ML20207M306

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Corrected SALP Rept 50-247/85-98 for Aug 1985 - Jul 1986, Based on Discussions During 861121 Mgt Meeting
ML20207M306
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 07/31/1986
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20207M241 List:
References
50-247-85-98, NUDOCS 8701130138
Download: ML20207M306 (60)


See also: IR 05000247/1985098

Text

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ENCLOSURE 2

SALP REPORT

U.S. NUCLEAR REGULATORY COMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

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INSPECTION REPORT 50-247/85-98

CONSOLIDATED EDISON COMPANY, INC.

-INDIAN POINT STATION - UNIT 2

ASSESSMENT PERIOD: AUGUST 1, 1985 TO JULY 31, 1986

BOARD MEETING DATE: SEPTEMBER 23, 1986

8701130138 87010s 7

DR ADOCK 0500

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TABLE OF CONTENTS

Page

I. INTRODUCTION. . . . . . . . . . . . . . . . . . . . . . . . . 1

A. Purpose and Overview . . . . . . . . . . . . . . . . . . 1

B. SALP Board Members . . . . . . . . . . . . . . . . . . . 1

C. ' Background . . . . . . . . . . . . . . . . . . . . . . . 2

C.1 Licensee Activities. . . . . . . . . . . . . . . . 2

C.2 Inspection Activities. . . . . . . . . . . . . . . 2

II. CRITERIA. . . . . . . . . . . . . . . . . . . . . . . . . . . 4

, III. SUMMARY OF RESULTS. . . . . . . . . . . . . . . . . . . . . . 6

3.1 Overall Facility Evaluation. . . . . . . . . . . . . . . 6

3.2 Facility Performance . . . . . . . . . . . . . . . . . . 7

IV. FUNCTIONAL AREA ASSESSMENTS . . . . . . . . . . . . . . . . . 8

A. Plant Operations . . . . . . . . . . . . . . . . . . . . 8

8. Radiological Controls and Chemistry. . . . . . . . . . . 11

C. Maintenance. . . . . . . . . . . . . . . . . . . . . . . 15

D. Surveillance . . . . . . . . . . . . . . . . . . . . . . 18

E. Fire Protection. . . . . . . . . . . . . . . . . . . . . 20

F. Emergency Preparedness . . . . . . . . . . . . . . . . . 22

G. Security and Safeguards. . . . . . . . . . . . . . . . . 24

H. Outage Activities. . . . . . . . . . . . . . . . . . . . 27

I. Training and Qualification Effectiveness . . . . . . . . 30

J. Assurance of Quality . . . ............... 33

K. Licensing Activi ties . . . . . . . . . . . . . . . . . . 36

V. SUPPORTING DATA AND SUMMARIES . . . . . . . . . . . . . . . . 39

i A. Investigation and Allegation Review .......... 39

B. Escalated Enforcement Actions. . . . . . . . . . . . . . 39

C. Management Conferences . . . . . . . . . . . . . . . . . 39

D. Licensee Event Reports . . . . . . . . . ........ 39

, TABLES

Table 1 TABULAR LISTING OF LERs BY FUNCTIONAL AREA . . . . . . . 41

Table 2 INSPECTION HOURS SUMMARY . . . . . . . . . . . . . . . . 42

Table 3 ENFORCEMENT SUMMARY . . . . . . . . . . . . . . . . . . 43

Table 4 INSPECTION REPORT ACTIVITIES . . . . . . . . . . . . . . 46

Table 5 LISTING OF ALL AUTOMATIC TRIPS AND UNPLANNED SHUTOOWNS . . 49

Table 6 NRR SUPPORTING DATA AND SUMMARY . . . . . . . . . . . . . 52

FIGURES

Figure 1 ' NUMBER OF DAYS SHUT DOWN . . . . . . . . . . . . . . . . . 54

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I. INTRODUCTION

A. Purpose and Overview

The Systematic Assessment of Licensee Performance (SALP) is an inte-

grated NRC staff effort to collect the available observations and

data on a periodic basis and to evaluate licensee performance based

upon this information. The SALP program is supplemental to normal

regulatory processes used to ensure compliance to NRC rules and

regulations. The SALP program is intended to be sufficiently

diagnostic to provide a rational basis for allocating NRC resources

and to provide meaningful guidance to the licensee's' management to

promote quality ni safety of plant construction and operation.

An NRC SALP Board, composed of the staff members listed below, met on

September 23, 1986, to review the collection of performance observa-

tions and data and to assess the licensee performance in accordance

with the guidance in.NRC Manual Chapter 0516, " Systematic Assessment

of Licensee Performance." A summary of the guidance and evaluation

criteria is provided in Section II of this report.

This report is the SALP Board's assessment of the licensee's safety

performance at the Indian Point Station, Unit 2 for the period

August 1, 1985 through July 31, 1986.

B. SALP Board Members

W. F. Kane, Director, Division of Reactor Projects (DRP)

W. V. Johnston, Deputy Director, Division of Reactor Safety

4 S. J. Collins, Deputy Director, Division of Reactor Projects

R. M. Gallo, Chief, Projects Branch No. 2, DRP

L. J. Norrholm, Chief, Reactor Projects Section 28, DRP

S. A. Varga, Director, PWR Project Directorate #3, NRR

J. D. Neighbors, Licensing Project Manager, NRR

L. W. Rossbach, Senior Resident Inspector, Indian Point 2

C. J. Cowgill, Acting Chief, Emergency Preparedness and

Radiological Protection Branch

Other NRC Attendees

M. M. Shanbaky, Chief, Facilities Radiation Protection Section

W. J. Lazarus, Chief, Emergency Preparedness Section

R. R. Keimig, Chief, Safeguards Section

G. C. Smith, Safeguards Specialist

D. P. LeQuia, Radiation Specialist

P. W. Kelley, Resident Inspector, Indian Point 2

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C. Background

1. Licensee Activities

e unit set several station performance records in 1985. These

in luded the highest capacity factor (88.8%) and most days of

con nuous operation (156). The unit shut down automatically on

Janua 13, 1986 when a main boiler feedwater pump tripped due to the

failure of a hose in its high pressure oil system. The unit remained

shut dow and began the cycle 7/8 refueling outage. The low pressure

turbine ro rs were replaced during the outage and tests of the main

electrical nerator revealed a number of shorts. The rotor was

pulled and ex nsive examination and repairs to the stator coils were

begun. Althoug the electrical generator remained out of service,

the refueling, r or replacement, and other scheduled maintenance

items were complet on schedule and the unit was brought critical

for zero power physi s testing on March 12. The unit was then shut

down while the electr al nerator repairs continued.

Plant heatup was begun on 3, however, reactor criticality was

delayed until May 25 due t everal component failures. The unit

reached 100% power on June 2

During this assessment period, nit tripped twelve times and had

two unplanned shutdowns, giving a t rate of 2.32 trips per 1000

hours critical. This is higher tha average trip rate of 1.04

for all Westinghouse units in 1985. rips and shutdowns are

described in Table 5 and are discusse ection IV.A.

The licensee made several organizational during this SALP

assessment period. The managers of Quality rance and Nuclear

Training, the Instrumentation and Control En , and the

Maintenance Engineer were newly assigned. The for Projects Manager

was given increased planning and materials contr 1 responsibilities

under the title of Planning and Projects Manager; nd, now reports to

the Nuclear Power Generation Manager. The position f Manager -

Fire, Safety and Security was created and filled. Th's position

provides for additional management oversight of the se rity program

and incorporates supervision of the security, safety, an fire pro-

tection programs under one administrator. The licensee a o created

a Records Management Center. On August 1, 1986, the licens began

the onsite consolidation of several engineering support group previ-

ously located at corporate headquarters. A new General Manage of

Technical Support began his duties on August I as part of this

consolidation.

2. Inspection Activities

Two NRC resident inspectors were assigned to the unit throughout

the entire assessment period,

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C. Background

1. Licensee Activities

The unit set several station performance records in 1985. These

included the highest capacity factor (88.8%) and most days of

continuous operation (156). The unit shut down automatically on

January 13, 1986 when a main boiler feedwater pump tripped due to the

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failure of a hose in its high pressure oil system. The unit remained

shut down and began the cycle 7/8 refueling outage. The low pressure

turbine rotors were replaced during the outage and tests of the main

electrical generator revealed a number of shorts. The rotor was

pulled and extensive examination and repairs to the stator coils were

begun. Although the electrical generator remained out of service,

the refueling, rotor replacement, and other scheduled maintenance

items were completed on schedule and the unit was brought critical

for zero power physics testing on March 12. The unit was then shut

down while the electrical generator repairs continued.

l Plant heatup was begun on May 3, however, reactor criticality was

l delayed until May 25 due to'several component failures. The unit

reached 100% power on June 20.

During this assessment period, the unit tripped twelve times,

I including one subcritical trip, and had two unplanned shutdowns,

giving a trip rate of 2.13 trips per 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> critical. This is

higher than the average trip rate of 1.04 for all Westinghouse units

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in 1985. These trips and shutdowns are described in Table 5 and are

discussed in Section IV.A.

The licensee made several organizational changes during this SALP

assessment period. The managers of Quality Assurance and Nuclear

Training, the Instrumentation and Control Engineer, and the

Maintenance Engineer were newly assigned. The Major Projects Manager

was given increased planning and materials control responsibilities

under the title of Planning and Projects Manager; and, now reports to

the Nuclear Power Generation Manager. The position of Manager -

Fire, Safety and Security was created and filled. This position

provides for additional management oversight of the security program

I

and incorporates supervision of the security, safety, and fire pro-

tection programs under one administrator. The licensee also created

a Records Management Center. On August 1, 1986, the licensee began

! the onsite consolidation of several engineering support groups previ-

ously located at corporate headquarters. A new General Manager of

Technical Support began his duties on August I as part of this

consolidation.

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2. Inspection Activities

Two NRC resident inspectors were assigned to the unit throughout

the entire assessment period.

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Special team inspections were conducted as follows:

Environmental Qualification, May 12-16, 1986

  • Health Physics Appraisal, June 16-20, 1986

Probabilistic Risk Assessment Based Inspection,

July 21-August 1, 1986

The scope of the probabilistic risk assessment team inspection

was formulated based on a review of the Indian Point

Probabilistic Safety Study and an NRC sponsored peer review by

Sandia Laboratory (NUREG/CR-2934). The risk significant

accident initiators, equipment failures, and operator errors

contained in the top twenty four dominant accident sequences

were studied. Major areas selected for review included recovery

actions from a loss of offsite power, as well as from a loss of

coolant accident. Assessments were made of the ability of the

operations staff to respond to events, of the reliability of

plant hardware, and of the effectiveness of management controls

in areas such as maintenance, testing, and quality assurance.

The overall results showed an experienced and knowledgeable

staff. A number of weaknesses in Emergency Operating Procedures

were identified, as discussed in Section IV.A. Several hardware

discrepancies relating to configuration management were identi-

fled, as discussed in Sections IV.A and C.

Inspection hours are summarized in Table 2 and total 4241 hours0.0491 days <br />1.178 hours <br />0.00701 weeks <br />0.00161 months <br />

for the assessment period. Table 3 lists specific enforcement

data. Inspection report activities are summarized in Table 4.

