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POLICY ISSUE (Notation Vote) 1 March 22, 1994 SECY-94-075
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The Commissioners i
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James M. Taylor Executive Director for Operations
SUBJECT:
PROPOSED ENFORCEMENT ACTION AGAINST GEORGIA POWER COMPANY, V0GTLE ELECTRIC GENERATING PLANT (EA 93-304, EA 94-036, EA 94-037, and EA 94-052)
PURPOSE:
To consult with the Commission i
t nee of a Notice of Violation t
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Contacts:
J. Gray, OE HQII: ENFORCEMENT RELATED - LIMITED 504-2747 TO NRC UNLESS THE COMISSION R. Pedersen, OE DETERMINES OTHERWISE 504-2742 j
Information in this record was deleted i
in accordance with (ne fgedom of information a
Act, exemptions
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1 The Commissioners :
BACKGROUIE:
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On March 20, 1990, during a refueling outage at Vogtle Electric Generating Plant (VEGP) Unit 1, GPC declared a Site Area Emergency (SAE) when offsite i
power was lost concurrent with the failure of the only Unit 1 Diesel Generator I
(DG) that was available (IA). The other Unit I DG (18) was unavailable due to l
maintenance activities.
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The NRC imeediately responded to the SAE at the VEGP site with an Augmented Inspection Team (AIT) which was subsequently upgraded to an Incident j
Investigation Team (IIT) on March 23, 1990.
On March 23, 1990, the NRC issued a Confimation of Action Letter (CAL) to GPC that, among other things, confirmed that GPC had agreed not to return VEGP j
Unit I to criticality until the Regional Administrator was satisfied that j
appropriate corrective actions had been taken, and that the plant could safely return to power operations.
t On April 9, 1990, GPC made a presentation to the NRC in the Region II offices in support of GPC's request to return VEGP Unit I to power operations. As part of this presentation, GPC provided information on DG starts in response to a specific NRC request that GPC address DG reliability in it: April 9 j
presentation. GPC submitted a written summary of its April 9 presentation in an April 9,1990 letter, "Vogtle Electric Generating Plant Confirmation of Action Letter." The NRC formally granted permission for VEGP Unit I to return i
to criticality and resume power operations on April 12, 1990.
On April 19, 1990, pursuant to 10 CFR 50.73, GPC submitted Licensee Event Report LER Emergenc(y.") 50-424/90-006, " Loss of Offsite Power Leads to Site Area On June 29, 1990, GPC submitted a revised LER, 50-424/90-006-01. The purpose of the submittal was to clarify infomation related to successful DG starts j
that were discussed in the April 9, 1990 letter and the April 19, 1990 LER, j
and to update the status of corrective actions in the original LER.
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From August 6 through August 17, 1990, the NRC conducted a Special Team j
Inrpection (STI) at VEGP, as a result of NRC concerns about, and allegations related to, VEGP operational activities. This inspection examined the technical validity and safety significance of the allegations, but did not j
investigate alleged wrongdoing. The Special Team infomed GPC that the June 29, 1990 submittal failed to address the April 9,1990 data and requested that GPC clarify DG starts reported on April 9, 1990.
On August 30, 1990, GPC submitted a letter, " Clarification of Response to Confimation of Action Letter." The purpose of the submittal was to clarify the diesel start information that was addressed in the April 9,1990 submittal.
On December 17, 1993, an investigation of licensed activities was completed by the NRC's Office of Investigations (0I). The investigation was initiated in response to allegations received in June 1990 by NRC Region II asserting, in
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I the matter and recommended that the NRC continue its administrative proceeding.
D0J also advised the NRC to contact D0J in the event subsequent NRC investigation identified additional evidence of criminal activity.
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discussed the final results of its investigation with 00J on December 16 j
1993, and D0J verbally declined criminal prosecution of the matter.
es orme a specia orce on Septe er
, composed of representatives from the Office of Enforcement, Region II, the Office of Nuclear Reactor Regulation, and the Office of the General Counsel to conduct a detailed review of the evidence collected by OI on the allegations.
The Vogtle Coordinating Group (Group) was also tasked with identifying any violations and developing a detailed analysis of the evidence in support of its conclusions.
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Currently there is an ongoing Atomic Safety and Licensing Board (ASLB) l proceeding considerin he transfer of operating authority from GPC to j
Southern Nuclear.
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Discussion:
i The 01 investigation concluded that the evidence supports a finding of deliberate failures on the part of GPC officials to provide the NRC with information that is complete and accurate in all material respects.
01 concluded that:
3 (1) the VEGP General Manager (George Bockhold, Jr.) deliberately presented incomplete and inaccurate information regarding the testing of the VEGP Unit 1 DGs during an oral presentation to the NRC on April 9, 1990, i
(2)
GPC submitted inaccurate and incomplete information regarding DG test results in a letter to NRC dated April 9, 1990, as a result of j
deliberate actions by Mr. Bockhold,
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Licensee organizational charts are included in Enclosure 2.
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GPC submitted inaccurate and incomplete information regarding DG air quality in the April 9 letter to the NRC, as a result of deliberate actions by Mr. Bockhold, (4) the Senior Vice President - Nuclear Operations (George W. Hairston, III), with, at a minimum, careless disregard, submitted a false l
statement of diesel test results to the NRC in Licensee Event Report (LER) No.90-006, dated April 19, 1990, as a direct result of deliberate actions by a group of senior managers including Mr. Hairston, the Vice President - Vogtle Project (C. Kenneth McCoy), the Corporate General Manger of Plant Support (William B. Shipman), and Mr. Bockhold, (5)
Mr. Hairston, with, at a minimum, careless disregard, submitted a false statement to NRC in the letter of transmittal of a revision to LER 90-006, dated June 29, 1990, (6)
Mr. McCoy, with, at a minimum, careless disregard, submitted both a false statement and a mirleading statement in the GPC clarification of Confirmation of Action response letter to NRC dated August 30, 1990, and (7)
GPC provided inaccurate information in its response to a 10 CFR 2.206 petition, dated April 1, 1991. 01 could not conclude that these actions were deliberate.
