LER 93-002-01:on 930107,determined Potential for Premature Opening of Containment Bldg Spray Sump Isolation Valves. Caused by Failure to Adequately Recognize Potential Sys Interactions.Affected Procedures RevisedML20045D679 |
Person / Time |
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Site: |
Seabrook ![NextEra Energy icon.png](/w/images/9/9b/NextEra_Energy_icon.png) |
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Issue date: |
06/21/1993 |
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From: |
Peschel J NORTH ATLANTIC ENERGY SERVICE CORP. (NAESCO) |
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To: |
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Shared Package |
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ML20045D677 |
List: |
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References |
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LER-93-002, LER-93-2, NUDOCS 9306290292 |
Download: ML20045D679 (4) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B8951993-07-30030 July 1993 LER 93-008-01:on 930518,determined That Control Air Not Analyzed to Function During Seismic Event Due to Lack of Understanding Significance of Control Air Availability for Long Term DG Operation.Ufsar Will Be Updated ML20046B8961993-07-30030 July 1993 LER 93-011-00:on 921219,930209 & 0415,SW Pumps SW-P-41B, SW-P-41B & SW-P-41D Declared Inoperable,Respectively Due High Vibration.Caused by Excessive Abrasive Particles in Ocean Water.Pumps replaced.W/930730 Ltr ML20045G6641993-07-0101 July 1993 LER 93-006-01:on 930401,Train a Svc Water Inoperable Due to Corrosion Product Buildup Between Valve Stem & Packing Follower.Returned SW-V54 to Operable Status & TS 3.7.4 Action D Exited on 930402.W/930701 Ltr ML20045D6791993-06-21021 June 1993 LER 93-002-01:on 930107,determined Potential for Premature Opening of Containment Bldg Spray Sump Isolation Valves. Caused by Failure to Adequately Recognize Potential Sys Interactions.Affected Procedures Revised ML20045C5421993-06-18018 June 1993 LER 93-010-00:on 930522,SG Level Oscillations Occurred in One SG Resulting in SG Being Overfed & Causing high-high SG Water Level.Caused by Personnel Error.Power Reduced to Approx 2.5% & FW to SGs restored.W/930618 Ltr ML20045D3681993-06-18018 June 1993 LER 93-009-00:on 930520,manual Reactor Trip from 100% Power Initiated When MSIV Closed During Quarterly Testing, Resulting in Feedwater & Two Emergency Feedwater Isolations. Caused by Debris in Valves.Valves Replaced ML20045C5341993-06-16016 June 1993 LER 93-008-00:on 930518,identified That Failure of Air Supply to EDG Jacket Cooling Water Temperature Control Valves During Seismic Event Could Cause Overcooling of Edgs. Operability Determination Performed for EDGs.W/930616 Ltr ML20045B5181993-06-11011 June 1993 LER 93-007-00:on 930512,protective Devices Not Analyzed to Function During Environ Excursions Due to Unknown Cause Which Is Under Review.Operability Determination Was performed.W/930611 Ltr ML20024H1621991-05-23023 May 1991 LER 91-004-00:on 910401,steam Generator Indicated That Valve Was Not Opening Properly During Plant Restart.Caused by Differential Pressure Across Dash Plate.Dash Plate Machining Performed on Valves to Prevent Valve disk.W/910523 Ltr ML20044B2281990-07-12012 July 1990 LER 90-014-00:on 900612,discovered That Sample Pump for Steam Generator Blowdown Flash Tank Drain Radiation Monitor Not Running.Caused by Suspended Solids in Steam Generator Blowdown Sys.Solids Cleared from Flow switch.W/900712 Ltr ML20043B6741990-05-23023 May 1990 LER 90-008-01:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Air Cleanup Sys Incapable of Producing Negative Pressure.Latching Mechanism Repaired & Mods to Doors/Hardware planned.W/900523 Ltr ML20043B3551990-05-21021 May 1990 LER 90-013-00:on 900419,discovered That Containment Personnel Hatch Unsecured for Approx 28 H.Caused by Installation of Locking Plate Upside Down & Placing Lock Through Only 1 Eyelet.Instructions posted.W/900521 Ltr ML20042F5521990-05-0202 May 1990 LER 90-012-00:on 900402,transmitter Failed to Provide Pressure to Reactor Protection Sys Due to Closed Isolation