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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20085F6511976-04-12012 April 1976 Update to AO AO-75-15 Re Containment Air Cooler Temp Control Valve Body Failure.Spare Valve Procurement Requirement Changed from ASME Section III Stds to ANSI B31.1 Stds. Sys Built to B31.1 Std ML20085E7841975-11-14014 November 1975 Telecopy Message Ao:On 751113,CB Exhaust Valves Leaked in Excess of Total Allowable Rate Back Through Inside Valve. Valves to Be Tagged Shut Until Repaired During Next Plant Shutdown ML20085E7971975-10-30030 October 1975 Telecopy Message Ao:On 751029,interchanged W Prime Curves Resulted in Nonconservative Heat Rate Calculation for Core Limiting Assemblies.Caused by Improper Conversion of Flux to Power by Inca Power Distribution on 730619 ML20085E8231975-10-24024 October 1975 AO 75-024:on 751015,thermal Discharge of Blowdown from closed-cycle Cooling Sys Found Above Permissible Temp Limit. Caused by Shutoff Dilution Pumps During Installation of New Thermal Discharge Monitoring Equipment.Procedure Revised ML20085E8081975-10-15015 October 1975 Telecopy Message Ao:On 751015 Discharge Water Temp Exceeded Tech Spec Limits by 5 Degrees During Temp Monitoring Equipment Installation ML20085F7071975-09-19019 September 1975 Updated AO AO-74-11 Revising Analysis of Occurrence.Loss of Dc Control Power to Bus 1D Feeder Breaker 72-203 Results in Breaker Not Being Able to Operate If Equipment Malfunctions ML20085E8721975-09-18018 September 1975 Telecopy Message AOs 75-022 & 75-021:boron Concentration Found Below Tech Spec Limits & HPSI Safety Injection Valve Found W/Apparent Disc Separation.Valve MOV-3007 to Be Disassembled & Evaluated.Investigation Continues ML20085E8811975-09-15015 September 1975 Telecopy Message Aos:Safety Tank Boric Acid Concentration Found Below Tech Spec Limits & HPSI Valve MOV-3007 Failed. Further Info Will Be Submitted ML20085F7201975-09-0909 September 1975 AO 75-019:on 750830,control Rod 11 Dropped Into Core.Caused by Shorted Clutch Coil.Clutch Replaced ML20085F6891975-09-0808 September 1975 Telecopy Message of AO 75-020:on 750905,control Rod 16 Dropped.Flux Tilt & Ejected Rod Worth Resulting from Dropped Rod within Tech Spec Limits.Clutch Coil Replaced ML20085F7491975-08-28028 August 1975 AO 75-018:on 760817,control Rod 19 Dropped Into Core.Caused by Shorted Clutch Coil.Clutch Replaced.Preventive Maint,To Include Insulation & Component Resistance Measurements on Control Rod Drive Mechanisms,To Be Evaluated ML20085F7671975-08-18018 August 1975 Telecopy AO 75-018:on 750817,control Rod 19 Dropped Into Core.Caused by Shorted Clutch Coil in Control Rod Drive Mechanism ML20085F7961975-08-12012 August 1975 AO 75-016:on 750722,radwaste Batch 75-021 R Discharge Rate Exceeded.Caused by Inaccurate Flow Control Due to Water Loss in One Leg of Flow Controller FIC 1050.Radwaste Release Procedures Revised ML20085F7721975-08-12012 August 1975 AO 75-017:between 750718-28,waste Gas Decay Tank T 101C Lost Pressure.Probably Caused by Small Valve Leak.Tank Will Be Monitored During Next Period of Use Since Tests Did Not Determine Pressure Drop Cause ML20085F8731975-07-25025 July 1975 Telecopy Ao:On 750716,util Water Storage Tank T-91 Removed from Svc to Replace Liner Coating ML20085F8041975-07-24024 July 1975 Telecopy AO 75-016:radwaste Batch Discharge Rate Exceeded During Release of Radwaste Batch 75-021-R.Caused by Malfunctioning Flow Controller FIC 1050 ML20085F8631975-07-22022 July 1975 Telecopy Ao:On 750719,MOV-3011 Functioned Improperly During QO-1 Test.Caused by Failure of Spring Return Switch,Ge Type CR 2940 ML20085F3581975-07-11011 