01 also concluded from the combination of the above findings, and the overall review of numerous audio tape recordings of internal GPC conversations regarding their communications with the NRC on a range of issues, that, at least in the March-August 1990 time frame, there was evidence of a closed, deceptive, adversarial attitude toward NRC on the part of GPC senior management.
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Finally, the Group reviewed numerous audio tapes and other evidentiary materials associated with DG testing during the March-August 1990 time frame.
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i fElIE: This paper and its issues should not be publicly disclosed because the matter involves sensitive as well as predecisional enforcement issues.
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ecutive frector for Operations i
Enclosures:
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01 Report 2-90-020R 2.
Licensee Organization Charts l
3.
Vogtle Coordinating Group Analysis i
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Q nd Demand or oma on i
5.
Letters to Individuals Inviting Responses to DFI.
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DISTRIBUTIONL Conunissioners 1
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NOT FOR RELEASE WITHOUT APPROVAL OF THE DIRECTOR, NER LICENSEE MANAGEMENT STRUCTURE (Mid-1990) 4 enesente emme w L
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NOT FOR RELEASE WITHOUT APPROVAL OF THE DIRECTOR, NRR CURRENT POSITIONS OF KEY INDIVIDUALS Southem Nuclear Operating Company 1
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Vice President Execushe i
Technical Services Vice President l
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A40 REY hecCOY "
BECNHAM General nennegw Vice President Vice President Vice Prooklent Nuc Tech Sves Farley Project Vogee Project Hoech Project
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l SHIPREAN "
i General teenager Nuclear Support j
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Persons identified in Of and Staff reports.
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Docket No.
50-424 License No. NPF-68 EA 93-304, EA 94-036, EA 94-037, and EA 94-052 Georgia Power Company ATTN: Mr. H. Allen Franklin President and Chief Executive Officer Post Office Box 1295 Birmingham, Alabama 35201
SUBJECT:
M AND DEMAND 5 FOR INFORMATION (NRC Office of Investigations Report No. 2-90-020 and NRC Inspation Report No. 50-424,425/90-19, Supplement I)
This refers to the investigation conducted by the Nuclear Regulatory Commission's Office of Investigations (01) at Georgia Power Company's (GPC or Licensee) Vogtle Electric Generating Plant (VEGP) which was completed on December 17, 1993. The investigation was initiated as a result of information received in June 1990 by Region II alleging, in part, that material false statements were made to the NRC by senior officials of GPC regarding the I
reliability of the Diesel Generators (DGs). The pertinent events involved in this matter are described below.
j On March 20, 1990, during a refueling outage at VEGP Unit 1, GPC declared a Site Area Emergency (SAE) when offsite power was lost concurrent with the failure of the only Unit 1 DG that was available (IA). The other Unit 1 DG (18) was unavailable due to maintenance activities.
The NRC immediately responded to the SAE at the VEGP site with an Augmented Inspection Team (AIT). The NRC effort was upgraded to an Incident Investigation Team (IIT) on March 23, 1990. The IIT was composed of NRC Headquarters technical staff and industry personnel. The results of this j
investigation are documented in NUREG-1410, " Loss of Vital AC Power and the Residual Heat Removal System During Mid-Loop Operations at Vogtle Unit 1 on March 20, 1990."
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On March 23, 1990, the NRC issued a Confirmation of Action Letter (CAL) to GPC that, among other things, confirmed that GPC had agreed not to return VEGP Unit I to criticality until the Regional Administrator was satisfied that appropriate corrective actions had been taken, and that the plant could safely return to power operations.
On April 9, 1990, GPC made a presentation to the NRC in the Region II offices in support of GPC's request to return VEGP Unit I to power operations. As pe,L of this presentation, GPC provided information on DG starts in response to a specific NRC request that GPC address DG reliability in its April 9
Georgia Power Company presentation. GPC submitted a written summary of its April 9 presentation in an April 9,1990 letter, "Vogtle Electric Generating Plant Confirmation of Action Letter."
On April 12, 1990, the NRC fonnally granted permission for VEGP Unit I to return to criticality and resume power operations.
On April 19, 1990, pursuant to 10 CFR 50.73, GPC submitted Licensee Event Report (LER) 50-424/90-006, " Loss of Offsite Power. Leads to Site Area Emergency."
On June 29, 1990, GPC submitted a revised LER, 50-424/90-006-01. The purpose of the submittal was to clarify information related to successful DG starts that were discussed in the April 9, 1990 letter and the April 19, 1990 LER, and to update the 'statsus.of corrective actions in the original LER.
From August 6 through August 17, 1990, the NRC conducted a Special Team
' spectic, at VEGP, a; a result of NRC concerns about, and allegacions related to, VEGP operational activities. This inspection examined the technical validity and safety significance of the allegations, but did not investigate alleged wrongdoing. The Special Team informed GPC that the June 29, 1990 submittal failed to address the April 9,1990 data and requested that GPC clarify DG starts reported on April 9,1990. Results of this inspection are documented, in part, in fiZ Inspection Report No. 50-424,425/90-19, Supplement 1, dated November 1, 1991.
On August 30, 1990, GPC submitted a letter, " Clarification of Response to Confirmation of Action Letter." The purpose of the submittal was to clarify the diesel start information that was addressed in the April 9, 1990 submittal.
