ML20155J614

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SALP Rept 50-331/86-01 for Sept 1984 - Feb 1986.Overall Performance Continued to Improve.Weaknesses Identified in Pump Operability & Control of Instruments
ML20155J614
Person / Time
Site: Duane Arnold NextEra Energy icon.png
Issue date: 05/21/1986
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20155J607 List:
References
50-331-86-01, 50-331-86-1, NUDOCS 8605270123
Download: ML20155J614 (42)


See also: IR 05000331/1986001

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SALP 5

SALP BOARD REPORT )

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U. S. NUCLEAR REGULATORY COMMISSION

REGION III

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SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

50-331/86001

Inspection Report

Iowa Electric Light and Power

Name of Licensee

Duane Arnold Energy Center

Name of Facility

September 1, 1984 through February 28, 1986

Assessment Period

8605270123 860521

PDR ADOCK 05000331

0 PDR

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I. INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated NRC staff effort to collect available observations and data on

a periodic basis and to evaluate licensee performance based upon this

information. SALP is supplemental to normal regulatory processes used to

ensure compliance to NRC rules and regulations. SALP is intended to be

sufficiently diagnostic to provide a rational basis for allocating NRC

resources and to provide meaningful guidance to the licensee's management

to promote quality and safety of plant construction and operation.

A NRC SALP Board, composed of staff members listed below, met on April 18,

1986, to review the collection of performance observations and data to

assess the licensee's performance in eccordance with the guidance in NRC

Manual Chapter 0516, " Systematic Assessment of Licensee Performance." A

summary of the guidance and evaluation criteria is provided in Section II

of this report.

SALp Board, for Duane Arnold Energy Center:

Name Title

J. A. Hind Director, Division of Radiological

Safety and Safeguards

C. J. Paperiello Director, Division of Reactor Safety

E. G. Greenman Deputy Director, Division of Reactor

Projects

D. R. Muller Project Director, NRR

W. G. Guldemond Chief, Reactor Projects Branch 2

L. R. Greger Chief, Facilities Radiation Protection

Section

M. Schumacher Chief, Radiological Effluents and

Chemistry Section

M. A. Ring Chief, Test Programs Section

D. C. Boyd Chief, Reactor Projects Section 2D

R. B. Landsman Project Manager, Reactor Projects

Section 20

M. Thadani Duane Arnold Project Manager, NRR

J. S. Wiebe Senior Resident Inspector

N. V. Gilles Resident Inspector

P. R. Rescheske Inspector

S. M. Hare Inspector

P. L. Eng Inspector

J. P. Patterson Inspector

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II. CRITERIA

Licensee performance is assessed in selected functional areas, depending

upon whether the facility is in a construction, preoperational, or

operating phase. Functional areas normally represent areas significant to

nuclear safety and the environment. Some functional areas may not be

assessed because cf little or no licensee activities, or lack of meaningful

observations. e pecial areas may 'be added to highlight sionificant

observations.

One or more of the 0 Mowing evaluation criteria were used to assess each

functional area.

1. Management inv'olvement and control in assuring quality

2. Approach to the resolution of technical issues from a safety

standpoint

3. Responsiveness to NRC initiatives

4. Enforcement history

5. Operational and Construction events (including response to, analyses

of, and corrective actions for)

6. Staffing (including management)

However, the SALP Board is not limited to these criteria and others may

have been used where a,3propriate.

Based upon the SALP Board assessment each functional area evaluated is

classified into one of three performance categories. The definitions of

these performance categories are:

Category 1: Reduced NRC attention may be appropriate. Licensee management

attention and invo'lvement are aggressive and oriented toward nuclear safety;

licensee resources are ample and effectively used so that a high level of

performance with respect to operational safety and ccnstruction quality is '

being achieved.

Category 2: NRC attention should be maintained at normal levels. L.icensee r

management attention and involvement are evident and are concerned with

nuclear safety; licensee resources are adequate and are reasonably

effective so that satisfactory. performance with respect to operational

safety and construction quality is being achieved.

Category 3: Both NRC and licensee attention should be increased. Licensee

management attention and involvement is acceptable and considers nuclear

safety, but weaknes;es are evident; licensee resources' appear to be strained

or not effectively used so that minimally satisfactory performance with

respect to operational safety or construction quality is being achieved.

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III. SUMMARY OF RESULTS

Based on SALP 3, 4, and 5 ratings, the overall regulatory performance of the

Duane Arnold Energy Center has continued to improve. Improved performance '

in the areas of Emergency Preparedness and Security is noted during the

SALP 5 assessment period. The rating in the area of Surveillance and

Inservice Testing improved from a Category 3 to a Categcry 2 tnis period.

Actual improvement is marginal when one considers the weaknesses identified

in pump operability and control of instruments. Performance in the area of

Maintenance / Modifications is given a Category 2 rating this period. This

is an apparent decrease from the Category 1 rating given during the last

period. The apparent decrease is a result of more in depth inspection in

this area during the SALP period and is not considered an actual decrease

in performance.

April 1, 1983- September 1, 1984-

Functional Area August 31, 1984 February 28, 1986

A. Plant Operations 1 1

B. Radiological Controls 2 2

C. Maintenance / Modifications 1 2

D. Surveillance and

Inservice Testing 3 2

E. Fire Protection 1 1

F. Emergency Preparedness 2 1

G. Security 3 2

H. Outages 2

I. Quality Programs and

Administrative Controls

Affecting Quality 2

J. Licensing Activities 1 1

K. Training and Qualification-

Effectiveness *

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  • f.ot Rated (new functional areas for SALP 5)
    • Not Ratr: (no basis for evaluation)

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IV. PERFORMANCE ANALYSIS <

A. Plant Operations

1. Analysis-

Portions of nine routine inspections were performed by the

resident inspectors covering plant operations. The inspections

included observation's of control room operations, reviews of

logs, discussions with licensed,and unlicensed operators,

verification of operability of' emergency.:ystems, and reviews

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of reactor building and turbinetbuilding equipment status.

Three violations were identified as follows:

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a. Severity Level IV - Failure to have two Average Power

Range Monitor (APRM) downscale trip functions (331/85021).

b. Severity Level IV - Two examples of personnel errors

(331/85021).

(1) Failure to identify Inoperable High Pressure Coolant

Injection deluge system.

(2) Failure-to establish baseline Average Power Range

Monitor and Local Power Range Monitor neutron flux

noise levels.

c. Severity Level IV - Violation of secondary containment

integrity (331/84012).

The first'two violations resulted from personnel errors during

recovery from the 1985 refueling outage. Although these errors

were identified by the licensee, the violations were issued as a

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result of' reoccurrence of personnel errors. The licensee took

extensive corrective action to reduce the administrative work

load and distractions of the Snift Supervisor so that he was~ free

to supervise plant operations. The action included designating

. an off-duty Shift Supervisor to screen all personnel and paper-

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work going to .the control room to ensure that personnel had a

need to go to-the control room and that'all administrative

requirements were met prior to requesting Shift Supervisor's

The corrective action was very

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approval to commence work. -

successful and ro further personnel errors c:ccurred during the

recove ry.' In additiori, no significant personne1' errors occurred

in thid : area during the rest of the assessment period.

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The th,ird violation occurred prior to the assessment period but

wa.s not addressed in the last SALP report. The licensee's

corrective' action was prompt and effective. This instance is

< considered an isolated case and is not representative of licensee

, performance during this assessment period.

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The small number of violations is a result of an aggressive effort

by plant management to ensure operations are conducted only after

proper planning and establishment of priorities. This was evident

during the period by the prior planning of control rod sequence

changes, a power reduction to evaluate and repair a reactor feed

pump, and the removing from and placing in service of the

Condensate Demineralizer and Reactor Water Cleanup Demineralizers.

Corporate management is frequently involved in site activities

and visits the site regularly. During recovery from the 1985

refueling outage, several personnel errors prompted management

to take timely and effective action to correct the trend. Action

was effective as evidenced by the sudden reduction in errors.

Only two scrams from power occurred during this assessment period.

These scrams occurred in 1984 as a result of equipment problems.

In addition, the licensee's success in this area is demonstrated

by a plant record of 234 days of continuous operation during the

assessment period. The run was terminated by a scheduled outage

for technical specification required surveillance testing.

The licensee demonstrated a clear understanding of technical

issues. Conservatism is routinely exhibited during application

of technical specification requirements and in determining

operability of equipment as was evidenced by licensee response

to an inadvertent relief valve lift due to an apparent ground and

the licensee response to a design anomaly which would prevent

sequencing of loads onto the Emergency Diesel Generators during

certain conditions. In both cases, the affected equipment was

declared inoperable and the action statement entered until a

thorough review by operators, engineers, management, the

Operations Review Committee, and the Safety Review Committee

showed that action was taken to ensure proper operation of the

affected equipment.

The licensee is responsive to NRC initiatives and timely and

technically sound responses are given in almost all cases.

The operations area staffing is adequate and the positions are

identified with authorities and responsibilities well defined.

Overtime is controlled and not excessive.

Plant Management places importance on the professional conduct of

operating personnel. A dress code has been established and is

usually adhered to. Control Room atmosphere, although improving,

needs further work. At times the noise level becomes slightly

elevated. Although no effect on plant safety or operator

awareness has been noted, this detracts from the overall

professionalism of the Control Room.

