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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20199L5301999-01-19019 January 1999 Special Rept:On 981214,seismic Monitor Was Declared Inoperable.Caused by Spectral Analyzer Not Running.Attempted to Reboot Sys & Then Sent Spectral Analyzer to Vendor for Analysis & Rework.Upgraded Sys Will Be Operable by 990331 ML20237F0291998-08-27027 August 1998 Special Suppl Rept:On 960425,one Loose Part Detection Sys (Lpds) Was Identified to Be Inoperable.Initially Reported on 960531.Caused by Loose Parts Detector Module.Repairs Performed & Intermittent Ground No Longer Present ML20198S6621997-11-10010 November 1997 Special Rept:On 971009,during D21 EDG Monthly Surveillance Test,Engine Speed Was Cycling Unusually,Load Oscillations Observed on Control Room Indicators & Flame Emanated from Exhaust Stack.Caused by EDG Internal Forces.Repaired EDG ML20211H7951997-09-29029 September 1997 Special Rept:On 970828,EDG Failure Occurred Due to Fuel Oil Leak on Fuel Oil Return Header Tube at Number Four Cylinder. Interim Repair Performed by Removing & Replacing Damaged Section of Tubing ML20198E7391997-08-0404 August 1997 Special Rept:On 970703,diesel Generator Failed Surveillance Test Procedure ST-6-092-311-2.Caused by Motor Operated Potentiometer (Mop) Set Below Its Normal 60 Hz Position. Stroked Mop Through Full Travel While Monitoring Resistance ML20136H2101997-03-14014 March 1997 Special Rept:On 961001,suppl for Inoperability of loose-part Detection Sys Channel for More than 30 Days.Channel/Detector Malfunction Isolated to Instrumentation Contained within Inerted Unit 2 Primary Containment ML20136H1291997-03-10010 March 1997 Special Rept:On 970103,LPDS Declared Inoperable.Caused by Defective Latch Board.Board Replaced & ST Procedure Was Completed Satisfactorily on 970114 ML20134D2391997-01-30030 January 1997 Special Rept:On 970101,failure of Diesel Generator Occurred. Caused by Loose Wire.Removed Banana Jacks from Terminals, Tightened Wires on Terminal Block & Returned Diesel Generator to Operable Status ML20128H3391996-10-0101 October 1996 Special Rept:On 960828,channel/detector Which Monitors Acoustic Level on 'B' Main Steam Line Annunciated in Mcr. Channel/Detector Malfunction Was Isolated to Instrumentation Contained within Inerted Unit 2 Primary Containment ML20112F7921996-06-0606 June 1996 Special Rept:On 960507,D22 EDG Declared Inoperable.Caused by D22 EDG Crankcase Overpressurization Exhaust Backpressure. D22 EDG Exhaust Stack Scraped & Ion Oxide Scale Sheets Removed from Sidewalls ML20117J9751996-05-31031 May 1996 Special Rept:On 960425,inoperability of loose-parts Detection Sys Channel for More than 30 Day Identified. Work Order Initiated to Inspect Instrumentation ML20107L2501996-04-23023 April 1996 Special Rept:On 960312,two loose-part Detection Sys Channels Inoperable for More than 30 Days.Caused by Failure of Sensor.Repaired Control Rod Housing 02-31 Lpds Channel Sensor ML20101G7811996-03-25025 March 1996 Special Rept:On 960224,D21 EDG Declared Inoperable,Due to Inability to Control EDG Load.Loose Connection at Output of Motor Potentiometer Tightened ML20099L7651995-12-28028 December 1995 Special Rept:On 951130,EDG D21 Experienced Pressurization of Crankcase During Performance of Surveillance Tests.Analysis of Failure Continuing.Corrective Actions to Prevent Recurrence Will Be Developed & Implemented as Necessary ML20094M0141995-11-15015 November 1995 Special Rept:On 951017,valid Failure of EDG Occurred While Performing Surveillance Test Procedure ST-6-092-316-1.Caused by Overvoltage Permissive Relay in Output Breaker Closing Logic Not Picking Up.Relay Recalibr & Returned to Svc ML20086G5921995-07-0707 July 1995 Special Rept:On 950507 & 10,loose Part Detection Sys (Lpds) Channel Sensor Found to Be Not Mounted on Piping.Cause Not Yet Determined.Sensor Reattached to Pipe & Channel Returned to Operable Status ML20077E2511994-12-0505 December 1994 Special Rept:On 941124,accelerograph Sensor Inoperable for More than 30 