The NRC has carefully reviewed the evidence associated with these events, submittals, and representations to the NRC. Specifically, the NRC reviewed information gathered as part of the 01 Ir.vestigation, information gathered during the llT, NUREG-1410, Supplement 1 of NRC Inspection Report 90-19, discovery responses in the Vogtle operating license amendment procaeding (Docket Nos. 50-424 OLA-3, 50-425 OLA-3), and other related information.
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persona involved in the preparation of the data regarding the DG 4
reliability and tasked the Unit Superintendent with co tin the number of successful DG starts for the 1A and IB DGs.
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l In et, the V GP General Manager stated no criteria or su cessful starts, a term not formally defined, when he directed the Unit j
Superintendent to gather successful DG starts. The Unit Superintendent collected DG start data from the Control Room and the Shift i
Su ervie r's L and orally cony ed totals to the VEGP General a
Mana er for the and I diesels.
Information was t en presente NRC in an Apr
, 1990 ora esentation by the VEGP General Manager and in an April 9,1990 letter that since i
March 20, 1990,. there were 18 and 19 successful consecutive starts on on and letter included three starts with problems that occurred during DG overhaul / maintenance activities (a high lube oil temperature trip on i
March 22, 1990; a low jacket water pressure / turbo lube oil pressure low trip on March 23, 1990; and a failure to trip on a high jacket water temperature alarm occurring on March 24, 1990). The correct number of f
consecutive ccessful starts was 12 for the IB DG--a number j
less than that ed by GPC to the NRC on April 9, In considering a restart decision,
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the NR was especially intereste n the reliability of the DGs and j
specifically asked that GPC address the matter in its presentation on f
i restart. The NRC relied, in part, upon this information presented by j
GPC on April 9, 1990 in the oral presentation and in the GPC letter in j
reaching the NRC decision to allow Vogtle Unit I to return to power operation.
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The air for starting a ud ano operating its instrumenu anu t.vuu via j
derived from the starting air system. The starting air system contains
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1 Georgia Power Company dr h designed to mailtain moisture content (i.e., dew point) at acceptable levels.
I A review of maintenance records and deficiency cards I
associated wt nit I would have revyled$that high dew points were also attributable to system air dryers occasionally being out of service k
'ar extended periods and to system repressurization following sintenance, as documented in NRC Inspecti Re ort 50-42 2
0-plement 1, dated November 1, 1991.
I It'1 cons' ering a restart decision, the NR cially interested in the reliability of the DGs and specifically asked that GPC address the matter in its presentation on restart. The NRC relied, in part, upon this information presented by GPC in its letter of April 9, 1990 in reaching the decision to allow Vogtle Unit I to return to power operation.
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d lek 90-0Qp,submittedtotheNRConfpril 19, 1990, was based, in part, on information presented to the NRC on April 9, 1990. During t'ne preparation of the LER, the Acting VEGP Assistant General Manager -
Plant Support questioned the accuracy of the April 9, 199 etter iven that there were trips on the IB DG after March 2 1
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In later discussions regarding the draft LER, the Genera j
- anager, nical Support Manager and Acting VEGP Assistant General Manager - Plant Support acknowledged that they could not identify the j
specific DG start that represented the starting point for the count A_,.
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Georgia Power Company j Manager, Technical Support Manager and Acting VEGP Assistant General Manager - Plant Support acknowledged that they could not identify the specific DG start that represented the starting point for the count presented to the NRC, i.e., the first start following completion of the CTP. The General Manager - Plant Support (Vogtle Project), the VEGP Technical Support Manager, and the Acting VEGP Assistant General Manager
- Plant Support were aware that the VEGP General Manager had earlier stated that his April 9 count began after instrument recalibration. The Acting VEGP Assistant General Manager - Plant Support stated that his understanding of the CTP was that it would be a test program to determine root causes and restore operability.
ec e he original April 9th data adviseu the Acting VEGP Assistant General Manager - Plant Support aad the VEGP Technical Support Manager that he started his counts on March 20, prior to the time when a CTP could have been completed.
l the lA and IB DG start counts reported on April 19, 1990 overstated the actual counts by including starts that were part of the test m.
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i e very issue that caused an extended shutdown. GPC was clearly aware of the NRC's interest in the DGs, in that the NRC specifically asked GPC to ad restart presentation for April 9, 1990.
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a On April 30, 1990, the Acting vtbr assistent ue..c...
l Manager - Plant Support gave the VEGP General Manager a listing of IB DG 4
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Georgia Power Company 1 After being informed that the April 19 DG start counts were in error, the Senior Vice President - Nuclear Operations informed the Regional f
Administrator that a revision to the April 19 LER would be submitted, in part, to correct the DG start counts. After being provided conflicting j
data for the second time, the Senior Vice President - Nuclear Operations again notified the Regional Administrator. He also requested that an audit be conducted by GPC's Safety Audit and Engineering Review (SAER) i group to establish the correct data and to determine why the errors were j
made. The audit, completed June 29, narrowly focused on a review of I
diesel records (Test Data Sheets, Shift Supervisor's Log, and Diesel Generator Start Log) to verify the number of DG starts. The audit did not identify any specific cause for the error in the number reported in the LER. The audit stated, however, that the errur appeared to result from sncomplete documentation. The audit also noted that there appe,ently was some confusion about the specific point at which the test orocram was comoleted. ~
On June 29, 1990, the draft cover lett67for the LER revision was being reviewed at the site. The draft had originated in GPC corporate headquarters and included language personally developed by the Senior Vice President - Nuclear Operations and the Vice President - Vogtle Project. During the site review, a VEGP Technical Assistant (TA)
(formerly the Acting VEGP Assistant General Manager - Plant Support) noted that the letter was incomplete and challenged the accuracy of the reasons stated in the draft cover letter in conversations with the Supervisor - SAER, the VEGP Assistant General Manager - Plant Support, the VEGP Manager - Engineering Support, and a Licensing Engineer -
Vogtle Project. The VEGP TA stated that: (1) the letter failed to clarify the DG starts reported on April 9 (2) DG record keeping practices were not a cause of the difference in the DG starts reported in the April 19 LER because adequate information was available when the counting errors were made, and (3) the err counts resulted from personnel errors in devel the count.