This report also discusses " Training and Qualification

Effectiveness" and " Assurance of Quality" as separate functional

areas. Although these topics, in themselves, are assessed in

the other functional areas through their use as criteria, the

two areas provide a synopsis. For example, quality assurance

effectiveness has been assessed on a day-to-day basis by

resident inspectors and as an integral aspect of specialist

inspections. Although quality work is the responsibility of

every employee, one of the management tools used to measure

Quality Assurance effectiveness is reliance on quality inspec-

tions and audits. Other major factors that influence quality,

such as involvement of first-line supervision, safety

committees, and worker attitudes, are discussed in each area.

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II. CRITERIA

Licensee performance is assesssed in selected functional areas. Each

functional area represents areas significant to nuclear safety and the

environment and are normal programmatic areas.

The following evaluation criteria were used to assess each functional

area:

1. Management involvement in assuring quality.

2. Approach to resolution of technical issues from a safety standpoint.

3. Responsiveness to NRC initiatives.

4. Enforcement history.

5. Reporting and analysis of reportable events.

6. Staffing (including management).

7. Training effectiveness and qualification.

However, the SALP board is not limited to these criteria and others may

have been used where appropriate.

Based upon the SALP Board assessment each functional area evaluated is

classified into one of three performance categories. The definitions of l

these performance categories are:

Category 1: Reduced NRC attention may be appropriate. Licensee manage-

ment attention and involvement are aggressive and oriented toward nuclear

safety; licensee resources are ample and effectively used such that a high

level of performance with respect to operational safety and construction -

quality is being achieved.

Category 2: NRC attention should be maintained at normal levels.

Licensee management attention and involvement are evident and are con-

cerned with nuclear safety; licensee resources are adequate and are rea-

sonably effective such that satisfactory performance with respect to

operational safety and construction quality is being achieved.

Category 3: Both NRC and licensee attention should be increased.

Licensee management attention or involvement is acceptable and considers

nuclear safety, but weaknesses are evident; licensee resources appear

strained or not effectively used such that minimally satisfactory

performance with respect to operational safety and construction quality is

being achieved.

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The SALP Board has also categorized the performance trend over the last

quarter of the SALP assessment period. The categorization describes the

general or prevailing tendency (the performance gradient) during the last

quarter (May - July 1986) of the SALP period. The performance trends are

defined as follows:

Improving: Licensee performance has generally improved during the last

calendar quarter of the current SALP assessment period.

, Consistent: Licensee performance has remained essentially constant

during the last calendar quarter of the current SALP

assessment period.

Declining: Licensee performance has generally declined over the last

calendar quarter of the current SALP assessment period.

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III. SUMMARY OF RESULTS

3.1 Overall Facility Evaluation

j The major site management changes made during the last assessment-

period have contributed to improved performance in several areas.

The leadership of the Vice President, Nuclear Power was instrumental

in bringing about these improvements and is continuing to have a

positive impact on overall performance.

Management effectiveness has improved as noted in the recent program

inspection for Appendix R and also, in the control of outage activi-

ties. Program changes in the Radiation Protection area have been

effectively implemented resulting in an improved program and SALP

rating. Based on inspections conducted during this assessment period,

the terms of the September 27, 1984 Order Modifying License were

determined to have been satisfactorily completed. Some recent

organizational changes have not been in effect for a sufficient time,

however, to adequately assess their impact, such as your recent

security initiatives.

Despite the overall improvements noted during this assessment period

two areas warrant specific attention. Our review notes that reactor

trips occurred at a rate higher than the industry average. Previous

efforts to reduce this rate have not been effective. We acknowledge

that a response team was recently initiated to provide a more in-

depth investigation of trips. Our analysis indicates to us a need

for additional operator training dedicated to normal evolutions.

Correspondingly, your actions should assure that the simulator

upgrade is properly and expeditiously completed, so that such training

will be available to provide a more accurate simulation of those

evolutions.

Secondly, the amount of maintenance remaining to be completed is of

concern to us. Your actions should consider the review of maintenance

staffing and prioritization including efforts to integrate probabilistic

risk assessment into the maintenance program to provide a work

prioritization system based on risk.

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3.2 ~ Facility Performance

Category Category Recent

Functional Area Last Period This Period Trend *

(August 1, 1984 to (August 1, 1985

July 31, 1985) to July 31,1986)

A. Plant Operations 2 2 Consistent

B. Radiological Controls 3 2 Consistent

and Chemistry

C. Maintenance 2 2 Consistent

D. Surveillance 1 1 Consistent

E. Fire Protection 2 1 Consistent

F. Emergency 1 2 Improving

Preparedness

G. Security and 1 2 Improving

Safeguards

H. Outage Activities 2 1

I. Training and Qualification Not Evaluated 2 Consistent

Effectiveness

J. Assurance of Quality Not Evaluated 2 Consistent

K. Licensing Activities 2 2 Improving

  • Trend during the last quarter of the assessment period.
    • No basis to determine a performance trend.

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IV. FUNCTIONAL AREA ASSESSMENTS

A. Plant Operations (23%, 981 Hours)

1. Analysis

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The previous SALP determined the operations area to be

Category 2. Nine trips occurred during the previous SALP period

and it was recommended that the licensee review the causes of

trips to reduce their frequency. It was also recommended that

the integration of the shift technical advisors (STAS) on shift

be evaluated and that the quality of written and verbal reports

be improved.

During this assessment period, the unit was critical for

approximately 5175 hours0.0599 days <br />1.438 hours <br />0.00856 weeks <br />0.00197 months <br /> (216 days) and had twelve trips. These

trips were distributed as follows: ten automatic trips while

critical, one manual trip while critical and one manual trip

while subcritical. Two other unplanned shutdowns also ocorred

during this assessment period.

Four trips can be attributed to operator errors, three by

licensed operators, one by a nonlicensed operator. The three

errors by licensed operators occurred during normal operations

and indicate a need for additional training time dedicated to

the conduct of evolutions such as power escalation and a need

for increased accuracy in the simulation of these evoldtions.

The error by the nonlicensed operator was due to failure to

follow procedures. Other instances of operators failing to

follow procedures have not been identified.

One trip occurred due to a drawing not being updated following

plant construction. The licensee's corrective actions in this

area are being followed by the inspectors.

In March 1986, at the end of the refueling outage, the licensee

initiated a trip response team whose goal is to reduce the

number of trips. The group investigates the event, determines

root causes, and recommends and tracks corrective actions. The

trip response team leader is also an active participant in the

Westinghouse owners group trip reduction and assessment program.

The effectiveness of this effort has not been assessed.

In October 1985 the licensee implemented symptom-oriented

Emergency Operating Procedures (EOPs). All licensed operators

received six weeks of training in their use prior to implementa-

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tion. Operators have been observed to use the E0Ps proficiently

during actual events. General simulator performance and exami-

nation results of SR0 classes in this assessment period and the

. previous assessment period were above average. Operators have

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accepted the E0Ps and appear to be well trained in their use.

All six SR0 candidates examined during this assessment period

received licenses.

E0Ps were not being evaluated and updated in a timely manner.

Apparently, due to a cumbersome change process in place for

E0Ps, changes were being accumulated for single revisions.

Also, the E0Ps were not being thoroughly reviewed as evidenced

by several procedure inadequacies identified by the PRA team

inspection.

The control room environment is a strength, consi- mtly neat

and orderly. Operators conduct themselves in a .ssional

manner. Shift turnovers are thorough and effect1ve.

Daily morning meetings chaired by the operations manager, are

used to coordinate each day's activities in the areas of

maintenance, surveillance, irad waste and modification

construction. In addition to a representative in each of these

areas, the meetings are attended by QA, health physics, and

security.

There are currently 43 licensed Senior Reactor Operators (SR0s)

and 14 licensed Reactor Operators (R0s). The shift staffing

consists of two SR0s and two R0s. One of the R0s is a roving RO

who can perform duties outside of the control room as long as he

is not more than ten minutes away. There are a total of six

shifts with the above manning. Starting at the end of the

refueling outage the licensee changed to twelve hour shifts.

The overtime usage is kept to a minimum and well within the

limits of NRC Generic Letter 82-12.

The licensee has evaluated how to provide better shift integra-

tion of STAS as recommended in the previous assessment. Assess-

ment of study findings and scheduled implementations are under

consideration.

The quality of the Station Nuclear Safety Committee (SNSC) and

the Nuclear Facilities Safety Committee (NFSC) reviews of events

and other items remains good. As discussed in Section 4.10, a

new SNSC Chairman was appointed effective August 1, 1986 as part

of a consolidation of Corporate office engineering personnel

with the onsite organizatio'n.

The licensee has been responsive to several NRC findings during

this assessment period, taking prompt corrective actions.

However, one area that has been a continuing problem since the

previous assessment period is in making prompt notifications by

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the Emergency Notification System. -Instances were identified in

which the required notifications were not made, were made late

or were incomplete. Required corrective actions are currently

being developed by the licensee in this area.

The four operations training programs (NPO, R0, SR0/SWS, STA)

were submitted to INPO on schedule during this SALP period.

Management attention to housekeeping has been evident by the

emphasis given to housekeeping at morning planning meetings and

by frequent plant tours by management. Despite management

attention, performance in this area has been inconsistent.

Control of contamination has improved, and as a result of a large

effort by the licensee, contaminated areas have been reduced by

50% since January 1985. The licensee continues to demonstrate a-

resolve to maintain a clean plant through programs to

decontaminate the Maintenance and Outage Building and utility

tunnel. Control of trash has generally been good, however,

various inspections have identified construction debris in the

pipe penetration area and containment building and trash in the

fuel storage building. Contrary to administrative control

measures, unsecured gas cylinders have been observed during NRC

inspections. Loose gas cylinders were also identified in a QA

surveillance report but no effective actions were taken to

resolve the finding.

In summary, plant operations are well managed. However, trips

are occurring at a rate higher than the industry average.

Emergency operating procedures were implemented well but need

to be thoroughly reviewed and updated in a timely manner.

2. Conclusion

Rating: Category 2

Trend: Consistent

3. Board Recommendations

Licensee: None

NRC: None

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B. Radiological Controls and Chemistry (21%, 903 Hours)

Analysis

On September 27, 1984, an Order Modifying License was issued due

programmatic deficiencies in the licensee's radiological

co trols program. During the previous SALP assessment period,

the icensee developed a completely revised radiation protection

prog m and trained personnel in the implementing procedures.

Full i lementation of the revised program occurred one month

prior to the end of the previous SALP assessment period. During

the curre SALP assessment period, the NRC conducted several

inspections to verify the licensee's program improvements and to

evaluate the ffectiveness of program implementation.

There were nine nspections and a Health Physics Appraisal by

radiation special f areas affecting radiological controls

during this period, sident inspectors also monitored radio-

logical controls rel activities.

Radiation Protection

The licensee has demonstra timely and thorough development of

program elements, including: fective communication cnd dis-

semination of radiological co information to the site

staff; establishment of coopera w rking relationships with ,

all plant groups; initiation of t ALARA incentives; and

development of concise health phys cs cedures. The licensee

has also demonstrated aggressive ac io d strong management

oversight in implementing the progra ements.

