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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20202F9161998-01-29029 January 1998 Special Rept:On 980128,two of Three Fire Protection Pumps Were Removed from Svc as Result of Sys Configuration Necessary to Support Planned Maintenance.Fire Pumps Were Returned to Svc on 980128 ML20138F5801997-04-29029 April 1997 Special Rept:On 970402,declared Reactor Bldg Wide Range Gas Monitor Inoperable.Caused by Ruptured Pump Diaphragm. Initiated Work Order,Installed Replacement Pump & Declared Pump Operable ML20137Y2171997-04-15015 April 1997 Special Rept:On 961220,util Rail Car Was Released to Burlington Northern Railroad from Monticello Nuclear Plant. Rail Car Was Delayed in Chicago as Result of Problems W/Bill of Lading on Computer Sys.Rail Car Was Delivered on 970131 ML20101E8321996-03-15015 March 1996 Special Rept:On 960314,two of Three Fire Pumps Removed from Svc for Planned Mod Work.Returned Both Fire Pumps to Svc Same Day ML20094E4371995-10-31031 October 1995 Special Rept:On 951010,sys Engineer & Technicians Reintiated Work on B Channel of Reactor Bldg Vent Radiation Monitor, After Providing Proper Notification to Main Control Room. Caused by Incorrect Channels Removed from Svc ML20082R6601995-04-19019 April 1995 Special Rept:On 950404,discovered That Manual Isolation Valves for 'A' Channel in Closed Position.Cause of Failure to Correctly Position Valves Will Be Assessed.Valves Placed in Required Position & Demonstrated Operability ML20082E5661995-04-0606 April 1995 Special Rept:On 950326,pump Discharge Relief Valve for Electric Screen Wash/Fire Pump Became Inoperable.Valve Had to Be Secured to Permit Installation of an Isolation Device. Pump Returned to Operational Status After Device Installed ML20080G4731995-02-0101 February 1995 Special Rept:On 950119,two of Three Fire Protection Pumps Out of Svc for Period of Approx 15 H.Action Taken for Planned Preventative Maint on Two Check Valves & Drain Valve in Fire Suppression Sys.Roving Fire Watch Established ML20067D1351994-02-23023 February 1994 Special Rept:On 940126,fire Door 105 Declared Inoperable Due to Inability to Close Properly.Caused by Higher than Normal Differential Pressure Between Plant Administration Bldg & Turbine Bldg.Cause of Failure Corrected ML20117A5801992-11-24024 November 1992 Special Rept:On 921020,determined That RHR Sample Supply Loops a & B Excess Flow Check Valves Not Included in ASME Section XI Program.Caused by Lack of Proven Test Procedure. Valves Incorporated Into Third 10-yr ASME Program ML20082G9261991-08-15015 August 1991 Special Rept:On 910719,potential for Inoperable Penetration Fire Barrier Identified.Caused by Use of Less Conservative, But Technically Acceptable,Design Alternatives in Plant Const.Vents Will Be Rerouted ML20244E5941989-06-16016 June 1989 Special Rept:On 890603,two Out of Three Diesel Fire Pumps Were Inoperable for Less than 12 H.Caused by Diesel Fire Pump Day Tank Outlet Valve Being Closed Instead of Fill Valve During Performance Test 1158.Test Revised BECO-86-173, Partially Withheld Security Event Rept:On 861107,HVAC Duct, Penetrating Vital Area,Removed by Contracted Craft Workers Before Notifying Security.Cause Not Stated.Security Oversight of Subj Contract Work Intensified1986-11-12012 November 1986 Partially Withheld Security Event Rept:On 861107,HVAC Duct, Penetrating Vital Area,Removed by Contracted Craft Workers Before Notifying Security.Cause Not Stated.Security Oversight of Subj Contract Work Intensified BECO-86-171, Partially Withheld Security Event Rept:On 861106,temporary Vital Area Barrier Insp Found Barrier Could Be Breached. Barrier Modified & Compensatory Security Measures Released1986-11-10010 November 1986 Partially Withheld Security Event Rept:On 861106,temporary Vital Area Barrier Insp Found Barrier Could Be Breached. Barrier Modified & Compensatory Security Measures Released ML20211E0731986-09-26026 September 1986 Unplanned Operating Event Rept 85-6, Manual Reactor Trip Following MSIV Closure Due to Inadvertent Emergency Feedwater Actuation,851009 BECO-86-125, Partially Withheld Security Event Rept:On 860826,bomb Threat Received.Search Initiated.No Suspicious Objects Found1986-08-29029 August 1986 Partially Withheld Security Event Rept:On 860826,bomb Threat Received.Search Initiated.No Suspicious Objects Found ML20238E4601986-08-28028 August 1986 Partially Withheld Secrity