The Licensing Engineer - Vogtle Project had staff responsibility for preparing the cover letter for the LER revision and was specifically instructed by the Senior Vice President - Nuclear Operations to work closely wi site to ensure that the submittal was accurate and complete.
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The VEGP Manager - Engineering Support was responsible for the Diesel i
Start Logs and agreed with the audit report findings regarding deficiencies in their condition. Given that his logs had not been used to collect the DG start data, he pointed out that it was wrong to state that the condition of his logs caused errors in the information initially provided to the NRC.
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h the Supervisor - SAER was made aware by the VEGP TA on June 12, 1990 that, to identify the root cause of the error in the April 19, 1990 1
LER (i.e., personnel errors), the audit scope would need to include an
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assessment of the performance of the Unit Superintendent and the VEGP General Manager, the individuals that developed the initial count. Yet, the audit report did not include either of these individuals in the list of persons contacted during the audit. On June 29, 1990, the Supervisor
- SAER was again made aware by the VEGP TA that the root cause for the i
The VEGP Assistant General Manager was apprised of concerns regarding l
the June 29, 1990 letter by the VEGP TA (an individual who had been involved in preparing the April 19, 1990 LER and had been involved in developing an accurate DG start count). The VEGP TA identified to him
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the failure of the June 29, 1990 draft cover letter to address the inaccuracies in the ril 9, 1990 letter that it reference 4
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1 Georgia Power Company ce President - Nuclear Operations were actively involved in the preparation of the June 29 cover letter. The VEGP General Manager and Vice President - Vogtle Project reviewed, and the Senior Vice President -
Nuclear Operations signed, the June 29 cover letter which stated that its purpose was, in part, to clarify information provided to the NRC on an, n o ~ -
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letter and presentation and the April 19 LER were caused, in part, by I
confusion in the distinction between a successful start and a valid test.
I During the August
, 1990 ant Review Board (PRB) meeting, the VEGP Manager - Technical Support questioned if the Unit Superintendent (the individual who originally collected the DG start data) was :onfused in the distinction between a successful start and a valid test. The VEGP General Manager admitted that the Unit Superintendent was not confused about the distinction when he collected l
the data which was used to prepare the April 9 letter, but stated that the sentence was not in error because other people were confused. The i
VEGP General Manager acknowledged that there was confusion among individuals after April 9, but admitted that the Unit Superintendent was mnotconfuse n he develo ed the i
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The August 30 etter states that the error in pri etter an presentation and the April 19 LER were l
caused, in part, by an error made by the individual wh rfo j
count of DG starts.
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The Senior Vice President - Nuclear Operations ano the Vice President - Vogtle Project were direct) involved in the i
development of the June 29 letter.
Subsequently, the NRC requested that GPC make a submittal addres he A il 9 letter.
The Vice Presi ent - Vogtle Project committed during the August 17 n.eeting with the NRC special inspection team to provide clarification to the NRC regarding the April 9 letter.
l GPC forwarded a submittal regarding the April 9 ietter on August 30 that was drafted at corporate hea uarters under the mdirectionofthe i
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The responses directed by this letter and the enclosed Notice are not subject to the clearance procedures of the Office of Management and Budget as required j
by the Paperwork Reduction Act of 1980, Pub. L. No.96-511.
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k Sincerely, James L. Hilhoan Deputy Executive Director for Nuclear Rear. tor Regulation, Regional Operations,and Research
Enclosures:
1.
2.
Demand For Information
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Georgia Power Company
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DISTRIBUTION:
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i SECY CA JTaylor, EDO JMilhoan, DEDR JLieberman, 0E SEbneter, RII LChandler, OGC JGoldberg, DGC d
i WRussell, NRR EReis. OGC Enforcement Coordinators RI, RII, RIII, RIV, RV Fingram, GPA/PA EJordan, AE00 BHayes, 0!
EA File j
DCS Vogtle Coordinating Group:
i D. Matthews, Chairman R. Pedersen, OE P. Skinner, RII i
D. Hood, NRR i
D. Wheeler, NRR D. Hoefling, OGC 4
M. Young, DGC i
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NOTICE OF VIOLATION Georgia Power Company Docket No. 50-424 Vogtle Electric Generating Plant License No. NPF-68 j
EA 93-304 l
During an NRC inspection conducted from August 6, 1990 to August 17, 1990 and an NRC investigation completed on December 17, 1993, violations of NRC l
equirements were identified.
In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, endix C, l
the Nuclear Regulatory Commission proposes to impose ursuant to Sect'on 234 of
.. Atomic Energy Act of 1954, as a (Act),
U.S.C.
2282, and 10 CFR 2.205.
The particular violations j
re set forth below:
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10 CFR 50.9(a) requires that information provided to the NRC by a licen ee shall be complete and accurate in all material respects.
a DG has been started 18 times, and the 18 DG has been started 19 times, j
No failures or problems have occurred during any of these starts."
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oil, Start 134 tripped on low pressure jacket water and Start 136 had a high temperature jacket water trip alarm.
As of April 9, 1990, the IB DG had only 12 consecutive successful starts without problems or failures rather than the 19 represented by GPC.
The same inaccuracy was presented to the NRC at its Region 11 Office during an oral presentation by GPC on April 9, 1990.
