ML20203G921

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Insp Repts 50-352/97-10 & 50-353/97-10 on 971118-980119. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20203G921
Person / Time
Site: Limerick  Constellation icon.png
Issue date: 02/23/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20203G899 List:
References
50-352-97-10, 50-353-97-10, NUDOCS 9803030108
Download: ML20203G921 (44)


See also: IR 05000352/1997010

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U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos. 50 352

50-353

License Nos. NPF-39

NPF 85

Report Nos. 97 10

97-10

Licensee: PECO Energy

Facilities: Limerick Generating Station, Units 1 and 2

Location: Wayne, PA 19087-0195

Dates: November 18,1997, through January 19,1998

inspectors: A. L. Burritt, Senior Resident inspector

F. P. Bonnett, Resident inspector

J. D. Noggle, Senior Radiological Specialist, DRS

A. J. Blamey, Reactor Engineer, DRP

W. B. Higgins, Reactor Engineer, DRP

Approved by: Clifford Anderson, Chief

, Projects Branch 4

Division of Reactor Projects

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9803030108 980223

PDR ADOCK 05000352

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EXECUTIVE SUMMARY

Limerick Generating Station, Units 1 & 2

NRC Inspection Report 50-352/97-10,50-353/97-10

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This integrated inspection included aspects of PECO Energy operations, engineering,

maintenance, and plant support. The report covers a 9-week period of resident inspection.

Operatigng

  • Control room supervisors at both units logged over 100 Technical Specification

Limiting Conditions for Operations for primary containment isolation valves during

the follow up inspection and testing event. Overall, log entries were adequately

controlled. However, several issues involving the accuracy of the unified log were

identified by the inspection. The most significant of these was the failure to log

inat two safety systems were inoperable resulting in a violation of controls stated in

the Operation Manual for maintaining the unified log (Section 02.1).

Maintenance

  • Overall, maintenance technicians completed the rep = ament activity of the 1D

125vdc safeguards battery well. However, there wee several housekeeping and

work practice issues which could have impacted battery operability (Section M1.3).

  • The large number of similar hydraulic control unit (HCU) discrepancies identified

during PECO's follow-up investigation to an individual control rod that fully inserted

during a reactor protection system surveillance test indicated that inadequate

maintenance had been performed during the recent on line maintenance activities

and during prior maintenance activities. The Nuclear Maintenance Division (NMD)

appeared to have established adequate control and oversight of the on-line HCU

work activities and NMD technicians demonstrated a good awareness and

responsibility toward quality by stopping work to notify his supervision of a wiring

discrepancy. However, PECO did not establish adequate measures to assure that

the applicable design requirements were adequately maintained during HCU on line

maintenance resulting in a violation (Section M1.4).

  • The licensee's response to the failure of the power monitor card in the Unit 1 RRCS

was excellent. The licensee promptly established RRCS operability and corrected

the problem. Adequate consideration was given to the method used to prevent an

inadvertent plant trip during the maintenance repair, including use of the training

simulation to heighten technician awareness (Section M1.5).

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  • In general, Limerick has adequate control of portable and/or temporary equipment in

the reactor and turbine building such that it will not interact with equipment

important to safety. Furthermore, this program is strengthened by periodic

walkdowns and critiques with first line supervisors. However, while reviewing plant

housekeeping, the inspector noted several discrepancies that were not identifie by

the PECO staff. Further, in the case of the deficient bolting associated with tb ,

monorail hoist it appeared the condition existed for a long period of time (Section

M2.1 ).

Verification, overstated the requirements to meat Technical Specification 3.6.5, by

equating the floor drain plugs with the components required to maintain secondary

containment. Control of the configuration of these plugs remains necessary to

prevent creating an opening in the secondary containment that would prevent the

standby gas treatment system from maintaining secondary containment in the event

of an accident. Inadequate control of the plugs demonstrated in October and the

lack of timeliness for incorporating the proposed procedure revision have resulted in

a violation (Section M8.1).

Enaineerina

  • The PECO engineer demonstrated excellent awareness of component configurntion

by recognizing a mis wired closing circuit for an Unit 1 reactor core isolation cooling

steam isolation valve. Engineering promptly identified that the PCIVs were not

adequately tested and implemented adequate measure to complete the required

testing within the time allowed by technical specifications (Section E1.1).

  • The engineering assessment and supporting safety evaluation to support operability

of the HPCI exhaust valve was inadequate in that it did not address the valve

closure time requirements. The plant operations review committee (PORC)

approved the safety evaluation, but failed to challenge the engineering assessment

discounting the requirement for the valve to close the first time to meet the closure

time required oy technical specifications in assessing operability. PORC accepted

the degraded condition of the valve without having identified the root cause or

evaluating the corrective actions to ensure future valve reliability and thereby the

ability to meet the required closure time (Section E2.1).

The use of a safety evaluation to accept the delay in further investigations and

testing of the HPCI exhaust valve, until the next scheduled refueling outage, in

effect inappropriately modified the technical specifications required closing time.

The use of the safety evaluation in addressing operability was not necessary nor

consistent with NRC guidance on operability provided in generic letter 91-18.

isochronous mode of operation wa good, particularly since another EDG was

inoperable for planned maintenance and was competing for the same personnel

resources. The D22 EDG was returned to an operable status in about two and a

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half days after a thorough assessment of the overpower event which including a

variety of followup inspections and measurements. The root cause analysis of this

event was adequate; however, documentation weaknesses were noted including the

as found conditions not being documented in detailin the work order (Section

E2.2).

e The licensee appropriately implemented the commitment change process for the

main safety relief valve commitment change. Although the timing of NRC

notification for the change was sooner than required by the process, the letter was

misleading in that it implied that the change had been implemented as of the date of

the letter, whereas three months later at the end of the inspection period the

change had not been implemented. However, no violation of NRC requirements

was identified. In addition the engineering evaluation to support the modification of

the commitment was not comprehensive in that it did not correlate the performance

data to specific changes in the thresholds values (Section E6.1).

Plant Sucoort

e The radiation protection program controls for preveming internal exposures was

effective. No significant personnel exposures were apparent. However, the whole

body measurement capability appeared to lack sufficient rigor in assuring that all

internally deposited radio nuclides, that the whole body counting instrument was

expected to detect, were effectively identified and evaluated. It was not apparent

that staff were cognizant of the inherent limitations of the equipment relative to

discreet resolution of energy peaks to effect radio nuclide identification (Section

R 1.1 ).

e The respiratory protection program met regulatory requirements (Section R1.2).

e The air samplo counting laboratory provided properly calibrated and reliable sample

analysis services (Section R1.3).

e The inspector oetermined that the licensee's radiation protection instrument

calibration program generally utilized sound principles and techniques. However,

the process did not address or compensato for certain uncorrected calibration errors ,

that could eff 3ct instrument accuracy. Notwithstanding, the instrument calibration

process was cetumined to be effectively implemented. The TLD program oversight

was very effective in enhancing the accuracy of vendor TLD processing results

(Section R1.5),

e The bases upon which the licensee resolves exposure discrepancies between TLD

and electronic dosimeter quarterly results was not apparent. The area will be

further reviewed in a subsequent inspection (Section R4.1).

o Oversight of the ras.ation protection program consisted of independent and self-

assessments that generally provided for effective insights and recommendations for

program improvements (Section R7).

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e The Radiation Protection (RP) training program was adequate. The licensee

identified a weakness in the RP fundamentals training provided to RP technicians in

the continuing training program, and has made some progress in addressing this

concern (Section R5.1).

e The licensee has limited procedural controls over the advanced radiation worker

program. Some survey and contamination area deposting activities have been

performed by the advanced radiation workers that involved evaluation and

judgement determinations without qualified RP technician supervision. Further

investigation in the advanced radiation worker training and performance are needed

to determine whether a violation of TS 6.3.1 has occurred (Section R5.2).

  • An unqualified person had been assigned to perform tasks which require formal

qualifiuation. Generally, there was evidence of direct supervision for the more

critical tasks performed by unqualified individual such as the performance and

evaluation of whole body counts. However, for administrative tasks, generally there

was no recorded evidence of direct supervision as required by the licensees training

and qualification procedures. Although, the practice of using unqualified and

unsupervised personnel is inconsistent with the licensee's procedure, this was

determined not to be a violation of regulatory requirements since the position or job

functions are not specifically addressed through the technical specification

requirements for the training of plant staff. However, the failure of the licensee to

appropriately control the use of unqualified personneIis of concern since the same

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procedure control are used to address positions which have specific training

requirements (Section R5.3).

  • Although, the licensee was not in full compliance with Procedure ERP-600-1, Health

Physics Team, they were proactive in identifying the issues and their corrective

actions are adequate for preventing recurrence. The inspector also noted that

these issues were not identified in previous exercises or drills because the licensee

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had typically conducted their exercises during working hours in which HP

technicians were onsite and available for immediate response (Section P4),

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TABLE OF CONTENTS

Summ ary of Plant St atu s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1. Operations . . . . . . . . . . . . . . . . . . ..................................2

01 Conduct of Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

01.1 G e neral Com ments . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

O2 Operational Status of Facilities and Equipment ...................2

O 2.1 Primary Containment isolation Valve Configuration Control . . . . . . 2

I I M aint e n a n c e . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

M1 Conduct of Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

M1.1 General Comments on Maintenance Activities . . . . . . . . . . . . . . . 4

M1.2 General Comments on Surveillance Activities . . . . . . . . . . . . . . . 5

M1.3 Division 4 Safeguards 8attery Replacement - Unit 1. . . . . . . . . . . 5

M1.4 Hydraulic Control Unit Maintenance Activities . . . . . . . . . . . . . . . 6

M1.5 ReJundant Reactivity Control System Corrective Maintenance . . . 9

M2 Maintenance and Material Condition of Facilities and Equipment . . . . . . 10

M2.1 Plant Material Condition Reviews: ..... ................ 10

M8 Miscellaneous Maintenance issues . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

M8.1 (Closed) URI 97-03-01, Performance of Reactor Enclosure Secondary

Containment integrity Verification. . . . . . . . . . . . . . . . . . . . . . . 11

111. Eng i n e e ri n g . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1 3

E1 Conduct of Engineering . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

E1.1 Primary Containment Isolation Valve Configuration Error and

inadequate Te sting . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

E2 Engineering Support of Facilities and Equipment .... ............ 15

E2.1 (Closed) LER 1-97-011 Unit 1 High Pressure Coolant injection (HPCI)

Turbine Exhaust Valve Failure . . . . . . . . . . . . . . . . . . . . . . . . . * 5

E2.2 Emergency Diesel D22 Loss of Control During Monthly Load Test

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E6 Engineering Organization and Administration ................19

E6.1 Main Safety Relief Valve Commitment Change . . . . . . . . . . . . . 19

IV. Pl a nt S u p p o rt . . . . . . . . . . . . . . . . . . . . . . . . . .......................21

R1 Radiological Protection and Chemistry (RP&C) Controls . . . . . . . . . . . . 21

R1.1 Internal Exposure Assessment . . . . . . . . . . . . . . . . . . . . . . . . . 21

R1.2 Respiratory Protection ..............................23

R1.3 Counting Laboratory Calibrations . . . . . . . . . . . . . . . . . . . . . . . 24

R 1.4 Release of Material from Turbine 8uilding Roof . . . . . . . . . . . . . 24

R1.5 Instrumentation Calibration . . . . . . . . . . . . . . . . . . . . . . . . . . . 25

R2 Status of RP&C f acilities and Equipment . . . . . . . . . . . . . . . . . . . . . . . 26

R4 Staff Knowledge and Performance in RP&C ....................27

R4.1 Exposure Discrepancy Reports . . . . . . . . . . . . . . . . . . . . . . . . . 27

R5 Staff Training and Qualification in RP&C , . . . . . . . . . . . . . . . . . . . . . 28

RS.1 RP Technician Training and Qualifications . . . . . . . . . . . . . . . . . 28

R5.2 Advanced Radiation Worker Program . . . . . . . . . . . . . . . . . . . . 28

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RS.3 Health Physics Personnel Qualification . . . . . . . . . . . . . . . . . . . 29

R7 Quality Assurance in RP&C Activities . . . . . . . . . . . . . . . . . . . . . . . . . 31

-R8 Miscellaneous RP&C losues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3 2

R8.1 Dose Assessment Review of an August 2,1991 Contamination

incident ........................................32

P4 Staff Knowledge and Performance in EP , . . . . . . . . . . . . . . . . . . . . . . 32

V. M anageme nt Meeting s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3 3

X1 Exit Meeting Summ ary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 33

X2 Review of UFSAR Commitments . . . . . . . . . . . . . . . . . . . . . . . . . . . . 34

INSPECTION PROCEDURES USED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3 5

ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 35

f LIST O F AC RO NYMS U S ED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3 6

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R,oort Details

Summary 3f Plant Status

Unit 1 began this inspection period operating at 100% power. The unit remained at full

. power throughout the inspection period with exceptions for testing, rod pattern

adjustments, and the following plant events.