The licensee has a sufficient number of qualified and

trained individuals functioning at all le is within the

radiation protection organization. There re, however, some

changes within the organization during this sessment period.

Specifically, the Radiation Protection Oversig t Committee was

dissolved. This committee had been chartered t provide

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oversight of the Radiation Protection (RP) Progra following

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issuance of the Order Modifying License in 1984. e respon-

sibilities previously delegated to this committee ha been

reassigned to the Radiation Safety Committee, a subco ittee of

the Nuclear Facilities Safety Committee. In addition, e

position of Radiological Assessor, which had been vacant or

several months, was filled through the promotion of a plan

radiological engineer. This is a high visibility position, nd

a key link to help assure the continued quality of the RP

program.

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B. Radiological Controls and Chemistry (21%, 903 Hours)

1. Analysis

On September 27, 1984, an Order Modifying License was issued due

to programmatic deficiencies in the licensee's radiolcgical

controls program. During the previous SALP assessment period,

the licensee developed a completely revised radiation protection

program and trained personnel in the implementing procedures.

Full implementation of the revised program occurred one month

prior to the end of the previous SALP assessment period. During

the current SALP assessment period, the NRC conducted several

inspections to verify the licensee's program improvements and to

evaluate the effectiveness of program implementation.

There were nine inspections and a Health Physics Appraisal by

radiation specialists of areas affecting radiological controls

during this period. Resident inspectors also monitored radio-

logical controls related activities.

Radiation Protection

The Itcensee has demonstrated timely and thorough development of

program elements, including: effective communication and dis-

semination of radiological controls information to the site

staff; establishment of cooperative working relationships with

all plant groups; initiation of strong ALARA incentives; and

development of concise health physics procedures. The_ licensee

has also demonstrated aggressive action and strong management

oversight in implementing the program elements.

The licensee has a sufficient number of well qualified and

trained individuals functioning at all levels within the

radiation protection organization. There were, however, some

changes within the organization during this assessment period.

Specifically, the Radiation Protection Oversight Committee was

dissolved. This committee had been chartered to provide

oversight of the Radiation Protection (RP) Program following

issuance of the Order Modifying License in 1984. The respon-

sibilities previously delegated to this committee have been

reassigned to the Radiation Safety Committee, a subcommittee of

the Nuclear Facilities Safety Committee. In addition, the

position of Radiological Assessor was filled through the

promotion of a plant radiological engineer. This is a high

visibility position, and a key link to help assure the continued

quality of the RP program.

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An effective RP training program has been established for plant

Health Physics (HP) personnel. This program includes the use of

mock-ups as practical learning aids. In the area of contractor

HP technician training, apparent weaknesses were identified.

Specifically; formal lesson plans had not been established,

written performance tests were technically shallow, and

management oversight was not sufficient to assure that

contractor technician training was adequately prepared and

planned. Upon NRC identification of these weaknesses, licensee

management immediately committed to rectify them prior to

implementation of the contractor technician training program.

Subsequent re-inspection of this area verified that the licensee

had taken timely and effective action to correct program

weaknesses.

External radiation exposure controls were well established and

effective as evidenced by clear administrative and physical

controls of High Radiation Areas, Radiation Areas and Airborne

Areas. An effective Radiation Work Permit (RWP) system,

supported by adequate radiological assessments and measurements

is now in place. Improvements continued in the personnel

dosimetry program, with the purchase of a new TLD dosimetry

system and proposal for additional training of dosimetry

technicians and supervisory personnel. However, some weaknesses

in the implementation of the radiation protection program during

the outage were noted. Specifically, a high radiation area was

not posted or barricaded and several instances of failure to

follow RWP requirements occurred. The additional workload

associated with the outage appeared to stress the newly upgraded

program. The licensee is aware of this and it will be the

subject of further NRC reviews.

Internal radiation exposure controls were well established as

evidenced by: ongoing efforts to minimize contamination of

areas and components; adequate air sampling and evaluation of

airborne hazards; use of engineering controls; and use of

respiratory protection equipment. In addition, the licensee has

established an acceptable bioassay program. Minor program

weaknesses were noted which impact on program effectiveness: a

limited supply of high volume air samplers which reduced the

effectiveness of the licensee's ability to evaluate airborne

hazards; a poor maintenance program for self-contained-breath-

ing-apparatus; and poor whole body counting facilities. Whole

body counting facilities were not sufficiently environmentally

controlled to limit radio-signal interference with counting

equipment. In addition, high temperatures cause counting system

errors. A potential also exists for losing all whole body

counting capability during an emergency, since the same facili-

ties are used for worker decontamination. Once identified, the

licensee was responsive to these issues.

I

i

.

.. 13

Considerable improvement has occurred in the ALARA program due

to good management support and worker involvement. The program

is well staffed with qualified radiological engineers. ALARA

procedures and policies are well documented to implement the

prograrr , Significant exposure reductions were achieved in the

early stages of the improved program; however, the collective

exposure at Indian Point-2 remains higher than the average for

pressurized water reactors. Subsequent exposure reductions, as

the ALARA program matures, may require a substantial commitment

of resources to address the higher than normal source term at

the plant, and the less than optimum equipmerit shield design.

Licensee management was aware of this situation and is

considering alternate routes to reduce exposure.

The licensee's internal audits and assessments of the radio-

logical control program have substantially improved. However,

some weaknesses were identified in this area. Specifically,

. Radiological Occurrence Reports (ROR) were not actively used to

address deficiencies; no generic reviews of RORs were performed

to determine if any commonality existed in deficiencies; and the

independent radiological assessor did not have a system to track

his findings to resolution. The licensee corrected this situa-

tion by broadening the previously narrow scope of deficiencies

documented in RORs.

Transportation

The licensee is implementing an effective radioactive waste

transportation program. Licensee personnel at all levels in

radwaste transportation are very knowledgeable with regard to

their functions and responsibilities. On going training is

evident.

The licensee performed several QA Department audits of the

transportation program during the period. The audits were

performed in accordance with the requirements of 10 CFR 50,

Appendix B.

One concern was identified, in that the licensee did not ade-

quately communicate to the department responsible for implemen-

ting the radwaste program, that their responsibility includes

performing the quality control function associated with their

activities. This was corrected through comprehensive training

and procedures.

Effluent Control and Post-Accident Sampling

A review of the licensee's effluents program indicated it was

generally being effectively implemented; however, it was noted

that QA involvement was not evident in observing Technical

.-

, 14

Specification required surveillances on plant ventilation

systems.

A follow-up review of the licensee's Post-Accident Sampling

Systems indicated that the systems remain operative, well-

maintained, and that the licensee has adequately addressed

several of the concerns identified in-the previous inspection in

this area.

. Water Chemistry Controls

The licensee's nonradiological water chemistry program has been

upgraded with state of the art laboratory equipment and

procedures. They have initiated an effective QC program.

In summary, the licensee has made significant improvements in

the Radiation Protection Program since the Order Modifying

the License. A health physics appraisal team found all facets

of the program to be acceptable for routine and outage radio-

logical control activities. Management attention has been

appropriately focused toward continued improvements to the

program.

2. Conclusion

Rating: Category 2

Trend: Consistent

3. Board Recommendations

Licensee: None

NRC: Conduct a review of site radiochemistry program.

,

, - ~ - - . . ~ , . .- . . - . . . - , . - . , . , , . - , .,--.,.-~.,.----.,,----_n -n,-,n n,,,,.-,- - . , - - , , , . - . . - . _ . . . , - - , - , _ , - , .

.

. . 15

C. Maintenance (13%, 550 Hours)

1. Analysis

During the previous assessment period, the maintenance program was

recognized as strong with capable management and a large, experienced

staff. A large maintenance backlog had developed and was a concern.

Licensee management was taking steps to improve the physical

condition of the plant.

A total of four reactor trips were attributed to inadequate

maintenance during this assessment period. Two of these trips

occurred due to the loss of main boiler feed pumps and two occurred

due to capacitor failures. One of the feed pump trips occurred when

a high pressure oil hose failed. The hose failed one day before a

scheduled outage, during which it was to be replaced. The other feed

pump trip occurred due to the bearing oil trip setpoint screw being

turned after maintenance. This is one of several examples of

inadequate job site restoration which is discussed later in this

section. One trip occurred due to a capacitor failing in a reactor

coolant flow trip circuit. The capacitor failed before its

scheduled replacement. One trip occurred due to the failure of

'

the steam dump controller. A failed capacitor contributed to the

controller failure. As a result of this failure, the licensee

extended the capacitor replacement program to control circuits.

Several instances were rx:ed where maintenance work was considered

complete but the job site was not completely restored to its original

condition. One reactor trip resulted from not returning a boiler

feedwater pump trip setpoint to its correct position after mainte-

nance. Other instances of incomplete post-maintenance job site

restoration include: failure to replace a seismic restraint on a

reactor coolant pump; improperly reinstalling the reactor coolant

pump oil collection system; improperly reinstalling the recirculation

sump grating; and, cutting away portions of the service water pump

seismic restraints to simplify replacement of the pumps. Also,

tools, removed parts, trash, and leaked oil were observed to remain

at work sites after jobs were completed. Procedural inadequacies for

job site restoration and inadequate post-maintenance job site walk-

downs contributed to these events. Also, in the service water pump

seismic restraint event, the licensee identified that these

restraints were degraded but they were not repaired due to improper

prioritization of the work order. Upon identification of these

concerns, the licensee took prompt and effective corrective action.

However, proper completion of the job restoration phase of mainte-

nance requires increased management involvement.

4

i

1

--

- - , - , --ry. .- , - - . . _ . - - - - . .- ,,,_-_s

. . - . .

..

. 16

A large work order backlog continues to be of concern. The licensee

has taken measures to reduce this backlog. Additional maintenance

staff have periodically been assigned to the station from the Power

Generation Maintenance department and Electric Construction Bureau to

support the increased workload. The major projects manager was given

increased maintenance planning and materials control responsibilities

under the title of planning and projects manager. Senior plant

management actively assesses progress on a station goal to reduce

work order backlogs. The work order backlog, however, was about the

same at the end of this assessment period as it was at the beginning.

The backlog appears to be due in part to an increase in worker

awareness and responsibility for reporting equipment deficiencies.

Staffing level appears sufficient so that there is a decreasing trend

in the number of backlogged work orders although increased staff or ,

worker efficiency would further help to lower the backlog.

The licensee filled promptly and effectively the vacancy left by the

maintenance engineer who left the company at the end of the 1986

refueling outage. The current maintenance engineer was promoted to

the position from within the licensee's organization. The overall

personnel turnover rate is minimal at both the laborer level and

management level. The staffing level remains fairly constant

throughout, with the exception of outages when the licensee's offsite

maintenance personnel come to the site.

The licensee plans to use the probabilistic risk assessment to aid in

prioritizing work orders. Although this effort is not yet underway,

the licensee is planning to transfer the probabilistic risk

assessment staff to the site, where they will be available to support

4

this effort which should result in a reduction in risk from

inoperable equipment.

Due to difficulty in retrieving completed work packages, the licensee

4

'

is reducing the number of status changes the package goes through

during its life. The work packages will also be kept in one place

rather than distributing the packages to the various reviewing

organizations. The licensee's actions to resolve this problem appear

to be working.