July 1975 AOs AO-75-6,AO-75-7 & AO-75-13 Have Been Canceled.Tech Specs Re Heated Discharge Do Not Apply to Svc Water Sys or Other Discharge ML20085F9101975-07-0808 July 1975 AO 75-014:on 750630,bus 1D Failed to Transfer from Station Power to Startup Power.Caused by Failure of Incoming Breaker 152-202 to Close Automatically Due to Diesel Generator Breaker 152.213 Interlock.Synchrocheck Circuitry Repaired ML20085F9271975-07-0202 July 1975 AO 75-014 & RO 75-004:on 750701,bus 1D Failed to Fast Transfer from Station to Startup Power & Control Rod 38 Deviated by 9 Inches,Respectively.Ao Caused by Faulty Auxiliary Contact.Ro Caused by Shorted Capacitor ML20085F9151975-07-0202 July 1975 Telecopy Message AO 75-014:on 750701,bus 1D Failed to Transfer from Station Power to Startup Power.Caused by Faulty Auxiliary Contact on Incoming Bus Breaker.Ro 75-004, on 750701,control Rod 38 Deviated Due to Capacitator Short ML20085F9501975-06-30030 June 1975 AO 75-013:on 750619,plant Discharge Water Temp & Heat Rate Exceeded Tech Spec Limits.Caused by Changing Lower Basin Level.Addl Operating Procedures to Be Formulated for Raising & Lowering Cooling Tower Basin Levels ML20085F9601975-06-23023 June 1975 Telecopy AO 75-013:on 750619,mixing Basin Outfall Exceeded Lake Temp Differential While Adjusting Cooling Tower Makeup to Allow Evaporation Changes.Details Will Follow ML20085F5821975-06-18018 June 1975 Updated AOs AO-21-74,AO-6-75 & AO-7-75,in Response to 750512 Request for Addl Info.Cause of Failure of Diesel Generator 1-1 Air Start Motor Not Determined ML20085F9761975-06-13013 June 1975 AO 75-012:on 750603,required Measurements & Observations Re Closed Cycle Condenser Cooling Sys Chlorination Treatment Not Performed.Caused by Incorrectly Conceived Tech Specs ML20085F9961975-06-0606 June 1975 Telecopy Message AO 75-012:on 750606,difficulty Encountered in Adhering to Tech Spec Section 3.9.7-3.9.9 Re Cooling Tower Chlorination Limits ML20085F9991975-05-30030 May 1975 Telecopy AO 75-011:on 750529,overpower Trip Setpoint on NI005 Found Out of Spec During Surveillance Test MO1 ML20085F3251975-04-28028 April 1975 AO AO-75-9:on 741223,three Reactor Trip Pressure Switches, PS-1801,PS-1802 & PS-1803 Found Out of Calibr.Caused by Use of Incorrect Procedure for Switch Calibr.Instrument Index Revised to Ref Proper Tech Spec Section ML20085F3221975-04-23023 April 1975 AO AO-10-75:on 750413,in-core Readings on Primary Data Logger Failed to Update.Caused by Deficient Software Program.Program Being Analyzed to Find & Correct Deficiency ML20085F3341975-04-18018 April 1975 Telecopy AO AO-75-8:three Containment High Pressure Switches Found Out of Calibr ML20085F3281975-04-17017 April 1975 AO AO-75-8 Has Been Canceled.Review of Temp Measuring Techniques Disclosed Temp Measurements in Error.Revised Measurements Show Discharge Temp within Allowable Limits ML20085F3771975-04-16016 April 1975 AO AO-75-7:on 750406,plant Discharge Effluent Heat Rate & Discharge Temp Increase Found Greater than Tech Spec Limits. Apparently Caused by Plant Procedure Problems & Beginning Operation of Newly Installed Closed Cycle Cooling Sys ML20085F3981975-04-14014 April 1975 AO AO-75-6:on 750404,plant Discharge Effluent Heat Rate Exceeded Tech Specs.Apparently Caused by Plant Procedure Problems & Beginning Operation of Newly Installed Closed Cycle Cooling Sys ML20085F4201975-04-11011 April 1975 AO AO-75-5:on 750411 Unsampled South Filtered Waste Tank W/Laundry Waste Released.Caused by Use of Wrong Batch Card. Tank Release Terminated Until Appropriate Analysis Could Be Made ML20085F3441975-04-0808 April 1975 AO AO-75-8:from 750406-07,indicated Temp of Mixing