Days.Seismic Recorder XR-VA-105 & Accelerograph Sensor XE-VA-105 Declared Inoperable on 941025.Loose Power Cable to Seismic Record XR-VA-105 Tightened ML20073F7451994-09-23023 September 1994 Special Rept:On 940810,describing Sequence of Events & Decisions Surrounding Potential Noncompliance W/Safe Shutdown Commitments ML20069D6961994-05-31031 May 1994 Special Rept:On 940422,noted Inoperability of loose-part Detection System for More than 30 Days.Caused by Tape Recorder Not Advancing in Play Mode.Tape Recorder Was Repaired,Tested & Declared Operable ML20062L6071993-12-23023 December 1993 Special Rept:On 930526,discovered That Triaxial Response Spectrum Analyzer (Trsa) Could Not Be Properly Calibr & Was Inoperable.Trsa Returned to Vendor on 930626 But Could Not Be Repaired Due to Lack of Spare Parts ML20128B9561993-01-28028 January 1993 Special Rept:On 930102,ST Procedure in Progress D21 EDG Kilowatt Output Was Erratic & Unstable.Caused by Loose Wire on D21 EDG Electronic Governor.Unit 1 EDGs Were Inspected & Verified Not to Have Same Conditions ML20126E8751992-12-18018 December 1992 Special Rept:On 921125,EDG D21 Output Began Erratically Increasing & Decreasing When Control Logic Converted to Isochronous Mode.Caused by Test Start Circuit Deenergizing. Damaged Wire Repaired & Shortened & Governors Inspected ML20115D8981992-10-16016 October 1992 Special Rept:On 920909,discovered That Channel 1 (Longitudinal Axis of Three Orthogonal Axes) of Accelerograph Sensor Failed Test Criteria.Cause Not Yet Determined.Maint Work Request Initiated on 920922 ML20114B9551992-08-25025 August 1992 Special Rept:On 920730,intermittent Operation of Speed Control Response Occurred While Attempting to Synchronize EDG D24 to 4 Kv Safeguard Bus.Caused by Loose Fuse Clip Contacts in 125-volt Dc Circuit.Contacts Tightened ML20083B9371991-09-18018 September 1991 Special Rept:On 910823,D23 Emergency Diesel Generator Declared Inoperable While Plant Personnel Performed Troubleshooting Activities to Resolve Discrepancy Between D23 EDG Local & Remote Kw Meters ML20153G3131988-09-0101 September 1988 Special Rept:On 880817,primary & Secondary Meteorological Towers Declared Inoperable.Caused by Towers Being Struck by Lightning During Thunderstorm.Tower Sensors Returned to Svc on 880823 & Air Temp Difference Sensors Being Replaced ML20151P1071988-07-12012 July 1988 Special Rept:On 880602,six Triaxial Time History Accelerographs Declared Inoperable Due to Inadequate Calibr Surveillance Tests.Tests Revised to Incorporate tilt-table Testing of Accelerographs ML20215C0781987-06-12012 June 1987 Special Rept:On 870518,triaxial Peak Recording Accelerograph XR-VA-151 Inoperable.Caused by Need to Remove Instrument in Support of Removing Vessel Head for Refueling.Recording Accelerograph to Be Reinstalled After Refueling ML20214X1071987-06-0505 June 1987 Special Rept:On 870505,diesel Generator Excitation Circuitry Failed.Caused by Loose Connection of Two Leads on Bottom of Relay K1.Relay K1 Contactor & Two Damaged Leads Removed & Replaced ML20210S3901986-09-29029 September 1986 Special Rept:On 860624,performance of Surveillance Test on Triaxial Response Spectrum Analyzer (Trsa) Indicated That Unit Inoperable.Caused by 240-ohm Resistors Overheating. Defective Amplifier Replaced.Related Correspondence ML20210S3531986-09-16016 September 1986 Special Rept:On 860903,north Stack Wide Range Accident Monitor Declared Inoperable Due to Failure of Sample Pump to Provide Proper Sample Flow.Caused by Torn Diaphragm.Pump Replaced.Related Correspondence ML20209G8171986-07-31031 July 1986 Special Rept:On 860624,discovered Triaxial Response Spectrum Inoperable During Semiannual Surveillance Test. Cause Unknown.Analyzer Will Be Shipped to Mfg for Repairs. Related Correspondence 05000000/LER-1986-009, Ro:On 860312,discovered That LER 2-86-04 & LER 86-009 Not Submitted to Nrc.Caused by Misplaced Repts.Repts Telecopied to Nrc.Procedure for Distribution of Repts Revised1986-04-14014 April 1986 Ro:On 860312,discovered That LER 2-86-04 & LER 86-009 