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2. Conclusions

The licensee is rated Category 1 in this area which is the same

rating as the last assessment.

3. Board Recommendations

None.

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B. Radiological Controls

1. Analysis

Seven inspections were conducted during this assessment period by

region based inspectors. These inspections included operational

and outage radiation protection, plant chemistry / radiochemistry,

confirmatory measurements, environmental protection, effluent

releases, TMI action plan items, radiological waste management,

and transportation activities. The resident inspectors also

reviewed this area during routine inspections including frisking

techniques, anti-contamination clothing use, radiological barrier

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use, step-off pad use, and radiation surveys. Five violations

were identified as follows:

a. Severity Level IV - Failure to follow the proper procedure

for work it a locked high radiation work area, resulting

in unnecessary radiation exposure (331/85012).

b. Severity Level IV - Failure to adequately evaluate radiation

hazards associated with entering a locked high radiation

area (331/85012).

c. Severity Level V - Failure to identify the waste

classification for a drum of radioactive waste on the

shipping manifest (331/85005).

d. Severity Level V - Failure to follow release procedures when

releasing (to the river) circulating water system contents

which had been slightly contaminated with water from the

condenser hot well (331/85022).

e. Severity Level V - Failure to collect one of the wildlife

samples for the second half of 1983 and one for the first

half of 1984, and one of the triannual soil samples during

the growing season (May-September) in 1984 for the

radiological environmental monitoring program (REMP)

(331/85009).

The licensee was responsive to these violations; corrective

actions were timely and appeared to be effective as recurrence

of the problems have not been evident. The violations appear to

be isolated incidents rather than indications of programmatic

weaknesses.

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Staffing in this functional area has generally improved. The

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staff appears to be experienced and competent. Efforts are

continuing to reduce reliance on contractor personnel. The

Dosimetry Coordinator, formerly a contractor position, was

filled internally during this assessment period. Additionally,

, the licensee has reduced the number of contract radiation

protection engineers and HP technicians during this assessment

period. Contractor heal ~th physics technicians are scheduled to

be replaced by licensee technicians as the licensee technicians

become shift qualified. A new position, Corporate Chemist, was

created and filled by the former Chemistry Coordinator. Several

additional staffing changes including the ALARA Coordinator,

Assistant Radwaste Coordinator, Acting Chemistry Coordinator,

and Assistant Chemistry Coordinator positions, were necessitated

by internal reassignments during this assessment period. These

positions were expeditiously filled with no observed lack of

continuity.

Management involvement in the functional area is evident. There

is consistent evidence that managers and supervisors are involved

in the day-to-day activities of the plant. The radiation protec-

tion group is represented at a weekly plant planning meeting,

where representatives from all plant areas discuss work scheduled

for the next week and the support required from other plant

groups. Representatives from health physics, dosimetry, deconta-

mination, radwaste, ALARA, and chemistry meet daily to discuss

problem areas, activities in progress, and activities scheduled.

These types of meetings are indicative of positive management

involvement in the coordination of plant activities.

Responsiveness to NRC initiatives has been adequate during this

assessment period. The licensee made significant progress in

reducing reliance on contractor personnel in both technical and

supervisory positions, was responsive to a gaseous effluent

monitor alarm setpoint problem, and resolved previous discrepan-

cies in the laboratory intercomparison analyses.

A conservative approach to resolution of radiological control

issues is routinely exhibited. Personnel radiation exposures

during 1984, a nonoutage year, were considerably lower than the

U.S. average for BWRs. Exposures for 1985, however, were

significantly elevated due to the licensee's ten year Inservice

Inspection (ISI) of the drywell and torus, the Induction Heating

Stress Improvement program (IHSI) in the drywell, and the recir-

culation piping weld overlay repair, in addition to the work

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normally performed during routine outages. The ISI/IHSI,

drywell, torus, and weld overlay doses contributed approximately

740 person-rem of the 1500 person-rem dose for 1985. The

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licensee's dose average over the last five years has been

approximately 800 person-rem. The U.S. average for BWRs over

this period was approximately 1000 person-rem. An Exposure Goals

Program was implemented during this assessment period as part of

a continuing effort to reduce radiation exposure to as low as

reasonably achievable (ALARA). This program sets annual exposure

goal limits by work groups and is intended to provide a method to

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measure cost-effective results in exposure reduction and ensure

supervisory awareness of personnel exposure. The licensee has

placed a considerable and continuing effort into reducing the

number of contaminated areas in the turbine building, reactor

building, and the radwaste building during this assessment

period.

The licensee continues their conservative policy of prohibiting

routine liquid radioactive releases. There were two liquid

releases during this assessment period: (1) a small planned

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release of about one liter of water occurred during condenser

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tube leak repair, and (2) a release of about a million gallons

of water occurred after the circulating water system inadver-

tently received about 8,000 gallons of slightly contaminated

water from the condenser hotwell during the refueling outage.

Concentrations of liquid as well as gaseous effluents have

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remained well below applicable release limits during this

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assessment period A minor problem with the procedure for

calculating the alarm setpoint for normal range gaseous effluent

monitors was identified. In response, a timely change was made

to the procedure.

The volume of solid radioactive waste shipments, normally elevated

because of the restriction on liquid radioactive releases, was

further increased this assessment period by the extensive plant

cleanup program and efforts to ship as much radwaste as possible

prior to possible burial site restrictions after January 1,1986.

The licensee has implemented methods of reducing solid radwaste,

including compacting, hand sorting, and segregation. The

licensee appears to have adequately implemented the 10 CFR Part 61

and 10 CFR Part 20.311 requirements for radwaste classification

and form. Radwaste procedures were appropriately mcdified to

include these requirements and suitable correlation factors.

Licensee chemistry and radiochemistry programs were satisfactorily

implemented with no apparent problems in meeting regulatory

requirements. Laboratory equipment was of generally good quality

and adequate to perform required analyses. Quality controls were

in place for major analytical equipment with results indicating

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stable operation. Supervisory personnel were well acquainted with

the instruments and aware of operating problems and limitations.

Technicians observed were proficient and knowledgeable in the

analyses performed. The licensee has a generally satisfactory

program for testing technician competence using vendor supplied

blind samples and results have generally agreed with vendor

values. Two small problems noted in this program were the

generous ( 30%) deviations accepted by the licensee for metals

analyzed by atomic absorption spectroscopy and a systematic bias

(about 10%) in radioactive sample comparisons with the vendor.

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Laboratory space is quite crowded but the laboratory appeared to

be efficiently run. Climate control remained poor with unreliable

air conditioning, minimal air movement, and temperatures higher

-than optimal for analytical instruments and personnel. The

licensee is aware of the ventilation problems, having identified

them in a 1982 internal audit, but the design change package for

corrective action was given a low priority.

In confirmatory measurements the licensee achieved generally

satisfactory results, with 36 out of 39 comparisons in agreement

with the NRC. During the previous assessment period a continuing

problem was noted with Sr-89 and Sr-90 analyses comparison.

During this assessment period licensee performance improved in

this analysis.

Other than the failure to perform certain technical specification

required sampling and analyses (see violation above), implementa-

tion of REMP was generally satisfactory during this assessment

period. As a result of a licensee audit of the REMP, management

control over the program was improved to minimize errors and

omissions. The improvement included assigning specific responsi-

bility for the program and developing a method to keep management

informed of the program status.

2. Conclusions

The licensee is rated Category 2 in this crea. Licensee

performance was determined to be improving.

3. Board Recommendations

None.

C. Maintenance / Modifications

1. Analysis

Portions of nine routine inspections were perfonned by the

resident inspectors covering this area. In addition, one

inspection was performed by a resident inspector from another

plant and two regional based inspections were performed in this

area. The inspections included reviews of normal maintenance

and modification activities to ensure that approvals were

obtained prior to initiating work, activities were accomplished

using approved procedures, post maintenance testing was completed

prior to returning components or systems to service, and parts

and materials were properly certified. In addition, work planning

and scheduling was reviewed as well as the effectiveness of

administrative controls to ensure proper priority is assigned.

Five violations were identified as follows:

a. Severity Level V - Failure to follow Main Steam Line

Isolation Valve (MSIV) repair procedure (331/85010).

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b. Severity Level IV - Failure to perform post maintenance

testing on secondary containment interlocks -(331/85029).

c. Severity Level IV - Equipment drain sump pump timers

installed incorrectly (331/85029).

d. Severity Level IV - Inadequate engineering review of field

change request (331/85029).

e. Severity Level IV - Failure to conduct maintenance trending

(331/85032).

Item a. was a minor instance where the maintenance procedure

required certain data to be taken on Main Steam Line Isolation

Valve (MSIV) stems. This type of data was previously used to

evaluate MSIV performance improvement actions. In this instance,

the MSIV stems were being replaced with improved stems, and

therefore, the data was not taken. The licensee took action

to ensure that the workers are aware that procedures should be

changed in such cases.

Item b. was a result of not specifying a post maintenance test

after repairs to a secondary containment interlock. The

licensee has made major changes to the method used to specify

post maintenance testing.

Item c. was a result of a modification made in 1974 and is not

considered representative of present performance in this area.

Item d. was a result of a reviewing engineer's failure to recognize

the effect of changing the orientation of a flow detector. The

licensee changed the administrative requirements to ensure that

whenever possible the engineer that approves such changes is the

same engineer who initially approved the design.