Basin Discharge More than 5 F Above Indicated Temp of Plant Intake Water.Caused by Excess Amount of Water Going Over Cooling Tower Pump Makeup Basin Overflow ML20085F4271975-04-0707 April 1975 Telecopy AO AO-75-5:on 750401,unsampled Liquid Waste Tank of Laundry Waste Released.Caused by Two Tank Analyses on Same Tank.Tank Release Stopped & Analysis of Tank Contents Made. Tank Released on 750403 ML20085F3881975-04-0606 April 1975 Telecopy AO AO-75-7:on 750406,plant Discharge Effluent from Mixing Basin Exceeded Tech Spec Limit.Caused by Cracking Open of Condenser Inlet Valve MOV-5301 to Reduce Hotwell Temp to Avoid Thermal Shocking Condenser Tubes ML20085F4081975-04-0404 April 1975 Telecopy AO AO-75-6:on 750404,plant Discharge Effluent Heat Rate Exceeded Tech Specs.Caused by Diversion of Dilution Water Through Unused Side of Condenser.Personnel Unaware of Difference in Temp Between Inlet Water & Basin Outfall ML20085F4511975-03-27027 March 1975 Update to AO AO-4-75,revising Analysisi of Occurrence.Util Discovered 102 restraints,12 Restraint Replacements & 74 Restraint Mods Required or Added for Addl Conservatism. Sys Studied Listed ML20085F4561975-03-17017 March 1975 AO AO-4-75:on 750307,util Determined Certain Seismic Class I Piping Sys Restraints Do Not Comply W/Fsar Design Criteria. Investigation Into Cause Underway.Sys Studied Listed ML20085F5181975-02-0404 February 1975 AO AO-2-75:on 750126,vol Control Tank Gas Lost to Auxiliary Bldg.Caused by Bank Pressure Due to Venting of Vol Control Tank Which Blew Loop Seal on Evaporator Vacuum Pump Air Water Separator ML20085F5091975-02-0404 February 1975 AO AO-3-75:on 750122,leak in Component Cooling Water to Svc Water Header Discovered.Cause Not Stated.Leak Developed 750116.Leaking Tube Plugged ML20085F5231975-01-31031 January 1975 AO AO-75-1:on 741206,allowable Leak Rate Exceeded on Purge Air Supply Valve CV-1808 During Test.Caused by Lack of Sufficient Lubricant Aggravated by Unusual Svc Condition. Packing Properly Greased & Leakage Reduced ML20085F5151975-01-28028 January 1975 AO Telecopy 75-2:on 750126,vol Control Tank Gas Lost to Auxiliary Bldg.Caused by Discharge of Orificed Recirculation Line from Vacuum Pump Back to Evaporator,Causing Erratic Evaporator Operation ML20085F5061975-01-26026 January 1975 AO 75-3:on 750122,leak Suspected in One Component Cooling Water Hx.Component Cooling Water a Isolated.Leak Developed on 750116.Caused by Leaking Tube.Tube Plugged ML20085F5361974-12-26026 December 1974 AO AO-28-74:on 741215,north Filtered Waste Tank of Laundry Waste Released W/O Prior Sampling.Caused by Technician Error.Wrong Tank Identification Wrote on Batch Card When Transposing Data ML20085F5391974-12-17017 December 1974 Telecopy AO AO-74-28:on 741215,north Filtered Waste Tank of Laundry Waste Released W/O Prior Sampling.Caused by Technician Error.Technician Wrote Down Incorrect Tank Identification on Batch Card ML20085F5471974-12-12012 December 1974 AO AO-27-74:on 741130,released to Plant Vent Stack from Waste Gas Surge Tank.Caused by Waste Gas Surge Tank Leakage, Due to Leaky Relief Valve.Valve Repaired & Pressure Tested ML20085F5521974-12-0202 December 1974 AO AO-74-27:on 741130,waste Gas Surge Tank Vented to Plant Stack.Continuous Stack Monitor Alarmed.Caused by Malfunction of Waste Gas Surge Tank Pressure Relief Valve.Total of 40 Mci Released in 3 Cubic Meters Radioactive Gases ML20085F5291974-11-18018 November 1974 Updated AO AO-24-74 Re Greater than Allowed Ph Difference Between Lake Inlet & Outlet Water.Caused by Cooling Tower Acid Injection Sys Continuing to Operate After Pump Shut Off Due to Incorrect Relocation of Sample Probe 1976-04-12