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in considering a restart decision, the NRC was especially interested in the reliability of the DGs and specifically j
asked that GPC address the matter in its presentation on restart.
The NRC relieu, in part, upon this information presented by GPC on April 9, 2
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1990 in the oral presentation and in the GPC letter in reaching the NRC decision to allow Vogtle Unit I to return to power operation.
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1 Notice an Apri
, 1 90 letter states, when discussing the air quality of the DG starting air system at the Vogtle facility, that: "GPC has reviewed air quality of the D/G air system including dewpoint control and has concluded that air quality is satisfactory. Initial reports of higher i
than expected dewpoints were later attributed to faulty instrumentation."
actual high dew points had occurred at the Vogtle facility, ggEEEb the causes of those high dew points included failure to use air dryers for extended periods of time and repressurization of the DG air start system receivers following maintenance.
In considering a restart decision, the NRC was especially interested in the reliability of the DGs and specifically asked that CPC address the matter in its presentation on
-estart. The NRC relied. in part, upon this information presented by GPC in its letter of April 9,1990 in reaching the decision to allow Vogtle Unit I to return to power operation, a
Licensee Event Report (LER), dated i
19, 1990 states: " umerous sensor calibrations (inc u ing jacket water temperatures), special pneumatic leak testing, and multiple engine starts and runs were performed under various conditions. After the 3-20-90 event, the control systems of both engines have been subjected to a comprehensive test program.
Subsequent to this test program, DGIA and DGlB have been started at least 18 times each and no failures or problems have occurred during any of these starts."
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- er.a ei une states that:
"In accordance with 10 CFR 50.73, Georgia Power Company C) hereby submits the enclosed revised report related to an 4
event which occurred on March 20, 1990. This revision is necessary to i
clarify the information related to the number of successful diesel generator starts as discussed in the GPC letter dated April 9, 1990...."
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I The letter states that:
"If the criteria for the completion of the test program is understood to be the first successful test in accordance with l
Vogtle Electric Generating Plant (VEGP) procedure 14980-1 " Diesel Generator Operability Test," then there were 10 successful starts of Diesel Generator IA and 12 successful starts of Diesel Generator 18 between the completion of the test program and the end of April 19, 1990, the date the LER-424/1990-06 was submitted to the NRC. The number of successful starts included in the orig:nal LER (at least 18) included some of the starts that were part of the test program. The difference is attributed to diesel start record keeping practices and the definition of the end of the test program."
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states that: "The confusion in the April 9th letter and the origina R appear to be the result of two factors. First, there was confusion in the distinction between a successful start and a valid test...
Second, an error was made by the individual who performed the count of DG starts for the NRC April 9th letter."
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Dated at (City, State) this day of (Month) 19(g) t I
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UNITED STATES NUCLEAR REGULATORY COMMISSION In the Matter of
)
)
GEORGIA POWER COMPANY
)
(Vogtle Electric Generating
)
Docket Nos. 50-425/50-425 Plant, Units 1 & 2)
)
License Nos. NPF-68/NPF-81
)
EA 94-036 DEMAND FOR INFORMATION REGARDING THOMAS V. GREENE, GEORGIE R. FREDERICK, HARRY MAJORS, AND MICHAEL W. HORTON l
I Georgia Power Company (Licensee) is the holder of Facility License Nos. NPF-68
[
and NPF-81 (Licenses) issued by the Nuclear Regulatory Commission (NRC or Cvamission) pursuant to 10 CFR Part 50. The Licenses authorize the operation i
of the Vogtle Electric Generating Plant (VEGP) Units 1 and 2, in accordance A
[
with conditions specified therein.
1 II On December 17, 1993, an investigation of licensed activities' was completed by the NRC's Office of Investigations (01) at Licensee's VEGP facility. The investigation was initiated in response to information received in June 1990 3
by NRC Region 11 alleging, in part, that material false statements were made l
to the NRC by senior Licensee officials regarding the reliability of the Diesel Generators (DGs). The pertinent events involved in this matter are described below.
On March 20, 1990, during a refueling outage at VEGP Unit 1, GPC declared a Site Area Emergency (SAE) when offsite power was lost concurrent with the 4
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1
. failure of the only Unit 1 DG that was available (IA). The other Unit 1 DG (IB) was unavailable due to maintenance activities.
The NRC immediately responded to the SAE at the VEGP site with an Augmented Inspection Team (AIT). The NRC effort was upgraded to an Incident Investigation Team (IIT) on March 23, 1990. The IIT was composed of NRC Headquarters technical staff and industry personnel. The results of this investigation are documented in NUREG-1410. " Loss of Vital AC Power and the Residual Heat Removal System During Hid-Loop Operations at Vogtle Unit 1 on March 20, 1990."
On March 23, 1990, the NRC issued a Confirmation of Action Letter (CAL) to GPC that, among other things, confirmed that GPC had agreed not to return VEGP Unit I to criticality until the Regional Administrator was satisfied that j
appropriate corrective actions had been taken, and that the plant could safely return to power operations.
On April 9, 1990, GPC made a presentation to the NRC in the Region 11 offices in support of GPC's request to return VEGP Unit I to power operations. As part of this presentation, GPC provided information on DG starts in response to a specific NRC request that GPC address DG reliability in its April 9 presentation. GPC submitted a written summary of its April 9 presentation in an April 9, 1990 letter, "Vogtle Electric Generating Plant Confirmation of Action Letter."
, On April 12, 1990, the NRC formally granted permission for VEGP Unit I to return to criticality and resume power operations.
i On April 19, 1990, pursuant to 10 CFR 50.73, GPC submitted Licensee Event l
Report (LER) 50-424/90-006, " Loss of Offsite Power Leads to Site Area
?
j Emergency."