Item e. was previously identified by the licensee and corrective

actions have been in progress since 1983 to complete a historic

computerized trending system.

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There were no major violations. There were several minor

violations which may indicate minor programmatic breakdown in

this area. The licensee has taken action to perform a major

revision to the administrative controls for maintenance

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activities which should correct this minor breakdown.

No significant events occurred relevant to this functional area.

Events are promptly reported, and in most cases completely

reported and analyzed. A large number of equipment failures

occurred which may be indicative of the adequacy of the corrective

and preventative maintenance program. Several reportable events

were the result of the High Pressure Coolant Injection or Reactor

Core Isolation Cooling systems being inoperable. Some of these,

however, were the result of the licensee intentionally removing

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the system from service for corrective maintenance in order to

improve the system's reliability. The licensee has also formed

a task force to review and recommend corrective action covering

these systems' reliability. The licensee has greatly reduced the

number of Reactor Water Cleanup Isolations which were caused by

false signals.

There has been increasing evidence of prior planning and

assignment of priorities. Corporate management is usually

involved and decision making is usually at a level that ensures

adequate review. As evidenced by spare parts problems with the

drywell Hydrogen-0xygen analyzers (caused unusual event and start

of required shutdown) and the Electric Fire Pump (caused pump to

twice exceed seven day out-of-service limit), increased

management attention appears to be warranted.

Technical issues are generally understood and conservatism is

generally exhibited. The licensee is responsive to NRC

initiatives with acceptable resolutions proposed initially in

most cases. This is evidenced by licensee response to problems

concerning control of maintenance activities, NRC concerns about

High Pressure Coolant Injection and Reactor Core Isolation

Cooling reliability, and trending of corrective maintenance.

During the special inspection of the licensee's reliability

program for HPCI and RCIC, it appeared that the licensee (1) was

not using trend information that was available in their deviation

report listings, (2) had excessively used cause codes " unknown"

and "other," (3) had a weak corrective maintenance policy

regarding root cause determinations, and (4) had an apparent

need for more QC or peer type inspections on maintenance work

involving technical specification required equipment.

In regards to these concerns, the licensee did provide generally

timely resolutions to quality related technical issues; however,

corrective action to preclude recurrence was weak. Corrective

action was usually taken but was not always effective at

correcting the root cause of the problems in the HPCI and RCIC

systems as indicated by their occasional repetition. On some

occasions, proposed corrective action was delayed or found to be

not effective in producing the desired reliability improvement in

HPCI and RCIC. This observation was limited to the apparent

conditions and work related to HPCI and RCIC systems and may not

apply to other areas. The licensee has responded very well to

'hese areas of concern and have a reliability improvement program

underway for HPCI and RCIC.

A high percentage of Main Steam Isolation Valves (MSIVs) have

repeatedly failed local leak rate tests. The licensee has

replaced the stems and disks of these valves in an attempt to

improve their reliability. Although the MSIVs were leak tested

immediately following this replacement, they have not been tested

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after placing the plant in service following the 1985 refueling

outage. The next required test is during the 1987 refueling

outage and the NRC has requested the licensee to consider leak

testing at least one of these valves on a noncontrolling basis

during an outage prior to the 1987 refueling outage. During the

only outage since the replacement stems and disks were installed,

the licensee considered and rejected the testing of these valves.

The rejection was based on (1) the licensee's confidence that the

replacement stems and disks will increase valve reliability, and

(2) the leak testing could not be performed on a noncontrolling

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basis.

Key positions are filled on a priority basis with experienced

personnel. This is evic'enced by the prompt filling of the

Maintenance Engineering Supervisor position with a former

Operations Shift Supervisor (Senior Reactor Operator Licensee).

The Maintenance Superintendent is in Senior Reactor Operator

training, and the acting Maintenance Superintendent has taken

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an aggressive role in improving prior planning of maintenance

activities and overall maintenance performance. Permanent plant

staffing is marginally adequate. Maintenance has approximately

a three month backlog of work and high reliance is placed on

contractor help to keep the backlog manageable. The licensee

is reducing dependence on contractor help by hiring more

maintenance personnel.

Equipment problems were the cause of a high number of LERs which

could be reduced by improvement in preventive and corrective

maintenance practices; however, the long continuous run

(234 days) supports the conclusion that material conditions

are not significantly affecting plant operation. The licensee

has repeatedly demonstrated this commitment to maintaining the

plant by delaying recovery from outages until all necessary

maintenance is complete.

2. Conclusions

The licensee is rated Category 2 in this area, which is a change

from the last SALP rating. In hindsight, and after more indepth

inspection the Board concluded that the prior Cr.tegory 1 rating

may have been too high. However, improvement has been noted

during this period, especially in the area of prior planning.

3. Board Recommendations

None.

D. Surveillance and Inservice Testing

, 1. Analysis

During the assessment period, the resident inspectors routinely

inspected this area. These inspections included observations of

technical specification required surveillance testing to verify

adequate procedures were used, that instruments were calibrated,

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and that test results conformed with technical specification

and procedure requirements. In addition, several regional

inspections were conducted in this area. These inspections

included startup core performance, Containment Integrated Leak

Rate Tests, and inservice testing. Eight violations were

identified as follows:

a. Severity Level V - Maintenance and test equipment not

adequately controlled by surveillance procedures

(331/85001).

b. Severity Level V - Failure to document equipment use

history evaluation (331/85001).

c. Severity Level IV - Failure to perform as found

Containment Integrated Leak Rate Test (331/85017).

d. Severity Level IV - Failure to determine safety-related pump

operability via vibration measurements as delineated in the

ASME Code (331/85024).

e. Severity Level V - Failure to properly implement

surveillance procedures (331/85025).

f. Severity Level IV - Use of defective flow meter to obtain

surveillance data (331/85026).

g. Severity Level IV - Inadequate surveillance on drywell

equipment drain sump timers (331/85029).

h. Severity Level IV - Use of an unidentified instrument to

determine equipment operability (331/85026).

Items a., b., f., and h. are examples of insufficient control of

instruments used for equipment operability determinations. In

response to this issue, the licensee established a program to

identify inoperable or degraded instruments using tags and to

specify required instruments in appropriate procedures; however,

it is noted that communications among Operations, Plant

Performance and Instrument and Controls personnel must be

improved to assure use of proper instruments for surveillance

and inservice testing. The licensee is encouraged to pursue

this concern aggressively.

Item c. resulted from the licensee's failure to follow their

technical specifications in the area of Containment Testing,

specifically the requirement for an as found Type A test. While

the licensee has the largest allowable containment leakage in

Region III, they also have had consistent difficulty with

excessively leaking containment isolation valves, the primary

source of containment leakage. Any lack of containment integrity

due to excessively leaking isolation valves or personnel error

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may not have been realized because of their incorrect practice of

performing maintenance and repairing leaky containment isolation

valves prior to the performance of Type A tests. The licensee

is presently pursuing an exemption from these requirements that

will allow them to perform containment leak tests at the end

instead of the beginning of outages. The exemption will require

that they keep detailed records of containment leakage path

repairs to facilitate the calculation of an as found Type A

test result.

Item d. identifies the licensee's failure to determine

safety-related pump operability in accordance with the methods

delineated in the ASME Code for vibration monitoring. The

licensee subsequently verified the operability of all safety-

related pumps and has agreed to revise the appropriate procedures

to ensure future compliance with Code requirements; however, due

to past plant practices, valid vibration histories for six out of

18 safety-related pumps, including all the ECCS pumps, do not

exist.

Item e., as well as several open and unresolved items identified

in the areas of Integrated Leak Rate Testing, inservice testing

and portions of the startup test programs, are evidence of the

licensee's failure to follow procedures and properly record test

data. Inconsistencies regarding procedural requirements and

plant practices as well as the licensee's interpretation of the

term " operable" as it relates to inservice testing requirements

were also noted. Although inspections of the licensee's surveil-

lance programs were not conducted by Region based inspectors

during the last SALP period, the number and scope of the problems

identified indicate that identified deficiencies have existed for

an extended period of time.

Item g. is a result of a surveillance test not adequately testing

the technical specification required alarm function of the

drywell equipment drain sump timers. This resulted in this

alarm function being inoperable since a modification was made

to the timers in 1974. The licensee has initiated action to

review all surveillances to ensure adequate testing is performed.

There are multiple violations which do not indicate a major

programmatic weakness. Corrective actions are timely and in most

cases effective. However, in the case of Item d., the licensee's

actions were inadequate and resulted in Violation f.

ihere is evidence of prior planning and assignment of priorities;

however, as evidenced by two missed surveillances, additional

attention is warranted. Improvement has been noted as not as

many surveillances were missed in this assessment period compared

with last assessmen'. period. Decision making is usually at a

level that ensures adequate management review; however, inservice

testing problems sometimes do not receive timely management

i

15

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s

review and therefore, questionable equipment may not be declared

inoperable. Repeated difficulties resulting from test instrument

inadequacy have been noted. This problem has not caused any

technical specification action statements to be exceeded. The

licensee has taken action to correct this problem.

Attention to detail is sometimes lacking in record keeping,

procedure compliance, and testing techniques. This is evidenced

by violations for failure to follow procedures, and failure to

take proper vibration measurements. Corrective action is usually

taken but is not effective in all cases in correcting the root

cause as evidenced by occasional repetition of problems.