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18066A6901999-11-0101 November 1999 Rev 5 to Palisades Nuclear Plant Colr. ML18066A6761999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Palisades Nuclear Plant ML18066A6271999-09-0202 September 1999 LER 98-011-01:on 981217,inadequate Lube Oil Collection Sys for Primary Coolant Pumps Was Noted.Caused by Design Change Not Containing Appropriate Level of Rigor.Exemption from 10CFR50,App R Was Requested.With 990902 Ltr ML18066A6351999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Palisades Nuclear Plant ML18066A6771999-08-31031 August 1999 Operating Data Rept Page of MOR for Aug 1999 for Palisades Nuclear Plant ML18066A6221999-08-20020 August 1999 LER 99-002-00:on 990722,TS Surveillance Was Not Completed within Specified Frequency.Caused by Failure to Incorporate Revised Frequency Into Surveillance Schedule in Timely Manner.Verified Implementation.With 990820 Ltr ML18066A6061999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Palisades Nuclear Plant.With 990803 Ltr ML18066A5201999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Palisades Nuclear Plant.With 990702 Ltr ML18066A4841999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Palisades Nuclear Plant.With 990603 Ltr ML18066A6371999-04-30030 April 1999 Revised Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant ML18068A5941999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Palisades Nuclear Plant.With 990503 Ltr ML18066A4161999-04-0101 April 1999 Rev 4 to COLR, for Palisades Nuclear Plant ML18066A4501999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Palisades Nuclear Plant.With 990402 Ltr ML18066A4671999-03-31031 March 1999 Rev 0 to SIR-99-032, Flaw Tolerance & Leakage Evaluation Spent Fuel Pool Heat Exchanger E-53B Nozzle Palisades Nuclear Plant. ML18068A5351999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Palisades Nuclear Plant.With 990302 Ltr ML18066A3931999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Palisades Nuclear Plant.With 990202 Ltr ML18066A3781999-01-20020 January 1999 LER 98-013-00:on 981222,safeguards Transfer Tap Changer Failure Caused Inadvertant DG Start.Caused by Failed Motor Contactor.Contactor Was Replaced.With 990120 Ltr ML20206F6131998-12-31031 December 1998 1998 Consumers Energy Co Annual Rept. with ML18066A3651998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Palisades Nuclear Plant.With 990105 Ltr ML18066A3421998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Palisades Nuclear Plant.With 981202 Ltr ML18066A3301998-11-11011 November 1998 Part 21 Rept Re Potential Safety Hazard Associated with Wrist Pin Assemblies for FM-Alco 251 Engines at Palisades Nuclear Power Plant.Caused by Insufficient Friction Fit Between Pin & Sleeve.Supplier of Pin Will No Longer Be Used ML18068A4921998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Palisades Nuclear Plant.With 981103 Ltr ML18068A4851998-10-29029 October 1998 LER 97-011-01:on 971012,starting of Primary Coolant Pump with SG Temps Greater than Cold Leg Temps Occurred.Caused by Inadequate Procedures & Operator Decision.Sop Used for Starting Primary Coolant Pump Enhanced ML18066A3181998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Palisades Nuclear Plant ML18066A2901998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Palisades Nuclear Power Plant.With 980903 Ltr ML18066A3191998-08-31031 August 1998 Revised Monthly Operating Rept Data for Aug 1998 for Palisades Nuclear Plant ML18066A2831998-08-18018 August 1998 LER 98-010-00:on 980721,reactor Manually Tripped.Caused by Failure of Coupling Which Drives Feedwater Pump Main Lube Oil Pump.Main Lube Oil