Valve.Caused by Failure to Identify Valve in Procedures. Valves Manipulated to Correct positions.W/900502 Ltr ML20042E1781990-04-0606 April 1990 LER 90-006-01:on 900206,control Room Ventilation Sys Train a Radiation Monitor Went Into High Alarm Condition.Caused by Mechanical Binding of Check source.Geiger-Muller Tube Replaced & Monitor Returned to svc.W/900406 Ltr ML20042E1741990-04-0505 April 1990 LER 90-011-00:on 900306,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Failure of Geiger-Muller Tube.Monitor Removed from Svc & Tube replaced.W/900405 Ltr ML20012F5181990-04-0404 April 1990 LER 90-010-00:on 900305,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Moisture in Detector Housing.Air Intake Monitors Cleaned & Desiccant Placed in housing.W/900404 Ltr ML20012C2461990-03-12012 March 1990 LER 90-008-00:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Emergency Air Cleanup Sys Inoperable.Plant Cooldown Initiated,Latching Mechanism Repaired & Door Returned to svc.W/900312 Ltr ML20012C2481990-03-12012 March 1990 LER 90-007-00:on 900208,when Source Check Removed from Control room,RM-6506B Entered High Alarm Condition,Causing ESF Actuation of Emergency Air Cleanup Sys.Caused by Mechanical Binding.Check Source replaced.W/900312 Ltr ML20012B4491990-03-0808 March 1990 LER 90-006-00:on 900206,Train a Radiation Monitor Went Into High Alarm Condition,Resulting in Actuation of Control Room Emergency Air Cleanup & Filtration Subsystem.Caused by Mechanical Binding.Detector Tube remounted.W/900308 Ltr ML20011F4671990-02-22022 February 1990 LER 90-004-00:on 900123,wide-range Gas Monitor Process Flow Rate Value for Vent Radiation Monitor Discovered at Default Instead of Actual Value.Caused by Personnel Error.Process Flow Restored & Technician counseled.W/900222 Ltr ML20006E4591990-02-15015 February 1990 LER 90-003-00:on 900116,wide-range Gas Monitor Low Range Pump Found Inoperable.Caused by Failed Pump Diaphragm Weakened by High Flow Condition.Ruptured Pump Diaphragm Replaced & Pump Returned to Normal operations.W/900215 Ltr ML20006E1731990-02-0808 February 1990 LER 90-002-00:on 900109,discovered That Auxiliary Sample Pump Used to Satisfy Action Requirements of Tech Spec Was Not Operating.Caused by Dislodged Power Fuse.Pump Relocated & Caution Tape Installed to Protect pump.W/900208 Ltr ML20006E1801990-02-0808 February 1990 LER 90-001-00:on 900109,wide Range Gas Monitor Low Range Pump Found to Be Inoperable,Resulting in Noncompliance W/ Tech Specs.Caused by Regulator Isolation Valves Being Left in Open Position.Walkdown of Skids conducted.W/900208 Ltr ML20005E2461989-12-29029 December 1989 LER 89-014-00:on 891129,auxiliary Transformer Supply Breaker to Vital Bus E5 Tripped When Remote Manual Override Relay Energized.Caused by Procedure Inadequacies in Procedure 0S1048.01.Procedure revised.W/891229 Ltr ML20011D4381989-12-19019 December 1989 LER 89-011-01:on 890905,three Unsealed Piping Penetrations in Condensate Storage Tank Encl Identified.Caused by Failure to Transfer Sealing Requirements Into Detail Drawings.Penetrations sealed.W/891219 Ltr ML19332C8511989-11-22022 November 1989 LER 89-013-00:on 891023,discovered That Monitor Used to Satisfy Requirements of Tech Spec 3.3.3.1,Action 27 Had Been Unplugged.Caused by Personnel Error.Individual Counseled & Meeting Held W/Health Physics technicians.W/891122 Ltr ML19325F3301989-11-10010 November 1989 LER 89-012-00:on 891011,one of Two Suction Valves on RHR Train a Pump Closed,Causing Loss of All RHR Cooling Capability.Caused by Procedure Inadequacies.Procedure Revised to Specify Sequence of restoration.W/891110 Ltr ML19325C7891989-10-0505 October 1989 LER 89-011-00:on 890905,determined That Three Piping Penetrations in Condensate Storage Tank Encl Not Sealed.Root Cause Under Investigation.Penetrations Sealed & Tech Specs Surveillance Log revised.W/891005 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B8951993-07-30030 July 1993 LER 93-008-01:on 930518,determined That Control Air Not Analyzed to Function During Seismic Event Due to Lack of Understanding Significance of Control Air Availability for Long Term DG Operation.Ufsar Will Be