Not Submitted to Nrc.Caused by Misplaced Repts.Repts Telecopied to Nrc.Procedure for Distribution of Repts Revised ML20203G0241986-03-24024 March 1986 Special Rept:On 860102,HPCI Sys Actuated & Water Injected Into Reactor Pressure Vessel Through Loop B Core Spray Nozzle Only.No Corrective Action Will Be Taken Since HPCI Operated as Designed to Control Level ML20155F2461986-03-0505 March 1986 Special Rept:On 860102 & 13,RCIC Sys Actuated & Injected to Reactor Pressure Vessel.Caused by Potential Low Water Level During Planned Turbine Trip & Decreasing Water Level, Respectively.Related Correspondence ML20140F1271986-02-28028 February 1986 Rev 1 to 860131 Special Rept:On 851109,HPCI Into Reactor Vessel Occurred.Rev Changes Reactor Parameter Entitled Coolant Pressure to Coolant Temp. Related Correspondence ML20141E6171986-02-12012 February 1986 Special Rept:On 851218,RCIC Sys Actuated & Injected Water Into Reactor Vessel During Startup Test Condition 6.Reactor Water Level Dropped & RCIC Quick Started Manually to Control Reactor Level.No Corrective Action Taken ML20154G0681986-01-31031 January 1986 Special Rept:On 851105 & 09,two HPCI Sys Actuations & Injections Into RCS Occurred During Startup Testing.No Adverse Effects Noted.No Corrective Actions Necessary ML20137C4861985-11-14014 November 1985 Special Rept:On 850816,0911,12 & 16 During Startup Testing, RCIC Sys Actuations & Injections Into RCS Occurred.Incidents Part of Startup Testing.No Corrective Actions Required ML20132D3701985-07-15015 July 1985 Revised Special Rept Re Cause & Corrective Actions for Inoperable Seismic Monitoring Instrumentation.On 850626,test Results of Triaxial Response Spectrum Analyzer Satisfactory. Related Correspondence ML20128K1841985-06-13013 June 1985 Special Rept:On 850501,surveillance Test for Triaxial Response Spectrum Analyzer Revealed That Acceptable Limits for Specific Acceleration Input of Negative 0.05g Could Not Be Met.Cause Undetermined.Investigation Continuing ML20129J0081985-05-24024 May 1985 Special Rept:On 850227,0301,0403,06,09 & 12,during Startup Testing,Rcic Sys Actuations & Injections Into RCS Occurred. No Corrective Action Required ML20127E8001985-05-0101 May 1985 Ro:On 850131,full Reactor Scram Occurred.Caused by Operator Opening Instrument Isolation Valve on Jet Pump PDI-42-IR005. Shifts Notified That Valving on Racks to Be Done by or W/Instrument & Controls Technicians ML20113B8721985-03-18018 March 1985 Ro:On 850308,peak Acceleration Recorder Declared Inoperable Following Insp.Caused by Melting of Mounting Matl Used to Support Recorder Due to High Temp Inside Drywell Head Area.Recorder Replaced ML20114A0331984-12-27027 December 1984 Ro:On 841118,alarms Received in Control Room Indicating Downscale,Upscale & Inoperability of Source Range Monitor D & intermediate-range Monitors D & H Detector Channels. Caused by 20-volt Dc Power Shorted by Technician 1999-01-19
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D1211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Lgs,Units 1 & 2. with ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A8861999-09-13013 September 1999 Safety Evaluation Authorizing First & Second 10 Yr Interval Inservice Insp Plan Requestss for Relief RR-01 ML20212A4481999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Limerick Generating Station,Units 1 & 2.With ML20211E9891999-08-20020 August 1999 LGS Unit 2 Summary Rept for 970228 to 990525 Periodic ISI Rept Number 5 ML20210L7051999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Limerick Generating Station,Units 1 & 2.With ML20209G0211999-06-30030 June 1999 GE-NE-B13-02010-33NP, Evaluation of Limerick Unit 2 Shroud Cracking for at Least One Fuel Cycle of Operation ML20209D7741999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Limerick Generating Station,Units 1 & 2 ML20207H8331999-05-31031 May 1999 Non-proprietary Rev 0 to 1H61R, LGS - Unit 2 Core Shroud Ultrasonic Exam ML20195G4651999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Lgs,Units 1 & 2 