Event Rept:On 860824,bomb Threat Received for Plants.Bomb Search Initiated.No Suspicious Objects Found ML20211K8211986-06-18018 June 1986 Special Rept:On 860521,valid Failure Occurred on Div 2 Diesel Generator During Performance of Tech Spec Surveillance 4.8.1.1.2.Caused by Failure of Jacket Water Thermostatic Control Valve to Open ML20238E4591986-06-17017 June 1986 Partially Withheld Security Event Rept:On 860612,withheld Discovery Made Re 860604 Moderate Loss of Security Effectiveness.Caused by Inadequate Post Orders & Training for Assignment.Assignments Will Be Specifically Addressed 05000000/LER-1986-009, Ro:On 860312,discovered That LER 2-86-04 & LER 86-009 Not Submitted to Nrc.Caused by Misplaced Repts.Repts Telecopied to Nrc.Procedure for Distribution of Repts Revised1986-04-14014 April 1986 Ro:On 860312,discovered That LER 2-86-04 & LER 86-009 Not Submitted to Nrc.Caused by Misplaced Repts.Repts Telecopied to Nrc.Procedure for Distribution of Repts Revised BECO-86-016, Partially Withheld Security Event Rept:On 860215 Security Officer Appeared to Be Asleep at Post at Vital Area Penetration.Unathorized Entry of Vital Area Did Not Occurr. Security Officer Relieved of Duty & Suspended1986-02-20020 February 1986 Partially Withheld Security Event Rept:On 860215 Security Officer Appeared to Be Asleep at Post at Vital Area Penetration.Unathorized Entry of Vital Area Did Not Occurr. Security Officer Relieved of Duty & Suspended BECO-85-220, Partially Withheld Security Event Rept:On 851204 Vertical Pipe Chase Not Locked.Lock Removed When Surveys Indicated Radiation Level Below Requirement for Locked High Radiation Level.Pipe Chase Will Be Secured1985-12-0909 December 1985 Partially Withheld Security Event Rept:On 851204 Vertical Pipe Chase Not Locked.Lock Removed When Surveys Indicated Radiation Level Below Requirement for Locked High Radiation Level.Pipe Chase Will Be Secured AECM-84-0204, Special Rept 84-017/0:on 840304,Fire Doors 1A401 & OC219 Blocked Open to Support Maint Activities.Fire Watches Established Until Doors Restored1984-04-0606 April 1984 Special Rept 84-017/0:on 840304,Fire Doors 1A401 & OC219 Blocked Open to Support Maint Activities.Fire Watches Established Until Doors Restored ML20198H3691983-11-14014 November 1983 Ro:On 831003,results of as-found Tests Indicated Crosby Main Steam Relief Valves Had Lift Points Exceeding Tech Spec Limits.Valves Disassembled & Rebuilt by Mfg ML20081G9561983-10-25025 October 1983 Ro:On 831024,trip Coil for Reactor Recirculation Motor Generator Set 11 Drive Breaker Failed to Trip Automatically. Investigation Ongoing.Trip Coil Replaced ML20105D2431983-06-24024 June 1983 Special Rept:Five Individuals Found to Have Received Radiation in Excess of 10CFR20.101 Limits W/O Required Documentation.Caused by computer-based Sys Feature Allowing Use of Outdated Info & Personnel Error.Procedures Revised ML20066E0131982-11-0101 November 1982 Ro:On 821031,thru Wall Defect Found on C 12-inch Recirculation safe-end to Pipe Weld Joint.Resolution Under Investigation ML20064E5141982-10-21021 October 1982 Ro:On 821020,thru Wall Defect Found on E 12-inch Recirculation Sys Safe End to Pipe Weld Joint.Indications Will Be Documented as Revision to RO 82-16 Reported on 820928.Resolution Being Investigated ML20064E4761982-10-11011 October 1982 Ro:On 821009,linear Indications Confirmed to Exist on Three Addl Welds in Recirculation Sys.Indications Will Be Documented as Revision to RO 82-16 Reported on 820928. Resolution Being Investigated ML20071N4361982-09-28028 September 1982 Ro:On 820928,crack Indication in End Cap of a Recirculation Riser Confirmed by Radiography.Indications Initially Detected by Ultrasonic Exam During Normal Inservice Insp. Remedial Measures Under Investigation ML20071L8261982-09-16016 September 1982 Ro:On 820915,leak Discovered on Primary Containment Suppression Chamber Nitrogen Control Sys Inboard Isolation Valve (AO-2378).Leakage Less than Tech Spec Allowable Leakage ML20053E8071982-06-0202 June 1982 RO Iii:On 810224,failure of Discharge Valve on Instrument & Svc Air Compressor Resulted in Loss of Instrument Air Sys Pressure Causing Plant Scram.Failed Check Valve Replaced W/Similar Unit ML20137G4501981-03-24024 March 1981 Ro:During walk-through of Operator Training Program, O-ring Seal of Filter Holder Found Not Seated Properly Causing Partial Bypass of Filter for Air Sucked Into instrument.Filter-in Lock