  • December 6 Operators entered a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> shutdown limiting condition for

operation (LCO) in accordance with Technical Specification (TS) 3.6.3 after declaring several primary containment isolation

valves inoperable for not meeting all requirements. The valves

were properly tested and declared operable. Operators exited

the LCO prior to the end of the 12-hours,

e December 13 Operators reduced power to 65% to perform on-line

maintenance'on 52 hydraulic control units (HCUs),

Maintenance activities were completed and the unit returned to

full power on December 17.

e December 28 Operators reduced power to 70% to remove the 1 A

condensate pump from service after operator noted degraded

discharge pressure and significant vibration conditions with the

pump's performance. Unit power was increased to 77%

power during the period that maintenance technicians replaced

the pump. Operators restored the unit to full power on

- January 4,1998.

Unit 2 began this inspection period operating at 100% power. The unit remained at full

power throughout the inspection period with exceptions for testing, rod pattern

adjustments, and the following plant event.

  • December G Operators entered a 12-hour shutdown LCO in accordance

with TS 3.6.3 after declaring several primary containment

isolation valves inoperable for not meeting all surveillance

requirements. The valves were properly tested and declared

operable. Operators exited the LCO prior to the end of the 12-

hours.

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1. Operations

01 Conduct of Operations'

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of ongoing

plant operations. In general, PECO Energy's conduct of operations was professional and

focused on safety principles.

02 Operational Status of Facilities and Equipment

02.1 Primary Containment Isolation Valve Confiauration Control

a. Insocction Scone

On December 5, an engineer inspecting the breaker cubical for the Unit 1 reactor core

isolation cooling (RCIC) inboard steam isolation valve (HV-491F007) identified a mis wired

closing circuit (see Section E1.1). During the subsequent investigation the engineering

staff identified a testing deficiency that potentially affected the operability of numerous

other primary containment isolation valves (PCIVs). Between December 5 and 7 (about 48

hours), the operations staff maintained control of safety-related system operability per TS

during the plant wide follow-up investigation and testing of the affected motor operated

valves at both units. The inspector reviewed the unified control room log and the LCO log

I to ensure the appropriate LCO entries were made for PCIV and safety system inoperability.

The inspector discussed his findings with representatives of the Operations Department

staff. A Performance Enhancement Program (PEP 10007700) evaluation was initiated to

address the inspectors concerns,

b. Observations and Findinas

Shift management entered over 100 TS LCO entries into the control room's unified log in a

48-hour period. The unified log is a computer based log that records riarrative log entries

from both unit reactor operators, the chief operator, control room supervisor (CRS) and

Shift Manager. The log also tracks TS LCO entries. During the 48-hour period, a unit

supervisor was assigned to each unit to assist the CRS in maintaining control of the large

number of TS LCO entries at both units for the inspection and testing of the effected valve

motor operator circuits. Overall, the activities were generally performed well, with the

exceptions noted below.

Station engineers determhd that tne closing circuita for the PCIVs had r.ot been

adequately tested. Therefore, shift management entered TS 4.0.3, allowing 24-hours to

satisfy the missed surveillance testing prior to having to implement the required action as

per the TS LCO. Shift management entered this TS at 10:30 a.m. of December 5. The

1 Topical headings such as 01, M8, etc., are used in accordance with the NRC standardized

reactor inspection report outline. Individual reports are not expected to address all outline topics.

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consequences for not completing the required surveillance testing within the 24-hour

period would be to shutdown both units within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. While technicians tested each

PCIV, the unit supervisor also entered the four hour action statement for TS 3.6.3 (primary

containment isolation valves) as appropriate.

The inspector identified several problems from the unified log review. Two safety related

systems were made inoperable during the valve testing and no TS LCO log entry for the

system's inoperability was made in the unified log. The Unit 2 suppression pool spray

mode of residual heat removal (RHR) system (TS 3.6.2.2) and high pressure coolant

injection (HPCI) system (TS 3.5.1.c.2) were made inoperable (separately) for about two

hours. The inspector verified that all alternate and low pressure coolant injection systems

were operable during the time both systems were unavailable as required in each of the

associated TS action statements. Therefore, the technical specifications for these two

cases were technically met. Hewever, Operations Manual OM-L-12.1, Rogulatory Action,

step 4.4, requires a narrative log entry in the unified log for the safety system inoperability

LCO numbers were not unique. Several factor = caused this problem including:

  • Duplicate LCO numbers were created when log entries were mMe within the

10-minute time period between system updates.

  • LCO entries were inadvertently edited, changing the LCO from the original

entry.

  • The same LCO number was repeated several time throughout the year for

different iS LCO entries.

The above mentioned variations were apparently caused by the computer software. For

example, if the operator intended to initiate an LCO entry, the computer displayed the next

chronological TS LCO entry number. This number, however, appeared on every computer

terminal that allowed more than one supervisor to be entering differing TS LCOs with the

same number. Operations management stated that the computer system software was

unable to keep pace with the large number of entries made from multiple terminals.

Further, the inspector identified several significant typographical errors, These included a

TS LCO closure at midnight, about six hours prior to the time logged initiating the LCO, and

a core spray (system 52) valve that was typed as an RHR valve (system 51). The

inspector raised concerns regarding the frequency and quality of log reviews performed by

operations supervision. Operations management assured the inspector that the unified log

is the official record of plant activities and that it was crucial that the log be complete and

accurate.

Operations management agreed with the discrepancies noted, but stated that they were

administrative in nature and in no case did they result in the inappropriate control of

equipment operability or in non-compliance with TS. Management also stated that no

narrative log entry was made for making the Unit 2 HPCI and suppression pool spray

systems inoperable, however, a narrative log entry would be reconstructed and a late log

entry made. Notwithstanding management's intent, the inspector presented his findings to

the operations management three days following the event and no edits had been made in

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the log up to that point. Therefore, the inspector concluded that the log did not accurately

reflect conditions as they occurred in the plant. OM-L-8.2, Narrative Logs / Scope of

Entry, states that items are to be entered into the log pertaining to system operability or

affecting the station. This action was not performed on two occasions. This is a violation.

(NOV 9710-01)

c. Ggnclusion

Control room supervisors at both units logged over 100 Technical Specification Limiting

Conditions for Operations for primary containment isolation valves during the follow up

inspection and testing event. Overall, log entries were adequately controlled. However,

severalissues involving the accuracy of the unified log were identified by the inspection.

The most significant of these was the failure to log that two safety systems were

inoperable resulting in a violation of controls stated in the Operanns Manual for

maintaining the unified log.

II. Maintenance

M1 Conduct of Maintenance

M 1.1 General Comments on Maintenance Activities (62707)

The inspectors observod selected maintenance activities to determine whether approved

procedures were in use, details were adequate, technical specifications were satisfied,

maintenance was performed by knowledgeable personnel, and post maintenance testing

was appropriately completed.

The inspectors observed portions of the following work activities:

  • Unit 1 Division 4125vdc Safeguards Battery Replacement - November 18 -

21;

e Unit 1 High Pressure Coolant Injection Inboard Steam Valve Backseating -

November 19;

  • Unit 1 HCU on-line maintenance - replacement of SSPVs,- December 15;
  • Unit 2 D2318-month inspection, December 8 - 12;

Observed maintenance activities were conducted well using approved procedures, and

were comp!eted with satisfactory results. Comn.unications between the various work and

support groups were good, and supervisor oversight was good.

Overview of Raisina M/G Set Stoos Der SP-147

The inspector observed the adjustment of the 1B reactor recirculation motor generator

scoop tube stops. The reactor operator and control rooni crew had effectively minimized

distractions during this adjustment. Contingency procedures were opened and ready if

required during the adjustment. The maintenance and engineering personnelinvolved in

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the physical adjustment at the scoop tube positioner were aware of the potsntial reactivity

effect associated with working on this equipment. The supervisor in the field was aware

of the requirement for a senior reactor operator (SRO) to control this evolution. The

adjustment was completed satisf actorily.

M1.2 Ger ;ral Comments on Surveillance Activities (61726)

The inspectors observed selected surveillance tests to determim whether approved

procedures were in use, details were adequate, test instrumentation was properly

eclibrated and used, technical specifications were satisfied, testing was performed by

knowledgeable personnel, and test results satisfied acceptance criteria or were properly

dispositioned.

The inspectors observed portions of the following surveillance activities:

  • Unit 2 D23 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> Endurance Test and Hot Restart December 15;
  • Unit 2 Inservice Inspection Functional Pressure Test of HPCI Pump

Discharge and Turoine Exhaust Piping December 17;

  • Unit 2 HPCI Quarterly Surveillance Test December 17;
  • Unit 2 D21 Weekly Surveillance Test, December 31;

Observed surveillance tests were conducted well using approved procedures, and were

completed with satisf actory results. Communications betwocn the various work and

support groups were good, and supervisor oversight was good.

M1.3 Division 4 Safenuards Batteiv Reolacement - Unit 1

a. Insocction Scons

During the week of November 17, maintenance electricians and l&C technicians replaced

completely the Division 4125vde safeguards battery. Th work acSvities included

replacing the 60 battery cells and the inter f onnecting hardware, and inspecting and

cleaning of the battery rack. The inspector observed portions of the activity and discussed

the observations with several maintenance representatives. The inspector reviewed the

operations log for appropriate TS LCO entries,

b. Observations a.nd Findinns

The technicians completed the activity over a four day period, replacing 15 cells per day

without making the battery inoperable. The battery was maintained operable throughout

the evolution by jumpering the 15 cells to be replaced with a temporary safeguards

battery. The temporary battery is maintained in the same condition as the inservice

battery, is mounted in a seismically qualified cart, and meets the requirements of technical

specifications.