ML20209D7791999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Limerick Generating Station,Units 1 & 2 ML20195B3021999-05-0606 May 1999 Rev 0 to PECO-COLR-L2R5, COLR for Lgs,Unit 2 Reload 5 Cycle 6 ML20206N2901999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Limerick Generating Station,Units 1 & 2.With ML20195G4761999-04-30030 April 1999 Revised Monthly Operating Repts for Apr 1999 for Lgs,Units 1 & 2 ML20206D8971999-04-22022 April 1999 Rev 2 to PECO-COLR-L1R7, COLR for Lgs,Unit 2 Reload 7, Cycle 8 ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205N9311999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Limerick Generating Station,Units 1 & 2.With ML20204G9851999-03-11011 March 1999 Safety Evaluation Re Revised Emergency Action Levels for Limerick Generating Station,Units 1 & 2 ML20207J7461999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Limerick,Units 1 & 2.With ML20199G2371999-01-31031 January 1999 Rev 0 to NEDO-32645, Limerick Generating Station,Units 1 & 2 SRV Setpoint Tolerance Relaxation Licensing Rept ML20199L5301999-01-19019 January 1999 Special Rept:On 981214,seismic Monitor Was Declared Inoperable.Caused by Spectral Analyzer Not Running.Attempted to Reboot Sys & Then Sent Spectral Analyzer to Vendor for Analysis & Rework.Upgraded Sys Will Be Operable by 990331 B110078, Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 11998-12-31031 December 1998 Rev 1 to GE-NE-B1100786-01, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 1 ML20205K0381998-12-31031 December 1998 PECO Energy 1998 Annual Rept. with ML20199F9611998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Limerick Generating Station.With ML20198C7151998-12-10010 December 1998 Rev 1 to COLR for LGS Unit 1,Reload 7,Cycle 8 ML20198A3871998-12-10010 December 1998 Safety Evaluation Supporting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power- Operated Gate Valves ML20206N4061998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Limerick Generating Station,Units 1 & 2.With ML20199E3281998-11-23023 November 1998 Rev 2 to PECO-COLR-L2R4, COLR for Lgs,Unit 2,Reload 4,Cycle 5 ML20195C9771998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Limerick Generating Station,Units 1 & 2.With ML20154H5691998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Limerick Generating Station,Units 1 & 2.With ML20151X3511998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Limerick Generating Station Units 1 & 2.With ML20237F0291998-08-27027 August 1998 Special Suppl Rept:On 960425,one Loose Part Detection Sys (Lpds) Was Identified to Be Inoperable.Initially Reported on 960531.Caused by Loose Parts Detector Module.Repairs Performed & Intermittent Ground No Longer Present ML20237D1041998-08-17017 August 1998 Books 1 & 2 of LGS Unit 1 Summary Rept for 960301-980521 Periodic ISI Rept 7 ML20237A7761998-08-10010 August 1998 SER Accepting Licensee Response to NRC Bulleting 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20236X7641998-07-31031 July 1998 Rev 0 to SIR-98-079, Response to NRC RAI Re RPV Structural Integrity at Lgs,Units 1 & 2 ML20237B4711998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Limerick Generating Station,Units 1 & 2 ML20236N6751998-07-0909 July 1998 Part 21 & Deficiency Rept Re Notification of Potential Safety Hazard from Breakage of Cast Iron Suction Heads in Apkd Type Pumps.Caused by Migration of Suction Head Journal Sleeve Along Lower End of Pump Shaft.Will Inspect Pumps ML20151Z4881998-06-30030 June 1998 GE-NE-B1100786-02, Surveillance Specimen Program Evaluation for Limerick Generating Station,Unit 2 ML20236P9781998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Limerick Generating Station,Units 1 & 2 ML20196K1801998-06-30030 June 1998 Annual 10CFR50.59 & Commitment Rev Rept for 970701-980630 for Lgs,Units 1 & 2. with ML20249B3501998-06-11011 June 1998 Rev 1 to PECO-COLR-L2R4, COLR for LGS Unit 2 Reload 4,Cycle 5 ML20249A5331998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Limerick Units 1 & 2 ML20247M7071998-05-14014 May 1998 Safety Evaluation Supporting