,

,

Positive elements noted in the previous assessment period continue to

be exhibited. The maintenance staff is exper enced. Management in-

volvement in the maintenance program is evident and generally effec-

tive from preplanning to work completion, except as noted above.

Overall maintenance records and work packages are complete and accu-

rate. Maintenance procedures are, overall, adequate to perform work.

Work steps are listed in order of performance and sign-off steps are

well defined. Work orders are tracked using the computerized power

plant maintenance information system (PPMIS). With PPMIS, all work

order status, priority and post-maintenance testing requirements are

assigned. The licensee is continuing the effort to increase the

, utilization of PPMIS capabilities for tracking purposes. QC hold

f

1

, , - - - - , . - , . . . , , . , - - - , - , . - . , . ----.--,-,,-.-n

.

-- - -n- - - - -- , , - ..,

.:

. 17

points were astablished in most work activities inspected. Quality

related maintenance records reviewed were complete. QC involvement

was appropriate for the work activities. QC performs random sur-

veillances of the job sites.

During this assessment period, the licensee developed training pro-

grams for Mechanical, Electrical and Instrumentation and Control

staff. The training is adequate for the staff to perform its routine

duties. No training-related problems were evidenced by the main-

tenance staff's performance. Self Evaluation Reports (SERs) for

these programs were submitted to INPO for accreditation.

In summary, the maintenance function is being performed satisfac-

torily by competent and skilled personnel. A considerable amount of

maintenance remains to be done. It is not known what system inter-

actions could result or what operator needs would go unmet in an

event due to the outstanding maintenance activities. The licensee's

efforts to integrate probabilistic risk assessment into the mainte-

nance program to reduce the risk from inoperable equipment is

therefore encouraged. Additional staffing and improved efficiency

would aid in working off the maintenance backlog. Increased atten-

tion to post-maintenance job site restoration is needed.

2. Conclusion

Rating: Category 2

Trend: Consistent

3. Board Recommendations

Licensee: Integrate the probabilistic risk assessment into the

maintenance program. Increase efforts to reduce maintenance

backlog, including review of staffing levels and work prioritization.

NRC: None

.

, 18

0. Surveillance (14%, 585 Hours)

1. Analysis

During the previous assessment period, this area was identified as a

strength, Category 1. During this assessment period, surveillance

activities were routinely observed by the resident inspectors.

Region-based inspectors also reviewed surveillance activities.

In general, the licensee's surveillance program is well defined uti-

lizing computerized schedules and technically adequate procedures.

Management conducts reviews of completed surveillances to ensure the

results are acceptable and meet Technical Specification reatirements,

records are complete, and the necessary follow-up is completed.

Surveillance procedures are well maintained and easily retrievable.

Technical Specification - limited conditions for operation entered

for testing purposes are tracked by Senior Reactor Operator and

Senior Watch Supervisor log books.

The licensee has' upgraded surveillance procedures during this assess-

ment period. Included in the upgrade were generic statement changes,

format changes, personnel notification changes, and procedure clari-

fications. The surveillance test writing staff consists of

knowledgeable people with a strong background in test writing. The

testing is performed by members of the operations, performance, and

I&C departments. The test documents and test document changes are

strictly controlled.

During the assessment period, there were three separate cases of

minor surveillance performance problems. One case was a late daily

heat balance check due to the operators being preoccupied with a

plant transient. The second case was an incomplete surveillance tect

due to the I&C technician omitting the source check of a radiation

monitor in the field. The third case was an incomplete surveillance

due to operations personnel omitting one control rod from the rod

exercise test because it had an inoperable position indicator. All

three of these cases were identified by the licensee while reviewing

completed test results and they were promptly reported and corrected.

Except for these three cases, the licensee completed surveillance

testing in a timely manner.

One subcritical reactor trip occurred due to a personnel error during

surveillance testing. While performing the reactor protection logic

functional test, a technician tripped reactor trip breaker A instead

of B as required by the test procedure. This is considered an iso-

lated instance.

The staffing of the Test and Performance department has remained

relatively constant throughout the assessment period. The department

writes the majority of the surveillance tests and post-maintenance

1

, , 19 l

l

l

i

i

tests. The tests are performed by members of the operations, I&C, 'l

and the Test and Performance department. Staffing is adequate to l

perform this function. Based on the performance of the Test and  ;

Performance personnel, training appears adequate.

QA/QC personnel review a sample of completed tests. QA/QC also

performs certain hydrostatic test inspections in which certified

inspectors are required.

~

In summary, surveillance tests are well written and easy to follow.

Test data is in tabular form for ease of review. Reviews of

completed tests are effective in identifying problem areas. The

program is adequately staffed and effectively managed.

2. Conclusion

Rating: Category 1

Trend: Consistent

3. Board Recommendations

Licensee: None

NRC: None

_ _ _ _ _ _ _ . _ _ - _ _ _ - _ _ _ _ _ _ _ _

-

C-

, 21

Fire brigade drills were promptly responded to by the brigade. The

brigade leader gave clear instructions to the brigade and good com-

munications were maintained with the control room.

During this assessment period, the Itcensee assigned the additional

responsibilities of managing the security program to the person in

charge of the fire protection program. Although no degradation in

the management of the fire protection program has been observed, the

effects of this change will be evaluated during the next SALP period.

In summary, the implementation of Appendix R and the routine conduct

of the fire protection program show that the fire protection program

is well organized and effectively implemented.

2. Conclusion

Rating: Category 1

Trend: Consistent

3. Board Recommendations

Licensee: None

NRC: None

l

l

l

l

i

.

, 20

l

i

E. Fire Protection (6%, 234 Hours)

l

l 1. Analysis

! During the previous assessment period, satisfactory performance was

l evident in the fire protection program.

,

During this period, a team inspection was conducted of fire protect-

l ion and alternate safe shutdown modifications required by 10 CFR 50,

Appendix R. The team included specialists in fire protection,

'

mechanical and electrical systems from NRR and Brookhaven National

Laboratory.

The inspection focused on the plant's safe shutdown capability. In

particular the team reviewed the plant's fire protection measures

.

which ensure that one train of equipment necessary to achieve and

!

maintain safe shutdown remains available in the event of a fire at

any location within the plant.

The review included an inspection of the fire barriers separating

redundant safe shutdown components and miscellaneous fire protection

systems. A review of the safe shutdown systems, safe shutdown

methodology and the emergency safe shutdown procedures was also

performed.

l The safe shutdown analysis performed by the licensee was comprehen-

sive. The established emergency procedures are clear and easily

! implemented, although a large number of operators is required

for this task. The licensee demonstrated that this crew is always

'

available and is well trained in these procedures.

The licensee's associated circuit analysis also adequately addressed

the regulatory concerns such as common bus, spurious signals, current

transformer secondaries and high-low pressure interfaces. All of the

above are indications of strong management involvement in fire

protection issues.

The licensee also routinely exhibits conservatism in areas of safety

significance and is innovative in the use of Unit 1 equipment, such

as the gas turbine, to provide backup power to the emergency diesels.

The fire protection program was also included in routine inspections

by the resident inspectors.

The fire protection program was found to be effectively implemented

i during this assessment period. Frequent plant tours are made by fire

l protection staff and supervision. Transient fire hazards are kept to

a minimum. Fire protection starf exhibited a good understanding and

l effective implementation of procedures for control of the removal and

reinstallation of fire barriers.

i

o

. 22

F. Emergency Preparedness (6%, 265 Hours)

1. nalysis

Du ng the previous assessment period, licensee performance in this

area as rated as Category 1, based on performance during the annual

exerc e, and management involvement in emergency preparedness as

evidenc by staffing levels, training, and responsiveness to identi-

fying an correcting program deficiencies.

During the c rrent assessment period, one full participation exercise

was observed, hanges to on and offsite emergency plans were re-

viewed, and NR staff attended meetings called by the Chairman of the

Regional Assista e Committee (for FEMA Region II) to resolve offsite

emergency planning issues.

During the full parti tion exercise conducted on June 4, 1986, the

licensee demonstrated ng emergency response capability. Per-

sonnel were well traine n alified in their emergency response

roles. In particular, em ency action levels were identified

promptly and the re-entry a covery planning was unusually thor-

ough ard complete. No signi nu deficiencies were identified re-

lating to onsite activities, ppmanceremainedatthepreviously

noted high levels. One onsite R at has remained unresolved,

is th2 question over whether the this EOF is adequate to

allow an effective onsite NRC prese ing an emergency. The

licensee contends that it is adequat )lan no changes. The

issue will be addressed during an upco i F appraisal.

Some significant deficiencies identified he offsite portion of

the exercise will necessitate a remedial e i e. A partial failure

of the Alert and Notification System (ANS) o red when fourteen

sirens failed to function due to "co-channel terference" which

occurred, blocking the activation signal. The terference occurred

because the frequency employed for siren activat n is also used by

the New York State Department of Transportation, R kland County

Highway Department and the Town of Clarkstown Highwa Department.

The licensee has taken administrative steps (broadcas ng a message

to clear the frequency prior to siren activation) to a id a repeti-

tion, and satisfactorily tested the system on June 28,1 6.

Although this action was the fastest way to correct the de'iciency,

more effective solutions are available, but would involve h dware

changes. Several offsite issues have persisted for a number f

years. Licensee participation with FEMA and the State and fou

Counties in resolving these issues could have been more aggressi ,

and has shown dramatic improvement recently (although outside the

assessment period).

e,

, 22A

F. Emergency Preparedness (6%, 265 llours)

1. Analysis

During the previous assessment period, licensee performance in this

area was rated as Category 1, based on performance during the annual

exercise, and management involvement in emergency preparedness as

evidenced by staffing levels, training, and responsiveness to identi-

fying and correcting program deficiencies.

During the current assessment period, one full participation exercise

was observed, changes to on and offsite emergency plans were re-

viewed, and NRC staff attended meetings called by the Chairman of the

Regional Assistance Committee (for FEMA Region II) to resolve offsite

emergency planning issues.

During the full participation exercise conducted on June 4, 1986, the

licensee demonstrated a strong emergency response capability. Per-

sonnel were well trained and qualified in their emergency response

roles. In particular, emergency action levels were identified

promptly and the re-entry and recovery planning was unusually thor-

ough and complete. No significant deficiencies were identified re-

lating to onsite activities. Performance remained at the previously

noted high levels. One onsite issue that has remained unresolved,

is the question over whether the size of this EOF is adequate to

allow an effective onsite NRC presence during an emergency. The

licensee contends that it is adequate, but is evaluating changes.

The issue will be addressed during an upcoming ERF appraisal.

Some significant deficiencies identified in the offsite portion of

the exercise will necessitate a remedial exercise. A partial failure

of -the Alert and Notification System (ANS) occurred when fourteen

sirens failed to function due to "co-channel interference" which

occurred, blocking the activation signal. The interference occurred

because the frequency employed for siren activation is also used by

the New York State Department of Transportation, Rockland County

Highway Department and the Town of Clarkstown Highway Department.

The licensee has taken administrative steps (broadcasting a message

to clear the frequency prior to siren activation) to avoid a repeti-

tion, and satisfactorily tested the system on June 28, 1986.