Updated ML20046B8961993-07-30030 July 1993 LER 93-011-00:on 921219,930209 & 0415,SW Pumps SW-P-41B, SW-P-41B & SW-P-41D Declared Inoperable,Respectively Due High Vibration.Caused by Excessive Abrasive Particles in Ocean Water.Pumps replaced.W/930730 Ltr ML20045G6641993-07-0101 July 1993 LER 93-006-01:on 930401,Train a Svc Water Inoperable Due to Corrosion Product Buildup Between Valve Stem & Packing Follower.Returned SW-V54 to Operable Status & TS 3.7.4 Action D Exited on 930402.W/930701 Ltr ML20045D6791993-06-21021 June 1993 LER 93-002-01:on 930107,determined Potential for Premature Opening of Containment Bldg Spray Sump Isolation Valves. Caused by Failure to Adequately Recognize Potential Sys Interactions.Affected Procedures Revised ML20045C5421993-06-18018 June 1993 LER 93-010-00:on 930522,SG Level Oscillations Occurred in One SG Resulting in SG Being Overfed & Causing high-high SG Water Level.Caused by Personnel Error.Power Reduced to Approx 2.5% & FW to SGs restored.W/930618 Ltr ML20045D3681993-06-18018 June 1993 LER 93-009-00:on 930520,manual Reactor Trip from 100% Power Initiated When MSIV Closed During Quarterly Testing, Resulting in Feedwater & Two Emergency Feedwater Isolations. Caused by Debris in Valves.Valves Replaced ML20045C5341993-06-16016 June 1993 LER 93-008-00:on 930518,identified That Failure of Air Supply to EDG Jacket Cooling Water Temperature Control Valves During Seismic Event Could Cause Overcooling of Edgs. Operability Determination Performed for EDGs.W/930616 Ltr ML20045B5181993-06-11011 June 1993 LER 93-007-00:on 930512,protective Devices Not Analyzed to Function During Environ Excursions Due to Unknown Cause Which Is Under Review.Operability Determination Was performed.W/930611 Ltr ML20024H1621991-05-23023 May 1991 LER 91-004-00:on 910401,steam Generator Indicated That Valve Was Not Opening Properly During Plant Restart.Caused by Differential Pressure Across Dash Plate.Dash Plate Machining Performed on Valves to Prevent Valve disk.W/910523 Ltr ML20044B2281990-07-12012 July 1990 LER 90-014-00:on 900612,discovered That Sample Pump for Steam Generator Blowdown Flash Tank Drain Radiation Monitor Not Running.Caused by Suspended Solids in Steam Generator Blowdown Sys.Solids Cleared from Flow switch.W/900712 Ltr ML20043B6741990-05-23023 May 1990 LER 90-008-01:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Air Cleanup Sys Incapable of Producing Negative Pressure.Latching Mechanism Repaired & Mods to Doors/Hardware planned.W/900523 Ltr ML20043B3551990-05-21021 May 1990 LER 90-013-00:on 900419,discovered That Containment Personnel Hatch Unsecured for Approx 28 H.Caused by Installation of Locking Plate Upside Down & Placing Lock Through Only 1 Eyelet.Instructions posted.W/900521 Ltr ML20042F5521990-05-0202 May 1990 LER 90-012-00:on 900402,transmitter Failed to Provide Pressure to Reactor Protection Sys Due to Closed Isolation Valve.Caused by Failure to Identify Valve in Procedures. Valves Manipulated to Correct positions.W/900502 Ltr ML20042E1781990-04-0606 April 1990 LER 90-006-01:on 900206,control Room Ventilation Sys Train a Radiation Monitor Went Into High Alarm Condition.Caused by Mechanical Binding of Check source.Geiger-Muller Tube Replaced & Monitor Returned to svc.W/900406 Ltr ML20042E1741990-04-0505 April 1990 LER 90-011-00:on 900306,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Failure of Geiger-Muller Tube.Monitor Removed from Svc & Tube replaced.W/900405 Ltr ML20012F5181990-04-0404 April 1990 LER 90-010-00:on 900305,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Moisture in Detector Housing.Air Intake Monitors Cleaned & Desiccant Placed in housing.W/900404 Ltr ML20012C2461990-03-12012 March 1990 LER 90-008-00:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Emergency Air Cleanup Sys Inoperable.Plant Cooldown Initiated,Latching Mechanism Repaired & Door Returned to svc.W/900312 Ltr ML20012C2481990-03-12012 March 1990 LER 90-007-00:on 900208,when Source Check Removed from Control room,RM-6506B Entered High Alarm Condition,Causing ESF Actuation of Emergency Air Cleanup Sys.Caused by Mechanical Binding.Check Source replaced.W/900312 Ltr