Amend 128 to License NPF-39 ML20217Q5101998-05-0404 May 1998 Safety Evaluation Supporting Amend 127 to License NPF-39 ML20247H5071998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Limerick Generating Station ML20216F3601998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Limerick Generating Station,Units 1 & 2 ML20217M0791998-03-31031 March 1998 Safety Evaluation Supporting Amends 125 & 89 to Licenses NPF-39 & NPF-85,respectively ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20216F9471998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Limerick Generating Station,Units 1 & 2 ML20216F3471998-02-28028 February 1998 Revised Monthly Operating Rept for Feb 1998 for Limerick Genrating Station,Unit 1 1999-09-30
[Table view] |
Text
_
_4 n.6.et w.s.r..-
- Plant Manager Limonck oeneratmg Station
.. PECO ENERGY sco. ";,va = l g ,
Po Dox 2300 Sanar p.PA 19464 0920 21s 3271200 Ext. 2000 -
T.S. 6.9.2 November 10,1997 '
Docket No. 50-353 License No. NPF-85
- U.S. Nuclear Regulatory Commission D Attri. ;)ocument Control Desk Washington,DC 20555
SUBJECT:
Limerick Generating Station, Unit 2 Special Report for a Valid Emergency Diesel Generator Test Failure
REFERENCE:
Technical Specifications Sections 4.8.1.1.3 and 6.9.2 This Special Report is submitted pursuant to the requirements of Technical Specifications (TS)
Section 6.9.2 as required by TS Surveillance Requirement 4.8.1.1.3. TS Surveillance Requirement 4.8,1.1.3 requires reporting of all diesel generator failures, valid or non-valid, within 30 days. The report is required to include the information recommended in Regulatory Position C.3.b of Regulatog Guide (RG) 1.108, " Periodic Testing of Diesel Generator Un:ts as Onsite Electric Power Systems at Nuclear Power Plants," Revision 1, August 1977.
On 10/09/97, the D21 Emergency Diesel Generator (EDG) was being run for a monthly surveillance test, which iricluded post-maintenance testing (PMT) for generator vibration balancing acdvities. At approximately 23:00 hours, abo's one half hour into a loaded test run, the engine speed was heard cycling unusually, load oscil.ations were observed on control room indicators, and a flame was observed emanating from the exhaust stack. The local crankcase high pressure alarm annunciated. The engine was secured and an ALERT was declared in accordance with plant procedures for a fire that could affect the operability of a Class IE system.
The ALERT was terminated at 03:05 hours on 10/10/97 when the remainder of Unit 2's Class 1 E power supply subsystems were determined operable and unaffected by the D21 EDG failure.
This special report addresses only the D21 EDG issues. Notification of the Emergency 7
Declaration was addressed sey,arately in accordance with 10CFR50.72(a)(1)(i) and Limerick's i Emergency Plan.
pg 9711140087 971110 PDR ADOCK 05000353
L l'
. November 10.1997 Pcge 2 of 4 Internal inspection of the engine revealed a failure in the #4 cylinder that involved damage to the lower piston, connecting rod, connecting rod to crankshan bearing, crankpin, and cylinder liner.
Hardware failure analysis was performed by PECO Nuclear personnel, with technical assis%nce from the EDG vendor, it was determined that the physical cause of the D21 catt. strophic failure was the failure of the #4 cylinder lower piston connecting rod joint with the crankshan. Refer to the attached figure for clarification as necessary. The joint failure began when the pre-stress on the opposite control side connecting rod bolt was relieved, allowing the connecting rod nut to back off. This occurred at some point following the last five year overhaul (completed September 1994). The nut then backed ofTsufficiently to allow thejoint to begin to open. As the joint was pulled ann, the joint bearing began to degrade, impacting the lubrication of the bearing and piston. The bearing was eventually extruded from the joint, the unlubricated piston lodged in the cylinder wall, the connecting rod joint was pulled apart, and the connecting rod was bent by the crankshaft.