Although this action was the fastest way to correct the deficiency,

more effective solutions are available, but would involve hardware

changes. Several offsite issues have persisted for a number of

years. Licensee participation with FEMA and the State and four

Counties in resolving these issues could have been more aggressive,

and has shown dramatic improvement recently (although outside the

assessment period).

.-

,. 23

In addition, the licensee failed to make the one hour. notification

required by 10 CFR 50.72 (Loss of significant alert / notification

capability) due to a lack of licensee guidance in defining a

"significant" loss of capability to the operators. A Notice of

Violation was issued covering this and several reporting violations.

The licensee's onsite emergency response capabilities remain

excellent, however more direct involvement in resolving offsite

deficiencies would have resulted in more timely resolution of those

problems.

2. Conclusion

Rating: Category 2

Trend: Improving

3. Board Recommendations.

Licensee: None

NRC: None

o

, 24

G. Security and Safeguards (2%, 86 hours9.953704e-4 days <br />0.0239 hours <br />1.421958e-4 weeks <br />3.2723e-5 months <br />)

1. Analysis

The previous SALP rating was Category 1. Strengths were identified

as: some increase in management attention to the program; improve-

ments in the training program; and no violations. Weaknesses in-

cluded: maintenance and testing program; security training for

contractors; audits; and program management.

Two unannounced physical protection inspections were performed during

the assessment period by region-based inspectors. Routine resident

inspections continued throughout the assessment period.

In December 1985, at the licensee's initiative, members of the

licensee's new plant management team met with NRC Region I represen-

tatives to discuss weaknesses in the security program that they had

recognized and to describe the actions they had taken and planned to

take to correct them.

A routine, unannounced physical security inspection was conducted in

January 1986. During that inspection several examples of ineffective

access controls and vital area barriers were identified. Also during

that inspection, the licensee's resolution to several findings of the

Regulatory Effectiveness Review (RER) conducted in May 1985 were

reviewed and found to be ineffective. These findings indicate the

following program weaknesses: security was not properly integrated

with other plant groups; there was a lack of program management

direction and coordination; and there was a poor understanding of NRC

program objectives. Some of these program weaknesses were identified

by the licensee in the December 1985 meeting but the licensee's

corrective action plan had not yet taken effect.

As a result of the inspection an enforcement conference was held in

February 1986, at which time the licensee's senior management rep-

resentative outlined planned corrective actions to effect improve-

ments on an expedited basis. Significant among these was the

immediate assignment of an individual, on site, as program manager.

The absence of such an individual to provide oversight and direction

to the program had previously been brought to the licensee's

attention on several occasions by NRC. Also discussed were the

corrective actions that had already been initiated and commitments

for an even more comprehensive review of the program to identify

other potential problems.

A followup inspection in June identified that the licensee promptly

implemented actions to correct the specific violations identified in

the January inspection and those actions were effective. In

addition, several program improvements and enhancements had been

implemented and others had been initiated as a result of the

.

. 25

censee's comprehensive program review. Noteworthy among these was

a ongoing major revision to the security program plans to improve

the comprehensiveness and usability. The revisions are scheduled

for > bmission to the NRC by the end of 1986.

License management also instituted the following changes to improve

coordinat~on, communication and interface among the plant organiza-

tional uni : key security supervisors have been directed to attend

all signifi nt plant meetings and to conduct weekly security super-

visors' revie meetings, in an effort to improve both internal

security and i erdepartmental communications; the proprietary and

contractor secur ty management, supervision and records have been

consolidated in a entral, onsite location; and, more active involve-

ment of corporate s curity management in site activities was

initiated, and a wel u fled security specialist from the

corporate staff was a -

ed to conduct periodic announced and

unannounced audits of t curity program.

The licensee submitted a t al f 11 event reports, in accordance

with 10 CFR 73.71, that per d to the security program. Four of

the events were attributable he lack of a quality maintenance and

surveillance program for secur elated equipment. Three events

involved failure to follow proc one by a member of the se-

curity force and two by other pla kers. One event resulted

from a human error by a member of urity force. The remaining

events involved contractors who had at lied with the licensee's

personnel screening program requireme were identified by the

licensee's routine and aggnssive audit ram of this aspect of the

security program. The event reports gen contained sufficient

information to permit adequate NRC assess . In a few cases,

however, telephone contact with the license was necessary to de-

termine the root cause of the event. The qu ity of event reports

showed notable improvement toward the end of t is assessment period.

Compensatory actions implemented as a result of he events were found

to be prompt and appropriate in all cases. The censee's program

for identifying and reporting security events is c sidered adequate

but could be strengthened by providing better docum tation of the

analyses of the root causes of events, which could as ist the li-

censee in earlier identification of potential problem eas.

As a result of an NRC-identified weakness in the security 'orce

training and qualification (T&Q) program, and in an effort o enhance

the administration of training, the licensee initiated the velop-

ment of comprehensive lesson plans about mid-way during the a ess-

ment period. The effectiveness of this effort has not yet been

assessed by NRC. This effort, in conjunction with the major rev fon

to the physical security program plans previously addressed, repre

sent a substantial resource expenditure on the part of the licensee

and demonstrates a recent initiative by management to implement a

high quality program.

a

. 25 A

licensee's comprehensive program review. Noteworthy among these was

an ongoing major revision to the security program plans to improve

their comprehensiveness and usability. The revisions are scheduled

for submission to the NRC by the end of 1986.

Licensee management also instituted the following changes to improve

coordination, communication and interface among the plant organiza-

tional units: key security supervisors have been directed to attend

all significant plant meetings and to conduct weekly security super-

visors' review meetings, in an effort to improve both internal

security and interdepartmental communications; the proprietary and

contractor security management, supervision and records have been

consolidated in a central, onsite location; and, more active involve-

ment of corporate security management in site activities was initi-

ated, and since 1980, a well qualified security specialist from the

corporate staff has conducted periodic announced and unannounced

audits of the security program.

The licensee submitted a total of 11 event reports, in accordance

with 10 CFR 73.71, that pertained to the security program. Four of

the events were attributable to the lack of a quality maintenance and

surveillance program for security related equipment. Three events

involved failure to follow procedures, one by a member of the se-

curity force and two by other plant workers. One event resulted

from a human error by a member of the security force. The remaining

events involved contractors who had not complied with the licensee's

personnel screening program requirements and were identified by the

licensee's routine and aggressive audit program of this aspect of the

security program. The event reports generally contained sufficient

information to permit adequate NRC assessment. In a few cases,

however, telephone contact with the licensee was necessary to de-

termine the root cause of the event. The quality of event reports

showed notable improvement toward the end of this assessment period.

Compensatory actions implemented as a result of the events were found

to be prompt and appropriate in all cases. The licensee's program

for identifying and reporting security events is considered adequate

but could be strengthened by providing better documentation of the

analyses of the root causes of events, which could assist the li--

censee in earlier identification of potential problem areas.

As a result of an NRC-identified weakness in the security force

training and qualification (T&Q) program, and in an effort to enhance

the administration of training, the licensee initiated the develop-

ment of comprehensive lesson plans about mid-way during the assess-

ment period. The effectiveness of this effort has not yet been

assessed by NRC. This effort, in conjunction with the major revision

to the physical security program plans previously addressed, repre-

sent a substantial resource expenditure on the part of the licensee

and demonstrates a recent initiative by management to implement a

high quality program.

"

.

.. 26

,

During the assessment period, the licensee submitted one revision to

the security force training and qualifications (T&Q) plan. The

changes were responsive to NRC comments on a previous revision and

were found acceptable under 10 CFR 50.54(p). In an effort to improve

the quality of the security plan, licenste representatives, on their

, own initiative, visited the Region I office during this period to

discuss the major plan revision.

The licensee has provided all functions of the security program with

adequate staffing to meet program requirements. The assignment of a

program manager should' continue to strengthen the management of

resources and the effectiveness of the program.

In summary, the effectiveness of the security program, in general,

and the performance of the security force have improved during the

latter portion of this assessment period. The improvement is

attributed to implementation of the new commitments by licensee

management. However, the full effect of the implemented changes

cannot yet be completely assessed, and will be monitored during the

next SALP period.

i 2. Conclusion:

Rating: Category 2

Trend: Improving

, 3. Board Recommendations

j

Licensee: None

NRC: None

1

)

. . - _ _ , _

.,__.-__.-._7- _ _ - _ , _ - , _ , , , - , . . -

. . , . _ , . _ . _ , _ . _ , , . . _ , _ _ - _ . - , _ _ . - . . . . _ _

-

. , , - . _ - _ . _

.. __. __ _________ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ - _ _

,.

O

, 27

H. Outage Activities (15%, 637 Hours)

1. Analysis

During the previous assessment period, this area was evaluated as

Category 2 on the basis of observing the cycle 6/7 refueling outage

completion. Strengths included reorganization of the planning effort

and sound startup test procedures. Weaknesses included high man-rem

exposure and inaccurate drawings.

The unit was shut down from January 14 to March 12, 1986 for its sey-

enth refueling.

Several inspections were performed to examine the preparation for and

execution of the outage health physics program. The Environmental

Qualification program was reviewed by a team inspection and by the

resident inspectors. Startup physics testing, outage and modifica-

tion activities, and the licensee's response to Inspection and

Enforcement Bulletin 80-11 regarding masonry walls were also

inspected.

Major preplanned activities during the outage included refueling,

steam generator examination, replacement of the turbine generator low

pressure rotors, replacement of condenser tube inserts and installa-

tion of a new control system for the main boiler feed pumps. In ad-

dition, many smaller maintenance and modification activities were

completed. The refueling, steam generator examination and turbine

rotor replacement were performed by Westinghouse. Refueling activi-

ties were monitored by Westinghouse QC inspectors with licensee QC

inspectors overseeing the activities. Extensive preplanning and man-

agement oversight were provided by the licensee for these major

projects.

As discussed in the previous SALP, licensee management has aggres-

sively pursued improvements in outage management. A projects plan-

ning group was created and applied modern planning and scheduling

techniques to the outage. Outage coordinators were appointed for

major projects and work areas and provided effective oversight, coor-

dination, and feedback to upper management. The institution of the

project resource evaluation and management information system

(PREMIS) and improved maintenance management had positive effects on

communication, planning, and control of outage activities. The re-

suits of the extensive preplanning and strong, effective, day-to-day

management of outage activities was evident, enabling management to

focus their attention during the outage on major activities and

unanticipated problems.

During the previous assessment period, problems with radiological

controls during an outage led to an Order Modifying License. During

this assessment period, radiological controls were found to be

e-

, 28

significantly improved although some weaknesses were noted (see

Section IV.8).

During this outage, the licensee completed the installation of

several self-initiated modifications which were to improve plant

safety and performance. These included a new control system for the

Main Boiler Feedwater System, a new dryer system for the Instrument

Air System, and replacement of the cooling coils in two Containment

Fan Cooler Units. There are, however, examples of inadequate and

untimely resolutions to technical issues. In July 1984, Indian Point

Unit 3 tripped due to an electrical fault caused by salt spray from

the main condenser lifting jet exhaust. As a result, the lifting jet

exhaust was planned to be rerouted at Unit 2 but this modification

was not implemented before Unit 2 tripped on September 20, 1985 due

to a transformer short from salt buildup from the If fting jet

exhaust. Increased management attention is needed to improve the

timeliness of the resolution of technical issues.