4 On June 29, 1990, GPC submitted a revised LER, 50-424/90-006-01. The purpose of the submittal was to clarify information related to successful DG starts j
that were.scussed in the April 9, 1990 letter and the April 19, 1990 LER, i
j and to update the status of corrective actions in the original LER.
1 From August 6 through August 17, 1990, the NRC conducted a Special Team
{
Inspection at VEGP, as a result of NRC concerns about, and allegations related
}
to, VEGP operational activities. This inspection examined the technical validity and safety significance of the allegations, but did not investigate l
alleged wrongdoing. The Special Team informed GPt that the June 29, 1990 submittal failed to address the April 9,1990 data and requested that GPC clarify DG starts reported on April 9, 1990..Results of this inspection are i
documented, in part, in NRC Inspection Report No. 50-424,425/90-19, Supplement 1, dated November 1,1991.
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On August 30, 1990, GPC submitted a letter, " Clarification of Response to Confirmation of Action Letter." The purpose of the rubmittal was to clarify the diesel start information that was addressed in tne April 9, 1990 submittal.
. III The NRC has reviewed the evidence associated with these events, submittals, and representations to the NRC. Specifically, the NRC reviewed information gathered as part of the OI investigation, information gathered during the !!T, NUREG-1410, Supplement I of NRC Inspection Report 90-19, discovery responses in the Vogtle operating license amendnent proceeding (Docket Nos. 50-424 OLA-3, 50-425 OLA-3), and other related information.
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On June 29, 1990, the draft cover letter for the LER revision was being reviewed at the VEGP site. The draft had originated in GPC corporate heaJguarters arid included language personally developed by the Senior Vice President - Nuclear Operations (George W. Hairston, Ill) and the Vice
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i 5-i President - Vogtle Project (C. Kenneth McCoy). During this review, a VEGP i
j Technical Assistant (TA) (formerly the Acting VEGP Assistant General Manager -
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Plant Support) (Alan L. Mosbaugh) noted that the draft cover letter was i
4 incomplete and challenged the accuracy of the reasons stated in the draft j
4 cover letter in conversations with the Supervisor - Safety Audit and i
i Engineering Review (SAER) (Georgie R. Frederick), the VEGP Assistant General 1
4 l
Manager - Plant Support (Thomas V. Greene), the VEGP Manager - Engineering 4
i Support (Michael W. Horton), and a Licensing Engineer - Vogtle Project (Harry l
W. Majors). Mr. Mosbaugh stated that: (1) the letter failed tn clarify the DG I
starts reportea on April 9, 1990 (2) DG record keeping practices were not a cause of the difference in the DG starts reported in the April 19, 1990 LER because adequate information to formulate an accurate count was available when I
the counting errors were made, and (3) the erroneous counts resulted from i
i personnel errors in developing the count.
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i Mr. Majors had staff responsibility for preparing the cover letter for the LER l
revision and was specifically instructed by the Senior Vice President -
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Nuclear Operations to work closely with the site to ensure that the submittal was accurate and complete.
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l Mr. Horton was responsible for the Diesel Start Logs and agreed with the audit 1
l report findings regarding deficiencies in their condition. Given that his 1
logs had not been used to collect the DG start data, he pointed out that it d
i was wrong to state that the condition of his logs caused errors in the
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information initially provided to the NRC.
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Mr. Frederick was made aware by l
Mr. Mosbaugh on June 12, 1990 that, to identify the root cause of the error in the April 19, 1990 LER (i.e., personnel errors), the audit scope would need to include an assessment of the performance of the Unit Superintendent and the d
l VEGP General Manager, the individuals that developed the initial count. Yet, J
l the audit report did not include either of these individuals in the list of 3
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l persons contacted during the audit. On June 29, 1990, Mr. Frederick was again
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made aware by Mr. Mosbaugh that the root cause for the difference was personnel error.
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Mr. Greene was apprised of concerns regarding the June 29, 1990 letter by Mr. Mosbaugh (an individual who had been involved in preparing the April 19, 1990 LER and had been involved in developing an accurate DG start count).
Mr. Mosbaugh identified to him the failure of the June 29, 1990 draft cover l
l letter to address the inaccuracies in the April 9, 1990 letter that it referenced and Mr. Mosbaugh pointed out the erroneous causes stated for the reasons for the difference in the June 29, 1990 DG start counts.
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. 1 FOR THE NUCLEAR REGULATORY COMMISSION James L. Milhoan Deputy Executive Director for Nuclear Reactor Regulation, Regional Operations, and Research Dated at Rockville, Maryland this day of (Month) 19(M)
i UNITED STATES NUCLEAR REGULATORY COMMISSION In the Matter of
)
)
GEORGIA POWER COMPANY
)
(Vogtle Electric Generating
)
Docket Nos. 50-425/50-425 Plant, Units 1 & 2)
)
License Nos. NPF-68/NPF-81
)
EA 94-052 DEMAND FOR INFORMATION REGARDING C. KENNETH McC0Y I
Georgia Power Company (Licensee) is the holder of Facility License Nos.
NPF-68, and NPF-81 (Licenses) issued by the Nuclear Regulatory Commission (NRC or Commission) pursuant to 10 CFR Part 50. The Licenses authorize the operation of the Vogtte Electric Generating Plant (VEGP) Units 1 and 2, in accordance with conditions specified therein.
II On December 17, 1993, an investigation of licensed activities was completed by the NRC's Office of Investigations (01) at Li isee's VEGP facility. The investigation was initiated in response to information received in June 1990 by NRC Region 11 alleging, in part, that material false statements were made to the NRC by senior Licensee officials regarding the reliability of the Diesel Generators (DGs). The pertinent events involved in this matter are described below.
