communication gap between this site and

the corporate engineering office. However, the licensee has made significant

progress in resolving issues and the performance for the assessment period has

shown improvement, particularly with regard to corporate activities.

IV.F.2 Conclusion

Category 2.

IV.F.3 Recommendations

Licensee: None.

NRC: Perform a SSFI during the fourth Quarter of FY 89.

t

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

__

___ _____ - -- . . _ _ .

,

e s

.

4

29

IV.G Safety Assessment / Quality Verification (417 Hrs., 5%)

IV.G.1 Analysis

In previous SALP reports, Assurance of Quality and Licensing Activities were evalu-

ated in separate sections of the report. This new section (Safety Assessment /

Quality Verification) has been created not only to consolidate those two sections

but also to encompass activities such as safety reviews, responses to NRC generated

initiatives such as Generic Letters and bulletins and to provide a broad assessment i

of the licensee's ability to identify and correct problems related to nuclear '

safety.

1

In the previous SALP, Assurance of Quality and Licensing Activities both received

Category 2 ratings. At that time, it was noted that the trend indicated that

the licensee had improved in the licensing area. The SALP report identified as

strengths management's commitment to safety and quality training programs for

management, craft personnel, and corporate level person'31, and other changes

made to improve overall management effectiveness and gosd communications between

licensee management and NRC staff. Weaknesses included procedure compliance,

unplanned outages from equipment malfunction, engineering support, and operations.

Licensee performance regarding timely submittals of LERs was also identified as

an area requiring improvement.

During the current SALP period 78 licensing actions were under review. Action

has been completed on 39 of these actions. Many of the significant actions com-

pleted involved complex issues and were generally well planned, technically sound,

showed thorough licensee analysis and in most cases were timely. Examples include

upper drywell .shell corrosion problems, compliance with ATWS Rule (10 CFR 50.62),

and new curves for operation beyond 10 effective full power years. However,

there were some issues where extensive staff interaction was required to resolve

issues and some miscellaneous amendments and SEP items were slow being submitted.

The licensee's safety review process is good and in general the quality of reviews

.

has improved. Also, the licensee is participating through industry groups to im-

prove overall guidance in this area. NRC review of the 50.59 review program at

Oyster Creek identified that in most cases reviews were of high quality. However,

in one case the licensee's justification was not clearly discussed and resulted

in accepting a situation not specifically authorized by regulation.

The staff has also audited the overall erosion / corrosion monitoring program in-

volving the pipe wall thinning of high energy carbon steel piping systems. As a

result of the audit, the staff concluded that in general the licensee's program

is above industry standards. The plant has appropriate controls in place and man-

agement has made a commitment to continue to implement an erosion / corrosion control

program at Oyster Creek.

!

_ _ _ - _ _ _ - -_-___ ____ ___--


- _ _ . . _ _ _ _ _ _ , _ _ _ , _ _ _ _ _ _ _ _ _

pir-----

O  %

.

.

30

The licensee's QA program remains generally effective. Staffing is adequate and

training is appropriate. QA monitorings were detailed, comprehensive, and con-

ducted by knowledgeable personnel. The licensee has a comprehensive system of

audits to verify conformance with all aspects of the QA p ogram. Audits were

thorough and comprehensive. The licensee has also substantially revised their

QA plan to enhance oversight and refocus QA responsibility.

Followup to QA findings in most instances was found to be appropriate. However,

in several instances, such as the inadequate safety review program for maintenance

short forms, the QA findings had to be escalated due to insufficient corrective

action and slow response from management. Also, the finding that certain plant

modifications were being used by the plant before completing the formal modifica-

tion turnover process was not addressed. QA reviewed storage of spare parts in

shop spaces and took some corrective action, but did not document those findings.

This is one instance in which both improper activities were being conducted and

QA was ineffective in correcting the condition.