Understanding of issues is generally apparent, and conservatism

is generally exhibited. The licensee's surveillance program is

conservative with respect to technical specification requirements.

Conservatism is demonstrated by: (1) except for the physics area

several systems / instruments are surveilled at a frequency greater

than required by technical specifications; (2) all core cooling

pumps (RCIC, HPCI, RHR, Core Spray) and many valve monthly

surveillances also include the performance of the quarterly

surveillance requirements of the technical specifications; and

(3) the licensee routinely implements and enforces surveillance

requirements prior to the technical specification amendment

issuance which requires the surveillance. '

There were two reportable events related to this functional area

during SALP 5. One of. these was caused by personnel error (1.5's

of all LERs). The other event was caused by an inadequate

surveillance procedure. During SALP 4 there were five events

related to this functional area that were caused by personnel

error (7.4?; of all LERs). The above data indicates improvement

has been made in this area.

Staffing is adequate; however, responsibility for ASME Code

compliance, including program implementation and decision making

regarding inservice testing matters, is delegated to a contractor-

employee. The licensee has recently hired an individual to

assume these duties, but increased management attention is

warranted to ensure improvement in this area while this employee

gains experience in this position.

2. Conclusions

The licensee is rated Category 2 in this area. While this is an

improvement from the Category 3 given in the last period, the

actual improvement is marginal when one considers the concerns

identified in pump operability and control of instruments.

3. Board Recommendations

None.

16

i

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E. Fire Protection

1. Analysis

During this assessment period, the resident inspectors performed

routine inspections in this area, including evaluation of

potential fire hazards, plant housekeeping and cleanliness, and

compliance with the plant fire protection plan. The inspections

showed that housekeeping and cleanliness is very good in readily

accessible areas of the plant, but improvement in equipment rooms

is desirable. One special inspection was conducted by Region III

personnel to assess the licensce's compliance with 10 CFR 50,

Appendix R, close out previously identified open items and verify

compliance with routine fire protection program requirements.

The inspection showed that implementation of the Appendix R

requirements was the best observed in Region III. One violation

in this area was identified:

Severity Level V - Failure to control aerosol cans of

flamable spray paint in reactor building (331/85003).

The violation occurred at the beginning of an extended refueling

outage. Extensive and effective corrective actions were taken

including administrative procedure changes and tours which

prevented additional problems during the outage with many

additional contractors onsite and extensive maintenance and

construction work in progress.

On two separate occasions the Electric Fire Pump was out of

service for greater than seven days. In both cases this resulted

from maintenance and spare parts problems. The licensee has

taken corrective action in this area and on another occasion

extensive effort was made to ensure the Diesel Fire Pump was

restored to service in the required seven days even though

extensive repair by a vendor was required.

Most of the responsibility for the fire protection program

implementation and Appendix R compliance was assigned to

contractor employees. Although management and station technical

staff were actively involved in the decision making process

regarding these matters, the licensee acknowledged the need for

greater involvement by members of their staffs and voluntarily

implemented positive corrective actions prior to the inspection

by Region III.

The licensee resolved technical issues with appropriate

justification and documentation and was enthusiastically

cooperative with regard to concerns raised by the NRC.

Response time was appropriate and communications were positive.

17

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.

Licensee personnel that were observed appeared to be

knowledgeable of their assigned responsibilities in most areas.

Some concerns were raised regarding training and experience of

some individuals and their overall qualifications to perform

assigned duties. The licensee acknowledged these concerns and

agreed to make additional efforts to provide required training

and experience for identified areas of weaknesses, thereby

developing a higher degree of in-house expertise in this area.

The level of staffing appeared to be adequate.

2. Conclusions

The licensee is rated Category 1 in this area. This is the

same rating as the last assessment.

3. Board Recommendations

None.

F. Emergency Preparedness

1. Analysis

Three inspections were conducted during the period to evaluate

the following aspects of the licensee's emergency preparedness

program: emergency detection and classification; protective

action decision making; notifications and communications;

implementation of changes to the emergency preparedness program;

shift staffing and augmentation; emergency preparedness training;

public information program; and independent audits of the

emergency preparedness program. One inspection involved the

observance of the annual exercise.

No_ violations were identified in the two routine inspections

conducted in January 1985 and January 1986.

Three weaknesses in the October 29, 1985, exercises were

identified as follows: (1) an unsatisfactory demonstration of

the Post Accident Sa.npling System (PASS) in both preparation

and timeliness; (2) one of the two offsite Radiological

Monitoring Teams (RMT) lost communications with the Emergency

Operations Facility (EOF) and the other RMT for approximately

one and a half hours; and (3) one of the two offsite RMTs failed

to follow the Emergency Plan Implementing Procedures (EPIPs) in

the collection, packaging and identification of soil, water, and

vegetation samples. The licensee's overall performance in the

October 1985 exercise was still rated above average. The

Control Room, the EOF, and the Emergency News Center performed

very well. The Technical Support Center (TSC) demonstrated an

above average performance with only minor problems. Subsequent

to this exercise an unannounced PASS drill demonstrating sample

acquisition and analysis was conducted successfully and

monitored by the Senior Resident Inspector. Therefore, the

response to this exercise weakness is considered satisfactory.

18

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.

In the previous SALP report, concern was raised by the NRC

regarding dose calculation and assessment capabilities. Licensee

performance in the October 1985 annual exercise and in " hands-on"

walkthroughs in the January 1986 inspection clearly indicated an

improvement and satisfactory competency in using the MIDAS

computer system for obtaining dose assessment values for

potential radiation release values based on in-plant radiation

levels. In addition, all licensee representatives observed by

NRC on both these inspections properly used a flow chart with

various plant conditions listed to " trigger" Protective Action

Recommendations (PARS) in conjunction with the dose assessment

values. The NRC's concern from the previous SALP period

regarding dose calculation and assessment capabilities for

potential release situations has been resolved by the licensee.

In June 1985, the licensee completed training, including simulator

training, for all Operations Shift Supervisors (OSSs) and other

key Control Room personnel, on the six new Symptomatic Emergency

Operating Procedures (EOPs). These Symptomatic E0Ps have been

revised to incorporate accident classification references to

assist the OSS as initial Emergency Coordinator to better

mitigate and classify accidents and cross-reference the E0Ps with

the EPIPs. These new E0Ps, integrated with the EPIPs, should be

helpful to OSS's from a cause and effect standpoint in

classifying an accident correctly and without undue delay.

The licensee has improved in their response to activations of

the Emergency Plan. A total of 20 emergency occurrences

(activations of the Emergency Plan) were evaluated by Region III

in two inspections during the SALP rating period. In each case

the appropriate EAL was chosen, and notifications were made to

State and local governmental agencies within the required time.

This improvement is partially due to a revised notification form

and also to continued training emphasis on emergency detection,

classification, and notification. Management has demonstrated

responsiveness to NRC emergency preparedness issues whether a

violation, major issue or minor issue is involved.

I The licensee has hired two staff assistants to assist the

Corporate Emergency Planner. One will be assigned to the plant

on a full time basis, while the other will be located at the

corporate office. A full time person at the site should improve

the interaction and cooperation for emergency preparedness from

the operating divisions and the health physics group.

Presently the licensee has been maintaining nine key staff

positions with 13 additional emergency support personnel

available for duty within 30 minutes. Shift augmentation was l

successfully demonstrated in the October 1985 exercise. The l

licensee improved its method to assure that individuals assigned

to Emergency Response Organization (ER0) positions were trained

annually.

19

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Lesson plans have been improved to include suggestions from

drill and exercise critiques. Two instructors are currently

assigned as full time EP instructors in the Training Center,

which was not the case earlier in the SALP period.

In summary, the licensee is continuing their effort to improve

the emergency preparedness program. Corporate and plant manage-

ment have demonstrated their involvement in this area and have

projected a positive attitude and response to our concerns.

Continued vigilance is needed in initiating action to correct and

improve the emergency plan implementing procedures. Also effort

should continue in improving the quality of the drills and the

annual exercise as a vital part of emergency preparedness

training.

2. Conclusions

The licensee is rated Category 1 in this area which is an

improvement over the previous SALP rating.

3. Board Recommendations

None.

G. Security

1. Analysis

Five security inspections were conducted by region based

physical security inspectors during the assessment period.

Three of these inspections were special and two were routine.

Additionally, the Resident Inspector routinely conducted

observations of security activities. Two violations were

identified relative to the security program as follows:

a. Severity Level IV - Some security officers had not

fulfilled training in some tasks required by the Training

and Qualification Plan. Additionally, supervisory

personnel failed to document the completion of training

for certain tasks (331/84015).

b. Licensee identified item - The licensee failed to conduct

maintenance in a timely manner (331/85031).

Allegations from a former licensee security guard were received

by Region III that dealt with security at the Duane Arnold

facility. The inspectors determined that the licensee took

adequate and immediate followup action after receiving the

information. Although the allegations could not be fully

substantiated, there was an apparent lack of communications,

and loss of some documents.

20

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.

With respect to the licensee identified item the following

actions were taken: (1) a security preventative maintenance

program was implemented; (2)-a security equipment hi: tory file

was established; and (3) corrective maintenance was conipleted

in a timely manner.