ML20012B4491990-03-0808 March 1990 LER 90-006-00:on 900206,Train a Radiation Monitor Went Into High Alarm Condition,Resulting in Actuation of Control Room Emergency Air Cleanup & Filtration Subsystem.Caused by Mechanical Binding.Detector Tube remounted.W/900308 Ltr ML20011F4671990-02-22022 February 1990 LER 90-004-00:on 900123,wide-range Gas Monitor Process Flow Rate Value for Vent Radiation Monitor Discovered at Default Instead of Actual Value.Caused by Personnel Error.Process Flow Restored & Technician counseled.W/900222 Ltr ML20006E4591990-02-15015 February 1990 LER 90-003-00:on 900116,wide-range Gas Monitor Low Range Pump Found Inoperable.Caused by Failed Pump Diaphragm Weakened by High Flow Condition.Ruptured Pump Diaphragm Replaced & Pump Returned to Normal operations.W/900215 Ltr ML20006E1731990-02-0808 February 1990 LER 90-002-00:on 900109,discovered That Auxiliary Sample Pump Used to Satisfy Action Requirements of Tech Spec Was Not Operating.Caused by Dislodged Power Fuse.Pump Relocated & Caution Tape Installed to Protect pump.W/900208 Ltr ML20006E1801990-02-0808 February 1990 LER 90-001-00:on 900109,wide Range Gas Monitor Low Range Pump Found to Be Inoperable,Resulting in Noncompliance W/ Tech Specs.Caused by Regulator Isolation Valves Being Left in Open Position.Walkdown of Skids conducted.W/900208 Ltr ML20005E2461989-12-29029 December 1989 LER 89-014-00:on 891129,auxiliary Transformer Supply Breaker to Vital Bus E5 Tripped When Remote Manual Override Relay Energized.Caused by Procedure Inadequacies in Procedure 0S1048.01.Procedure revised.W/891229 Ltr ML20011D4381989-12-19019 December 1989 LER 89-011-01:on 890905,three Unsealed Piping Penetrations in Condensate Storage Tank Encl Identified.Caused by Failure to Transfer Sealing Requirements Into Detail Drawings.Penetrations sealed.W/891219 Ltr ML19332C8511989-11-22022 November 1989 LER 89-013-00:on 891023,discovered That Monitor Used to Satisfy Requirements of Tech Spec 3.3.3.1,Action 27 Had Been Unplugged.Caused by Personnel Error.Individual Counseled & Meeting Held W/Health Physics technicians.W/891122 Ltr ML19325F3301989-11-10010 November 1989 LER 89-012-00:on 891011,one of Two Suction Valves on RHR Train a Pump Closed,Causing Loss of All RHR Cooling Capability.Caused by Procedure Inadequacies.Procedure Revised to Specify Sequence of restoration.W/891110 Ltr ML19325C7891989-10-0505 October 1989 LER 89-011-00:on 890905,determined That Three Piping Penetrations in Condensate Storage Tank Encl Not Sealed.Root Cause Under Investigation.Penetrations Sealed & Tech Specs Surveillance Log revised.W/891005 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H2841999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Seabrook Station. with ML20212D1461999-09-17017 September 1999 SER Accepting Request to Use Proposed Alternative to Certain Weld Repair Requirements in ASME Boiling & Pressure Vessel Code ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20212B8671999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Seabrook Station. with ML20210Q7581999-08-11011 August 1999 SER Approving Proposed Merger of CES & Bec,Which Will Create New Parent Company of Canal ML20210R9781999-08-0606 August 1999 ISI Exam Rept of Seabrook Station, for RFO 6,period 3 ML20210J8681999-08-0303 August 1999 SER Approving License Transfer from Montaup Electric Co to Little Bay Power Corp & Approval of Conforming Amend for Seabrook Station Unit 1 ML20210R6001999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Seabrook Station, Unit 1.With ML20210H1151999-06-30030 June 1999 Naesc Semi-Annual Fitness-for-Duty Rept for 990101-0630 ML20209H1371999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Seabrook Station, Unit 1.With ML20195G5391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Seabrook Station, Unit 1.With ML20195C0491999-05-25025 May 1999 Offshore Intake Seal Deterrent Barrier Design ML20206E4761999-04-30030 April 1999 LER 99-S01-00:on 990408,contractor Employee Was Granted Temporary Unescorted Access to Seabrook Station Protected Area.Caused by Failure of Contractor Employee to Provide Accurate Info.Individual Access Revoked.With