On March 20, 1990, during a refueling outage at VEGP Unit 1, GPC declared a Site Area Emergency (SAE) when offsite power was lost concurrent with the failure of the only Unit 1 DG that was available (IA). The other Unit 1 DG (18) was unavailable due to maintenance activities.
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! The NRC immediately responded to the SAE at the VEGP site with an Augmented Inspection Team (AIT). The NRC effort was upgraded to an Incident Investigation Team (IIT) on March 23, 1990. The IIT was composed of NRC Headquarters technical staff and industry personnel. The results of this investigation are documented in NUREG-1410, " Loss of Vital AC Power and the Residual Heat Removal System During Mid-loop Operations at Vogtle Unit 1 on March 20, 1990."
On March 23, 1990, the NRC issued a Confirmation of Action Letter (CAL) to GPC 1
tha.,
mong ot'.er things, confirmed that GPC had agreed not to return VEGP Unit I to criticality until the Regional Administrator was satisfied that appropriate corrective actions had been taken, and that the plant could safely return to power operations.
On April 9,1990, GPC made a presentation to the NRC in the Region II offices in support of GPC's request to return VEGP Unit I to power operations. As part of this presentation, GPC provided information on DG starts in response to a specific NRC request that GPC address DG reliability in its April 9 1
presentation. GPC submitted a written summary of its April 9 presentation in an April 9, 1990 letter, "Vogtle Electric Generating Plant Confirmation of Action Letter."
l On April 12, 1990, the NRC formally granted permission for VEGP Unit I to return to criticality and resume power operations.
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l On April 19, 1990, pursuant to 10 CFR 50.73, GPC submitted Licensee Event Report (LER) 50-424/90-006, " Loss of Offsite Power Leads to Site Area Emergency."
On June 29, 1990, GPC submitted a revised LER, 50-424/90-006-01. The purpose of the submittal was to clarify information related to successful DG starts that were discussed in the April 9, 1990 letter and the April 19, 1990 LER, and to update the status of corrective actions in the original LER.
From Augun 6 through August 1,, 1990, the NRC conducted a Special Team inspection at VEGP, as a result of NRC concerns about, and allegations related to, VEGP operational activities. This inspection examined the technical validity and safety significance of the allegations, but did not investigate alleged wrongdoing. The Special Team informed GPC that the June 29, 1990 submittal failed to address the April 9, 1990 data and requested that GPC clarify DG starts reported on April 9,1990. Results of this inspection are f
documented, in part, in NRC Inspection Report No. 50-424,425/90-19, Supplement 1, dated November 1, 1991.
On August 30, 1990, GPC submitted a letter, " Clarification of Response to Confirmation of Action Letter." The purpose of the submittal was to clarify the diesel start information that was addressed in the April 9, 1990 submittal.
f
. III The NRC has reviewed the evidence associated with these events, submittals, i
and representations to the NRC. Specifically, the NRC reviewed informatio-gathered as part of the OI investigation, information gathered during the 1
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NUREG-1410, Supplement I of NRC Inspection Report 90-19, discovery responses in the Vogtle operating license amendment proceeding (Docket f;os. 50-424 OLA-3, 50-425 OLA-3), and other related information.
i Mr. McCoy was actively involved in the preparation of the June 29, 1990 cover letter for an LER revision that was being submitted to the NRC and reviewed it prior to forwarding it to the Senior Vice President - Nuclear Operations for signature and issuance. The June 29, 1990 cover letter stated that its purpose was, in part, to clarify information provided to the NRC on April 9,
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l Special Inspection Team to provide clarification to the NRC regarding the April 9, 1990 letter.
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' FOR THE NUCLEAR REGULATORY COMMISSION l
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James L. Milhoan Deputy Executive Director for Nuclear Reactor Regulation, Regional Operations, and Research J
Dated at Rockville, Maryland this day of (Month) 19(M)
i UNITED STATES NUCLEAR REGULATORY COMMISSION In the Matter of
)
)
GEORGIA POWER COMPANY
)
(Vogtle Electric Generating
)
Docket Nos. 50-425/50-425 Plant, Units 1 & 2)
)
License Nos. NPF-68/NPF-81
)
EA 94-037 DEMAND FOR INFORMATION REGARDING GEORGE BOCKHOLD, JR.
I 1
Georgia Power Company (Licensee) is the holder of facility License Nos.
NPF-68, and NPF-81 (Licenses) issued by the Nuclear Regulatory Commission (NRC or Commission) pursuant to 10 CFR Part 50. The Licenses authorize the operation of the Vogtle Elect,-ic Gei9 rating Plant (VEGP) Units I and 2, in accordance with conditio% specified tt'erein.
II On December 17, 1993, an investigation of licensed activities was completed by the NRC's Office of Investigations (01) at Licensee's VFCP facility. The investigation was initiated in response to information received in June 1990 by NRC Region 11 alleging, in part, that material false statements were made i
to the NRC by senior Licensee officials regarding the reliability of the Diesel Generators (DGs). The pertinent events involved in this matter are described below.
On March 20, 1990, during a refueling outage at VEGP Unit 1, GPC declared a Site Area Emergency (SAE) when offsite power was lost concurrent with the failure of the only Unit 1 DG that was available (IA). The other Unit 1 DG (IB) was unavailable due to maintenance activities.
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l The NRC immediately responded to the SAE at the VEGP site with an Augmented
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l Inspection Team (AIT). The NRC effort was upgraded to an Incident Investigation Team (IIT) on March 23, 1990. The IIT was composed of NRC Headquarters technical staff and industry personnel. The results of this investigation are documented in NUREG-1410, " Loss of Vital AC Power and the Residual Heat Removal System During Mid-Loop Operations at Vogtle Unit 1 on March 20, 1990."