In the area of procurement and spare parts control, NRC reviews have identified

deficiencies which reflect weaknesses. These included procedural problems and the

absence of controls for spare parts housed outside the warehouse. The latter

problem had been identified by the licensee's QA organization, but effective cor-

rective action had not been implemented. Improper control of shop spare parts

permitted defective components to be installed in source range monitors prier to

refueling.

Satisfactory performance of the licensee's offsite review committee (G0RB - General

Office Review Board) was noted. The issues reviewed and the board's presentation

of findings to management is satisfactory. Improvement in the onsite review group

(PRG - Plant Review Group) was also noted particularly in the areas of review of

events and the more prompt issuance of procedure changes.

During this SALP period, NRC inspectors and the licensee were made aware of com-

plaints dealing with management relations which fostered poor worker attitudes,

low morale, high turnover rates, and low productivity. A completed licensee in-

vestigation was thorough and made certain recommendations aimed at improving wor-

ker/ management relations.

The licensee continues to maintain an adequate training facility and staff.

One deficiency noted was the submittal of out-of-aate and incomplete training

material for NRC exam preparation. Also, committed training of fire watches

was not conducted. A significant improvement has been made in the training of

maintenance mechanics. Maintenance management provided a new mechanical main-

tenance laboratory for improved on-the-job training. Plant engineering also

maintains their own training program for the purpose of providing in-depth

understanding of plant systems. It was noted little interaction between

operators and the newly created system engineers was taking place. The inservice

inspection staff demonstrated a good understanding of ASME Code and regulatory

requirements indicating effective training in this area. The licensee is

continuing to apply the concept of teamwork and leadership to programs in the

organization.

- __ _ -

o .

.

.

31

Problems were identified with operator training on E0Ps. As a result, contracted

time has been increased on a generic simulator. A plant specific simulator will

not be available until October 1990.

GPUN maintains a policy for its employees which stresses a high standard of

integrity and procedure adherence. This is frequently reinforced through

training and memoranda from management. In order to improve performance at

Oyster Creek, an employee attitude survey was conducted and efforts were made

to resolve concerns expressed. Surveys were conaucted to assess personnel

attributes in order to balance shift crews to maximize shift performance.

Also, the licensee has within the Onsite Safety Review Group initiated a Human

Performance Evaluation System to further aid in providing recommendations to

improve operations. The group's efforts were hampered due to the inability to

provide a full staff. In general, the licensee is taking many initiatives to

improve performance.

During the defueling recently conducted, numerous errors occurred. Each of these

individual errors were appropriately critiqued and corrective action taken. In

an effort to improve defueling activities, direct involvement of the Vice President

and Director, Dyster Creek, occurred. The direct involvement of a high level of

management becoming heavily involved in operations when other measures appear to

have failed is considered to be a positive move.

Quality Assurance audits of radiological controls effluent and surveillance acti-

vities was good. Hewever, due to the overall pocr performance of the onsite radi-

ation protection program, it was concluded that the quality assuring activities

such as audits, assessments, and critiques were not effective in assuring quality.

The licensee has in place a procedure by which employees may bring safety concerns

to the attention of management. These issues are processed as Preliminary Safety

Concerns (PSC). Although a good initiative, several problems have been identified,

including timeliness of resolution, quality of reviews performed and a perception

on the part of some licensee employees that the system will not effectively resolve

issues. In two cases, superficial reviews were performed and the items closed.

Subsequent review identified that corrective action was necessary. In these in-

stances, the PSC process failed to correct the valid safety concerns. NRC assess-

ment overall is that the PSC program is not performing as the licensee intended.

The quality of the licensee's LERs continues to be good. The late reporting of

LERs was a problem in the past. This deficiency has been corrected. Supporting

I data and summaries provide additional information related to LERs. Significant

findings associated with LERs include one instance where control room procedures

were not updated to reflect conditions described in a report, an instance where

information was not reported clearly, and one instance which described a condition

in which an improvement in control room command responsibilities may have pre-

vented a violation. In another instance, an incorrect fuel zone level instru-

ment evaluation was performed. This was not recognized by the licensee and the

item was closed. One noteworthy finding was that LERs reported conditions that

had been previously identified in Preliminary Safety Concerns. Overall, LERs

_ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ .

_ .. . _ _ - - . _- _ - - - _ _ . - _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ . _ _ _ _ .

,

1

e s

4

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32

reported 17 events related to Technical Specification requirements, 6 related to

design criteria, 4 to Appendix R, and one to Appendix J. In general, no single l

cause could be attributed as responsible for any significant number of events.

t

In summary, management attention and involvement were responsive to licensing

issues, and licensing problems have generally been dealt with effectively and

in a timely manner. QA monitoring and audits were generally good; however, I

correcting of some QA findings was not timely. Offsite committee performance i

is good and improvement in onsite committee performance has been noted. The

licensee has in place policies which stress high standards of integrity. A

strong emphasis on training is being maintained. Deficiencies needing attention

were noted in the areas of installation and storage of ' shop spare parts. A

more significant concern which requires prompt and thorough resolution is the

effectiveness of the Preliminary Safety Concern process to identify and correct

deficiencies.

IV.G.2 Conclusion

Category 2.

IV.G.3 Recommendation

Licensee: Review current and previously closed Preliminary Safety Concerns to

verify that no outstanding safety issues remain unresolved.

NRC: None.

_1___-______________ . _ _ _ _ _ . _ _ _ _ _ _ _

_ _ - -

p 4.g ,,

, , .

.. ~

..

.SUPp0RTING DATA AND SUMMARIES.

1

.A. Investigations and Allegations Review

-A.1 Investigations

The NRC Office of Investigations completed two investigations during the SALP

period. 0ne. involved a self-initiated investigation to determine whether or not

licensee' statements made to NRC inspectors constituted a willful' material false

statement. The other involved investigation into the reported destruction of a

portion of an alarm tape by a licensed control room operator following the viola-

tion of a Technical Specification Safety Limit.

'A.2 Allegations

'

During this assessment period, seven allegations were received and acted upon.

One remains open~and five were closed. One was closed with the subject incorpor-

ated into a future inspection plan. Only one allegation was substantiated. The

one open allegation was turned over to the licensee for evaluation.

B. Escalated Enforcement Actions

B.1 Civil Penalties

One civil penalty involving a Technical Specification Safety Limit Violation that

occurred during the previous SAlp period, was issued during the current evaluation

period.

B.2 Orders

None.

C. Confirmatory Action Letters

None.

D. Licensee Event Reports

During the last assessment period 45 LERs were generated and during this period

46 reports were generated with four of these identified as voluntary reports.

Reports for the last period were generated at the rate of 3.9/ month and for this

period at the rate of 2.8/ month.

The greatest single cause for the events reported is personnel error. Eleven of

the 46 LERs reported (24%) were attributed to personnel error. The next largest

cause was attributed to equipment failure which was 8 (17%). The number of LERs

attributed to personnel error is decreasing. During the last period 64% of the

reports were attributed to personnel error. Analysis of the cause of personnel

errors did not indicate a general training problem.

SD/S-1

- - - _--_______

___ _ _ - _ _ _ _ - -

,, ,,

'

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&

~

Four events resulted from reactor scrams when shutdown, generally due to neutron

system noise spikes. Three were due to standby gas treatment system initiations

! resulting from water accumulation in the offgas line. Action.has been taken to

correct this condition.

To the extent possible during the NRC review of the LERs, where applicable, a con-

tributing cause was assigned. The most frequently noted contributing cause was .)

judged to be lack of management attention / poor supervision. Eleven of the 46 LERs '

(24%) had this attributed as a contributing cause.

The most frequent methods of identification of the LERs were control room indica-

tion 15, surveillance testing (6) and design reviews (5). Types of equipment in-

l

volved were mechanical 18, instrumentation (12) and electrical (6). No specific

conclusions were drawn from.these statistics.