ML20206N1751999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Seabrook Station, Unit 1.With ML20196L2081999-04-19019 April 1999 Rev 01-07-00 to RE-21, Cycle 7 Colr ML20205K5441999-03-31031 March 1999 Decommissioning Update ML20205L8141999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Seabrook Station. with ML20205C1981999-03-24024 March 1999 Safety Evaluation Concluding That Proposed Relief Request IR-8,Rev 1,provides Acceptable Alternative to ASME Code Requirements.Recommends Authorization of Proposed Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20207F4941999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Seabrook Station. with ML20199E6731998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Seabrook Station, Unit 1.With ML20198P1831998-12-31031 December 1998 LER 98-S01-00:on 981214,incomplete pre-employment Screening Records Was Noted.Caused by Failure of Contractor Employee to Provide Accurate Info.Subject Contractor Employees Employment Was Terminated.With ML20202E8241998-12-31031 December 1998 Naesc Semi-Annual Fitness-for-Duty Rept for 980701-981231 ML20196F5741998-12-0202 December 1998 Safety Evaluation Concluding That Licensee Has Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Seabrook ML20198B8661998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Seabrook Station, Unit 1.With ML20195D0311998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Seabrook Station, Unit 1.With ML20154H5291998-10-0808 October 1998 Special Rept:On 980928,meteorological Monitoring Instrumentation Channel Inoperable for Period Greater than 7 Days.Caused by Vendor to Follow Std Industry Practice for Calibr of Instrumentation.Instruments Installed ML20154M8421998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Seabrook Generating Station,Unit 1.With ML20151V5951998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Seabrook Station, Unit 1.With ML20237B4501998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Seabrook Station ML20236R1781998-06-30030 June 1998 Naesc Semi-Annual Fitness-for-Duty Rept for 980101-0630 ML20236M3591998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Seabrook Station, Unit 1 ML20237A4871998-06-0303 June 1998 North Atlantic Seabrook Station 1998 Exercise on 980603 ML20248M2951998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Seabrook Station, Unit 1 ML20247G2641998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Seabrook Station ML20247H3171998-04-27027 April 1998 Rev 1 to Seabrook Station SGs B & C Isi,May/June 1997 ML20216F8891998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Seabrook Station 05000443/LER-1998-002, Re Potential Safety Injection Pump Runout Conditions Identified on 980113.LER 98-002-00 Retracted1998-03-20020 March 1998 Re Potential Safety Injection Pump Runout Conditions Identified on 980113.LER 98-002-00 Retracted ML20216H9211998-03-13013 March 1998 Fitness for Duty Program Performance Data Personnel Subject to 10CFR26 ML20248L2811998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Seabrook Station, Unit 1 ML20197A7531998-02-27027 February 1998 Safety Evaluation Accepting License Request for Relief from ASME Code,Section IX Requirements Re Inservice Insp of RHR Heat Exchanger Nozzle Welds & Reactor Vessel Closure Head Nuts ML20202G3701998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Seabrook Station ML20198G0271997-12-31031 December 1997 Commonwealth Energy Sys 1997 Annual Rept ML20248L7711997-12-31031 December 1997 Western Massachusetts Electric 1997 Annual Rept. Supporting Info,Encl ML20198G1021997-12-31031 December 1997 Baycorp Holdings 1997 Annual Rept ML20198N7021997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Seabrook Station, Unit 1 ML20198G0351997-12-31031 December 1997 Eastern Edison Co 1997 Annual Rept ML20198G0681997-12-31031 December 1997 Taunton Municipal Lighting Plant 1997 Annual Rept ML20248L7671997-12-31031 December 1997 North Atlantic 1997 Annual Rept ML20198F9511997-12-31031 December 1997 United Illuminating Co 1997 Annual Rept ML20236M9561997-12-31031 December 1997 Amended Public Service of New Hampshire 1997 Annual Rept 1999-09-30
[Table view] |
Text
- - - .