A lack of effective primary containment closeout was observed during

several inspections. Problems, including missing seismic supports

and poor housekeeping, that should have been identified by the

licensee prior to closecut have already been described in Sections

IV. A. and IV. C. of this report.

The Cycle 8 startup physics tests were performed in accordance with

approved test procedures by highly qualified personnel. The Reactor

Engineering staff is small, but highly qualified with reactor engi-

neering activities always performed in a highly professional manner

and well documented. The licensee's performance of startup physics

testing during the approach to criticality and subsequent zero power

physics tests and power ascension tests was deliberate and carefully

controlled. At each power level, all test results were analyzed and

thoroughly understood prior to raising power to the next level.

QA/QC involvement in startup physics testing was consistently visi-

ble. During the startup period, a QA auditor was present to witness

zero power physics testing and, at the conclusion of the testing, a

thorough and comprehensive audit was performed by the same QA audi-

tor. These examples are indicative of the involvement of management

in assuring quality programs are adequately performed.

'

Inspections were conducted of the licensee's Environmental Qualifi-

cation (EQ) program. Some problems were identified with activities

relating to the assurance of quality of the EQ program and these are

described in Section IV. J. Overall staffing was adequate to

properly administer the program.

Licensee response to the major inspection issue (potentially unquali-

fled Lewis Cable) was prompt and effective. The response included an

evaluation of potential failure modes, a temporary operating in-

struction, a justification for continued operations, the replacement

. _ _ _ _ _ _ - _ _ - _ _ _ _ _ _ _ _

. 29

of Lewis cable in the Hydrogen Recombiner thermocouple circuit prior

to startup from the refueling outage, and performance of testing

on the removed cable.

Management responsible for EQ maintained a file of related NRC

initiatives including records of licensee actions and final resolu-

tions. Licensee response to the most recent NRC initiatives relating

to issues of particular concern, such as the limitorque wiring def t-

ciencies identified in Information Notice 86-03, were prompt and gen-

erally thorough. The field execution of some of these corrective

actions was inadequate in some cases such as poorly sealed conduit

and unqualified splices. The licensee identified several deficien-

cies in the implementation of the EQ program including unqualified

terminal blocks. Corrective actions were prompt and effective

and included extensive direct involvement by top management in

investigating the root cause of the deficiencies.

Licensee responsiveness to NRC initiatives was also evidenced by Con

Edison's response to IE Bulletin 80-11. The response was adequate,

in that appropriate action was taken in a timely manner to assure

that those masonry walls in close proximity to or attached to

safety-related piping or equipment were independently identified and

evaluated for modification.

The licensee's initiatives to establish a program to repair cracked

mortar joints and evaluate the cause, adequacy of repair, and need

for a surveillance program is another example of the licensee's re-

sponsiveness to NRC concerns.

In summary, improvements in outage management were evident and

resulted in effective outage control. Startup testing continues to

be performed well. The licensee's implementation of Environmental

Qualification requirements and response to masonry wall issues were

effective.

2. Conclusion

Rating: Category 1

Trend: No basis for trend assessment

3. Board Recommendations

Licensee: Assess effectiveness of prioritization of proposed design

changes and modifications.

NRC: None

- - . _.

, 30

I. Training and Qualification Effectiveness (N/A)

1. Analysis

During this assessment period, training and qualification effective-

ness is being considered as a separate functional area for the first

time. Training and qualification effectiveness continues to be an

evaluation criterion for each functional area.

The various aspects of this functional area have been considered and

discussed as an integral part of other functional areas and the re-

spective inspection hours have been included in each one. Conse-

quently, this discussion is a synopsis of the assessments related to

training conducted in other areas. Training effectiveness has been

measured primarily by the observed performance of licensee personnel

and, to a lesser degree, as a review of program adequacy. The dis-

cussion below addresses thrce principal areas: licensed operator

training, nonitcensed staff training, and status of INPO training

accreditation.

During the assessment period, inspections routinely reviewed training

effectivenss. A programmatic nonlicensed training inspection was

conducted and radiological training effectiveness was examined during

the health physics appraisal. The plant radiological training

program was found to be effective; however, NRC identified

weaknesses in contractor HP technician training for which the

licensee took appropriate action. Non-licensed technician training

has resulted in some improvements, especially in the identification

of equipment deficiencies; in the conduct of surveillance

activities; and in the effective response by the fire brigade.

The performance of nonlicensed staff, indicates that the training and

qualification program contributes to an adequate understanding of

their work and adherence to procedures. The one instance of per-

sonnel error related to surveillance activities which resulted in a

reactor trip is considered an isolated case.

The licensee is proceeding on schedule with INP0 accreditation of

training programs. To effectively manage the activities for seeking

fu': INP0 accreditation the licensee has newly established and

staffed the position of Project Manager - INP0 Accreditation. All

Operations Training programs have been evaluated by INP0. All other

training programs have been submitted for INPO evaluation except for

the Management and Technical Staff program which was submitted

September 1, 1986. The licensee training staff has been increased to

develop and teach these new programs.

.E

, 31

In addition, the licensee has remodeled the simulator building to

provide a training library, four classrooms and additional offices.

An upgrade of the licensee's non-licensed training center has been

budgeted.

Training in the use of Emergency Operating Procedures (E0Ps) appears

to be effective as evidenced by their use following unit trips. The

licensee provided six weeks of classroom and simulator training on

E0Ps before they were implemented. Operators have accepted the.EOPs

and have performed well while using them in licensing exams.

Two areas in which training effectiveness appears weak are in

security and operations. The NRC identified a weakness in the

security force training and qualification program. The

effectiveness of the licensee's improvements has not yet been

determined. In addition, some enhancements are not yet in effect

due to an outstanding plan revision.

Several inadequacies exist in the plant simulator which is considered

marginally acceptable for examinations. In the past, the licensee

has not been aggressive in updating the simulator. -Although, the

licensee recently decided to upgrade the simulator, management

attention is warranted to assure that the upgrade is properly and

expeditiously completed or the upgrades may take several years to

complete.

Operator licensing candidates have been well prepared as evidenced

by all six license candidates passing their_ exams and being issued

licenses. However, three plant trips occurred which may be attri-

buted to licensed operator training. Two trips occurred when gen-

erator load was increased too quickly resulting in a high level Steam

Generator trip. One trip occurred on plant startup when the operator

failed to block the low setpoint high flux trip signal quickly

enough. These events occurred during normal evolutions. Insufft-

cient training dedicated to normal evolutions and inaccurate simula-

tion of these evolutions may have contributed to these events.

In summary, shortcomings exist in the plant simulator. E0P training

was effective and operator training in general is a strength although

isolated examples of ineffective operator action were identified.

The INPO accreditation program is on schedule. Non-licensed training

is adequate.

2. Conclusion

Rating: Category 2

Trend: Consistent

, 32

3. Board Recommendatior.s

Licensee: None

NRC: None

.

. 33

J. Assurance of Quality (N/A)

1. Analysis

Management involvement and control in assuring quality continues to

be.an evaluation criterion for each functional area. During this

assessment period, assurance of quality is being considered as a sep-

arate functional area. The various aspects of the programs to assure

quality have been considered and discussed as an integral part of

each functional area and the respective inspection hours are included

in each one. Consequently, this discussion is a synopsis of the

assessments relating to assurance of the quality of work conducted in

all areas.

The enhancement of design change / modification procedures to step-by-

step detailed instructions; a " traveler" type work control method;

and the allocation of human resources for effective work planning

indicates an increased involvement by senior management in assuring

efficient plant operations and better control over the work process.

The day-to-day involvement of QA and QC in the overview of ongoing

activities has been expanded and is under improved administrative

control. Completed work packages demonstrated that the QA and QC

functions were being properly implemented. For example the

licensee's QA/QC during masonry wall repairs in response to IE

Bulletin 80-11 was thorough. Hold points were established for review

and verification of work by Con Edison's Site Power Generating QA

engineers and for witnessing and verification of specific tests by

QC. The overall acceptability of the wall modification work was au-

dited by Con Edison's corporate quality assurance and reliability

organization. This involvement is not as evident in the areas of

operations and surveillance activities.

Assurance of quality is achieved by the craft worker's supervisors

through the supervisor periodically checking the work site and

verifying worker compliance with the procedure. The supervisors, QA,

and QC also review completed work packages for procedure compliance.

If, in the opinion of QA or the maintenance department, an indepen-

dent inspection is required to satisfy requirements, QC will perform

the independent inspection and these inspections are documented in

the work procedure. This approach appears to be effective.

Surveillance test procedure results are reviewed by the operations

department for acceptability requirements and then finally reviewed

by the test engineering department. The test procedures themselves

are reviewed by the test engineering department and the Station

Nuclear Safety Committee (SNSC) for safety considerations, ease of

^~

..

m

, 34

performance, and meeting Technical Specification requirements. The

performance of tests is monitored as necessary by the test engineers

to verify compliance with the written test procedures. -

QA is responsible for the proper performance of material receipt

inspection. Written instructions are used by receipt inspectors to

check the materials for damage, conformity to procurement documents

and the level of quality of the vendor's material prior to the

inspector accepting the material.

The licensee has revised and updated QA and corporate engineering

procedures to include Environmental Qualification (EQ) program

implementation. However, only one QA audit of the EQ program was

conducted.

The QC outage surveillance program, which has provisions to increase

surveillance frequencies in areas of high unsatisfactory performance

and to decrease surveillance frequencies for areas with acceptable

performance, was effectively implemented during this appraisal

period. The NRC found during a review of this program that the

licensee effectively prioritized their work load so that areas (or

work items) demonstrating poor performance, received a greater amount

of surveillance.

There was no apparent QC involvement in initial field work done to

implement the EQ program except for modifications involving the

replacement of non-EQ equipment. Deficiencies in the application of

sealants were identified by NRC EQ inspections and resulted in a large

effort to reinspect and reapply seals. Also in the QC area, weak-

nesses in performing close out inspections of the Containment Building

and other areas after outages were apparent. One additional concern

was identified due to inadequately establishing and executing the QC

program for radwaste. The licensee's corrective actions were res-

ponsive to this concern.

'

The quality of the SNSC review of events, procedures and other items

continues to be good although in one instance, the plant trip on

June 9, the committee did not identify a root cause for the trip and

focused their review almost exclusively on a safety injection actu-

ation which followed the trip. On August 1, 1986, the SNSC chairman

and General Manager of Technical Support transferred within the

company. The SNSC chairman had a major impact on improv Ng the

quality of the SNSC reviews. The Nuclear Engineering group at cor-

porate headquarters has now been consolidated at the site with the

Technical Support Department as of August 1. The Chief, Nuclear

Engineering, is now General Manager of Technical Support and the new

SNSC chairman.

. . -- -

.

.

. 35

The Nuclear Facilities Safety Committee (NFSC) reviews of licensee

activities have been thorough. NFSC discussions of operational

events and equipment failures have focused on evaluating their safety

significance, root causes, and corrective actions. The use of

sub-committees contributed to the thoroughness of these evaluations.

In summary, the attention of management appears to be focused on

quality. Quality programs are generally effective although their

involvement in operations and surveillance is not as evident as in

other areas.