Through formal root cause analys.s, it was concluded that the most likely cause of the joint failure was a combination of EDG intemal forces and reversal of the lower connecting rod bearing halves during the last five-year overhaul completed in September 1994. These bearings have been installed with the halves reversed on three prior occasions in PECO Nuclear diesels, but have not led to failure. The most probable scenario is that the reversed bearing, made of aluminum, eventually yielded, allowing the joint to loosen over time Reverst ' ' earing installation would be caused by a combination ofless than adequate: human penormance, procedural guidance, and immediate supervision.
Three other possible causes, which are considered less likely but could not be eliminated, are:
failure to properly torque the connecting nut and bolt assembly, foreign material between the mating surfaces of the joint, and bearing dimensions out of specification.
Corrective measures takan involved immediate stions in response to the failure and generic implications, repair of the EDG, and longer term actions to address the causal factors, immediate actions included the following. Upon indications of a significant problem, the D21 EDG was secured. All of the remaining Unit 2 Class 1E subsystems and buses were inspected. The other tlree Unit 2 EDGs were tested (satisfactorily) within the next 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Following the initial internal inspection of D21 and preliminag analysis, the other 7 EDGs (both units) were visually inspected to verify the presence of the lower connecting rod castle nut cotter pins. No missing cc,tter pins were identified.
Repair of the EDG was accomplished via a complete five-year overhaul, and included the following. The damaged #4 cylinder assembly was removed and replaced in its entirety. The #4 lower crankpin journal, damaged by the impact forces of the broken connecting rod during the event, was machined and non-destructively examined. The lower crankshaft was further inspected by performing various runout checks to assure that it was not distorted. Lower crankshaft main bearings near the failure (4 through 6) were inspected along with other normally
. November 10,1997 Pcge 3 of 4 heavily loaded main bearings (7,10, and 13). Main bearings 4 and 5 were replaced. All connecting rod bearings were inspected on both upper and lower crankshafts and all bolting retorqued and repit.ned. All upper and lower crankshaft main bearing bolts were retorqued and repinned. Adjoining upper piston insert assemblies were pulled (#4,5,6, and 7) to assure no damage occurred from the injection ofjacket water inte the #4 cylinder. All upper piston floating bushingr were verifica foi proper clearance. The lube oil system was completely drained and all debris (associated with the failure) was removed. The vertical drive and turbochargers were disassembled and inspected. The exhaust system was inspected. A complete set of post-maintenance and performance tests were performed. No abaormalities were obse ved.
Longer term actions to address the causal factors for this event include the following.
. A series ofinspections are planned on each EDG, which include inspecting all lower crankshaft connecting rod bearings for orientation, presence of castle nut cotter pins, and sample torque checks. These inspections are 50% complete with no deficiencies identified.
s An assessment of the EDG overhaul procedures regarding human factors.
. An assessrnent of the work environment during an EDG overhaul, related to the possible impact on human performance.
. Inspection of a sample of new connecting rod bearings to determine the consistency ofdimensions.
The D21 EDG was inoperable from 23:50 on 10/09/97 until 04:23 on 10/31/97, for a total of 21 days,4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, and 33 minutes.
This event constitutes a valid test failure, and represents the 4* valid test failure in the last 20 valid tests for D21. The current surveillance test interval for D21 is once per eve;y 7 days, in accordance with Limerick's Technical Specifications. Limerick is not committed to the surveillance interval specified by Regulatory Position C.2.d. in Regulatory Guide 1.108 Revision
- 1. This event is the 5* valid test failure in the last 100 attempts for the unit.
If you have any questions, please do not hesitate to contact Mr. Timothy A. Moore at (610) 718-3400.
' truly yours, I
c> f .
TST cc- H. Miller, Administ.ator Region I, USNRC A. Burritt, USNRC Senior Resident Inspector, LGS l
. November 10,1997 Page 4 of 4
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