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The inspector noted soveral deficiencies in housekeeping and maintenanco practices during

the first day's activities. A temporary battery charger was lef t unattended without being

properly secured. Battery cables from the temporary battery were routad through and/or

tied to structural supports without using a sof toning material to protee'. the cabbs from

cheffing from the sharp edges of the support. One sable was routed und':r a florescent

lamp fixturo. The inspector raised concern that the cablo may have affected the seismic

class ll ovaluation for the lamp fixture over the seismic class I component. Tools were not

stored properly and an atmosphere monitoring device was lef t on a panel overtop of the

temporary battery. Further, a battery lead, disconnected from the removed battery cells,

was routed through the battery support rack to keep it out of the way, presented a

potential electrical hazard. The inspector discussed thoto observations with the

maintenanco foreman.

Revisiting the area the next day, the inspector observed general improvement in the

condition of the battery room. The temporary battery cables were routed through an

industrial cable guard on the floor, tools and other materials were properly stored, and the

disconnected battery cable properly isolated. A sei .mc engineer evaluated the overhead

lighting and determined that the cable running under the lamp did not present a concern.

The seismic class 11 over class I concern deals with the S hooks used to suspend the lamp

from the ceiling. The lamp could possibly be jarred out of the S hooks if the hook was not

closed or scaled properly, in this case, the S hooks were closed and sealed and therefore

did not croate a problem.

The inspector noted that this was the first battery replacement performed by the

maintenanco electricians. The task had been the responsibility of the I&C technicians and

was now being turned over to the electricians,

c. Conclusion

Overall, maintenance technicians completed the replacement 1ctivity of the 1D 12Svde

safeguards battery well. However, there were several housekeeping and work practice

issuos which could have impacted battery operability.

M1.4 Hydraulic Control Unit Mairitenance Activities

a. Insocetion Scone (62707)

Several maintenance related activities involving HCU's at both units occurred during the

inspection period. PECO Energy's Nuclear Maintenance Division (NMD) performed an on-

lino maintenance outage on selected Unit 1 HCUs beginning on December 12. On

December 26, at Unit 2, a single control rod fully inserted without operator acti?n during

the performance of a reactor protection system (RPS) surveillance test. The inspector

observed portions of the on line maintenance activities performed at the HCUs. Further,

the inspector reviewed the Unit 2 event, the PEP ovaluation, and d scussed the event with

several PECO representatives.

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b. Observations and Findinas

Hydraelle Control Unit On line Maintenance Unit 1

The HCU maintenance focused on replacing the remaining scram solenoid pilot valve

(SSPV) assemblies which utilized diaphragms made of BUNA-N material. Maintenance

technicians used maintenance procedure M 047 027, Preventive Maintenanc for HCUs,

throughout the activities. NMD technicians replaced 52 SSPV assemblies over a five day

period.

Work activities were planned, coordinated, and executed well between the Operations and

NMD Departments, and the reactor engineering staff. Optrators and reactor engineers

performed t,large number of control rod manipulations with3ut error. Further, NMD

personnel performed clearance and tagging responsibilities, maintenance activities, and '

HCU restoration without error. Following HCU restoration, operators performed scram time

testing to verify the control rod's operability.

A technician identified a wiring discrepancy at HCU 38 43. The wiring for the SSPVs (V-

117 and V 118) was found reversed. The technicians found the V 117 wired to the

terminals supplied by 'D' reactor protection system (RPS) and V 118 wired to the terminals

supplied by 'A' RPS. The technician immediately stopped work and notified his supervisor.

Technicians checked all other HCUs to determine the scope of the problem No other

discrepancies were noted.

The system manager issued Non Conformance Report (NCR) 97 03427 to address the

issue. The NCR determined that the HCU would have performed its scram function

regardless of which RPS bus the eSPVs were wired to. Further, the configuration problem

did not present a single f ailure concern or have an impact on channel separation, and

therefore was operable. The inspector found NCR's determinations to be acceptable.

Maintenance was last performed on the HCU during an overhaulin 1993.

As a result of this discrepancy, NMD revised procedure M-047 027 to include several

procedural enhancements. A ' Note' to enhance the po ' identification of the V-

117/118 SSPVs was added to the section for the SSPV replacement, as well as improved

wire identification, and the wiring termination locations. The inspector determined that the

safety consequances of this discrepancy were minor,in that, the scram function of the

HCU was not effected by the wiring configuration. Further, the procedures changes

appeared to enhance HCU wiring configuration control.

Sinale Control Rod Scram Durina Reactor Protection System Surveillance - Unit 2

On December 20, a single control rod fully insarted without operator action during the

performance of a reactor protection system (RPS) surveillance test. An l&C technician was

performing ST 2 042 645 2,RPS and NSSS Steam Dome Pressure, Channel A Functional,

when the event occurred. The control room staff notified the NRC per the requirements of

10 CFR 50.72(b)(2)(li), but later retracted the notification.

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Control room operators immediately entered off normal procedure, ON 104, Control Rod

Problems, verified that control rod 10 47 was fully inserted, and verified all thermallimits

were normal. The shift manager declared the control rod inoperable and directed that the

HCU be hydraulically isoleted. Nuclear Maintenance, l&C personnel, and reactor engineers

initiated troubleshooting activities under troubleshooting control form TCF 97 0905.

The plant staff's inves: Jation at the HCU revealed !cose terminal block connections on the

load side leads to SSPV supplied from the 'B' RPS channel. The terminal block screws X

were found to be backed off about three to four turns. The plant personnel at the HCU *

observed that the SSPV de energized intermittently when the l&C techrt ien attempted to )

i tighten the scrown. The reactor engineer hypothesized that the SSPV supplied ...,m B RPS

l channel de energlwd due to the loose connection prior to or when the surveillance test

initiated the A RPS half scram signal. The I&C technician tightened the connections and

reactor engineers performed a partial scram timing test to prove the operability of the

control rod.

Technicians performed an inspection of all Unit 2 HCUs for similar problems and found 22

other HCus with variations of the same discrepancy. These findings were documented in

PEP 10007742. Several other maintenance discrepancies were also identified and

corrected during thir inspection. A terminallug was improperly landed at HCU 38-07. The

lug was held in place by the screw head " pinching" down on the outside of the lug

because the screw did not fit through the eyelet of the lug. At HCU 34 27, the technicians "

found a loose screw that had backed out to its last two threads. The inspection at Unit 1

identif%d v lCU discrepancios. One HCU was found with a cross threaded terminal

screw.

The inspector reviewing the maintenance history of the affocted HCUs determined that

HCU 10-47 was last worked in January 1996 as were 13 other of tne 32 HCU identified at

both units during this event. 11 HCUs were worked during the recent on-line maintenance

activities in November and December 1997, one in March 1997, two in July 1995, and

four HCUs were worked in December 1994. The inspector determined that the above

examples demonstrated inadequate maintenance of the in-flaid changes cerformed during

these previous on line maintenance activities.

The inspectors concluded that the safety consequence of the event was minimal, but was

concerned with the large number of examples of poor quality craf tsmanship and design

control during on line maintenance. Appendix 0, Criterion lil, of 10 CFR 50 states, in part,

that measures shall be provided for verifying or checking the adequacy of design changes

performed during maintenance and repair, and that design changes, including field changes

shall be subject to design control measures commensurate with those applied to the

original design. Contrary to the above, PECO did not establish adequate measures to

assure that the applicable design requirements were ad3quately maintained during HCU on-

line maintenance. This was a violation of 10 CFR 50, Appendix B, Criterion Ill. (NOV 97-

10 02)

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PECO retracted the four hour notification of the event based on the guidance of NUREG-

1022,(Event Reporting Guidelines 10 CFR 50.72 and 50.73). The single control rod

insertion was not considered an ESF actuation by itself and was not the result of an

actuation of the RPS system. Further review by reactor engineering determined that the

capability of the RPS and scram function of all control rods was not adversely impacted by

the identified loose screws,

c. Conclusion

The large number of similar hydraulic control unit (HCU) discrepancies identified during

PECO's follow up investigation to an individual control rod that fully inserted during a

reactor protection system surveillance test indicated that inadequate maintenance had been

performed during the recent on-line maintenance activities and during prior maintenance

activities. The Nuclear Maintenance Division (NMD) appeared to have established

adequate control and oversight of the on line HCU work activities and NMD technicians

demonstrated a good awareness and responsibility toward quality by stopping work to

notify his supervision of a wiring discrepancy. However, PECO did not establish adequate

measures to assure that the applicable design requirements were adequately maintained

during HCU on line maintenance as required per 10 CFR 50, Appendix B, Criterion ill,

Design Control.

M1.5 Redundant Reactivity Control System Corrective Maintenance

a. [03nection Scone (71707)

A review of the licensoo corrective action response to the failure of a power monitor card

in the Unit 1 Mundant Reactivity Control System (RRCS) Division I was performed. The

inspector reviewed the logs and discussed the f a'. ure with operators and the RRCS system

manager,

b. Observations and Findinag

On October 18, Unit 1 received a Division i RRCS Out of Service annunciator and an

equipment operator was sent to investigate. The equipment operator reported that a "181

310 PWR MON TST/PWR SUPPLY FAILURE" error was displayed on Division i RRCS. The

RRCS would not reset and an equipment trouble tag was written to document the f ailure.

Subsequent troubleshooting identified that the power supplies were functioning and that

the power monitor card had f ailed indicating that all RRCS functions were still operable.

On October 20, the licensee successfully replaced the f aulty power monitor card with the

RRCS energized returning the RRCS a to fully operational condition.

Prior to implementing repairs, the licensee cont.ulted the RRCS vendor, to determine if the

power monitor card could be replaced with the system energized without causing an

inadvertent trip. The vendor indicated that a trip should not occur but could not guarantee

this assessment. The licensee also verified with the vendor that an updated power monitor

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card stocked in their supply system was completely compatible with the earlier model

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power monitor card that was malfunctioninc. To provide further assurance, the licensee

simulated the power monitor card replacemint on a RRCS training simulator on loan from

another plant and determined that the card replacement would not cause an inadvertent

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trip.

The licensee system manager indicated that, although there is no regulatory time

constraints involved, repair of the RRCS is treated as an immediate concern since a faulty

RRCS can cause an inadvertent plant trip.

c. Conclusions

The licensee's response to the f ailure of the power monitor card in the Unit 1 RRCS was

excellent. The licensee promptly established RRCS operability and corrected the problem.

Adequate consideration was given to the method used to prevent an inadvertent plant trip

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during the maintenance repair, including use of the training simulator to heighten technician

awareness.

M2 Maintenance and Material Condition of Facilities and Equipment

M 2.1 Plant Material Condition Reviews:

a. Insoection Scone

Plant walkdowns specifically focused on equipment important to safety were conducted to

overview the plant material condition. This inspection also reviewed procedure A C 030,

Plant Material Condition and Housekeeping Controls which describes the licerisee's

controls for material condition,

b. Observations and Findinag

The general plant areas in the reactor and turbine build'..gs were free of clutter.

Emergency lighting necessary for plant shutdown under some postulated conditions

appeared to be aimed at appropriate equipment and showed an acceptable battery charge.

In general, material storage was away from equipment important to safety and properly

anchored. Sensitive equipment that could initiate a plant transient was clearly labeled to

caution personnel. The inspector noted that periodic walkdowns and critiques of

housekeeping areas are performed by peer first line supervisors. However, several

deficient conditions were identified N the inspector and are described below.