2. Conclusion

Rating: Category 2

Trend: Consistent

3. Board Recommendations

Licensee: None

NRC: None

O

, 36

K. Licensing Activities (NA)

1. Analysis

During the SALP evaluation period, the licensee has shown good man-

agement overview in the area of licensing activities. This was evi-

dent through the timely submittal and subsequent approval of several

license amendments aimed at improving the cycle 7/8 refueling outage

which occurred during the rating period. The licensee's management

demonstrated active participation in licensing activities and kept

abreast of current and anticipated licensing actions. All open li-

censing actions are scheduled and tracked through use of the

licensee's Regulatory Action Tracking System. During the rating pe-

riod, a system for identifying both licensee and NRC priority items

was initiated.

The licensee's submittals are most often timely. However, in many

instances, additional information or revisions are necessary before

review can be completed. This occurs most often in the area of

plant-specific licensing actions. The licensee's treatment of the no

significant hazards standards of 10 CFR 50.92 has shown some im-

provement, however, further improvement in this area is needed. The

licensee tends to provide too little detail in most discussions.

There were several instances during the period when submittals were

made following their scheduled submittal date. These submittals

were, in all instances, required because of NRC requests for infor-

mation. In most instances, the original schedules were set by

the licensee after receipt of the information request, and, in most

cases, the licensee informed the staff that the submittals would be

late. The schedular delays are usually limited to one or two weeks

and seem to be more a management problem that a responsiveness

problem. The fact that schedule dates were not arbitrarily imposed

by the staff, but instead agreed upon or set by the licensee, and

that the licensee appears to be more responsive to those items for

which it has placed a high priority rather than those for which the

NRC had indicated a high priority demonstrates need for more

management attention to ensure prompt resolution of safety issues. A

new policy has been initiated whereby both the licensee and the NRC

will agree on prioritization of certain licensing actions. This

should belp alleviate some of the past problems in this area.

The licensee maintains a significant technical capability in almost

all engineering and scientific disciplines necessary to resolve items

of concern to the NRC and the licensee. In addition, the licensee

utilizes the services of other nuclear support groups to assist in

the resolution of technical problems or to utilize new and proven

techniques that will enhance the operation and safety of the Plant.

,

I

l

- - , _ . - - - _ _ - -

C

, 37

The licensee's extensive and improving technical capability is re-

flected in the submittals made in support of, or in response to,

licensee or NRC initiated actions. Although, as discussed above, the

licensee is not always forthcoming with all of the information neces-

sary to complete a review without requests for additional informa-

tion, few licensee responses to NRC requests for additional

information require subsequent questions.

It should be noted that during the assessment period the licensee was

requested to provide a detailed submittal concerning the alternate

shutdown capability of Indian Point 2 in the remote chance of loss of

certain capabilities due to high winds at the site. The information

was requested with a fairly short turnaround time. The licensee

provided a timely and thorough submittal.

The licensee's licensing activities are conducted by a well staffed

and well trained group resulting in an overall efficient operation.

Management overview is evident in that the licensing group is well

integrated into other plant activities and licensing activities re-

flect a uniform approach. Upper management becomes involved in 11-

censing actions when necessary to assist in resolving potential

deadlocks.

The licensing group has exhibited a high degree of cooperation with

the NRC staff. The good communication between the licensing group

and the NRC has been !.aneficial to both in the processing of licens-

ing actions. Areas of expertise are well defined within the group.

In addition the group does an excellent job of coordinating the ef-

fort when input is required from the different groups within Consoli-

dated Edison. However, the group could be more effective if

management would emphasize to all Consolidated Edison supporting

organizations the need for meeting ccmmitted licensing schedules for

responding to the NRC. The licensing group holds informal training

sessions on topics of current and future interest. The group also

participates in corporate-wide training programs and participates in

industry-wide training programs provided by various organizations.

In summary, the licensee's greatest strengths appear to be in its

extensive technical capability that is reflected in its submittals

and discussions with the NRC, and, in the continued upgrading of the

experience, capability and effectiveness of the licensing group and

the supporting administrative and technical personnel required to

operate a good facility. More detail in submittals would require

fewer iterations during the review process, and, closer attention to

submittal schedules would avoid short term schedular slippages.

., . - _ - - . - - -

C

', 38

2. Conclusion:

Rating: Category 2

Trend: Improving

3. Board Recommendations

Licensee: None

NRC: None

.

. 39

V. SUPPORTING DATA AND SUMMARIES

A. Investigation and Allegation Review

No investigations were conducted during the assessment period.

Four allegations were received during the assessment period:

improper ALARA performance;

individual disciplined for refusing to work in the containment

building;

security guards discouraged from talking with NRC inspectors;

radioactive spill released to river, inadequate radiation pro-

tection for workers during spill cleanup.

All four allegations were inspected and closed out with no violations

identified.

B. Escalated Enforcement Actions

No civil penalties, or confirmatory action letters were issued. No

orders were issued for enforcement action. One enforcement confer-

ence was held on February 13, 1986 for security violations.

C. Management Conferences

October 25, 1985: SALP management meeting;

December 17, 1985: 1986 refueling outage preparations and

plans, review of maintenance related LERs for the previous SALP

period, and analysis and corrective actions for reactor trips.

D. Licensee Event Reports (LERs)

1. Causal Analysis

Thirty-five LERs, numbered 85-07 thru 86-24, were reviewed for

this assessment period. These LERs are characterized in Table 1

by cause for each functional area. The following causally-

linked event sets were identified:

LER No. Cause

85-10 These events are reactor trips due to personnel

85-12 error.

85-14

85-16

85-24

86-08 These events are instances of instrument setpoint

86-09 drift.

86-11

86-22

'

..

. 40

2. AE0D Review

The Office for Analysis and Evaluation of Operational Data

(AE00) assessed a third of the LERs submitted during the

assessment period using a refinement of the basic methodology

presented in a report entitled "An Evaluation of Selected

Licensee Event Reports Prepared Pursuant to 10 CFR 50.73

(DRAFT)," NUREG/CR-4178, March 1985. The results of this eval-

uation were forwarded to the licensee on October 3,1986, _ and

indicate that Indian Point 2 LER's are above average.

The principal weaknesses identified in the LERs, in terms of

safety significance, involve the requirement to provide identi-

fication of failed components. The failure to adequately iden-

tify the manufacturer and model number of the components that

fail prompts concern that others in the industry won't have im-

mediate access to information involving possible generic

problems.

Strong points for the Indian Point 2 LERs cre the c'i3cussions of

the mode, mechanism, and effect of failed components, and the

discussion of personnel errors.

..

-. 41

,

TABLE 1

TABULAR LISTING OF LERs BY FUNCTIONAL AREA

INDIAN POINT STATION - UNIT 2

Area Number /Cause Code Total

A B C D E X

A. Plant Operations 7 1 8

B. Radiological Controls 0

and Chemistry

__ C. Maintenance 2 1 3

D. Surveillance 2 2

E. Fire Protection 0

F. Emergency Preparedness 0

G. Security and Safeguards 0

H. Outage Activities 0

1. Training and Qualification 0

Effectiveness

, J. Assurance of Quality 1 1

K. Licensing Activities 0

L. Other 2 1 1 15 2 21

TOTALS 11 3 1 3 15 2 35

Cause Codes:

A - Personnel Error

B - Design, Manufacturing, Construction, or

Installation Error

C - External Cause

D - Defective Procedure

E - Component Failure

X - Other

.

w y_ -- _ --_ p ---__#_ -

,,

-. 42

TABLE 2

INSPECTION HOURS SUMMARY (8/1/85 - 7/31/86)

INDIAN POINT STATION - UNIT 2

Area Hours % of Time-

A. Plant Operations ........................... 981 23

B. Radiological Control s and Chemi stry. . . . . . . . . 903 21

C. Maintenance ................................ 550 13

D. Surveillance ............................... 585 14

E. Fire Protection............................. 234 6

F. Emergency Preparedness ..................... 265 6

G. Security and Safeguards .................... 86 2

H. Outage Activities .......................... 637 15

I. Training and Qualification Effectiveness ** . N/A --

J. Assurance of Quality ** ..................... N/A --

K. Licensing Activities * ...................... N/A ---

TOTAL' 4241 100%'

  • Hours expended are not included with direct inspection effort statistics.
    • Hours expended in training and assurance of quality are included in other

functional areas. <

.

l

i

,

mr +=w-

. . . - .

, _

_

-

.

, 43

TABLE 3

ENFORCEMENT SUMMARY (8/1/85 - 7/31/86)*

,

INDIAN POINT STATION - UNIT 2

Severity Levels

AREA I II III IV V TOTALS

A. Plant Operations 1 3 4

B. Radiological Controls and Chemistry 2 2

C. Maintenance 2 2

D. Surveillance 0

E. Fire Protection 1 'l

F. Emergency Preparedness 0

G. Security and Safeguards 1 1 2

H. Outage Activities 0

i

I. Training and Qualification

Effectiveness 0

'

.

J. Assurance of Quality 1 1

K. . Licensing Activities 0

.

TOTAL 0 0 1 7 4 12

  • Does not' include Inspection Report 86-11

1

4

i

,.

.,n- .-n , .. ,. , _ n - -- - , , . , . , - . -

- ;7 _

.. 44

TABLE 3 (CONT'D)

Inspection Severity Functional

Report /Date Level Area Violation

86-01 IV Quality Inadequately established

1/6-10/86 Assurance and executed QC program

to assure compliance with

10 CFR 61.55 and 10 CFR

61.56.

86-02 III Security & Three instances of

1/13-17/86 Safeguards failure to control

access to vital areas.

V

"

Failure to perform an

adequate search of

contractor's vehicle

entering protected area.

86-08 IV Radiological Failure to post high

2/24/86 Controls radiation boundaries.

IV "

Failure to follow

-procedures for use of

protective clothing,

posting contaminated

areas, and writing

event reports.

86-10 V Operations / Failure to submit Annual

4/1-30/86 Radiological Radiation Exposure

Controls Report on time, failure

to make telephone

notification.

86-15 IV Maintenance / Unit brought out of cold

6/10-7/7/86 Outage shutdown with seismic

restraint disconnected.

86-19 IV Operations Failure to properly

7/2-8/1/86 establish and maintain

Emergency Operating

Procedures and Abnormal

Operating Procedures.

-

,

. ,

, 45

TABLE 3 (CON'T'D)

Inspection Severity Functional

Report /Date Level Area Violation

86-19 IV Maintenance / Recirculation sump

7/2-8/1/86 Outage grating not properly

reinstalled.

IV Housekeeping Failure to follow house-

keeping procedures.

86-23- V Operations Failure to notify the

7/8-31/86 NRC in accordance with

10 CFR 50.72 on three

separate occasions.

"

V Failure to perform

required operability

. checks on a Control Rod

Drive and Plant Vent

Noble Gas Activity

Monitor.

'I

-w--- e , - -- -rr- ,,-w ,-n,n-_-,m,- ---,-ve.-we---,,mer=-ww--- - - - --m--,, - -, - -w

. 46

TABLE 4

INSPECTION REPORT ACTIVITIES (S/1/85 - 7/31/86)

INDIAN POINT STATION - UNIT 2

Report / Dates Inspector Hours Areas Inspected

85-21 Resident 51 Routine, daily inspections

8/1-31/85 and unscheduled backshift

inspections.