The most frequently identified licensee corrective actions specified in the reports

were procedure changes (16), failed equipment repaired (10), increased training

(8), and making 'the report required reading (10). The effectiveness of the cor-

rective actions are difficult to assess, particularly the required reading of the

LERs.

Overall, LERs reported Technical Sr; edification violations (17), violations of de-

sign criteria (6),.of Appendix R (4), and one of Appendix J. In general, no single

cause could be attributed as responsible for any significant' number of events.

' Not identified as an LER at Oyster Creek but reported by another facility was the

design service water temperature being exceeded. The licensee has determined the

85 degree design service water temperature was exceeded. However, to date no de-

. termination of deportability has been made nor has the licensee's evaluation of

the effect of a higher than design service water temperature been comple~ted.

1

SD/S-2

, _ _ _ _ _ _ _ _ _ _ _ _ .___ _ _ _ _ _ _

_ _ _ _ _ . _ _ _ _ _ _ _ . _ _ _ __ _ _

go

l. .

.;

s

TABLE I

ENFORCEMENT ACTIVITY

A .~ Enforcement Activity

'

NUMBER OF VIOLATIONS BY SEVERITY LEVEL

Functional Area V IV III II I DEV ' TOTAL

Plant Operations 1 3 1 5

l

Radiological Controls 9 9

Maintenance / Surveillance 1 1

Emergency Preparedness

Security 1 3 4*

Engineering / Technical Support 2 8 10

Safety Assessment / Quality Verification 1 1

TOTAL 6 23~ 1 30*

  • 0ne additional security violation is pending final enforcement action ~ determina-

tion.

B. Violation Summary-

REPORT- SEVERITY FUNCTIONAL

NUMBER REQUIREMENT LEVfi AREA DESCRIPTION

87-28 10 CFR 50 App. B, V Maintenance / Identified maintenance

Criterion XII Surveillance and test equipment

discrepancies not )

evaluated as required.

87-37 Physical Security IV Security Vital area barrier

Plan found to have been

degraded. ,

87-39 T.S. 6.13, High IV Radiological Worker entered high

Radiation Area Controls radiation area without

dose rate instrument.

T-I-1

__ _ - _ _ _ _ _ _ - _ _ _ _ _ _ _ _ - _ _ _ ___ _

. .

-

__ - _ _- _ - -_ _ _ - _ _ -_ - _ -

,

f'+-'q.

-

,

'^

,

s. :

>

REPORT' SEVERITY FUNCTIONAL-

NUMBER- REQUIREMENT LEVEL AREA DESCRIPTION'

87-39 .T.S. 6.13, High IV Radiological Control of high radi-

Radiation Area Controls ation area access.

.

87-39 T.S. 6.11, Radiation IV Radiological Failure to adhere to ,

Protection Process Controls the requirement of a

radiation work permit.

87-41 T.S. 6.8.1, Station IV Operations Failure to follow pro-

Procedures cedures relating to

positioning of valves. ,

88-02 10 CFR 50.59_ IV Engineering / Failure to perform

Tech Support safety evaluation for

for reactor building

heating system being

out of service for ap-

proximately two years.

>

88-02 T.S. 6 8.1, Station IV Engineering / Inadequate procedure

Procedures Tech Support reviews.

88-04 T.S. 6.8.1, Station' IV Engineering / Controls to effect

Procedures Tech Support procedure revisions.

88-04 <T.S. 6.8.1, Station IV Engineering / Failure to adhere to

Procedures' Tech Support procedures relating

to snubber operability.

88-04 10 CFR 50, App. 8 IV Engineering / Failure to take prompt-

Tech Support corrective action tu

a nonconforming condi-

tion identified during  ;

snubber surveillance.  !

L 88-11- 10 CFR 10.101 (b) IV Radiological F.iilure to conduct

Controls adequate surveys.

88-13 T.S. 6.11, Procedure IV Radiological Failure to adhere to

for Personnel

.