A large structural steel support for a monorail hoist that penetrates the Unit 1 primary

containment access door had five of eight nuts not engaging the embedment plate in

several cases the nuts were backed off as much as an inch and appeared to have been in

this condition for some time since the exposed threads had been painted, in response to

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the discrepancy the licensee performed a field walkdown and removed the hoist from

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l service. The initial engineering review determined that this was a non conforming

condition, but the lateral supports would ensure that seismic loads would not damage the

containment door. The licensee plans to complete the engineering evaluation and

ultimately corrected the condition.

The inspector identified the instrument line to the Unit 2 Pressure Transmitter, PT 001

207, was vibrating. This is a small diameter line that provides the high pressere turbine

exhaust signal to the electro hydraulic control (EHC) system. This signal is utilized to

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provide a turbine trip if a load imbalance is sensed between the generator output and the

turbine power. Engineering reviewed the configuration of this line and initiated equipment

trouble tag (ETT) to provid) better support and reduce the vibration of the instrument line,

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Walkdown of the surrounding area did not identify any safety related equipment that could

be impacted by the failure of this small diameter steam line. The Unit 1 instrument line

was configured differently and had no observed vibration. i

The inspector identified two spare cubicles in 250 Volt DC MCC 1DB 1 that were open to

the reactor building atmosphere since no breaker was installed. Engineering determined

! that there was no environmental qualification (EO) concern because this area was not

subjected to high humidity following accident. However, the engineering staff also

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determined that the opening should be covered to prevent foreign material from entering

the cubicle. The system manager has initiated corrective actions to provide foreign

material barriers to cover these openings.

The inspector identified a minor issue, in which an unsecured cart was found next to a

safety related 480 vac motor control center (MCC D114 R-GU. The cart was promptly

removed af ter being brought to the attention of the control room staff,

c. Conclusions

In general, Limerick has adequate control of portable and/or temporary equipment in the

reactor and turbine building such that it will not interact with equipment important to

safety. Furthermore, this program is strengthened by periodic walkdowns and critiques

with first line supervisors. However, while reviewing plant housekeeping, the inspector

noted several discrepancies that were not identified by the PECO staff. Further, in the

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case of the deficient bolting associated with the monorail hoist it appeared the condition

existed for a long period of time.

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M8 Miscellaneous Maintenance !asues (92902)

M8.1 (Closed) URI 97 03-01, Performance of Reactor Enclosure Secondarv Containment

inteority Verification.

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a. Inspection Sqqp.g

The inspector raised concerns with the Operation Department's methodology to verify the

condition of plugged floor drains during the performance of ST 6-076 3601(2), Reactor

Enclosure Secondary Containment Integrity Verification. The concern focused on whether

an operator reviewing the locked valve log only, to determine that the floor drain plug's

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condition, met the requirements of the TS. Operations management enhanced the

procedure to include the review of the Barrier Breach Log (A C 134), and the LCO and

potential LCO logs. The inspector lef t the item unresolved pending the determination of

whether any violations using th6 original methodology had occurred. During the current

inspection period, the inspector discussed the issue with several engineering

representatives.

b. Observations and Findinas

PECO regulatory engineers defined the word " verify", as it is used in the Technical

Specifications (TS 4.6.5.1.1.B.), to clarify confusion that resulted from discussions within

various plant organizations over compliance with ST 6-076 3601(2). They determined

" verify" was to prove to be true by demonstration; to confirm or substantiate by

investigation, comparison with a standard, or reference to the facts. Regulatory concluded

that the intent of " verify" was to physically check the required configuration as much as

practical, and then refer to the next best alternative that provided relative assurance that

the configuration was correct based on the last known change to the configuration.

The engineering staff does not consider the floor drain plugs to be a Technical

Specification penetration required to be closed during an accident condition. This is based

upon establishing and maintaining secondary containment (a O.25 inch of vacuum water

the required TS surveillance which limits the scope of penetrations requiring surveillance to

doors, hatches, dampers, and valves. The SGTS is able to maintain the negative pressure

with a design leak tightness of 2500 cfm or lesi PECO conservatively had included the

floor drain plugs in the monthly surveillance test, although they were not explicitly required

by the TS definition for secondary containment. An engineering analysis indicated that the

rerroval of a small number drain plugs does not impede SGTS ability to maintain secondary

containment, but the removal of a significant number of drain plugs would. The engineers

therefore stated that tight configuration controls for the removal of drain plugs would

continue to be required and that an engineering evaluation would be performed to

determine the amount of air inleakage presented by the opening when several drain plugs

were removed to ensure the TS inleakage limit was not exceeded.

The int pector noted a licensee identified event that occurred on October 7,1997,in which

a floor drain plug at Unit 2 wha unlocked and removed from drain FD 74 without proper

configuration controls as stated in A C 8, Lantrol of Locked Valves and Devices. The

equipment operator (EO), performing GP-7, Plant Winterization, contacted and discussed

opening the fioor drain at Unit 1 with a licensed operator because he could not contact the

flex supervisor or the control room supervisor. Subsequently, the EO proceeded to Unit 2

to perform the same task. The EO, however, did not contact the control room prior to

opening the Unit 2 floor drain because he believed that his previous conversation covered

both units. The following day, another EO found the Unit 2 drain opened and that it had

been opened for about 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br />.

The inspector determined that this activity did not meet PECO's configuration controls as -

stated requirements of A C-8. A C 8, steps 7.2.2 and 7.2.3 states, in part, that the

individual requesting permission for the manipulation (of the locked device) should enter

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the valve or device laformation in the Locked Valve Log and obtain permission from the

Shif t Management. Shift Management shall then indicate authorization for the

manipulation by initiating and dating the Log entry. The EO did not properly fill out the

Lock Valve Log nor was Shif t Management approval granted prior to removing the floor

drain. The inspector determined that this activity was a vlotation. (NOV 9710-03)

The ST currently reflects the floor drains as a TS required component. PECO intends to

revise the ST to remove the asterisk defineating the component as a TS requirement. The

floor dreins will continue to be checked as stated in the ST. The difference being that they

will not have to be " verified" as required by TS. The inspector agreed that floor drains are

not defined penetrations as per TS, and drain plugs should not be equated with .

components required to maintain secondary containment integrity, as was discerned m the

ST. However, the ST was the only document delineating what components were

specifically required to meet the TS, configuration of the floor drains was not adequately

controlled through the normal vehicle (A C 8), and the proposed revision to the ST has not,

to date, been performed.

c. Conclusion

ST 6 076 3601(2), Reactor Enclosure Secondary Containment Integrity Varification,

overstated the requirements to meet Technical Specification 3.6.5, by equating the floor

drcin plugs with the components required to maintain secondary containment. Control of

the configuration of these plugs remains necessary to prevent creating an opening in the

secondary containment that would prevent the standby gas treatment system from

maintaining secondary containment in the event of an accident, inadequate control of the

plugs demonstrated in October and the lack of timeliness for incorporating the proposed

procedure revision have resulted in a violation.

Ill. Engineering

E1 Conduct of Engineering

E1.1 Primary Containment Isolation Valve Confiouration Error and inadeauste Testina

a. Insoection Scoce

On December 5, an engineer inspecting a breaker cubicle identified a mis wired closing

circuit for the Unit 1 reactor core isolation cooling (RCIC) inboard steam isolation valve

(HV 491F007). A contact that bypasses the closed limit switch and thermal overload

protection had been incorrectly terminated. During the subsequent investigation, the

engineering staff also identified a testing deficiency,

b.- Observations and Findinas - ---

The engineer recognized that circuit in the AC cubicle was wired in the configuration

normal for a DC breaker. Normally in the AC cubicle, the 42 C contact is terminated at

- terminal block 5&6 and is terminated at terminals 21&22 for the DC.

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The circuit, as wired, would permit the closed limit switch instead of the torque switch to

stop valve motion during an automatic isolation. Consequently, the valve may not close

fudy into the seat, creating the poten'.lal for leakage past this primary containment isolation

valve (PCIV). The licenses declared the RCIC inboard steam isolation valve inoperable and

isolated the penetration to comply with technical specifications.

The licensee identified that the computerized wire termination data base was consistent

with the mis wired RCIC circuit. The licensee evaluated the data base and determined that

a nutriber of PCIVs had the same or similar type closing circuits. Further review found

three additional database descriptions that appeared to be discrepant. Field inspections of

these three discrepancies revealed only one additional valve, the Unit 1 RCIC exhaust line

vacuum breaker, with the same mis wiring. The licensea also identified that the PCIVs

were not adequately tested. Specifically, the control circuit in question contains two

parallel paths; one for manual operation with thermal overload protection and thu other for

automatic isolation with the thermal overload protection bypassed. Both these paths are

energized during automatic valve isolation. The licensee identified that a failure of the

bypass contact could be masked by the proper operation of the valve via the thermally

protected portion of the circuit. Therefore, the test did not verify that a containment

isolation signal would fully close the valve with the thermal overload protection bypassed,

as required by technical specifications. The licensee implemented the appropriate technical

specification requiremot (s and subsequently tested the bypass contact for all affected

valves. All out one PCIV functioned correctly when proporly tested and the licensee

addressed this malfunction.

The valve mis wiring problern was identified by an engineer during a breaker cubicle

inspection to evaluate the use of some non quality parts. The licensee also determined

that the problem was introduced during a construction modification to add a closed limit

switch contact to address another issue with torque switch re-closure following valve

isolation.

The mis wired valve circuit and associated drawing issues are unresolved (URI 97-10-04)

pending NRC review of the licensee's identification of the root cause and implementation

of corrective actions. The inadequate testing issue is also unresolved (URI 9710-05)

pending NRC review of the licensee's identification of the root cause and implementation

of corrective actions,

c. Conclusion

The PECO engineer demonstrated excellent awareness of component configuration by

recognizing the terminal mis wiring. Engineering promptly identified that the r ':lVs were

not adequately tested and implemented adequate measure to complete the rs uired testing

within the time allowed by technical specifications.

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E2 Engineering Support of Facilities and Equipment

E2.1 (Closed) LER 1 97 011 Unit i Hlah Pressure Coolant inlection (HPCI) Turbine

Exhaust Valve dailure

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a. inspection Scop.g

On January 8,1998, the HPCI Turbine Exhaust Valve failed to stroke fully closed on the

first attempt during a routine valve stroke time surveillance test. The inspector reviewed

the engineering evaluations and corrective actions performed to address the survaillance

test f ailure,

b. Observations and Findinns

During stroke time testing of the HPCI turbine exhaust valve (HV- >1 F072L a loud

grinding noise was heard at the valve and the valve operator torque switch actuated,

stopping valve movement. The normally opca valve stopped at approximately twenty five

percent closed during the close stroke. The valve was then re opened and during a

subsequent attempt the valve closed without incident. This valve is a remote manual

containment isolation valve that is required, by technical specifications, to close within 120

seconds. Although the valve does not have an automatic isolation function, it is necessary

to isolate the HPCI system considered to be an c.'. tension of the containment boundary, in

the event of a HPCI system leakage. The valve was declared inoperable and closed to

comply with the primary containment isolation techn cal specifications.

The failure of a primary containment isolation valve and the associated isolation of HPCI

which caused the loss of the high pressure injsction safety function was reviewed for

reportability and appropriately found to be not reportable. Although the valve condition

resulted in the isolation of HPCI to comply with technical specifications, the PCIV

deficiency, by itself, would not have resulted in a loss of the a safety function prior to

identification and resultant actions taken by the operators. Tho inspector noted that the

licensee had reported the previous valve failure and considered this a conservative report.