NRC FORM 366 U.S. NUCLEAR REGULATOR 7 LOMMISSION APPROVED BV OMB NO. 3150-0104
, (5-92) . EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY
" t "
LICENSEE EVENT REPORT (LER) g T 159. INF0R"^r0RWARD MM N S R BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714),
(See reverse for required number of digits / characters for each U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555 0001, AND TO THE block) PAPERWORK REDUCTION PROJECT (3150-0104),
OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
F ACILIIY NAME (1) DOCKET NUMBER (2) PAGE (3)
Seabrook Station 05000443 1 OF 4 IIILE (4)
Potential Premature Opening of CBS Sump Isolation Valves EVENT DAll (5) LER NUMBER (6) REPORT DATE (7) OTHER F ACILITILS INVOLVED (8)
SE AL R N MONTH DAY YEAR YEAR MONTH DAY YEAR 0500
^ "#"' U" 01 07 93 93 --002 -- 01 06 21 93 050 ()
OPERATING y IHIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMEN1S OF 10 CFR %: (Check one or more)
MODE (9) 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b)
POWER 20.405(a)(1)(1) 50.36(c)(1) X 50.73(a)(2)(v) 73.71(c) 100 LEVEL (10) 20.405(a)(1)(li) 50.36(c)(2) 50.73(a)(2)(vil) OTHER 20.405(a)(1)(iii) X 50.73(a)(2)(i) 50.73(a)(2)(viii) (Specify in Ab$ trac ow 20.405(a)(1)(iv) X 50.73(a)(2)(11) 50.73(a)(2)(viii) nl 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) NRC form 366A)
LICENSt[ CONTACI FOR THIS LFR (12)
NAME TELEPHONE NUMBER (Include Area Mr. James M. Peschel, Regulatory Compliance Manager Code)
(603)474-9521 ext. 3772 COMPLLIE ONE LINE F OR EACH COMPONENT F AIL URE DESCRIBED IN THIS RE PORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER R 0 E CAUSE SYSTEM COMPONENT MANUFACTURER R 0 E SUPPLEMENI AL REPORT EXPLCIED (14) EXPECTED MONTH DAY YEAR YES SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE). X NO DATE (15)
ABSlRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On January 7, 1993, North Atlantic Operations personnel questioned whether performance of surveillance testing on the Refueling Water Storage Tank (RWST) [BP] level instrumentation, which tripped two level channels in Mode 1, was consistent with Technical Specifications. Evaluation has determined that the RWST level instruments were inoperable during performance of the surveillance testing, in addition, it has been determined that if a Safety Injection (SI) [JE] signal had occurred while the RWST level low-low bistables were tripped during surveillance testing, the Containment Building Spray (CBS) [BE] recirculation sump isolation valves would open earlier than previously analyzed. At that time it was postulated that the premature opening of the valves during a steam line break could potentially cause air binding of the CBS and Residual Heat Removal (RHR) [BP]
pumps. Therefore, the event was reported to the NRC on January 8, 1993 pursuant to 10CFR50.72(b)(2)(iii).
Engineering evaluation has determined that a large loss of Coolant Accident (LOCA) occurring while two RWST level low-low btstables were in the tripped condition could have resulted in containment temperatures and pressures, and peak cladding temperatures which may not have been bounded by the current analyses.