Adjusted ML20071F0861980-09-25025 September 1980 Ro:On 800912,sample Analysis Taken from Hydrazine Addition Tank Indicated Sodium Chloride in Tank.Anonymous Telcon Indicated Salt May Have Been Added Prior to Labor Strike by Unknown Persons ML20058L3431978-07-31031 July 1978 Ro:On 780728,control Rod Drive 30-47 Delayed Approx 1.4 Before Scramming.Buna N Disk in Plunger Broken in Pieces.Plungers on 242 Scram Pilot Valves & Two Backup Scram Pilot Valves Removed & Replaced ML20090L8311978-06-0202 June 1978 Ro:On 780505,steam Leak Noted in RCIC Inlet Steam Line & Drain Line to Condenser.Caused by Pinhole Failure on Weld on 300 Lb Socket Weld.Hole Temporarily Patched ML20091A9941978-03-10010 March 1978 Ro:On 780309,smear Survey of Chem Nuclear Sys Inc Model 4-45 Shipping Cask Disclosed Max Surface Contamination of 25,900 Disintegrations Per Min Per 100 Square Centimeters.Cask Will Be Decontaminated ML20127G6171978-02-0202 February 1978 Advises That on 780202,during Surveillance Test,One Suppression Chamber to Drywell Vacuum Breaker Failed to Reclose Following Exercise.Plant Shutdown Initiated ML20086D5141978-01-0606 January 1978 Telecopy Ro:On 780105,discovered That One of Two Nuclear Engineering Co Model B3-1 Shipping Casks Provided w/1-inch Diameter Lid Bolts Rather than 1-1/4 Inch Size Specified in Certificate of Compliance 6058 ML20086D5201977-12-14014 December 1977 Telecopy Ro:Heating Steam Coil Leak in Reactor Bldg Ventilation Supply Unit V-AH-4A Resulted in Freezing of Condensate at Inlet to Unit & Subsequent Inoperability of Associated Secondary Containment Isolation Dampers ML20086D5371977-10-14014 October 1977 Telecopy Ro:Insp of Internal Torus Catwalk Support Structure Revealed That Catwalk Mitered Sections Not All Attached to Horizontal Catwalk Support Plates in Some Manner.Attachment Locations Will Be Upgraded ML20086D5501977-10-13013 October 1977 Telecopy Ro:On 771012,local Leak Rate Testing of MSIV AO-2-80A & Nitrogen Instrument Air Sys Isolation Valve CV-7436 Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation ML20086D5541977-10-0505 October 1977 Telecopy Ro:On 771004,local Leak Rate Testing of HPCI Sys Discharge Isolation Check Valve HPCI-9 Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation ML20086D5571977-09-29029 September 1977 Telecopy Ro:On 770929,local Leak Rate Testing of Core Spray Inboard Isolation Check Valve AO-14-13A Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Cause Under Investigation ML20086D5611977-09-14014 September 1977 Telecopy Ro:On 770913,local Leak Rate Testing of Core Spray Inboard Isolation Check Valve AO 14-13B Indicated That Leakage Exceeded Tech Spec Acceptance Criteria.Related Event on 770914 ML20086D5671977-09-12012 September 1977 Telecopy Ro:Main Steam Drain Isolation Valve MD 2373 & Main Steam Outboard Isolation Valve AO 2-86A Exceeded Tech Spec Acceptance Criteria for Local Leak Rate Tests ML20086D6421977-07-11011 July 1977 Telecopy Ro:On 770709,determined That Recombiner Sys a Offgas Flow Control Valve PCV 7489A Could Be Opened W/ Controlling Solenoid Valve Deenergized.Valve Held from Svc Pending Investigation ML20137G4461977-06-23023 June 1977 Ro:On 770621,radioactive Source Containing 200 Mci Cs-137 Recovered from Brine Well 33.Incident Described in ML20086F0801977-06-0606 June 1977 Ro:On 770506,plant Iodine & Particulate Release Rate Exceeded 4% of Facility Tech Spec Averaged Over Second Calendar Quarter of 1977.Caused by Fuel Perforations Coupled W/End of Cycle Testing & Reactor Coolant & Steam Leaks ML20058K6111977-03-0909 March 1977 Ro:On 770223,discovered Withdrawal of in-sequence Control Rod Resulted in Period Less than 5-s & IRM Scram 1998-01-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D1261999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Monticello Nuclear Generating Plant.With ML20216E7031999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Monticello Nuclear Generating Plant.With ML20210Q0521999-08-0404 August 1999 Safety Evaluation Approving Relief Request 10 to License DPR-22 Per 10CFR50.55a(g)(6)(i).Inservice Exam for Relief Request 10,Parts A,B,C,D & E Impractical & Reasonable Assurance of Structural Integrity Provided ML20210Q6611999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Monticello Nuclear Generating Plant.With ML20209F7901999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Monticello Nuclear Generating Plant.With