On March 23, 1990, the NRC issued a Confirmation of Action Letter (CAL) to GPC that smong other things, confirmed that GPC had agreed not to return VEGP Unit I to criticality until the Regional Administrator was satisfied that appropriate corrective actions had been taken, and that the plant could safely return to power operations.
On April 9, 1990, GPC made a presentation to the NRC in the Region II offices in support of GPC's request to return VEGP Unit I to power operations. As part of this presentation, GPC provided information on DG starts in response to a specific NRC request that GPC address DG reliability in its April 9 presentation. GPC submitted a written summary of its April 9 presentation in an April 9, 1990 letter, "Vogtle Electric Generating Plant Confirmation of Action Letter."
On April 12, 1990, the NRC formally granted permission for VEGP Unit 1 to return to criticality and resume power operations.
1 1,
On April 19, 1990, pursuant to 10 CFR 50.73, GPC submitted Licensee Event Report (LER) 50-424/90-006, " Loss of Offsite Power Leads to Site Area Emergency."
i On June 29, 1990, GPC submitted a revised LER, 50-424/90-006-01. The purpose of the submittal was to clarify information related to successful DG starts that were discussed in the April 9, 1990 letter and the April 19, 1990 LER, and to update the status of corrective actions in the original LER.
i From Augu. 6 thrcogh August l~, 1990, the NRC cos. ducted a Special Team 4
Inspection at VEGP, as a result of NRC concerns about, and allegations related i
to, VEGP operational activities. This inspection examined the technical validity and safety significance of the allegations, but did not investigate alleged wrongdoing. The Special Team informed GPC that the June 29, 1990 i
submittal failed to address the April 9,1990 data and requested that GPC 4
clarify DG starts reported on April 9, 1990. Results of this inspection are documented, in part, in NRC Inspection Report No. 50-424,425/90-19, Supplement 1, dated November 1, 1991.
On August 30, 1990, GPC submitted a letter, " Clarification of Response to f
4 Confirmation of Action Letter." The purpose of the submittal was to clarify j
the diesel start information that was addressed in the April 9, 1990 submittal.
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The NRC has reviewed the evidence associated with these events, submittals, i
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and representations to the NRC. Specifically, the NRC reviewed information gathered as part of the OI investigation, information gathered during the !!T, i
NUREG-1410, Supplement 1 of NRC Inspection Report 90-19, discovery responses i
in the Vogtle operating license amendment proceeding (Docket Nos. 50-424 OLA-3, 50-425 OLA-3), and other related information. M i
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t Prior to GPC briefing the Regional Administrator, Region II, on VEGP's readiness for restart, the NRC asked GPC to address DG reliability as part of its restart presentation on April 9, 1990. For that presentation, Mr. Bockhold was personally involved in the preparation of data regarding DG
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. reliability and tasked the Unit Superintendent with collecting the number of successful DG starts for the 1A and IB DGs.
l In fact, Mr. Bockhold stated no criteria for successful starts, a term not formally defined, when he directed the Unit Superintendent to gather successful DG starts.
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l Information was then presented to the NRC in the April 9, 1990 oral presentation by Mr. Bockhold and the April 9, 1990 letter submitted by GPC, after being reviewed by Mr. Bockhold, that there were 18 and 19 consecutive successful starts on the 1A and IB DGs, respectively, without problems or failures.
t GPC's report of starts in the presentation and letter included three IB DG starts with problems that occurred during DG overhaul and maintenance activities (a high lube oil temperature trip on March 22, 1990; a low Jacket water pressure / turbo lube oil pressure low trip on March 23, 1990; and a failure to trip on a high jacket water temperature alarm occurring on March 24, 1990). The correct number of consecutive successful starts without problems or failures was 12 for IB DG--a number significantly less than that reported by GPC to the NRC on April 9, 1990.
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j LER 90-006, submitted to the NRC on April 19, 1990, was based, in part, on l
information presented to the NRC on Aprf1 9, 1990. During review of the draft l
LER, site personnel questioned its accuracy. Given that there were trips in 1
i the IB DG after March 20, 1990, they did not think that the statement i
concerning "no problems or failures" was correct. A teleconference was subsequently held between site and corporate personnel i
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President - Nuclear. Operations also stated that he thought the April 19, 1990 j
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i GPC was specifically notified by the NRC that the revised LER did not i
j adequately clarify the DG start information contained in the April 9, 1990 I
letter, and NRC requested GPC to provide clarification of this submittal. GPC i
forwarded a submittal to the NRC on August 30, 1990 regarding the April 9, 1990 letter.
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- During an August 29, 1990 Plant Review Board (PRB) meeting which, among other things, reviewed the proposed August 30, 1990 submittal to the NRC, the VEGP Manager - Technical Support raised concerns about the accuracy of that statement. Mr. Bockhold admitted to the PRB that the Unit Superintendent (who originally collected the DG start data at Mr. Bockhold's direction) was not confused about the distinction between successful starts and valid tests when the start data was collected for the April 9, 1990 letter, but stated that the sentence was not in error because other people were confused.
Mr. Bockhold acknowledged that there was confusion among individuals after April 9, 1990, but admitted that the Unit Superintendent was not confused when he developed the information.
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l IV Mr. Bockhold was aware of the NRr+, interest in DG reliability in the context of an NRC decision on restart and he was aware of a
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< questions and concerns about the adequacy, accuracy, and completeness of i
information that GPC was providing to the NRC on this issue, i
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i FOR THE NUCLEAR REGULATORY COMMISSION l
l James L. Milhoan Deputy Executive Director for Nuclear Reactor Regulation, Regional Operations, and Research l
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Dated at Rockville, Maryland this day of. (Month) 19(g) l 1
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