Pump Coupling & Associated Components Replaced & Satisfactorily Tested ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237E0301998-07-31031 July 1998 ISI Rept 3-3 ML18066A2701998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Palisades Nuclear Plant.W/980803 Ltr ML18066A2311998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Palisades Nuclear Plant ML18066A2261998-06-30030 June 1998 LER 98-009-00:on 980531,small Pinhole Leak Found on One of Welds,During Leak Test Following Replacement of Pcs Sample Isolation Valves.Caused by Welder Error.Leaking Welds Repaired ML18066A3061998-06-18018 June 1998 SG Tube Inservice Insp. ML20249C4951998-06-17017 June 1998 Rev 1 to EA-GEJ-98-01, Palisades Cycle 14 Disposition of Events Review ML18066A1781998-06-0909 June 1998 LER 98-008-00:on 980511,noted That Procedure Did Not Fully Satisfy Requirement to Test High Startup Rate Trip Function. Caused by Misunderstanding of Testing Requirements.Revised TS Surveillance Test Procedure & Reviewed Other Procedures ML18066A1711998-06-0101 June 1998 Part 21 Rept Re Impact of RELAP4 Excessive Variability on Palisades Large Break LOCA ECCS Results.Change in PCT Between Cycle 13 & Cycle 14 Does Not Constitute Significant Change Per 10CFR50.46 ML18066A1741998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Palisades Nuclear Plant.W/980601 Ltr ML18066A2321998-05-31031 May 1998 Revised MOR for May 1998 for Palisades Nuclear Plant ML18068A4701998-05-31031 May 1998 Annual Rept of Changes in ECCS Models Per 10CFR50.46. ML18065B2451998-05-13013 May 1998 LER 98-007-00:on 980413,HPIS Sys Was Noted Inoperable During TS Surveillance Test.Caused by Performance of Flawed Procedure.Operators & Engineers Will Be Trained to Improve Operational Decision Making Through Resources & Knowledge ML18066A2331998-04-30030 April 1998 Revised MOR for Apr 1998 for Palisades Nuclear Plant ML18068A3461998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Palisades Nuclear Plant.W/980501 Ltr ML18066A3411998-04-22022 April 1998 Rev 0 to EMF-98-013, Palisades Cycle 14:Disposition & Analysis of SRP Chapter 15 Events. ML18065B2071998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Palisades Nuclear Plant.W/980403 Ltr ML20217C2741998-03-31031 March 1998 Independent Review - Is Consumers Energy Method (W Method) of Determining Palisades Nuclear Plant Best Estimate Fluence by Combining Transport Calculation & Dosimetry Measurements Technically Sound & Does It Meet Intent of Pts ML18066A2341998-03-31031 March 1998 Revised MOR for Mar 1998 for Palisades Nuclear Plant ML18068A3041998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Palisades Nuclear Plant.W/980302 Ltr ML18066A2351998-02-28028 February 1998 Revised MOR for Feb 1998 for Palisades Nuclear Plant ML18065B1641998-02-0505 February 1998 Rev 0 to Regression Analysis for Containment Prestressing Sys at 25th Year Surveillance. ML18067A8211998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Palisades Nuclear Plant.W/980203 Ltr 1999-09-30
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_$ General Offices: 212 West M chigan Avenue. Jackson, Mic hsgan 49201. Area Code 517 7HR-OSSO Ncvember 2, 1972
'j Mr. John F. O' Leary, Director Re:j9 Docket No 50-255 Directorate of Licensing N License No DPR-20 US Atomic Energy Commission [/
Washington, DC 20545 . N/
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Dear Mr. O' Leary:
This is written to apprise you of an abnormal occurrence that occurred at the Palisades Plant on October 23, 1972, involving the failure of the seal mechanism of control rod drive mechanism (CRDM) No 19 The