ML20195H0351999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Monticello Nuclear Generatintg Plant.With ML20206N1721999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Monticello Nuclear Generating Plant.With ML20205N0861999-04-12012 April 1999 Safety Evaluation Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20205P5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Monticello Nuclear Generating Plant.With ML20204H4951999-03-18018 March 1999 SER Concluding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Monticello.Therefore Staff Concludes Licensee Adequately Addressed Action Required in GL 96-05 ML20205G7391999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Monticello Nuclear Generating Plant.With ML20202F7901999-01-25025 January 1999 1999 Four Year Simulator Certification Rept for MNGP Simulation Facility ML20199E4871999-01-0606 January 1999 SER Accepting Licensee 951116,960214 & 0524 Responses to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode ML20205H0561998-12-31031 December 1998 Northern States Power Co 1998 Annual Rept. with ML20199F6211998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Mngp.With ML20198P0691998-12-28028 December 1998 Safety Evaluation Concluding That NSP Proposed Alternative to Paragraph III-3411 of App III to 1986 Edition of Section XI of ASME Code Provides Acceptable Level of Quality & Safety.Alternative Authorized ML20198D0751998-12-10010 December 1998 Safety Evaluation Supporting NSP Proposed Change to EOPs to Use 2/3 Core Height as Potential Entry Condition Into Containment Flooding ML20198B2531998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Monticello Nuclear Generating Plant.With ML20195E3691998-11-12012 November 1998 Safety Evaluation Concluding That Licensee USI A-46 Implementation Has Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20195D2381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Monticello Nuclear Generating Plant.With ML20198J4451998-10-22022 October 1998 Rev 2 to SIR-97-003, Review of Test Results of Two Surveillance Capsules & Recommendations for Matls Properties & Pressure-Temp Curves to Be Used for Monticello Rpv ML20154L3471998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Monticello Nuclear Generating Plant.With ML20153F0511998-09-21021 September 1998 Rev 2 to MNGP Colr,Cycle 19 ML20153E9361998-09-0808 September 1998 Rev 1 to MNGP Colr,Cycle 19 ML20153B0861998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Monticello Nuclear Generating Plant.With ML20237B8461998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Monticello Nuclear Generating Plant ML20236W5041998-07-21021 July 1998 ISI Exam Summary Rept - Refueling Outage 19 ML20236R1941998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Monticello Nuclear Generating Plant ML20249A5861998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Monticello Nuclear Generating Plant ML20247K3971998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Monticello Nuclear Generating Plant ML20217D8731998-04-13013 April 1998 Rev 0 to MNGP Colr,Cycle 19 ML20217F6431998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Monticello Nuclear Generating Plant ML20216D1041998-03-0505 March 1998 Rev 21 to Operational QA Plan ML20216H6481998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Monticello Nuclear Generating Plant ML20203G1431998-02-10010 February 1998 Rev 2 to Inservice Insp Exam Plan,Third Interval,920601- 020531 ML20203B2821998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Monticello Nuclear Generating Station ML20202F9161998-01-29029 January 1998 Special Rept:On 980128,two of Three Fire Protection Pumps Were Removed from Svc as Result of Sys Configuration Necessary to Support Planned Maintenance.Fire Pumps Were Returned to Svc on 980128 ML20216D2071997-12-31031 December 1997 1997 Annual Rept for Northern States Power Co ML20198P2201997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Monticello Nuclear Generating Plant ML20197J8131997-12-31031 December 1997 Revised Evacuation Time Estimates for Plume Exposure Pathway Emergency Planning Zone at Monticello Nuclear Power Plant. W/One Oversize Drawing ML20203J7131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Monticello Nuclear Generating Plant ML20199G7051997-11-19019 November 1997 Safety Evaluation Authorizing Relief Request 8 of Third 10 Yr Inservice Insp Interval ML20199H8181997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Monticello