Although the licensee's reportability determination for the most recent failure was

ultimately correct the inspector noted some inconsistencies with the licensee's bases and

the NRC guidance (NUREG 1022) on reportabilty. The licensee acknowledged the

inconsistency and plans to review and revise their reportability procedures as necessary.

The HPCI turbine exhaust valve is required to be tested quarterly; however, the valve was

being tested at a monthly periodicity as a result of previous stroke f ailures, consistent with

the in service test (IST) program requirements. T he inspector found that valve HV-055-

1F072 had four si.nilar f ailures in the last four years. Following each of these failures, the

valve was successfully closed on the tecond attempt af ter re-opening the valve.

Diagnostic testing on tho three most recent failures verified that there was no observable

valve damage and that subsequent diagnostic tests did not indicate a degradation in valve

performance. During the most recent failure, the licensee identified mechanicalinteraction

of valve internal components while performing diagnostic evaluations during the first

attempt to close the valve. The failures and associated corrective actions for valve HV-

0551F072 are as follows:

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March 1994 During routine HPCI system restoration the valve f ailed to fully close.

The root cause was identified to be lack of lubricatinn on the valve

stem. The stem was lubricated and the valve subsequently stroked

successfully.

December 1994 During a scheduleu HPCI system work window this valve experienced

mechanical binding near the full open position when stroked by hand.

The f ailure was attributed to thermal effects (binding). The valve was

placed on increased frequency IST testing (30 day intervals).

May 1995 The torque switch setting was increased to overcome the frictional

forces of internal valve binding exhibited in the December 1994

ovent. The valve was successfully stroked numerous times during

increased frequency IST testing (Dec.1994 to May 1995), subsequent

quarterly testing and HPCI system scheduled maintenance.

September 1937 During application of a HPCI system clearance for a planned outage

window this valve f ailed to fully close. Diagnostic testing did not

identify a root cause and the valve was again placed on IST increased

frequency stroke time testing (30 day intervals).

October 1997 During the monthly increased frequency valva stroke time testing the

valve f ailed to fully close on the first attempt. The valve failed in the

same manor as the September failure. Investigation of this failure did

not identify a root cause. The valve actuator output force was

increased, by adjusting the torque switch, as a precautionary measure

to improve valvo performance. Motor control center (MCC)

components were reviewed to ensure that the additionalload would

not adversely effect other equipment. The valve remained on

increased frequency IST valve stroke time testing,

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December 1997 Diagnostic testing identified that the valve operator motor was

degraded, but operable. Based on the test data the licensee

l concluded that this may have been a contributor but was not the root

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cause of the incomplete valve strokes,

January 1998 During increased frequency IST valvc atroke time testing this valve

f ailed to closed. The valve was reopened and successfully stroked

closed. Diagnostic testing performed during the failed stroks attempt

indicated internal valve binding. Subsequent diagnostic testing

verified there was no internal valve damage which was consistent

with past testing.

The inspector observed the site engineering interdisciplinary review and disposition of the

valvo performance at,d assoc:ated operability issues. This interdisciplinary review team

consisted of the system manager, component experts, engineering supervision, onsite and

off site licensing. The review was thorough with good candid discussions on the required

safety functicos, current licensing basis and technicalissues associated with this valve.

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Although the review was appropriately focused on plant safety, the interdisciplining team

did not adequately consider the compliance with the stoke time specified in technical

specifications. The review concluded that this valve is of minor safety significance, there

was no evidence of valve damage during the past failed attempts to close the valve and it

could be closed successfully on the second attempt. Therefore, engineering was confident

that the valvo would closo and if it did not close on the first attempt then the applicablo TS

would be entered. However, engineering did not recommend any additional or different

measures to improve the reliability of this valve to closo on the first attempt necessary to

ensure the requirod closure time would be met.

The plant operations review committee (PORC) review of this issue considered operational

impacts, including, current operator workarounds, accident progression, and operator

abilities and concluded that these additional operator actions would not adversely burden a

reactor operator. However, the inspectors observed that PORC failed to challenge the

engineering recommendation and aid not fully address compliance with the required stroke

time in light of the repeated f ailures of the valvo to close on the first attempt. In this

review, PORC discussed increasing the valve stroke testing to more frequent interval than

the 30 days specified by the IST program, but concluded that it was not necessary. The

overall recommendations were similar to the sito engineering recommendations discussed

in the above paragraph.

The inspector determined that the licensee did not establish an adequate bases for

operability and f ailed to fully address the required closing time specified in technical

specifications. The inspector questioned the ability of the valve to consistently meet the

required closure timo in light of the valvn p;itormance history coupled with the lack of a

definitive root cause. The concern was discussed with the plant manager.

As a result of the NRC concern, additional engineering evaluations were performed and the

PORC members reconvened to further address the bases for operability. The subsequent

engineering assessment concluded that stroking this valve more frequently than 30 days

would not damage the valve but also that the valve was fully operable in the current

condition. At the conclusion of the management meeting the PORC members determined

that stroking of the HPCI exhaust more frequently than a 30 day interval was acceptable.

Ultimately the licenseo determined that stroking the valve at a more frequent interval would

be prudent and provide the necessary assurance of valve operability. The valve was

declared operable following three successful stroke tests and placed on an increased test

frequency of seven days to ensure reliability of this valve.

The inspector determined that the purpose of the safety evaluation was to review the

impact of delaying further investigation and repairs to the HPCI exhaust valve until the next

scheduled refueling outago and the review of procedure changen being implemented to

address a f ailure of the valve to close on the first attempt. However, this was not an

appropriate vehicle to address the degraded condition of the HPCI exhaust valve sinco a

there was a technical specification requirement for valvo stroke time which was being

impacted by the valves performance. Although the engineering assessment and supporting

safety evaluation provided a strong safety bases for removal of the stroke time requirement

from the technical specifications, the requirements cannot be modified directly or indirectly

using the 10 CFR 50.59 process.

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The HPCI turbine exhaust valve (HV 0551T072)had f ailed five times in the last four

years. Three of the five failures have r>c':urred in the last five months. The inspector was

concerned regarding the adequacy of the corrective actions implemented during those

failures. This issue is unresolved (URI 97-10 06)pending the identification of the root

cause of the valve failures to close on the initial attempt and the subsequent corrective

actions.

c. Concludgna

The engineering assessment and supporting safety evaluation to support operability of the

HPCI exhaust valve was inadequate in that it did not address the valve closure time

requirements. The plant operations review committee (PORC) approved the safety

evaluation, but f alied to challenge the engineering assessment discounting the requirement

for the valve to close the first time to meet the closure time required by technical

specifications in assessing operability, PORC accepted the degraded condition of the valve

without having identified the root cause or evaluating the corrective actions to ensure

future valve reliability and thereby the ability to meet the required closure time.

The use of a safety evaluation to accept the delay in further investigations and testing of

the HPCI exhaust valve, until the next scheduled refueling outage, in effect inappropriately

modified the technical specifications required closing time. The use of the safety

evaluation in addressil.g operability was not necessary nor consistent with NRC guidance

on operability provided in generic letter 91 18.

E2.2 Emeraency Diesel D22 Loss of Control Durina Monthlv Load Test

a. Insnection Sqgng

On January 7, during the monthly load test of D22 EDG the control room operator was

notified by l&C personnel who noticed e change in pitch of the engine as well as the diesel

load at 3700 KW. The control room operator found the D22 EDG running at 2800 KW

and started to lower the load to 2750 KW, The engine load instantly increased to 3700

KW and the operator could not restore the load to normal. The operator secured the EDG

and declared it inoperable. The inspectors reviewed the root cause, corrective actions, and

operability determination for the EDG.

b. Obserygtions and Findinas

The cross current control relay (CCCR) was found in the de energized condition and its

contacts had high resistance. When energized the CCCR allows the EDG droop circuit to

control the loading of the diesel. When the CCCR is de-energized the droop circuit

feedback is removed and the EDG will operate in the isochronous mode (will attempt to

carry all the loads on the bus). The de-energization of this relay resulted in the EDG

loading as it would during an accident. The EDG attempted to carry all the loads on the

bus which was in parallel with the grid but was limited by the fuel rack stops.

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The root cause of the CCCR relay failure was found to be a high resistance en the relay 71n

to socket connections. Oxidation was found at the base of the pins, on the portion not

coated with solder, which caused intermittent contact and allowed the relay to de energize.

Since another EDG was inoperable for planned maintenance the CCCR from that EDG was

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also sent out for analysis, which found similar but less severe oxidation. The CCCR relays

for both EDGs were replaced. At the end of the inspection period the licensee was still

evaluating the cause of the oxidation and possible corrective measures. The inspector

determined'that although the root cause for this event appears to have been adequately

identified, there was no cause and effect analysis documented and the as found conditions

were not documented in detail in the work order.

PECO inspected areas that could have been over stressed during the overpower event

including the upper and lower piston rings, the connecting rod bearings, and thrust

measurements of both turbo chargers. No excessive wear or damage was identified and

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the turbo charger tole.ances were within specifications. The review of the generator

performance during this overpower condition concluded that the generator sizing was

adequate to support the increase load without degradation.

The inspector also reviewed the maintenance rule (MR) f ailure analysis. The required

function of the EDG is to supply AC power to the appropriate safeguards bus in the event

of a loss of offsite power with and without a coincident loss of coolant accident. For

these conditions the EDG starts with the governor controlin isochronous mode in which

case the CCCR relay is not energized. Since the CCCR relay is not required to energize for

the safety related function of the EDG, this failure would not have prevented EDG from

starting and loading as required by plant analysis. The licensee correctly evaluated this

f ailure to not be a maintenance rule functional f ailure,

c. Conclusions

The organization response to this event was good particularly since another EDG was also

inoperable for planned maintenance and was competing for the same personnel resources.

, The D22 EDG was returned to an operable status in about two and a half days following a

thorough assessment of the overpower event which including a variety of followup

! inspections and measurements. The root cause analysis of this event was adequate;

however, documentation weaknesses were noted including the as found conditions not

being documented in detail in the work order.

E6 Engineering Organization and Administration

E6.1 Main Safety Relief Valve Commitment Chanae

a. insoection Scoce (71707)

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The inspector reviewed a commitment change regarding the threshold for the licensees

actions related to leaking main safety relief valves (MSRV). In two letters dated October 6,

1995 and March 1,1996, between PECO Energy and the NRC, the licensee committed to

an action plan to address main steam safety relief valve leakage. This commitment was a

result of an inadvertent opening of an MSRV as a result of degradation from prolonged pilot

valve leakage (see Resident inspection Report 50 352/353 95 81).

b. Observations and Findinas

On October 15,1997, the licensee forwarded a letter to the NRC which stated, "the

purpose of this letter is to inform the NRC of a change to the commitment for MSRV

leakage action plan only " The letter discussed the revision of the temperature and leakage

parameter values for monitoring and performance of an operability assessment including

the bases for these changes. An overview of the revised action plan was provided as an

attachment.

PECO submitted the commitment cinange per the process as described in procedure t.R C-

1, exhibit 4. The inspector determined that the specific commitment change

documentation _ identified that implementation of the change was acceptable and that a 10

CFR 50.59 safety evaluation was not required. Normally, the NRC would be notified of the

revised commitment during the next annual summary report; however, PECO elected to

notify the NRC prior to the annual summary report due to the previous sensitivity of the

issue.