/ failure of this seal mechanism allowed a primary coolant system leakage of 28 gallons per minute, which exceeds the Technical Specifications
- allovable leakt ge rate of 10 gallons per minute, At u.: time the first indications or seal leakage were observed, the plant was generat'ing 405 MRe. The first indications of leakage from the seal of CRDM No 19 followed partial movement testing performed to fulfill Technical Specifications requirements. After receiving the in-dications of the leakage, CFDM No 19 was exercised several times in an attempt to reset the seal. This exercising procedure has been used with some success on previously experienced seal leaks which have all involved very small amounts of seal leakage. During the exercising of CRDM No 19, the seal leak off temperature continued to climb, indicating increasing seal leakage, and went off scale at 4500F. At this time, the primary system leak rate was determined to be 28 gallons per minute. At approxi-mately the same time, both the primary and secondary rod position indi-cations for CRDM No 19 failed. An orderly shutdown was initiated and the plant was cooled to the cold shutdown condition. Reactor coolant water level was lowered to a level below the CRDM seals and the leakage stopped.
The Palisades Plant CRDM seals are composed of three basic parts: collar, rotating seal half and stationary seal half. The collar rests on a shoulder of the CRDM shaft and is keyed to the shaft. In addition, it is held by three 1/h" allen head setscrews and these set-screws also transmit the motion of the collar to the rotating seal half.
The rotating half has a skirt which extends over the collar. The pro-trusion of the collar setscrew is accommodated by three slots in the sides of the skirt. A carbon seal surface is mounted at the top of the rotating seal half. The rotating seal half is sealed to the shaft by
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. O Mr. John F. O' Leary 2 Docket No 50-255 License No DPR-20 November 2, 1972 means of an 0-ring. The stationary seal half is mounted in the housing above the rotating half and an 0-ring provides a seal between the station-ary half and the seal housing. The seal halves are maintained in contact by springs in the rotating seal half which acts against the collar.
Disassembly of CRDM No 19 seal assembly revealed that one of the three collar setscrews had backed out and lodged between the rotating seal half skirt and the seal housing. The setscrev was destroyed and the rotating seal half skirt was heavily marked. The lodging of the setscrew caused the rotating seal half to cock, allowing the excessive leakage between the seal faces and severe erosion of the carbon seal face. When a seal leak occurs, the leakage path is in an upward direction between rotating seal half skirt and seal assembly, then horizonal between the seal faces and then upward between stationary seal face and CRDM shaft to the seal leak off cavity.
The collar setscrews are locked in place by staking (upsetting the collar and screw thread metal junction with a punch). The setscrew that backed out had not been properly staked.
A vapor seal is installed to prevent leakage from the CRDM mechanical seal leak off cavity to the motor package. . This seal has been bench tested in the cold condition to 1000 psig and has experienced temperatures up to 350 F under operating conditions without failure. The seal leak off cavity normally experiences temperatures of about 1500F to 2000F and atmospheric pressure. The seal was destroyed, allowing primary l coolant to escape along the motor shaft to the motor package as well as '
the normal leak off path, the drain line from the seal leak off cavity.