The root cause of the event is f ailure to adequately recognize potential system interactions during abnormal configurations occurring during surveillance testing.
Corrective action was to revise the af fected procedures to eliminate placing two RWST level channels in the tripped condition. In addition, North Atlantic will review surveillance procedures which provide a partial actuation of an ESF system to determine any potential safety implications. This event has been reviewed and discussed with the operating crews and other select North Atlantic personnel.
There were no adverse safety consequences as a result of this event.
9306290292 930621 PDR ADOCK 05000443 s PDR
NRC EORM 366A U.S. NUCLEAR REGULA10RY COMMISSION APPROVED BY OMB NO. 3150-0104
, (5-92) . EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST:
50.0 HRS. FORWARD COMMENTS REGARDING LICENSEE EVENT REPORT (LER) BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S.
TEXT CONTINUATION NUCLEAR REGULATORY COMMISSION WASHINGTON, DC 20555-0001 AND TO Tile PAPERWORK REDUCT]DN PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKE1 NUMBER LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVIS10 Seabrook Station "
05000443 93 01 2 OF 4
-- 0 0 2 --
1 Ext (lf more space is required, use addItlonaI coples of NRC form 366A) (17)
On January 7,1993, North Atlantic Operations personnel questioned whether performance of surveillance testing on the Refueling Water Storage Tank (RWST) [BP] level instrumentation, which tripped two level channels in Mode 1, was consistent with Technical Specifications. Evaluation has determined that the RWST level instruments were inoperable during performance of the surveillance testing. In addition, it was determined that if a Safety injection (SI) [JE] signal had occurred while the RWST level low-low bistables were tripped during surveillance testing, the Containment Building Spray (CBS) [BE] recirculation sump isolation valves woul! open earlier than previously analyzed. It was postulated that the premature opening of the valves during a steam line break could potentially cause air binding of the CBS and Residual Heat Removal (RHR) [BP] pumps. Therefore, the event was reported to the NRC on January 8,1993 pursuant to 10CFR50.72(b)(2)(iii). This event is now being reported pursuant to 10CFR50.73(a)(2)(i), (ii), and (v).
Backcround Information At Seabrook Station, the Emergency Core Cooling System (ECCS) takes a suction from either the RWST or the CBS sump. The RWST is utilized as the borated water supply during the injection phase of an accident.
When the supply of borated water in the RWST has been injected a transfer to the CBS sump is initiated.
The transfer is accomplished with both automatic and manual actions.
The RWST level instrumentation has four loops which provide an input into the two out of four logic required to generate a RWST level low-low signal. When actuated, this signal in combination with an SI signal will automatically open the Train A and B CBS sump isolation valves.
Technical Specification Table 4.3-2 specifies that a Channel Calibration be performed on the RWST level low-low coincident with a SI logie at least once per eighteen months. This surveillance also verifies that when two out of four RWST level channels are at their low-low level setpoint that a RWST level low-low signal is generated. As previously stated, this signal in combination with an SI signal will automatically open both CBS sump isolation valves.
Event Description On January 7,1993, with the reactor at 100% power, a Channel Calibration was performed on the RWST level circuitry. While performing Surveillance Procedure IX1622.231, "L-930 Refueling Water Storage Tank Level Calibration", the Unit Shift Supervisor questioned the presence of the RWST level low-low alarm in Mode 1. This indicated that two RWST level channels were in a tripped condition. Instrumentation and Control Department supervision were contacted and the RWST level transmitters were returned to service from the tripped condition. It was later determined that even though the RWST level instruments were in their required safeguards condition the level channels were inoperable because they would permit the CBS sump suction valves to open at a level other than the RWST low-low level setpoint.
During a preliminary evaluation of the condition it was postulated that if an SI actuation due to a steam line break occurred simultaneously with two out of four RWST level channels being tripped that the Train A and Train B CBS sump isolation valves would automatically open with the potential to air bind the CBS and RHR pumps. This was determined to be a condition which alone may have prevented the fulfillment of the safety
NRC E0RM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (5-92) . EXP!RES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST:
50.0 HRS. FORWARD COMMENTS REGARDING LICENSEE EVENT REPORT (LER) BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S.