Information received from the monthly reports indicated that the

corrective maintenance turnaround has improved. The licensee

sent a security force representative to another facility to

gather additional information which may help them to further

improve their maintenance program. Additionally, the licensee

has two maintenance technicians dedicated to security

maintenance.

The corrective action for violations is timely and effective in

most cases.

'

One identified weakness pertained to onsite organizations'

participation-in security contingency drills. The licensee was

receptive to the NRC's recommendation for improvement in this

area.

Two weaknesses were identified with the licensee's security force

training program. One weakness pertained to the nonuniformity

in the training received by guards. The second weakness pertained

to the significant reduction in the number of licensee-conducted

security related drills.

In 1984 and 1985, both the NRC and the licensee had identified

the need for a dedicated security training individual. The

licensee temporarily filled the position on January 6, 1986.

On March 12, 1986, the same individual accepted the official

position.

Although weaknesses had been identified with the training

program, it is a defined program and contributes to an adequate

understanding of work responsibilities. One unresolved item

was identified regarding the licensee's capability to maintain

the required minimum response force while in compensatory

measures. This issue has been forwarded to NRC Headquarters

for resolution.

The construction activities onsite have impacted on the security

program. The licensee has taken the additional steps necessary

to maintain an adequate level of plant security during this

phase.

There were no technical issues involving physical security from

a safety standpoint which required resolution during this

assessment period.

Events reported under 10 CFR 73.71 were properly analyzed and

reported in a timely manner.

21

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Positions within the security organizations are identified and

responsibilities are defined. There is good communication

between 'the security supervisor and the security force.

The records are generally complete, well-maintained and

available.

Good communications exist between site security, plant upper

management, and Region III.

Plant management's support for the security program has increased

and was made evident by the purchasing of new CCTV cameras; .

computer software modifications; handguns and walkthrough

explosive detectors.

In summary, the plant management's support for the program has

increased. This has been shown in the upgrading of some security

equipment and positive actions taken to improve the security

maintenance program.

2. Conclusions

The licensee is rated Category 2 in this area which is an

improvement from the previous SALP 3 rating achieved in the last

SALP assessment period. That rating was primarily based on the

enforcement history during the rating period which totaled two

Severity Level III violations and three Severity Level IV

violations. A positive trend has been identified during this

assessment period in that management support for security has

increased, and the licensee continues to increase its efforts in

upgrading security.

3. Board Recommendations

None.

H. Outages

1. Analysis

The resident inspectors performed routine inspections during

outages and four regional based inspections were performed

concerning outage related work. These inspections included

observation of maintenance activities including administrative

requirements, review of planning activities, refueling activities,

major plant modifications including the ARTS (Average Power

Range Monitor, Rod Block Monitor, and the associated Technical

Specification Improvements) Modification, weld overlays of

recirculation piping welds, and post outage testing. Five

violations were identified as follows:

a. Severity Level IV - Numerous examples of failure to have

or follow written procedures during the ARTS Modification

(331/85035).

s

22

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b. Severity Level V - Failure to maintain tool and material

logs during weld overlays (331/85011).

c. Severity Level IV - Failure to conduct Type B testing on

drywell penetration CV-4305 (331/85028).

d. Severity Level IV - Failure to control activities affecting

quality (removal of plug from CV-4305) (331/85028).

e. Severity Level IV - Failure to have an appropriate procedure

and failure to follow a hydrostatic test procedure valve

lineup for the Residual Heat Removal System (331/85028).

With respect to item a., the safety-related portion of the

modification (APRM's) constituted a very small portion of the

modification, and no problems were found in this area. The

main problems were identified in the Rod Block Monitor modifica-

tions which, while not safety-related, are considered important

to safety by virtue of minimizing conditions where plant safety

could be jeopardized. These problems were due to the following

weaknesses: (1) a high level of quality was not maintained

during the activities; (2) resolutions generally addressed

symptoms rather than root causes and a clear understanding of

significance and implications of technical issues was lacking;

(3) responses to inspector-identified concerns were generally

not timely or thorough, and frequently lacked technical depth;

and (4) the personnel responsible for or involved in the

modification activities frequently lacked the knowledge to

adequately respond to questions posed by the inspectors. It

should be noted that these observations are based on a narrow,

non safety-related area, and are not indicative of the entire

outage area.

Item b. appears to be an isolated case which was promptly

corrected by the licensee. Item c. resulted from not having

appropriate procedures for designation of post maintenance

testing. The licensee has extensively revised the administrative

requirements for designation of post maintenance testing to

ensure that knowledgeable individuals in the appropriate

departments specify appropriate post maintenance testing.

Items d. and e. resulted from inattention to detail by workers

and insufficient supervision to ensure attention to detail.

Contractors were primarily involved with this work. The licensee

is reducing dependence on contractors by increasing the number

of utility maintenance workers. Although contractors cannot

be completely eliminated from the workforce during outages,

additional utility maintenance workers will allow closer

supervision of the contractors. The licensee plans to utilize

more utility workers in the future, j

l

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No major violations were identified. Item d. did result in an

uncontrolled unauthorized breach of containment integrity;

however, the plant was not in a mode that required containment

integrity. Several examples of failure to follow procedures is

not indicative of a programmatic problem but is evidence of

inattention to detail and insufficient supervision. Corrective

action for the potential programmatic problem concerning post

maintenance testing was extensive and effective.

'

Increased evidence of prior planning and setting priorities has

been noted. The 1985 refueling outage was one of the best

planned outages in plant history. The outage included refueling,

10 year Inservice Inspection Activities, inspection and

refurbishing of several Control Rod Drive Mechanisms, rebuilding

of Main Steam Isolation Valves with new stems and disks, and

Induction Heating Stress Improvement of recirculation piping

welds. When cracks were identified in recirculation piping

welds, the additional work was integrated into the schedule. The

schedule was continually updated as work and concitions changed.

The effectiveness of the maintenance is evidenced by the long run

after the outage. The outage group was established prior to the

start of the SALP period, but during the SALP period has gained

new prominence as the authority concerning the outage schedule.

The outage group obtains input from the work group concerning

various activities and integrates them into the schedule. Since

the input comes from the work group, the work group is expected

to meet the schedule except for unforeseen circtmstances. As

work groups have gained experience in forecastir.g activity

resource requirements, the schedules have becoue better.

Refueling activities were conducted in an excellent manner. The

core was completely off loaded and reloaded without difficulty.

Communication between the control room and the refueling floor

was excellent. Continuous communications ensured that the

control room knew where each fuel bundle was at all times.

Decision making is generally at a level that ensures adequate

management review, and corporate management is frequently

involved in site activities. Management is kept informed of

maintenance status by a daily meeting at which all the new

maintenance requests are discussed and priorities evaluated.

Management is therefore able to obtain consistent information

and revise priorities as necessary. A weekly planning meeting

also provides a forum for discussion of complex activities

involving several departments to assign responsibilities and

track open items. This meeting also allows management to follow

priority maintenance. Corporate management is kept informed by

frequent plant visits and discussions with plant management.

l

24

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In some cases records are not complete and not well-maintained

as evidenced by problems noted with the ARTS modification

documentation and the unauthorized and undocumented removal of

a plug from containment isolation valve CV-4305. Minor procedure

violations occasionally occur but have not resulted in safety

significant events. Corrective action concerning programmatic

problems is prompt and effective, but minor procedure violations

continue.

The licensee generally demonstrates a clear understanding of

technical issues, and conservatism is normally exhibited. This

is demonstrated by the licensees approach to the recirculation

piping cracks and the problems associated with the CV-4305 valve

and penetration. The licensee is generally responsive to NRC

initiatives as evidenced by the extensive, prompt, and effective

corrective action taken to improve the Maintenance Action Request

(MAR) procedure.

Occasional events, attributable to causes under the licensee's

control, have occurred that are relevant to this functional area.

Examples of such events are: (1) A vent plug was removed and not

reinstalled in CV-4305: (2) Plugs were not reinstalled on Residual

Heat Removal relief valves following removal of gags after a

hydrostatic test; and (3) Failure to perform a Type B test on the

CV-4305 penetration. The first two events resulted in a failure

of a Type A Containment Integrated Leak Rate Test (CILRT). The

plugs were removed during the outage, and therefore, drywell

integrity was not required while the plugs were removed. A

Type B test was subsequently performed successfully on CV-4305

penetration, thereby showing that this item had no effect on

drywell integrity. As a result of these events, the licensee

has improved the maintenance procedures writer's guide to provide

guidance on procedure specificity and quality checks, has revised

tne hydrostatic test procedure, and has revised the MAR procedure

to provide more extensive review for designation of post

maintenance testing. The correttive action appears to be

extensive and appropriate.

Staffing is adequate with contractor support required during

outages and to support modification work. Key positions are

identified and responsibilities are defined. The licensee is

reviewing methods to minimize contractor dependency and to

integrate contractor and utility work force activities.

2. Conclusions

The licensee is rated Category 2 in this area. This is a new

area that was not included in the last SALP.

3. Board Recommendations

None.