Most of the steam and water primary coolant mixture that leaked into the CRDM No 19 motor package escaped through the motor package inspec-tion covers. As a result, approximately 50% of the reactor vessel head insulation was vetted. Several CRDM motor packages, junction boxes and electrical connectors showed signs of moisture and/or boron salt de-posits. In addition, both channels of start-up range instrumentation failed during the plant shutdown, most likely due to moisture but as of this writing this conclusion has not been proved or disproved.
The reactor was shut down by driving all CRDMs into their lower electrical limit except No 19 CRDM No 19 was left at an indi-cated position of 128" because it was concluded that either the position indication had failed or the CRDM vould not move. On the day after the leak was detected, attempts were made to drive CRDM No 19 to the full-in position. The primary position indication indicated an inward motion to 120"; the secondary position indication was meaningless. At this time, it was assumed the drive was stuck. However, during disassembly, it was determined that CRDM No 19 was fully inserted and the position indication ,
had been faulty. It is readily apparent that a CRDM will not move as i freely with a collar setscrev lodged between the rotating seal half J skirt and the seal housing as a normal CRDM; however, it was still oper- c' able . This condition is immediately apparent because the setscrew causes the rotation seal housing to cock, allowing gross leakage between the seal faces, which is indicated by an excessively high seal temperature.
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. (v3 Mr. John F. O'Le!.ry 3 Docket No 50-255 License No DPR-20 November 2, 1972 All CRDMs were trip tested from the lower electrical limit on October 26. The clutch halves failed to separate on four CRDMs. Inspec-tion revealed the presence of boron salt and moist tre inside the motor packages of these four CRDMs. This is the first time any CRDM motor packages have shown any signs of boron salt deposits or moisture, with the exception of CRDM No 17 in February 1972 (refer to our letter dated February 14,1972).
The following is a summary of corrective action currently in progress or that has already been completed:
- 1. The seal assembly for CRDM No 19 has been replaced.
- 2. All CRDM seal assemblies are being inspected. All collar setscrews found not properly staked are being properly staked.
3 The seal replacement procedure has been modified to pro-vide for inspection of the collar setscrew.
- h. All CRDM motor packages have been removed and are being inspected and cleaned as necessary.
5 The clutch spline areas on all CRDM are being vapor blasted and relubricated as described in our letter of September 26, 1972. The CRDMs vill be trip tested as described in the September letter prior to returning the plant to service.
- 6. CRDM motor package inspection covers, terminal boxes and connectors are being waterproofed to reduce the possibility of in-leakage in the event of a similar occurrence.
7 The detector for one start-up range channel has been re-placed and the channel returned to service. The removed detector has been returned to the vendor for further investigation into the cause of its failure. The detector in the second channel vill be replaced as soon as parts are received from the vendor.
- 8. All insulation has been removed from the reactor vessel head and the vessel head cleaned. The head will be reinsulated.
9 Plant operating procedures are being revised to incor-porate specific instructions to operators in the event a similar seal failure were to occur. The objective vill be to minimize the total leakage, thus reducing the possibility of demage to other plant equipment.
- 10. We are investigating the replacement of the vapor seal (the seal between the leak off cavity and the motor package) with a new seal which will withstand higher temperatures.
All the above items, except No 10, vill be completed prior to returning the plant to service.
t
O Mr. John F. O' Leary
.. O 14 Docket No 50-255 License No DPR-20 November 2, 1972 The Palisades Plant Safety Audit and Review Board has reviewed this abnormal occurrence. The Board concluded that restaking the collar setscrews would prevent recurrence of a similar incident. The Bor$rd also concluded that the corrective action outlined above is adequate to return the plant to operation.
It 10 presently anticipated that the plant will be returned to service during the week of November 5 Yours very truly, Ralph B. Sewell (Signed)
RBS/ map Ralph B. Sewell Nuclear Licensing Administrator CC: BHGrier, USAEC L
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