85-22 Specialist 108 Special, announced safety

9/17-20/85 inspection of masonry wall

design (Bulletin 80-11).

85-23 Resident 131 Routine, daily inspections

9/1-30/85 and unscheduled backshift

inspections.

85-24 Specialist 201 Routine, announced safety

9/16-20/85 inspection of 10 CFR 50,

Appendix R.

85-25 Resident 208 Routine, daily inspections

10/1-31/85 and unscheduled backshift

inspections.

85-26 Resident 120 Routine, daily inspections

11/1-30/85 and unscheduled backshift

inspections.

85-27 Specialist 65 Special, unannounced

11/12-15/85 dosimetry inspection.

85-28 Specialist Licensed operator exams.

12/10-13/85

85-29 Specialist 41 Routine, unannounced

12/2-6/85 inspection of design changes /

modifications and QA program.

85-30 Resident 217 Routine, daily inspections

12/1/85-1/15/86 and unscheduled backshift

inspections.

85-31 Specialist 46 Special inspection of

12/16-18/85 licensee's implementation of

radiological controls

improvement program.

a

. 47

TABLE 4 (CONT'D)

Report / Dates Inspector Hours Areas Inspected

86-01 Specialist 37 Routine, unannounced

1/6-10/86 inspection of transportation

activities.

86-02 Specialist 43 Routine unannounced

1/13-17/86 safeguards inspection.

86-03 Cancelled

86-04 Specialist 141 Routine, unannounced

1/21-24/86 inspection of radiation

protection program.

86-05 Resident 230 Routine, daily inspections

1/16-3/3/86 and unscheduled backshift

inspections.

86-06 Specialist 132 Special, unannounced

2/10-14/86 inspection of maintenance,

modifications, and outage

controls.

86-07 Specialist 30 Routine, announced inspection

2/10-13/86 of the nonradiological

chemistry program.

86-08 Specialist 128 Special, unannounced

2/24-28/86 inspection of radiological

controls program.

86-09 Resident 184 Routine, daily inspections

3/4-31/86 and unscheduled backshift

inspections.

86-10 Resident 148 Routine, daily inspections

4/1-30/86 unscheduled backshift

inspections.

86-11 Specialist 142 Special, announced inspection

5/12-16/86 of environmental qualification.

86-12 Resident 280 Routine, daily inspections

5/1-6/9/86 and unscheduled backshift

inspections.

-, 48

.

'

TABLE 4 (CONT'D)

Report / Dates Inspector Hours Areas Inspected

86-13 Specialist 242 Routine, announced emergency

6/2-5/86 preparedness inspection and

observation of emergency

exercise.

86-14- Specialist 50 Routine, un&nnounced

6/2-6/86 inspection of non-licensed

staff training.

86-15 Resident 145 Routine, daily inspections

6/10-7/7/86 and unscheduled backshift

inspections.

86-16 Specialist 25 Routine, unannounced

6/2-5/86 safeguards inspection.

86-17 Specialist 241 Special, announced health

6/16-20/86 physics appraisal.

86-18 Specialist 42 Special, unannounced

6/16-20/86 inspection of sewage

contamination.

.

86-19 Specialist 586 Special, announced

7/21-8/1/86 probabilistic risk

assessment based inspection.

86-20 Specialist 40 Special, announced inspection

7/10-17/86 of post-accident sampling

and monitoring.

86-21 Specialist 30 Routine, unannounced radio-

7/15-18/86 active effluents inspection.

86-22 Specialist 35 Routine, unannounced

7/14-18/86 inspection of startup

physics program.

86-23 Resident 122 Routine, daily inspections

7/8- /86 and unscheduled backshift

inspections.

4241 hours0.0491 days <br />1.178 hours <br />0.00701 weeks <br />0.00161 months <br />

i

a

, 49

TABLE 5

LISTING OF ALL AUTOMATIC TRIPS AND UNPLANNED SHUTDDWNS

INDIAN POINT STATION - UNIT 2

Power

No. Date Level Description Cause (Note 1)

1 9/20/85 95% Reactor trip on turbine Modification

generator trip. Turbine control. Untimely

generator tripped due to correction of

short on #21 main trans- design error.

former. Brackish water

drifting from lifting jet

exhaust caused short.

(LER 85-09)

9/23/85 Startup

2 9/23/85 12% Reactor trip on turbine trip. Personnel error -

Turbine tripped on high steam operations. Oper-

generator level . Steam gener- ator failed to an-

ator swell while picking up ticipato swell.

load after bus synchronization Simulator modeling

caused high level. (LER 35-10) and training con-

tributed to high

rate of load

pick-up.

9/24/85 Startup

3 9/27/85 77% Tech. Spec. required shutdown Natural event.

due to hurricane Gloria.

9/27/85 Startup

4 9/28/85 25% Reactor tripped on power range Personnel error -

high flux-low level trip signal. operations. Oper-

The high flux level occurred ator failed to

during power ascent. (LER 85-12) block trip signal

as required by

procedure due to

high rate of load

pickup.

9/28/85 Startup

Note 1 - Determined by SALP Board, may not agree with LER Analysis

a:

50

TABLE 5-(CONT'D)

Power

No. Date Level Description Cause (Note 1)

5 10/24/85 13% Reactor trip on turbine. trip. Personnel error -

Turbine tripped on high steam operations. Oper-

generator level. Steam gener- ator failed to an-

ator swell while picking up ticipate swell.

load after bus synchronization Simulator modeling

caused high level. (LER 85-14) and training con-

tributed to high

rate of load

pick-up.

10/24/85 Startup

6 12/12/85 100% Reactor tripped on loss of flow Equipment failure

signals from coolant loop #21. maintenance.

The loss of flow signal was due A failed capacitor

to a bistable tripping in one caused a bistable

channel and a separate flow to trip.

channel being previously placed

in the tripped position due to

a faulty flow transmitter.

(LER 85-16) -

12/13/85 Startup

7 12/31/85 100% Reactor tripped on low pressur- Equipment failure -

izer pressure when a pressurizer under review

spray valve failed open. (LER A spray valve

85-17) pneumatic operator

malfunctioned.

1/1/86 Startup

8 1/13/86 94% Reactor tripped on low low Equipment failure -

steam generator level. The maintenance.

low level resulted from low High pressure oil

feedwater flow due to a trip hose failed in

of #21 Main Boiler Feed Pump MBFP controls.

(MBFP). (LER 86-01)

3/12/86 Startup (Reactor critical -

zero power).

9 5/23/86 SD Subcritical trip of shutdown Personnel error -

banks when reactor trip breaker. Surveillance. Tech-

was inadvertently opened during nician tripped the

a test. (LER 86-16) wrong breaker.

5/25/86 Startup

e.

.o. 51

TABLE 5 (CONT'0)

.

10 5/28/86 30% Reactor tripped on Safety Equipment failure -

Injection: high steam flow / low maintenance Faulty

Tavg signal. The high steam steam dump control-

flow was caused by the steam ler.

dumps opening. (LER 86-17)

5/30/86 Startup

11 5/31/86 0% Unplanned shutdown due to short Personnel error -

in exciter. maintenance. Error

in re-assembly by

contractor.

6/7/86 Startup

12 6/9/86 56% Manual reactor trip due to Equipment control -

loss of MBFP. MBFP #21 operations and

tripped while starting MBFP maintenance. High

  1. 22. (LER86-19) bearing oil trip

setpoint; open oil

bypass valve.

6/11/86 Startup

13 6/25/86 43% Reactor trip on turbine trip. Personnel error -

The turbine tripped due to design control.

actuation of the independent Drawing was not

electrical overspeed protection updated following

system while a technician'was plant construction.

replacing relays in that system.

(LER 86-21)

6/26/86 Startup

14 7/18/86 100% Reactor tripped when control rod Personnel error -

motor generator set was tripped operations. Oper-

while starting second motor ator failed to

generator set. (LER 86-24) properly synchro-

nize motor

generators.

7/20/86 Startup

_

y y , , n--+ w w -- , -g - y m+- y -r~ -

r

.. 52

TABLE 6

NRR SUPPORTING DATA AND SUMMARY

INDIAN POINT STATION - UNIT 2

1. NRR/ Licensee Meetings

Fuel Removal Time Constraints T.S. Application 7/9/85

IST 11/13-14/85

DCRDR 12/4/85

Organization 7/25/86

12. NRR Site Visits / Meetings

Fire Protection Audit 9/16-20/85

PM/ Resident 11/18-21/85

Refueling Activities 12/17/85

EQ Audits 5/15-16/86

3. Commission Meetings

None

4. Schedular Extension Granted

None

5. Reliefs Granted

ASME Section XI Relief 3/17/86

6. Exemptions Granted

Appendix R 11/13/85

7. License Amendments Issued

Amendment Numbers Title Date

97 Limiting Overtime, Audit Frequency 9/30/85

For EP Program and Safeguards Contingency

Plan, Quality Assurance Record Retention

Requirements

98 Fuel Removal Time Constraints 9/30/85

i

4

1

-~ - - -.,---,--,-------.--..,,--e + - + - - - - - - , . . . - - -

--w c -,n - ,-- -

g

?

'e 53

TABLE 6 (CONT'D)

Amendment

Numbers Title Date

99 Surveillance Interval Limit Extension 9/30/85

100 Initial Reactor Core Design 10/17/85

101 Decay Heat Removal, Number of Operating 10/23/85

Reactor Coolant Pumps, Over Pressure.

Protection

102 Generic Letter 83-36, 83-37 Tech. Specs. 11/13/85

103 Temporary Closure Plate 11/13/85

104 BIT Removal 12/05/85

105 Boric Acid Addition Capabilities 12/05/85

106 Organizational Changes 12/31/85

107 Anticipatory Reactor Trip on Turbine 1/13/86

Trip

108 CTMT Cooling, Iodine Removal, CTMT 1/27/86

Isolation

109 Total Nuclear Peaking Factor Limits 1/29/86

110 Part Power Multiplier 3/31/86

111 Increased Enrichment 4/21/86

112 Hydraulic Snubbers 5/19/86

113 Code Safety Valves 6/11/86

114 RV and SV Failures and Challenges, 7/22/86

Monthly Operating Report

8. Emergency Technical Specifications Isseed:

Amendment Numbers Title Date

113 Code Safety Valves 6/11/85

9. Orders Issued

Revision of Supplement 1 to NUREG-0737 6/19/86

--

4

e

54

FIGURE 1 .

'

l

NUM8ER OF DAYS SHUT DOWN

INDIAN POINT STATION UNIJ 2

'

August, 85 No Days Shut down

September, 85 15 Days Shut down

October, 85 7 3 Days Shut down

November, 85 No Days Shut down

December, 85 ] 1 Day Shut down

January, 86 19 Days Shut downl Seventh Refueling Outage

February, 86' 28 Days Shut down 1

March, 86 31 Days Shut cown i

April, 86 30 Days shut down i

May, 86 27 Days Shut down 1

June, 86 1 10 Days Shut down

July, 86 ] 2 Days Shut down

. - - . - - -

. - - - ________