The inspector questioned when the revised commitment would be implemented. An MSRV

having an elevated tailpipe temperatore already existed at Unit 2. The inspector noted that

PECO's actions were as addressed using the originally comrnitted strategy. Three months

later, at the end of the inspection period, the inspector noted that PECO had not

implemented the revised methodology to address MSRV leakage. The licensee explained

that the advance letter was to notify the NRC of the upcoming change, and was not

intended to reflect that the change had occurred. PECO plans to implement the MSRV-

commitment change in the near future and consequently will not revise the letter. In

addition, PECO plans to review the procedures and make changes as necessary to ensure

that written communications clearly identify the dates by which commitments are expected

to become effective if not already implemented.

Although the revised methodology appeared technically sound, based on interviews and a

review of the available data, the technical evaluation to support the modification of the

commitment was not well documented. Specifically, the evaluation to support revised

monitoring and operability strategy was not comprehensive in that it did not correlate the

performance data to specific changes in the thresholds values. For example, the

operational data used as the bases for the threshold for performing an operability

assessment wers not delineated. The f ailure to appropriately detail engineering evaluations

creates a vulnerability to subsequent reviews such as plant operations review committee

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assessm:nts. Based on discussion with engineering management the documentation did -

not meet their expectations and would be enhanced in the future for similar evaluations.

The licensee plans to ensure complete and comprehensive evaluation of a change to an

NRC commitment is documented in a single change package.

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c. Conclusions

The licensee appropriately implemented the commitment change process for the main

safety relief valve commitment change. Although the timing of NRC notification for the

change was sooner than required by the process, the letter was misleading in that it

implied that the change had been implemented as of the date of the letter, whereas three

months later at the end of the inspection period the change had not been implemented.

However, no violation of NRC requirements was identified. In addition the engineering

evaluation to support the modification of the commitment was not comprehensive in that it

did not correlate the performance data to specific changes in the thresholds values.

IV. Plant Support

R1 Radiological Protection and Chemistry (RP&C) Controls

R1.1 Internal Exoosure Assessment

a. Inspection Scone (83750)

The inspector reviewed the licensee's internal exposure assessment program through a

review of positive whole body count measurements and resulting licensee assessments and

exposure record documentation. Calibration of whole body counters and measurement

capability were also reviewed.

b. Observations and Findinas

The inspector determined from a review of approximately 20 positive whole body counts

over the previous 18 month period, that approximately 2/3 of these whole body counts

had significant unidentified peaks with low error associated with them, it was not

apparent that whole body counts indicating unidentified peaks were effectively resolved

and dispositioned by the staff, though all were reviewed.

For example, a June 22,1996 whole body count determined an internal dose of 3.4 mrem,

however, the whole body count had an unknown peak that represented 23% of the total

counts abovs background (not including natural radioactivity). This peak may have been

cobalt 60 and if it had been properly dispositioned, would have added 12.5 mren to the

internal dose assessment for a total of ' mrem instead of 3.4 mrem.

.

Whole body counter Quality Control (QC) checks were performed prior to instrument use

each day. Cesium-137 and cobalt 00 sources were utilized and the detector performance

and trending data were not printed out or otherwise documented. The software program

.provides notification to the whole body counter operator if the QC check falls outside of

three standard deviations of the decay-corrected source activity. -= -- -

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The licensee had appropriate calibrations performed for both Sodium lodido (Nall detector

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whole body counters in October 1997 that utilized appropriate phantom geometry w3 th

National Institute of Standards Technology (NIST) traceable sources. Upon review of the

licensee's 10 CFR 61 waste stream analysis results, the inspector compared the principal

gamma emitter photon energy peaks for each radio nuclide with the whole body counter

peak resolution calibration. Both whole body counters exhibit photon peak resolution of

approximately 61 kev in the 800 kev range. The inspector noted that cobalt 58 and

manganese 54 have principal gamma photons separated by 24 kev, and that according to

the calibration results reviewed, the whole body counters would not be able to accurately

determine these two common radio nuclides. The licensee conducted two separate tests

with medium and high activity smears from the plant that contained significant quantitles

of both cobalt 58 and manganese 54. The whole body counter (Accuscan bed counter)

identified manganese 54, but failed to identify any cobalt 58 from either test. Other

gamma emitters that were identified in the test samples by the chemistry counting

laboratory, were also not detected by the whole body counter (zinc 05, chromium 51, and

iron 59). Approximately 04% total activity of the gamma emitters was not identified by

the whole body counter.

To demonstrate the potential effect, the inspector weighted the percentages of each

gamma-emitting isotope by their Annual Limit for Intake for inhalation and determined that

the whole body counter identified approximatoty 85% of the hypotheticalinternal exposure

from the gamma-omitters. Approximately 15% of the internal exposure was not

represented. Therefore,if the smears taken by the licensee were indicative of the plant

airborne inhalation hazard, the licensee's dose assessments, if based solely on whole body

count measurements, may be approximately 15% low.

The inspector reviewed approximately 20 whole body counts that indicated activity above

background (and natural radioactivity) and noted the same phenomenon. In addition, from

the review of a personnel contamination incident that occurred on August 2,1991

(documented in Section R8.1 of this report), the radio nuclide Cr 51 was the prominent

isotope found in urine samples collected, was detected in nasal smears, and in

contaminated clothing samples, however, none of the whole body counts identified this

radio nuclide. For that case, the licensee utilized the urine bloassay data to calculate the

exposure due to the Cr.51 and added it to the whole body count derived exposure.

The inspector determined that the licensee's program for use of the Nal whole body

counters at Limerick did not appear to have sufficient rigor relative to the disposition and

assessment of uridentified peaks. Further, it was not apparent that the staff was

cognizant of the equipment limitations posed by Sodium-lodide detectors relative to the

effective resolution and identification of all of ine detectable radio nuclides that may be

common to the plant,

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Notwithstanding this weakness, the effectiveness of the contamination control program at

Limerick has made it unnecessary for the licensee to document internal exposures of

workers. Consequently, weakness in this particular area does not currently effect

personnel exposure assessments. The licensee committed to perform further review of this

area to ascertain the adequacy of the equipment, procedures, and personnel training in this

area.

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The licensee utilizes personnel contamination monitors located at the egress from the RCA

and from the station protected area, for detecting the presence of internally deposited radio

nuclidos. The use of these monitors has replaced the use of routine entrance, exit and

annual whole body counting of station personnel. The Eberline PM 7 monitors are gamma

sensitive plastic scintillator detectors that appears to have, based on currently identified

station radio nuclides, the ability to detect approximately 4% of the annuallimit of intake

(All) based on the most restrictive radio nuclide within 7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> of the intake. This

corresponds to on internal exposure screening level of approximately 200 mrom. By

procedure, following a PM 7 alarm, contamination frisking and,if necessary, investigative

whole body counting is performed in order to quantify internal exposures. Regulations

require internal exposure determinations at 10% of an ALI (500 mrom for Limerick Station).

No discrepancies were noted,

c. Conclusion

The radiation protection program controls for preventing internal exposures was effective.

No significant personnel exposures were apparent. However, the whole body

measurement capability appeared to lack sufficient rigor in ssuring that allinternally

deposited redio nuclides, that the whole body counting inv..ument was expected to detect,

were effectively identified and evaluated. It was not apparent that staff were cognizant of

the inherent limitations of the equipment relative to discrete resolution of energy peaks to

offect radio nuclide identification. The licensee acknowledged the inspection finding and

stated their intent to procure a higher resolution whole body counter detector before the

next refueling outage.

R 1.2 Resoiratory Protection

a. Insoection Scoce (83750)

The respiratory protection equipment storage and issue controls were reviewed.

b. Observations and Findinag

The licensee's respirator processing is provided by a vendor service. The licensee has

conducted a vendor QA audit upon initial contracting for this service in 1997. The

radiation protection L.mager (RPM) indicated that periodic audits of this service would be

conducted by the RP group to ensure calibrated leak testing of respiratory protection

equipment is conducted as required. Proper onsite storage and control of respirators and

breathing air bottles was verified, issuance of respiratory protection is controlled through

computer verification of qualifications, which was verified by the inspector. The station

service air and Eagle air compressor (utilized for filling air bottles) air quality had been

tested quarterly and met Grade E quality standards (as defined by the Compressed Gas

Association). Allinspected areas of the respiratory protection program met regulatory

requirements.

c. Conclusions

The respiratory protection program met regulatory requirements.

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R1.3 Countina Laboratory Calibrations

a. Insoection Sjagg (83750)

The inspector reviewed the licensee's air sample counting laboratory instrument calibration

and OC response check program with respect to regulatory requirements and industry

standards. This review consisted of laboratory counting geometry observations, review of

calibration and detector response check documentation, and interviews with applicable

licenses staff,

b. Observations and Findinas

The inspector reviewed the calibration data for two gas flow proportional counters and four

germanium detectors that are utilized for counting air samples as well as chemistry '

samples. The calibration data indicated that appropriate voltage plateaus and counting

efficiencies had been determined utilizing NIST traceable sources following correct

methods. OC response checks for all the above counting instruments were kept up to date

and provided the appropriate trending data of detector performance.

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The inspector reviewed the most recent 10 CFR 61 radio nuclide analysis results for the

- dry active waste-stream, which represents average plant contamination, and therefore,

altborne contamination. Using this information, the inspector determined that

approximately 6.3% of the total activity consisted of non-gamma emitting rsdio nuclides

that were not measurable by the germanium detector counting equipment with respect to

average plant contamination. By reference to 10 CFR 20, Appendix B, the missing activity

would account for approximately 2.7% of Derived Air Concentration (DAC) measurements.

Although this is a relatively low amount, the licensee does not have a criteria for including

non gamma radio nuclides into DAC evaluations. The RPM indicated that this issue would

be reviewed,

c. Conclusion

The air sample counting laboratory provided properly calibrated and reliable sample analysis

services.

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R1.4 Release of Material from Turbine Buildina Roof

lhe licensee began replacing the turbine building and control structure roofs in August

1997 and work was in progress at the time of this inspection. The licensee had taken

j numerous core samples and found trace contamination in three samples of the outer rock

L layer from the control structure traf centerline while all other samples did not indicate any

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measurable activity. Approximately 8 drurm of rr cLs were collected from the control .

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structure roof to be shipped to a radwaste pi. . ssing vendo.. All other roof material was

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free released and disposed of in a conventionallocallandflil. The inspector reviewed the

licensee's sampling plans that included 188 core and rock samples and determined that a

good systematic sample plan had been conducted. The inspector reviewed the sensitivity

of sample counting. The licenset utilized the Offsite Dose Calculation Manual (ODCM) to

establish the counting sensitivity at the envirai.mentallower limits of detection (LLDs).

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Selected roof sample analysis results were reviewed and the inspector verified that for the

roof materials released for unrestricted use, no radioactivity was detected in those samples

and they were adequately counted to the environmental LLD sensitivity level as specified in

table 13.4 3 of the OCDM.

R1.5 lanigsentation Calibration

a. Insnection Senpe 183750)

The inspector reviewed the licensee's portable radiation detection instrumentation and

dosimetry calibration program through a review of plant radiation characterization; source

selection and instrument calibration; and instrument calibration method: logy and

instrument calibration records. This review included calibration laboratory observations,

instrutnent calibration record review, and interviews with plant staf f.

b. Observations and Findinas

Through a review of April 1997 in situ gamma scans of plant piping and a review of the

most recent waste stream characterization data, the inspector determined the average

gamma and beta energies at Limerick Station to be 1.2 MeV and 100 kev, respectively.