Nuclear Generating Plant ML20217K2081997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Monticello Nuclear Generating Plant ML20216H7771997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Monticello Nuclear Generating Plant ML20217K2741997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Monticello Nuclear Generating Plant ML20196H1081997-07-0808 July 1997 Rev 20 to Operational QA Plan ML20149E2921997-06-30030 June 1997 Monthly Operating Rept for June 1997 for MNGP ML20141B9271997-06-30030 June 1997 LOCA Containment Analyses for Use in Evaluation of NPSH for RHR & Core Spray Pumps ML20148S6341997-06-23023 June 1997 NPSH - Rept of Sulzer Bingham Pump 1999-09-30
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NSF NORTHERN STATES POWER COMPANE i NONTICELLO WCLEAR GENERATIfG PLANT Monticello, Minnesota 55362
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February 21, i972 S g W.,)k~ 4 c . ,
s h .?- t. F1 cu svw n 00CKETED A l
- c z i Dr. Peter A. Morris, Director FE820197& 5 % Vhadd!
j Division of Reactor Licensing -
REcuurosy
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United States Atomic Energy Commissio g grenosOk' cm e g g rg
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Washington, D. C. 20545 -
Dear Dr. Morris:
as N0f#1 CELLO WCLEAR GENERATIFG PLAfd Docket No. 50263 License No. OPR-22 ADDITIONAL I NFORMATION ON If6TRUMEfRATION Pf0BLEM3 This letter is to inform you of additional information obt ined concerning several plant instrumentation problems which were the subject of previously submitted reports.
- 1. Main Steam Line High Flow i instrumentation Problems (See report to Dr. Morris dated November 23, 1971)
Sixteen switches with a range of 0-70 psid were installed in the main steam line high flow isolation system on September 1,1971, to replace the original 0-200 psid switches. The lower range switches were ;
installed because of lower than expected differential pressure measure- J ments from the main steam line flow nozzles. During surveillance {
testing on November 11 and 12,1971,. three of the switches were found 1 to exhibit signs of high friction or binding in their mechanisms and l another switch was found to exhibit non-repeatable trip settings. The i four defective switches were immediately replaced by 0-200 psid l switches previously used for the protective function. The remaining I twelve swiiches were replaced on November 13, 1971. )I One of the defective switches was returned to the factory for inspection. }
The vendor's inspection revealed that the torque tube jewel bearing )
was contaminated by a lead paste compound that was used to seal the '
joint between the instrument case and the di fferential pressure unit.
The contamination which occurred during switch assembly at the factory, caused excessive hysteresis in the torque tube movement. The vendor '
l indicated that the jewel bearing contamination was a random occurrence in switches of this type and model, and 'therefore there was no assurance that other similar instruments did not have, the potential for similar ;
failures. A review of the instrumentation used in the plant protection system was conducted to identi fy all instruments with the potential for l
l 8709280271 870921 4 g 4 g) (' $' rl1 PDR FOIA MENZ87-111 PDR
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-a contaminated jewel bearing. A total of 39 instruments were so identified and inspected following the vendor's recommended proce-du ro. No jewel- bearing contamination was found.
.The switch which was found to exhibit _ a non-repeatable trip setting was investigated at the site. Tests disclosed that the erratic -
operation'was caused by a loose pivot pin on the cam follower assembly and was not due to the snap action switch, as previously reported.
The loose pivot- pin caused the trip point to vary between 109% steam flow and 127% steam flow. This problem also appears to have resulted a
from a manufacturing error. All plant instruments of this t inspected for excessive deadband (greater that 5% of range) ype and were:
were found to be satisfactory.
- 2. Failure of ECCS Pumo Start Permissive Switch and Relav (See report i to Dr. Morris dated December 20, 1971) x .1 i
On November 20, 1971, while performing a surveillance test, the trip ;
setting of ECCS Pump Start Permissive Switch PS 2-3-53 A, switch #2, '
was found to be 12 psi below the required setting of >_ 450 psig.