25

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I. Quality Programs and Administrative Control Affecting Quality

1. Analysis

During the assessment period, the resident inspectors routinely

inspected this area, which included administrative controls for

maintenance and operations as well as deviation reports and

quality control department involvement in accordance with the

Quality Assurance Plan. In addition, this functional area was

examined as part of an inspection of QA programs in procurement,

offsite support staff, and receipt, storage and handling. Two

violations were identified as follows:

a. Severity Level V - Violation of secondary containment

integrity occurred as a result of inadequate post

maintenance testing of secondary containment door

interlocks (331/85029).

b. Severity Level V - Failure to identify a condition adverse

to quality (inadequate post maintenance testing)

(331/85029).

The violations resulted from the licensee's QA Program not

assuring proper quality for non safety-related equipment which

may affect the performance of safety-related equipment or

structures. In regards to Violation a., the maintenance error,

without adequate post maintenance testing, allowed a violation

of secondary containment. The condition adverse to quality was

not identified since the licensee's QA Program did not require

post maintenance testing for this equipment. The licensee

initiated broad corrective action by establishing a review

group to identify equipment in this category. The QA Program

is being changed to apply the appropriate quality controls. The

ARTS modification, discussed in Section H. (Outage), is also

indicative of an occasion where appropriate quality assurance

was not applied to a non safety-related system which affects

safety-related equipment.

Administrative control procedures which implement management

control, verification and oversight activities continue to be

improved. Administrative procedures which control maintenance

activities have been significantly improved while problems in the

areas of Surveillance and Inservice Testing. indicate that further

attention is necessary in these areas.

The Operations Committee and Safety Review Committee review of

plant activities is detailed and effective. Additional attention

is necessary to define and implement the training program referred

to by the Operations Committee charter. Control of the design

change process is generally good with major TMI modifications

26

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.

being implemented without problems; however, problems have been

identified with documentation and review of minor modifications.

The licensee has developed a minor modifications procedure to

improve control in this area. Corrective action systems are

excellent in identifying and documenting problems, but weaknesses

in determining root causes of problems have been noted.

Requirements for records are adequate; however, many examples

have been noted where insufficient attention to detail has

resulted in an incomplete or inaccurate records.

Decision making is usually at a level that ensures adequate

. management review and corporate management is usually involved

in site activities.

2. Conclusions

The licensee is rated Category 2 in this area.

3. Board Recommendations

None.

J. Licensing Activities

1. Analysis

a. Methodology

The basis for this appraisal was the licensee's performance

in support of significant licensing actions that were either

completed or had a substantial level of activity during the

current rating period. Some of these actions, consisting of

amendment requests, exemption requests, responses to generic

letters, and TMI items, are listed below as either multiplant

actions or plant specific actions.

(1) Multiplant Actions - included in this category were:

-Inspection of BWR Stainless Steel Piping (Complete)

-Environmental Qualification of Electrical Equipment

(Complete)

-Post Accident Sampling Modifications (Complete)

-Appendix I Technical Specification Implementation

Review (Complete)

-Detailed Control Room Design Review (Complete)

-Mark I Containment Long Term Program Implementation

(Complete)

-Masonry Wall Design

-Procedures Generation Package Review

-Salem ATWS Related items

-Technical Support Center-0737 Supplement 1

-Operations Support Center-0737 Suppiment 1

+

27

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.

-Emergency Operations Facility-0737 Supplement 1

-Hydrogen Recombiner Capability

-Safety Parameters Display System (Complete)

-Safety Concerns Associated with Pipe Breaks in the

BWR Scram System

(2) Plant Specific Actions - included in this category were:

-Update NDT Operating Limits (Complete)

-Thermal Hydraulic Stability and Single Loop Operation

(Complete)

-Reactor Power Uprate (Complete)

-Amendment to Security Plan (Complete)

-Lead Test Asserrbly Review (Complete)

-ARTS Improvement Modifications (Complete)

-Stainless Steel Piping Repair and Plant Restart

(Complete)

-Technical Specification Changes Related to NUREG-0737

Modifications

-ASME Code Relief Applications

-Extension of Alternate Safe Shutdwon Capability

Deadline

-Exemption from the requirements of 10 CFR 50.48

Appendix R,Section III J

b. Management Involvement and Control in Assuring Quality

During the present rating period, the licensee's management

demonstrated active participation in licensing activities

and kept abreast of all current and anticipated licensing

actions, making effective use of its plan for integrated

schedules of actions, and its licensing commitments tracking

system. Licensee management actively participated in an

effort to work closely with the NRC staff to establish

realistic and integrated schedules for all modifications of

the DAEC facility. In addition, the management's involvement

in licensing activities assured timely response to the

requirements of the Commission's rules related to Fire

Protection and Environmental Qualification of Electrical

Equipment. The implementation schedules for compliance with

the rules were fully met by the licensee. During its

refueling outage early in 1985, the licensee's management

took an aggressive part in assuring (1) thorough inspection

of the plants stainless steel piping, (2) completion of

repairs of all detected cracks in the stainless steel piping,

(3) completion of fire protection related modifications,

(4) completion of modifications related to environmental

qualification of electrical equipment, and (5) modification

related to TMI action items. All the modifications fully

met and some exceeded the Commission's requirements. An

example of exceeding the requirements was noted by the

Region III fire protection inspection team, which found

that the modifications of the plant and the procedures

exceeded the Commission's requirements, and the fire

28

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protection measures at the DAEC were the best of all the

plants seen by Region III inspection team. The licensee's

management consistently exercised good control over its

internal activities and its contractors to assure quality,

and maintained effective communication with the NRC staff.

The management's active participation was evident in its

firm involvement in the issues of significant potential

safety impacts. This was illustrated throughout this

rating period in the management's initiatives to seek

early staff guidance on the scope of the safety reviews ,

l required for future actions involving complex licensing )

'

issues.

c. Approach to Resolution of Technical Issues from a Safety

Standpoint

The licensee's management and its staff have demonstrated

sound technical understanding of issues involving licensing

actions. Its approach to resolution of technical issues

has demonstrated extensive technical expertise in all

technical areas involving licensing actions. The decisions

related to licensing issues have routinely exhibited l

conservatism in relation to significant safety matters as l

illustrated by the approach taken by the licensee to exceed '

the Commission's requirements related to rules for fire

protection and environmental qualification of electrical

equipment.

On occasions, when the licensee deviated from the staff

guidance, the licensee has consistently provided good

technical justification for such deviations. The Fire l

Protection Program and the program for Environmental

Qualification of equipment are good examples illustrating

the soundness of the technical justifications for deviations

from the guidance. When unusual events have occurred at the

Duane Arnold Energy Center, the licensee has invariably used

conservative approaches in dealing with the situations, and

performed in-depth analyses of safety issues raised by such

events. The licensee has consistently monitored itself to

assure that the safety systems function as designed and the

plant's technical specifications are well-maintained. An

example of a response to unusual events and self-monitoring

was the thoroughness with which the licensee identified and

dealt with the concerns raised by its own training staff

related to a potential problem of diesel generator load

sequencer bypass. As a result of the licensee's efforts

and communications to the staff, an information notice was

sent to other licensees for a potential diesel generator

sequencer problem. As stated above, the licensee made

frequent visits to NRC to discuss the forthcoming requests

for staff actions prior to formal submittals. This approach

has been consistently found to improve both the staff's and

licensee's efficiency in processing such actions.

29

_ _ _ - _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _

, .

.

d. Responsiveness to NRC Initiatives

The licensee has been consistently responsive to NRC

initiatives. During the rating period, it has made every

effort to meet or exceed the established commitments as

illustrated by its responses to TMI action items, Appendix J

requirements and compliance with the rules related to Fire

Protection and Environmental Qualification of safety-related

electrical equipment. Perhaps the most significant

demonstration of the licensee's responsiveness to NRC

initiatives is its leadership of the industry in developing

and adopting an integrated schedule plan for all safety-

related modifications, and renewal of its license amendment

to continue to follow the integrated schedule plan. Since

establishing the integrated schedule plan over two and a

half years ago, the licensee has faithfully followed the

elements of the plan enhancing the ease with which it can

respond to NRC initiatives.

e. Enforcement History

This area is addressed in the other functional areas of

this report.

f. Reporting and Analyses of Reportable Events

The Duane Arnold Energy Center operated at power during the

first five months of the period and the last 7 1/3 months of

the period. The plant was in a scheduled refueling outage

during the 5 2/3 month period between February 3,1985 and

July 18, 1985. l

In the first five month operating phase, the unit operated I

with a reactor service factor * of 78% and reported 25

events ** to the NRC Operations Center per in CFR 50.72.

Three events involved reactor scrams, two of which involved

transients from operating power levels. The third occurred

inadvertently from less than 1% power while shutting down.

" Reactor Service Factor = (Hours of Critical Reactor

Operation /Possible Hours) x100%

    • The number of events reported to the operations center

may not be the same as the number of License Event Reports

because of different reporting criteria and in some cases

an event initially reported to the operations center may

be reassessed as not reportable.

30

- -- _ _ - . _ . . - . - _ _

- - _ _ _ _ _ _ . - _ _ _ ,

. .

.

Twelve reported events involved inadvertent actuations of

Engineered Safety Features (ESF) equipment and are considered

to have low safety significance. Nine reported events

involved temporary inoperability of safety-related equipment

requiring entry into a Technical Specification Action

Statement. In all cases, the equipment was made operable

within time limits, and plant shutdown was not required.

Two events reported during this period were discussed at the

Operating Reactor Events Briefings. They were the' Auxiliary

Transformer Fire on November 4, 1984, and Failure of the

Start-up Transformer on November 22, 1984. Two events

, reported during the period involved fires onsite.