The inspector reviewed the instrument calibration sources and determined that the Tc 99

beta source was appropriate for the beta spectrum in the plant, however, the Cs 137

source, at 662 kev, was a calibration source that was almost half of the average gamma

energy found in the plant. The inspector determined that the licensee's calibration '

methodology did not correct for this difference in gamma energy. By reference to

instrument vendor information for two of the most common portable radiation detection

instruments utilized at Limerick (Eberline RO 2, E 530), the response in the field would be

expected to be 2 5% higher than actual. Though this is a minor error in the conservative

direction, the inspector noted that the licensee's process compensated for other errore,

such es temnerature and pressure, that had a more minor effect on instrument accuracy.

Other minor discrepancies included:

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Source to-instrument distances needed for calibration were not determined prior to

source calibration. Consequently, during instrument calibration, dose rate values

needed to be interpolated between values, which may introduce a minor, but

unnecessary, calibration error.

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The vendor software program that provides decay corrected source calibration

tables of dose rate versus distance for each source attenuator was not inputted

with the current NIST traceable source calibration values. Accordingly, a minor

error may be included into the instrument calibration target values.

The RPM indicated that these source calibration discrepancies would be reviewed and

action taken as necessary to assuro the accuracy of the RP instrument calibration program.

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The inspector reviewed calibration documentation records for selected RP instruments that

were available for issue and determined that all were properly calibrated within the required

time period. The inspector also verified proper locked storage of calibration sources and

that the source calibrator interlocks were in proper operating condition to prevent

Ir. advertent exposure to personnel.

A review of the Rados Rad 51 electronic dosimeter calibrations and National Voluntary

Laboratory Accreditation Program (NVLAP) testing results indicated appropriate calibration

techniques and calibration frequencies were met and that the electronic dosimeter

demonstrates a positive 11% bias in the normal gamma energy range of the plant and a

positive 8% blos for high energy gammas associated with N 16 decay that might be

enn intered during personnel entries at power. The positive bias is desirable to ensure

conservatism in the exposure control program relative to later TLD processing and record

exposure determinations No discrepancies were noted.

A review of TLD processing quality controls were found to be excellent and well managed.

Af ter changing to (ICN), as a new TLD processing vendor in early 1997, quality control

badge processing results indicated combined bias and standard deviation values

approaching NVLAP limits. Both Peach Bottom and Limerick RP staffs actively pursued the

issue with ICN, which resulted in new Thermoluminescent Dosimeter (TLD) calibration

factors for e..;h TLD and resulting improved performance. Each calendar quarter Limerick

and Peach Bottom alternate sending spiked quality control TLD badges for testing of the

vendor's TLD processing capability. The TLD vendor maintains current NVLAP

accreditation as required,

c. Conclusion

The inspector determined that the licensee's radiation protection calibration program

utilized sound principles, however, minor discrepancies in the instrument calibration

process had the potential to introduce unnecessary errors. Notwithstanding, the

instrument calibration area was determined to be adequate. The TLD program oversight

was very effective in enhancing the accuracy of vendor TLD processing results,

a R2 Status of RP&C facilities and Equipment

During this inspection, the inspector conducted numerous tours of the plant during

operating conditions. The licensee made frequent use of radiation dose rate postings and

posting sources of radiation postings in applicable areas, which were excellent practices.

All radiological postings and locked areas mot regulatory requirements and areas were

generally clear of unnecessary equipment, wellilluminated and generally free of safety

hazards. One exception, an abandoned in place post accident sample skid, was noted in

Unit 1 Reactor Building, Room 501.

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R4 Staff Knowledge and Performance in RP&C

R4,1 Exoosure Discrenancy Reports

a. Insoection Scope 183750)

The inspector reviewed the disposition of external exposure discrepancies for the third

quarter of 1997 that indicated exposure differences between Individual's quarterly TLD

results and quarterly electronic dosimeter (ED) exposure results,

b. Observations and Findinas

The inspector observed that there were a large proportion of exposure discrepancies

derived from individuals making roof repairs from the turbine and control structure roofs.

Upon review of several of the roofers exposure discrepancy reports, the inspector observed

that all of them showed higher ED results, i.e., between 27% and 111% greater than TLD

results for the same time period, in all cases, the personnel exposures were well below

regulatory limits.

All of the subject exposure discrepancy reports assigned the lower TLD results rather then-

the more conservative decision to assign the electronic dosimeter results in the personnel

exposure records. The reasons stated in the individuals' personnel exposure records were

nonspecific, but indicated that degraded N 16 gamma photons and electro-magnetic field

(EMF) interference could have caused the discrepancy and that surveys of the roof

confirmed the TLD results.

Expecting that EMF radiation may be responsible, the licensee conducted a EMF survey but

did not detect any EMF fields. The inspector's review of the ED calibration testing

indicated a relatively accurate response in the N 16 gamma energy range. At the time of

the inspection, the licensee was still attempting to test the EDs response to cellular phone

broadcast interference, but no evidence had been uncovered that would explain the

exposure discrepancy results for the roofers. -

The inspector identified that this area will be followed to ensure the adequacy of the

licensee's process for evaluating personnel dosimeter result discrepancies.

(IFl 50 352,353/9710 07).

c. Conclusion

Several exposure discrepancies between T! D and electronic dosimeter quarterty results

were resolved but the adequacy of their disposition requires further review.

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R5 Staff Training and Qualification in RP&C

RS.1 RP Technicir.n Trainina and Qualifications

a. Insoection Scoce (83750)

The inspector reviewed the RP technician training program, reviewed selected RP

technician qualifications with respect to TS 6.3 requirements, and reviewed the control of

RP work task assignments to only qualified individuals,

b. Observattens and Findinas

During 1997 there were three individuals that completed the initial qualifications for Level 11

(senior) HP technician. Currently all RP technicians at Limerick Station arn fully qualified

Level ll RP technicians. The inspector reviewed the initial RP technician training prngram

and determined that it was comprehensive including sufficient classroom study and job

performance evaluations prior to qualifications.

The inspector determined that the licensee had an adequate process for reviewing staff

qualification signoffs prior to assigning staff duties. At the principal radiological controlled

area (RCA) access point (41 line), an RP technician qualification matrix is printed out

weekly and made avaliable for first line supervisor use in assigning only qualified staff to

perform tasks. By licensee procedure (TO C 7), it is the supervisor's responsibility to

ensure staff are not assigned to perform work they are not qualified to perform.

The Radiation Protection (RP) technician continut... training was found to be adequately

implemented, in February 1997 the licensee administered an RP fundamentals examination

to 36 permanent RP technicians. The results were poor. The licensee provided remedial

training and testing and the results improved to an adequate level. The licensee is aware

of the RP fundamentals training weakness and is working to improve the level of RP

technician knowledge in this area,

c. Concluiisnt

The RP training program was adequate. The licensee has self identified a weakness in the

RP fundamentals training provided to RP technicians in the continuing training program,

and has made some progress in addressing this concern Currently, all RP technicians are

fully qualified senior technicians and an active continuing training program and qualification

tracking program is in place.

RS.2 Advanced Radiation Worker Pro 2Lan]

a. Inuction Scooe (83750)

The inspector reviewed the licensee's advanced radiation worker procedure and selected

survey results with respect to Technical Specification 6.3.1 requirements.

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b. Observations and Findinas

The licensee has established a program to qualify experienced radiation workers on certain

se'ected RP tasks traditionally performed by RP technicians. Procedure HP C 111 requires

the advanced radiation worker (ARW) candidates to complete an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> class and

successfully pass a job performance measure evaluation to qualify for task specific RP

technician duties. The procedure limits the radiological conditions to less than high

radiation areas and less than 50,000 dpm/100cm' contamination levels. The procedure

indicates that specific task qualifications can only be added with the approval of the RPM.

The inspector reviewed recent surveys, completed by several advanced radiation workers

and observed that several radwaste technicians that were appropriately qualified ARWs,

had surveyed contanination areas after decontaminativn and based on their surveys,

removed postings and released the areas as clean areas without any RP technician

supervision or verification, it was not apparent to the inspector, wheth7r the ARWs were

within the limited specific task qualification or whether they were exercising broader RP

technician skills of judgement as to when an area of the plant should be deposted. Further

review of the ARW program is needed to properly evaluate whether a violation of staff

qualification requirements has occurred. This is an unresolved item (URI 9710-08),

c. Conclusions

The licensee has limited procedural controls over the scope of the advanced radiation

worker program. Some survey and contamination area control activities have been

performert by the advanced radiation workers that involved evaluation and judgement

determinations without qualified RP technician supervision. Further investigation in the

advanced radiation worker training and performance is nneded to determine whether a

violailon of TS 6.3.1 has occurred.

RS.3 Health Physics Personnel Qualification

a. Insoection Scone

The inspector reviewed the process and controls associated with personnel qualifications

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with a specific focus on the dosimetry clerk position, in addition, the implementation of

i controls for the use of unqualified personnel were evaluated,

b. Qblervations and Findinas

The individual selected for review was found to be fully qualified for the position of

dosimetry clerk. However, during the review the inspector identified that the individual had

performed the duties of dosimetry clerk prior to completing qualification for all tasks. The

job functions are typically broken down to a task or series of tasks for the purpose of

implementing qualifications. Qualification includes a classroom training session and a

subsequent demonstration of task competency during completion of a job performance

measure (JPMs). The individualin question had completed all required classroom training

but had not performed the required JPMs prior to performing the duties of a dosimetry

clerk,

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Technical specifications requires that the unit staff training meet or exceed the standards

of ANSI /ANS 3.1 1978. The dosimetry clerk position is not specifically addressed in this

standard. However, the licensee had establishea a training and qualification program for

this positions that is accredited by the Institute of Nuclear Power. The licensee's program

has provisions for the use of unqualified personnel to perform tasks provided that they are

appropriately supervised. Procedure TQ-C 7, "On The-Job Training and Qualification,"

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requires that unqualified personnel may only perform tasks under the direct, continual

observation of either a qualified worker or line supervision.

The primary functions of the dosimetry clerk include operation of the whole body counters

and an evoluation of the results, performance of respirator fit tests, and issuance of

dosimetry. The inspector reviewed the logs and documentation of whole body scans

performed by the individual that was not qualified and found that generally there was

evidence that a qualified person performed the whole body count reviews or provided

supervision to the unqualified individual. Specifically for the sample of documentation

reviewed, either a qualified individual counter signed the log sheets or signed the whole

body scan results as the reviewer. However,in the case of the other dosimetry clerk tasks

there was no evidence of direct supervision. For example, the dosimetry issue log does

not contain countersigned e les indicating that the task was supervised.

The most significance of the dosimetry clerk tasks is reviewing of the whole body scans

for anomalies. The rest of the tasks were generally found to be of low complexity and low

consequence if improperly performed. For example, operation of the respirator fit

equipment involve operation of a computer driven test routine which automatically prompts

the actions required by the person being tested. An incorrectly performed operational

check or test routine would result in a test f ailure, in the case of issuing dosimetry, this

task is administrative in nature and provisions are in place which would likely identify if

dosimetry issued was not recorded correctly. -

During the records review the inspector identified one instance in which there was no

signature for reviewing the results of a whole body count. Following discussion with the

inspector the licensee plans to perform a more comprehensive sample of personnel records

to determine if a more wlae spread problem exists. The licensee plans to sample a

minimum of 100 files containing whole body counts to confirm the required reviews were

performed and determ;ne any other administrative errors exist.

c. Conclusions

An unqualified person had been assigned to perform tasks which require formal

qualification. Generally, there was evidence of direct supervision for the more critical tasks

performed by unqualified individual such as the performance and evaluation of whole body

counts, However, for administrative tasks, generally there was no recorded evidence of

direct supervision as required by the licensees training and qualification procedures.