Controls radiation work permit }

qadiation Protection requirements. >

88-14 T.S. 3.12. A.1, Fi re V Operations Fire detection instru-

Detection-Instrumen- mentation pressure

tation switch valved out. 1

T-I-2

1

- _ _ _ _ _ . - _ - _ _ _ _ _ _ - _ _ _ - - _ _ - - - - _ _ _ _ _ _ _ - - - - - _ - - - -

. __ ._ _ _ - _ . . _ _ _ _ _

________-_,

"

.F 4

,

o

REPORT SEVERITY FUNCTIONAL

NUMBER REQUIREMENT LEVEL AREA DESCRIPTION

88-14 Fire Protection DEV Operations Inadequate training

Program program for ignition

source fire watches.

88-15 10 CFR 50.59 IV Engineering /. Performance of an

Tech Support improper safety

evaluation.

88-21 T.S. 3.4.C, IV Operations Operation with one

Containment Spray containment spray loop

and Emergency out of service for a-

Service Water period greater than  !

System Operability allowed.

'

88-21 T.S. 6.8.1, Station IV Operations System placed into

Procedures service without current

valve checkoff.

88-21 T.S. 6.8.1, Station IV Engineering / Modification placed

Procedures Tech Support into service without

control room drawing

being updated.

88-28 10 CFR 50, App. J IV Engineering / Containment airlock

Tech Support not tested as required.

88-29 10 CFR 50, App. R V Engineering / A failure to meet Ap- ,

Tech Support pendix R requirements

was promptly corrected

and no written viola-

tion was issued.

88-31 10 CFR 20.201, IV Radiological Failure to conduct a

Surveys Controls survey.

88-31 T.S. 6.11, Radiation IV Radiological Worker failed to comply

Protection Program Controls with the requirements

of a radiation work

permit.

88-32 10 CFR 50.54 (p), V Security Change to physical

Physical Security security plan without

System Commission approval.

l

T-I-3

_- -

_

- ___ - _-__ _-____ - ____-___._-_-_ _ __ _ _ _ _ _ _ - _ _ _ - _ - _ _ - _ _ - _ _ _ -_ ,- -,

.

. f ., , g

.

l; , y v' '

a

REPORT' . SEVERITY . FUNCTIONAL

l NUMBER REQUIREMENT LEVEL AREA DESCRIPTION'

E -88-33 10 CFR 50, App. B I V, . Safety Assess . Failure to control

ment / Quality storage of items out-

Verification side' warehouse.

'88-33 Physical Security IV Security ' Degraded vital area

' Plan barrier.

88-33- 10 CFR Part 73.71, IV. Security' Failure lto. report de-

App..G, Sect. I.(c)- graded vital area bar-

rier.

.

88-35 'T.S. 6.8.1, Station V Engineering / Several procedures

Procedures Tech Support- 1ssued without approval

signatures.

88-37 10 CFR 20.201 (b) IV Radiological Failure to evaluate

Controls -radiation hazard

created by control rod

drives awaiting pro-

cessing.

88-37 LT.S. 6.8.1, Station IV Radiological Inadequate procedure

Procedures Controls for the' control of rod

drive work.

.

T-I-4

- -- _ = - _ _ - _ _ _ _ _

, - _ - _

_ - _

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l

TABLE II

LISTING OF LERS BY FUNCTIONAL AREA  ;

l

AREA A B C D E X TOTALS

Operation 5 4 2 1 1 13

'

Radiological Controls 2 1 3

Maintenance / Surveillance 2 4 6 2 14

Emergency Preparedness

Ser.urity

Engineering / Technical Support 6 7 2 1 16

Safety Assessment / Quality Verification __ __ __ __ __ __

TOTALS 15 16 10 4 1 46

Cause Codes *:

A - Personnel Error

B - Design, Manufacturing, Construction or Installation Error

C - External Cause

D - Defective Procedure

E - Component Failure

X - Other

  • Cause Codes in this table are based on inspector evaluation and may differ from

those specified in the LER.

I

i

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!

l

l T-II-1

I

. . _ _ _ _ _ . _ _ _ _ _