During the 5 2/3 month refueling outage, 23 events were

reported to the NRC Operations Center. Almost all of these

events involved inadvertent actuations of ESF equipment

during testing and maintenance operations. One event

reported during this period was discussed at the Operating

Reactor Events Briefings. This event involved Failure of

Leak Rate Tests on four of eight MSIVs on February 6,1985.

In the past 71/3 months, the plant has operated relatively

trouble-free with a reactor service factor of 100's.

Accordingly, there have been no reports of reactor scrams.

Twenty events have been reported to the NRC Operations

Center during this period. Seventeen of these events

involved temporary inoperability of safety-related equipment

requiring entry into Technical Specification Action

Statements. In all cases, the equipment was made operable

within time limits and plant shutdown was not required.

Three events involved inadvertent actuation of ESF

equipment and were considered to be of low safety

significance. One event reported during the period was

discussed at the Onerating Reactor Events Briefings. This

event involved discovery of a Des'.gn Deficiency with the

Emergency Diesel Generator (EDG) Load Sequencer.

Licensee events at the Ouane Arnold Energy Center appear to

have been reported promptly, accurately, and conservatively

in the case of entry into Technical Specification Action

Statements, Performance during the past seven months has

been very good with a frequency of event reports of less

than three per month and no reactor scrams.

g. Staffing

The licensee maintains a large licensing staff. The

licensing staff is rotated through tours of duty at the

plant to gain first hand experience of plant operations.

The licensee's management key staff are identified with well

defined authority and responsibility. The plant shift staff

exceeds the Commission's requirements by having extra

operators on shift during refueling in addition to those

specified in the Commission's rule.

31

. .

'

.

h. Training and Qualification Effectiveness -

There is no basis for evaluating this attribute during the

reporting period.

i. Housekeeping

The DAEC site and the facility continues to be maintained

at a high level of cleanliness. The plant is maintained

with clear markings, well organized storage of supplies,

and color coded signs which constantly caution workers

about safety significance of various areas of the facility.

The workers have been observed to behave in a disciplined

manner in conformance with goed housekeeping practice. The

plant engineering and operating staff have been found to

conduct themselves in a highly professional manner, and no

adverse behavior of plant operators and other personnel was

observed during this reporting period.

2. Conclusion

An overall performance rating of Category I has been assigned

in the licensing area.

Not withstanding, we plan to give no less attention by NRC to the

DAEC licensing submittals. We further believe that no less

management effort on the part of the licensee should be exerted

in licensing activities.

3. Board Recommendations

None.

K. Training and Qual _ification _ Ef fectiveness

1. Analysis

Resident and regional inspectors have evaluated training and

qualification effectiveness during inspection of specific program

areas. No violations were identified in this area.

During inspection of operations activities; non-licensed

operators, control room operators, senior control room operators

(shift supervisors), and shift technical advisors were generally

knowledgeable and effective in carrying out their duties.

Examples of cases where knowledge and training appeared to be

deficient were: (1) Failure to have the required number of APRM

32

_ _ _ _ _ _

_- _ _ _ _ _ _ _ _ , _ _ . _ _ _ _ . _ _ _ _ . . . _ _ _ .

_.___ __ _.. -_ _

. .

'

-

. .

downscale trip functions;.and (2) Failure to obtain baseline APRM

and LPRM flux levels. These examples appeared to be isolated

cases and not programmatic., ,During the assessment period, ,

examinations were administered to 12 senior reactor operat'or and

five reactor operator applicants. The overall pass rate for

these candidates was 70%. This passing rate is lower than'the

national average. During the last. assessment period, the pass

rate was above the, national average. With the small number 'of

examinations, the significance of the pass rate cannot be

determined. The operating history during the assessment period

does not reflect any adverse effect.

During inspection of maintenance and outage activities,

instrument and control technicians, electrical maintenance

personnel, and mechanical maintenance pe'r'sonsfl wer'e generally

knowledgeable of their responsibilities. On several occasions

contractor personnel demonstrated inddequate' knowledge of the

importance of equipment and administrative controls. Examples of

-lack of contractor knowlddge discussed in'other sections of this

report were: (1) Unauthorized removal of a plug from drywell

isolation value CV-4305; and (2) Improper, implementation of the

return to normal valve lineup fe'. lowing residual Heat Removal

hydrostatic test. The problem with_ contractor knowledge may be

indicative of a programmatic pcobicm since contractor personnel

do not usually receive the plant oxperience or the plant specific

training that is normally given to' utility personnel.

'

During inspection of the radiological chemistry areas, regional

inspectors evaluated trsining and qQalification effectiveness.

Licensee training and qualification programs generally improved

during this assessment period. A step training program for new

HP technicians wai implemented. The training program consists of.

practical and academic tasks and represents the licensee's plan

for HP technician staffing for future needs. Despite some early

schedule slippage, the licensee plant to have their training

program INPO accredited by September 1986. Chemical Technician '

training is also being improved by implementa, tion of an eight- -

step program designed to be completed over a'four-year period.

The program, under the direction of the licensee's' Joint

Apprenticeship Training Committee, leads to a journeyman status

and appears quite adequate. Four of,the eight chemistry

technicians completed the program by'the summer of 1985.

Development of the program is directed toward eventual INP0

accreditation. Currently, training and qualification effective- ~

ness are characterized by an adequate understanding of work and

adequate adherence to procedures. '

.

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. .

.

During routine inspections, the knowledge of the technical staff

and managers appeared adequate. The licensee sends as many of

the technical staff to Senior Reactor Operator training as

possible. This takes knowledgeable individuals away from the

organization for long periods of time, but in the long run this

practice will improve performance overall. The licensee also

places design engineers in the quality assurance organization

for periods of time. This reinforces the importance of quality

assurance within the design engineering organization and will

lead to an overall improvement in this area. The Maintenance

Engineering Supervisor was a Senior Reactor Operator and the

Maintenance Superintendent is presently in Senior Reactor

Operator training. This further demonstrates the licensees

commitment to training.

The licensee is making good progress towards INPO accreditation

of training programs. Accreditation of the Shift Technical

Advisor, Senior Reactor Operator, Reactor Operator, Second

Assistant Nuclear Station Operating Engineer, and Nuclear Station

Auxiliaries Engineer training programs are expected in the near

future (May 1986) and the remaining training programs are expected

to be accredited by September 1986.

2. Conclusions

The licensee is rated Category 2 in this functional area.

3. Board Recommendations

None.

34

. .

.

V. SUPPORTING DATA AND SUMMARIES

A. Licensee Activities

The unit engaged in routine power operation throughout most of

SALP 5. A major schedu ed outage for plant refueling, modification,

maintenance, induction heating stress improvement treatment, and weld

overlays of recirculation piping began on February 3, 1985 and was

completed on July 18, 1985. After this outage the plant operated

for 234 consecutive days.

The remaining outages throughout the neriod are summarized below:

September 29 - October 25, 1984 Routine Maintenance

November 4 - November 11, 1984 Auxiliary Transformer

Failure

November 23 - November 26, 1984 Fire Suppression Deluge

System Tripped Startup

'

Transformer

The plant scrammed nine times (seven occurred while shutdown). In

1984, two at power scrams were caused by a short circuit in the

auxiliary transformer and a spurious fire protection deluge system

activation on the startup transformer. Six of the remaining scrams

were caused by spurious signals on the LPRM, IRM, or APRM channels.

One scram was caused by a failure to bypass the high Scram Discharge

Volume Level signal while resetting the RPS logic after another scram.

B. Inspection Activities

A special team inspection was conducted by Region III on November 24,

1984 to assess the licensee's actions in regard to the auxiliary

transformer failure. The inspectors found the licensee's staff to

function effectively in dealing with this emergency.

Additionally, a special in depth assessment of engineering,

maintenance, and surveillance testing activites associated with the

High Pressure Coolant Injection and the Reactor Core Isolation Cooling

systems was performed. The inspectors identified some concerns in

this area and the licensee initiated a reliability improvement program

'for these two systems.

Violation data for the Duane Arnold Energy Center is presented in

Table 1, which includes Inspection Reports No. 84012 through 86005.

35

. .

.

TABLE 1

ENFORCEMENT ACTIVITY

FUNCTIONAL NO. OF VIOLATIONS IN EACH SEVERITY LEVEL

AREA V IV III II I

A. Plant Operations 3

B. Radiological Controls 3 2

C. Maintenance / Modifications 1 4

D. Surveillance and

Inservice Testing 3 5

E. Fire Protection 1

F. Emergency Preparedness

G. Security 1

H. Outages 1 4

I. Quality Programs and

Administrative Controls

Affecting Quality 2

J. Licensing Activities

K. Training and Qualification

Effectiveness

TOTALS 11 19 0 0 0

C .~ Investigations and Allegations Review

1. A worker alleged that work hours were reduced as a result of

workers questioning why the chemical decontamination of the

recirculation system piping was cancelled. The chemical

decontamination was sc.heduled to reduce radiation levels to

workers. Inspection showed that the reduction in work hours

appeared to be unrelated to the concerns raised about the

decontamination cancellation. The inspection also showed that

the decontamination was cancelled as a result of possible

pitting and sensitization of piping. No violations were

identified.