Although, the practice of using unqualified and unsupervised personnelis inconsistent with

the licensee's procedure, this was determined not to be a violation of regulatory

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requirements since the position and job functions are not specifically addressed through the

technical specifi .:on requirements for tne training of plant staff. However, the failure of

the licensee to appropriately control the use of unqualified personnelis of concern since

the same procedure control are used to address positions which have specific training

requirements,

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R7 Quality Assurance in RP&C Activities

a. Insoection Scope (83750)

The inspector reviewed the licensee's quality assurance oversite of the RP program

consisting of a review of licensee documents of a recent GA audit, recent QC surveillance,

and RP self antossments,

b'. Observations and Findinas

The inspector reviewed the report of a Quality Division audit of the RP program that was

conducted in March of 1996. The report was detailed and comprehensive. One minor

radiation work permit (RWP) discrepency and some additional training was needed for

outage contractors was reported. The inspector noted that Limerick and Peach Bottom

Stations provide technical specialists to evaluate each other, but no outside PECO Energy

technical specialists were utilized in the independent program reviews.

Since March 1997, there have 16 OC surveillance of the RP program areas that indicated a

wide scope of program review and oversight.

The RP Section provides its own self assessment reviews and the inspector reviewed the .

September 30,1997," Annual Self Assessment of the RP Section," and found it to

represent all of the radiation protection functional areas t the Station and included many

recommendations. This appeared to be a valuable program review.

Other.RP Section program reports were also reviewed by the inspector included the

Radiation Protection Integrated Program Review and the Limerick Unit 2 fourth Refueling

Outage Report.

c. Conclusions

Oversight of the RP program consisted of independent and self assessments that generally

provided for effective insights and recommendations for program improvements,

notwithstanding the minor weaknesses in the instrument calibration and bioassay

measurement programs that were noted by the inspector.

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R8 Miscellaneous RP&C lasues

R8.1 Dose Assessment Review of an Auaust 2,1991 Contamtriction incident

The inspector reviewed a spent RWCU resin personnel contamination incident that

occurred on August 2,1991, where three individuals were contaminated. After repeated

decontamination, persistent skin contamination remained on the extremities of the

individuals. Multiple whole body counts and urine samples were taken and outside

consultants were involved to provide a comprehensive review of bloassay data and to

assess the radiation exposures to the affected individuals. Bioastny rneasurements

continued until August 9,1991, when the contamination levels dropped to below threshold

values for all affected individuals. The highest exposed individual was calculated to have

received 150 mrom to the skin of the right forearm due to the event. Based on

radiochemicallaboratory analysis of several urine samples,3.5 MPC hours was calculated

due to internal exposure. The inspector reviewed the licensee's exposure records and

verified that for each of the three individuale, the additional skin of the extremities

exposure was recordcd, however, no internal exposures were recorded because they were

all below procedural and regulatory rucording requirements, in 1991, the regulatory limits

for the skin of the extremities was 18750 mrom per quarter and the internal exposure

racording requirements were greater than 40 MPC hours per seven consecutive days and a

limit of 520 MPC hours per quarter. Based on the inspector's' review, the licensee

provided a comprehensive dole study related to the August 2,1991 incident; accurately

represented the personnel exposures; and was appropriately documented in the individuals'

exposure records.

P4 Staff Knowledge and Performance in EP

a. inspection Scone 182701)

Following an Alert emergency notification or above, the licensee's Emergency Responso

Procedure (ERP) 6001, Health Physics Team, Step 3.1, states that six Health Physica (HP)

technicians must be onsite within a half hour and six more within 60 minutes. Following

the October 9,1997 Alert incident, the HP Team Leader identified that he had difficulty in

locating 12 qualified HP Technicians and the timeliness of their response was not

acceptable. The inspector assessed the licensee's review of these concerns to determine

the adequacy of their self assessment and corrective actions.

b. Observations and Findinas

The licensee identified three concerns regarding HP emergency response staffing: (1)

untimely emergency notification to the HP staff; (2) not staffing the required HP Technician

positions in a timely manner; and (3) unavailability of qualified technhians.

With the exception of the HP Team Leader, the HP technicia.is are not included in the

emergency automated dialer callout system and are called by the on-shif t technicians

following direction from the Team Leader. The first available individual was not contacted

until 12:08 a.m., approximately 38 minutes af ter the ERO was notified by pagers. The

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inspector reviewed all the sign in logs and determined that the licensee diu not meet the

commitments made in ERP-6001 as stated above. The licensee stated that as a result of

this issue they are planning to add the HP technicians to the automated dialer callout

syttom to ensure an immediate and timely response.

HP technician availat'ility was diminished because the licensee had several technicians

working at Peach Bottom to assist in their refuel outage. The Radiation Protection

Manager is currently working with Peach Bottom management to revise the refuel outage

policy to ensure that there will always be an adequate number of HPs available to meet

their emergency response commitments. Also, a tracking system is being developed to

track all HPs as to whe e they can be located during off-hours.

The inspector reviewed Procedures, NSC 1.2, HP Technician ll Training; LEPP-9500,

Emergency Preparedness Training Plan and training records of the individuals that

responded to the Alert event and determined that their EP training was currer.t. However,

the :nspector noted that three of the HP 11 Technicians did not appear to have completed

all the Job Performance Measures (JPMs) tasks ac required by HP Procedure NSC 1.2,

Section 7.2.2, which states " Emergency Preparedness Training is developed and

conducted by the Site Emergency preparedness organization and is provided upon

completion of HP Technician il Qualifications." After further review of additional training

procedures, the licensee was able to adequately demonstrate that the pertinent JPMs

related to emergency response had been completed by the three individuals. However, the

licensee recogniud that Procedure NSC-1,2 was ambiguously written and clarity and

consistency was needed between HP training qualification procedures and the Emergency

Preparedness training and qualifications plan,

c. CgprJhigi9D

Although, the licensee was not in full compliance with Procedure ERP-000-1, Health

Physics Team, they were proactive in identifying the issues and their corrective actions are

adequate for preventing recurrence. The inspector also noted that these issues were not

identified in previous exercises or drills because the licensee had typically conducted their

exercises during working hours in which HP technicians were onsite and available for

immediate response. This non-repetitive, licensee identified and corrected violation is being

treated as a Nnn Cited Violation inlCV 50 352,353/97-10-09), consistent with Section

Vll.B.1 of the NRC Enforcement Policy.

V. Management Meetingt

X1 Exit Meeting Summary

The inspector presented the inspection results to members of plant management at the

conclusion of the inspection on January 28,199 . The plant manager acknowledged the

inspectors' findings. The inspectors asked whether any materials examined during the

inspection should be considered proprietary. No proprietary information was identified.

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X2 Review of UFSAR Commitments

A recent discovery of a licensee operating their facility in a manner contrary to the UFSAR

description highlighted the need for a special focused review that compares plant practices,

procedures and/or parameters to the UFSAR description, While performing the inspections

discussed in this report, the inspectors reviewed the apolicable portions of the UFSAR that

related to the areas inspected. The inspectors verified that the UFSAR wording was

consistent with the observed plant practices, procedures and/or parameters.

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INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observation

IP 62707: Maintenance Observation

IP 71707: Plant Operations

IP 71750: kant Support Activities

IP 83750: Occupation :l Radiation Exposure

IP 90712: In-office Review of Written Reports

IP 90713: Review of Periodic and Special Reports

IP 92904: Followup - Plant Support

IP 93702: Prompt Onsite Response to Events at Or.-cating Power Reactors

ITEMS OPENED, CLOSED, AND DISCUSSED

Qoened

NOV 50 352,353/97-10-01 Operations Log Did Not Accurately Reflect Conditions in

the Plant. (Lation O2.1)

NOV 50 352,353/97-10-02 Adequate Musures Not Established to Assure Design

Requirements were Adeqth tely Maintained During HCU

On-line Maintenance. (Sec' in M1.4)

NOV 50 352,353/97-10-03 Inadequate implementation af Locked-Valve Controls.

(Section M8.1)

URI 50 352,353/97-10-04 Mis wired Valve Breaker Circuit and Associated

Drawing issues. (Section E1.1)

URI 50 352,353/97-10-05 Inadequate Testing of Valve Breakers. (Section E1.1)

URI 50-352,353/97-10-06 Unit 1 High Pressure Coolant injection (HPCI) Turbine

Exhaust Valve Failure. (Section E2.1)

IFl 50-352,353/97-10-07 Resolution of non conservative exposure determinations

between TLD and electronic dosimeter results. (Section

R4.1)

URI 50 352,33/97-10-08 Datermine whether advanced radiation workers that

survey and release contamination areas should be

qual!fied RP technicians. (Section RS.2)

NCV 50 ?S2,353/97-10-09 Difficulty in Locating 12 Qualified HP Technicians and

the Timeliness of Their response During the October 9,

1997 Alert incident. (Section P4)

Closed

LER 1-97-011 Unit One High Pressure Coolant injection (HPCI) Turbine

Exhaust Valve Failure (E2.1)

URI 97-03-01 Performance of Reactor Enclosure Secondary

Containment Integrity Verification. (Section M8.1)

Discussed

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LIST OF ACRONYMS USED

ALARA As low as is reasonably achievable

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AR Action Request

J AWR Advanced Radiation Worker

g CFR Code of Federal Regulations

W- CRS Control Room Supervisor

DAC Derived Air Concentration

ED Electronic dosimeter

EDG Emergency Diesel Generator

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ERO Emergency Response Organization

E ERP Emergency Response Procedure

g EO Equipment Operator

R- ESF Engineered Safety Feature

FIT Focused improvement Team

FP Fire Protection

HCU Hydraulic Control Units

HEPA High Efficiency Particulate

E HPCI High Pressure Coolant Injection

] IFl

IR

Inspection Follow up Item

inspection Report

LCO Limiting Condition For Operation

LER Licensee Event Report

LGS Limerick Generating Station

Nal Sodium-lodido

NCR Non-Conformance Report

NCV Non Cited Violation

NED Nuclear Engineering Department

NIST National Institute of Standards Technology

NMD Nucleai Maintenance Division

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NRB Nuclear Review Coard

NRC Nuclear Regulatory Commission

NUPIC Nuclear Procurement issues Committee

NVLAP National Voluntary Laboratory Accreditation Program

ODCM Offsite Dose Calculation Manual

PCIV Primary Containment Isolation Valves

PDR Public Docket Room

PECO PECO Energy

PEP Performance Enhancement Process

PORC Plant Operations Review Committee

QA Quality Assurance

QC Quality Control

RCA Radiological controlled area

RCIC Reactor Core isolation Cooling

RHR Residual Heat Removal

RMS Radiation Monitoring System

RP&C Radiological Protection and Chemistry

RP Radiation Protection

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RPM Radiation Protection Manager

RPS Reactor Protection System

RWCU Reactor Water Clean-up j

RWP Radiation Work Permit

SGTS Standby Gas Treatment System

SSPV Scram Solenoid Pilot Valve

ST Surveillance Test

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TLD Thermoluminescent dosimeter

TS Technical Specification

UFSAR Updated Final Safety Analysis Report

URI Unresolved item

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VIO Violation