During this surveillance test it was also discovered that a relay in I the ECCS pump start permissive logic failed to energize when pump ;
start pernnssive switch PS 2-3-53 A, switch #1 was closed. l An investigation of the setpoint problem revealed that the two switches contained in PS 2-3-53 A were not designed for the 125 V DC application for which they were being used, but were designed for 115 !
V AC service. The wrong switches were initially specified for this application. An analysis performed by the instrument manufacturer revealed that the microswitch contacts in the instrument were burned due to excessive current. The vendor believes the burned contacts ;
may have caused the change in the instrument setpoint. J A check of plant instrumentation disclosed that 22 instruments with microswitches rated for 115 V AC were being used in 125 V DC ci rcui ts.
These switches (listed below) have all been' replaced with switches i
rated for 125 V DC.
Insirument Funetion PS 2-3-49 A & B LPCI Recire Loop Selection PS 2-3-50 A & B LPCI Recire Loop Selection PS 2-3-52 A ECCS Valve Open Permissive PS 2-3-53 A & B ECCS Pump Start Permissive PS 23-68 A through D HPCI Steamline Low Pressure Isolation PS 2-128 A & B RHR Shutdown Cooling Isolation PS 14-47 A & B Core Spray Header High Pressure Alarm PS 14-44 A through D Core Spray "AC Interlock" l PS 13-78 RCIC Turbine Exhaust Diaphram i
High Pressure Alarm l
1 W_- . _- _ _ - - $
Instre ent Function !
PS 13-72 A & 8 RCIC Turbine High Pressure Alarm The investigation of the relay which failed to energize when the
~
switch #1 of PS 2-3-53 A was closed, revealed that the pull-in voltage was set too high., This resulted in an intermittent failure of the relay to energize. The pull-in voltage of the relay was found to be 110 V DC (the operating voltage available at the relay was measured to be 125 V DC). The pull-in voltage was reset to 80% of the operating voltage and the relay ai r gap was reduced. All of the DC relays of this typeintheplanthadbeenpreviouslysetandtestedat80% pull-in voltage in accordance with a field engineering memo in August 1970.
Additional investigation revealed that the 80% setting is applicable only to AC relays. All DC relays of this type were reset to the factory recommended 60% pull-in voltage. The relay which failed to operate during the surveillance test was the only relay of this type to experience a failure since the DC relays were set and tested in August 1970.
- 3. Failure of ECCS Valve Ooenino Permissive Switch (See report to Dr.
Morris dated December 21, 1971.)
On November 24, 1971, while performing a surveillance test, the trip setting of ECCS Valve Opening Permissive Switch PS 2-3-53 B, switch
- 1, was found to be 42.5 psi below the required setting of >_ 450 psig. An investigation revealed that the instrument lacked a setpoint
" locking" device, a modification recommended by the instrument manu-facturer. The locking device was innediately installed and the instrument was calibrated to trip at 460 psig.
Locking devices were also installed on all sim-ilar instruments with snap action switches used in the plant protection systems.
The main steamline high flow instruments have mercury type switches and are not designed for setpoint locking devices. Since past-experience has shown the setpoints of these mercury switches to be quite stable, the switches have not been redesigned or modified to include a setpoint locking device.
Locking devices were installed on the following instruments:
I ns t runeni Function DPIS 23-76 A & B HPCI High Steam Flow Isolation DPIS 23-77 A & B DPIS 13-83 RCIC High Steam Flow isolation DPIS 13-84 DPIS 14-43 A & B Core Spray Line Break Detection PS 2-52 B ECCS Valve Opening Permissive r
- _ _ _ n
i:- * .
,; [. ' . . , - . . . . .
.- - 4'-
I ns t ru ent Funct ion DPIS 2-129 A through D LPCI Loop Selection
? DPIS 2-136 A & B " " "
DPIS 2-137 A & B " " -"
DPI S 2-138 A & B - " " "
DPIS 2-139 A & B " " "
DPS 10-92 A &' B RHRHeatEschanger/P.
All the above i-strumentation problems were corrected prior to plant startup on-January 24, 1972. Detailed reports on these problems -
have been prepa ed at -the plant and are svailable for the Compliance-I nspecto r.
Iours very trul.,
a" o.
L. O. Mayer Director of Nuclear Support Services .
LOWLLWkik cc: ~B H Grier i
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