2. A private citizen alleged certain individuals had never been

qualified as welders, but had " bought" their union cards.

Licensee records did not show that these individuals had ever

been to DAEC. No violations were identified.

3. While the unit has shutdown, an employee alleged that the

southeast corner room was flooded with three to four inches of

water and referred to the incident as an operations department

" screw-up." Inspection substantiated that the flooding had

occurred and further established that the cause was procedural

inadequacy and poor communications which led to personnel errors

in the system iineup. The licensee addressed this incident along

with several other personnel errors and initiated corrective

actions to prevent occurrence. No violations were identified.

36

. .

.

4. An anonymous allegation stated that the auxiliary transformer

had a history of problems and management had a " cavalier" attitude

towards the problems and made no attempt to investigate or

correct them. Inspection showed that the allegations were not

substantiated. No violations were identified.

5. A security guard alleged 12 security and one radiation protection

problems. Inspection showed the ellegation to be unsubstantiated.

The individual also filed a complaint of discriminatory employ-

ment practices with the Department of Labor. The complaint was

determined unproved. No violations were identified.

6. A contractor employee alleged harassment and employment

discrimination and identified four specific " defects."

Inspection showed the allegation concerning the four " defects"

to be unsubstantiated. Concerning harassment and employment

discrimination, the employee was informed how to file the

complaint with the Department of Labor. The complaint was

never filed. No violations were identified.

D. Escalated Enforcement Actions

There were no escalated enforcement actions during the assessment

period.

E. Licensee Conferences Held During Appraisal Period

1. November 27, 1984 (Glen Ellyn, Illinois)

Meeting to review Systematic Assessment of Licensee Performance

(SALP 4).

2. October 16, 1985 (Glen Ellyn, Illinois)

Meeting requested by the licensee to address concerns expressed

in recent NRC inspection reports.

F. Confirmation of Action Letters (CALs)

There were no CALs issued during this SALP assessment.

G. Review of Licensee Event Reports, Construction Deficiency Reports,

and 10 CFR 21 Reports Submitted by the Licensee

1. Licensee Event Reports (LERs)

LERs issued during the 18 month SALP 5 period are presented

balow:

37

_

r-

, .

.

_LERs No.

84-31 through 84-45

85-01 through 85-47

86-01 through 86-04

Proximate Cause Code * Number During SALP 5

Personnel Error (A) 1 (9)

Design Deficiency (B) 11 (13)

External Cause (C) 1 (1)

Defective Procedure (D) 4 (8)

Management / Quality Assurance

Deficiency (E) 5 (5)

Others (X) 24 (30)

No Cause Code Marked"* 20 ( 0)

Total 66 (66)

  • Proximate cause is the cause assigned by the licensee according

to NUREG-1022, " Licensee Event Report System."

    • NUREG-1022 only requires a cause code for component failures.

The numbers in parenthesis are the LERs in each category when all

the LER's are assigned cause codes.

In the SALP 4 period, the licensee issued 67 LERs in 17 months

for an issue rate of 3.94 per month. In the SALP 5 period the

licensee issued 66 LERs in 18 months for an issue rate of

3.67 per month. For most of the SALP 5 period, the technical

specifications prohibited any loss of secondary containment

thus requiring an LER to be issued regardless of the duration

of the loss. In January 1986, the NRC approved a revision to

the technical specifications to make them consistent with most

other technical specifications, and allow loss of secondary

containment for short periods of time without violation of

technical specifications. An LER, therefore, is no longer

-required if secondary containment is restored within the required

time period. If the LER's which would not be issued under the

revised technical specifications were deleted, the SALP 4 period

would have included 65 LER's for an issue rate of 3.82 per month,

and the SALP 5 period would have included 56 LER's for an issue

rate of 3.1 per month. The reduction in overall LERs and the

reduction in personnel errors is indicative of an improving

trend.

The office for Analysis and Evaluation of Operational Data (AE0D)

reviewed the LERs for this period and concluded that, in general

the LERs are of above average quality based on the requirements

contained in 10 CFR 50.73; however, they identified some minor

deficiencies. A copy of the AEOD report has been provided to the

licensee so that the specific deficiencies noted can be corrected

in future reports.

38

<

, . - .

. .

.

2. Construction Deficiency Reports

No construction deficiency reports were submitted during the

assessment period.

3. 10 CFR 21 Reports

No 10 CFR 21 reports were submitted during the assessment period.

H. Licensing Activities

1. NRR/ Site Visits / Meetings

a. Site Visits

March 20, 1985 - Detailed Control Room Design Review

(DCRDR) In Progress Audit

September 17, 1985 - Visual Inspection of the Impact of

Cooling Tower Drift on Vegetation

January 28, 1986 - Site Visit and Progress Meeting

i

b. Meetings

October 30, 1984 - SALP Board Meeting at Region III

November 27, 1984 - SALP Meeting with the Licensee at

-Region III

January 24, 1985 - Technical Specification Change Request

January 30, 1985 - Technical Specification Change Request

February 22, 1985 - TMI Modifications Related Technical

Specification Changes

March 7, 1985 - Technical Specification Changes for Lead

Test Assemblies (LTA's), Power Uprate, ARTS, and Reload

April 12, 1985 - DCRDR Program Change

April 22, 1985 - Stainless Steel Piping Inspection Results

June 14, 1985 - Emergency Technical Specification Change

Request

July 30, 1985 - Technical Specification Change Errors and

Actions to Prevent Them

October 3, 1985 - Meeting on Pipe Cracks and Technical

Specification Improvements

39

___ _ _ _ _ _ . _ _ __. __ _ _ _ -. _. - .

_ . _

. .

..

,

October 31, 1985 - Hydrogen Recombiner Capability

November 18, 1985 - Appendix I and Hydrogen Control

2. Commission Briefings

None.

3. Schedular Extension Granted

May 30, 1985 - extension of Alternate Shutdown Capability

requirements of 10 CFR 50, Appendix R to March 1987

4. Relief Granted

June 10, 1985 - Relief granted from ASME Coda Section XI

requirements related to torus-drywell vacuum breaker leakage

testing

5. Exemption Granted

July 1,1985 - Exemption from the requirements of 10 CFR 50.48

and 10 CFR 50 Appendix R Section III J

6. License Amendments

Amendment No. 107, dated September 4, 1984, incorporated the

containment high range monitor technical specifications.

Amendment No. 108, dated October 29, 1984, revised the technical

specifications to permit reduction in RHR service water flowrate

requirement.

Amendment No. 109, dated January 14, 1985, incorporated the

Radiological Effluent Technical Specifications (RETS).

Amendment No.110, dated February 1,1985, incorporated technical

specifications for Automatic Depressurization System (ADS) valve

automatic actuation.

Amendment No. 111, dated February 5, 1985 revised the setpoint

for turbine trip and low power load rejection reactor scrams.

Amendment No.112, dated February 26, 1985, revised the Security

Plan, and the guard training and qualifications.

Amendment No. 113, dated March 12, 1985, revised snubber testing

requirements.

Amendment No. 114, dated March 14, 1985, incorporated

administrative changes.

Amendment No. 115, dated March 27, 1985, incorporated technical

specification changes to permit uprating of the reactor rated

power.

40

, . __ _ _ _ _ _ _ __

._

.- . _ . .

. .

.

Amendment No. 116, dated April 11, 1985, incorporated changes to

permit storage of new and spent fuel Lead Test Assemblies in the

fuel pool.

Amendment No. 117, dated April 17, 1985, incorporated changes to

permit Cycle 8 reload.

Amendment No. 118, dated April 18, 1985, incorporated changes to

permit loading of the Lead Test assemblies in the core.

Amendment No. 119, dated May 28, 1985, incorporated changes to

assure thermal hydraulic stability and permit single loop

operation.

Amendment No. 120, dated May 28, 1985 incorporated extended load

limit line, and APRM and RBM technical specification improvements.

Amendment No. 121, dated May 28, 1985, revised the NDT operating

limits.

Amendment No. 122, dated May 28, 1985, incorporated changes to

conform to 10 CFR 50 Appendix J Type C testing.

Amendment No. 124, dated June 20, 1985, revised the effective

date'of Amendment No. 121.

Amendment No. 125, dated July 9, 1985, extended the effective

date of the license condition for integrated schedule.

Amendment No. 126, dated October 10, 1985, incorporated the

operator overtime restriction.

Amendment No. 127, dated December 5, 1985, incorporated

additional leak testing requirements for ADS accumulator check

,

valves.

Amendment No. 128, dated January 4, 1986, incorporated

corrections to RETS.

Amendment No.129, dated January 9,1986, incorporated an action

statement for maintaining pump discharge line filled.

Amendment No. 130, dated February 18, 1986, deleted the

terrestrial monitoring requirement and Appendix B to the

Technical Specifications.

7. Emergency / Exigent Technical Specification Changes

Emergency Amendment No. 124, dated June 20, 1985, revised the

effective date of Amendment No. 121 to permit testing against

pervious NDT operating limits.

8. Orders Issued

None

,

41

- - - -. . _ - _ . - - . _ _ _ - _,, -

. .

.

9. NRR/ License Management Conferences

None

10. Issues Pending

(a) Hydrogen recombiner capability.

(b) Appendix R exemptions.

(c) ATWS rule.

(d) Technical Specification changes for TMI Item III.D.3.4.

42