TEXT CONTINUATION NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER LER NUMBER (6) PAGE (3)
YEAR
, SEQUENllAL REVIS10 Seabrook Station "
05000443 93 01 3 OF 4
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TEXT (If more space is required, use additional copies of NRC form 366A) (17) function of structures or systems that are needed to remove residual heat and to mitigate the consequences of an accident. Therefore, a non-emergency four hour report was made to the NRC pursuant to 10CFR50.72(b)(2)(iii).
Safety Conscouences There were no adverse safety consequences as a result of the event.
Adverse safety consequences could have resulted if a large LOCA occurred concurrent with the surveillance testing which placed two RWST level channels in trip. The potential safety implications of this scenario are addressed below.
Potential Safety Imolications Further evaluation determined that air binding of these pumps would not occur during a postulated main steam line break event as the pumps would continue to take suction from the RWST due to the elevation head from the RWST exceeding the containment pressure during the relatively short duration of this event.
Two scenarios were evaluated ta determine the effect of a postulated LOCA occuring while the RWST level channels were tripped. The first scenario assumes that the ECCS and spray flows collect in the rceirculation sump. The second scenario considers the Seabrook Station design which traps 17,000 cubic feet of fluid.
This fluid is not available to the recirculation sump.
Engineering evaluation has determined that approximately eight minutes into a postulated large LOCA, specifically a double ended cold leg guillotine break, occurring with two RWST level channels tripped, the pressure from the CBS sump boosted by containment pressure would exceed the pressure from the RWST.
This would result in the CBS pumps taking suction from the CBS sump prior to the normal time for transfer to the recirculation mode of emergency core cooling. The early suction from the CIlS sump would result in an elevated containment spray temperature early in the accident sequence and reduced spray effectiveness for pressure control and heat removal. This could have resulted in containment temperatures and pressures, and peak cladding temperatures which may not have been bounded by the current analyses.
In addition, the premature transfer to the CBS sump would also result in the RHR pumps taking suction from the CBS sump earlier than analyzed. This would increase the temperature of the low head injection fluid.
The consequences of the increase fluid temperature is a change to the reactor vessel reflood rate and a decrease of the decay heat removal effectiveness. The ultimate effect of the increased injection fluid temperature could be an increase in peak clad temperature.
If the ECCS and containment spray flows are assumed to initially fill the volumes unavailable to the recirculation sumps, then in a postulated double ended pump suction guillotine break the containment pressure alone would exceed the RWST head at the RHR suction check valve approximately 6 minutes into l
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! NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION' APPROVED BY OM8 NO. 3150-0104 l '
( 5*-92 ) . EXPIRES 5/31/95 1 .
ESTIMATED BURDEN PER RESPGCSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST:
50.0 HRS. FORWARD COMMENTS REGARDING L'ICENSEE EVEN"' REPORT (LER) BURDEN ESTIMATE TO THE INFORMATION AND TEXT CONTINUATION RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S.
NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE- 0F MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. ;
FACILITY NAME (1) DOCKET NUMBER LER NUMBER (6) PAGE (3) l YEAR SEQUENTIAL REVIS10 ;
Seabrook Station 05000443 " - 4 OF 4 93 --
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TEK1 (11 more space is required, use additional copies of NHC Form 366A) (17) the event. This could result in inadequate sump levels for the operation of the CBS and RHR pumps. j Suction vortexing or air binding of the pumps could occur, potentially resulting in a loss of CBS capability i and RHR system operation, which could prevent the establishment of long term core cooling. In this scenario, the potential exists for containment bypass with significant offsite doses.
The surveillance which trips the RWST level channels has been performed five times in MODE 1.
Root Cause The root cause of the event is failure to adequately recognize potential system interactions resulting from an abnormal configuration during surveillance testing. The event represents a situation where the consequences of placing individual components in their safeguards configuration were not adequately reviewed in terms of the integrated system performance under postulated accident conditions.
Corrective Action
- 1. Station Procedures have been revised to climinate placing the plant in a configuration with two out of four RWST level channels in the tripped condition in Modes 1-4
- 2. North Atlantic will review surveillance procedures which provide a partial ESF actuation, similar to IX1622.231, to determine if any similiar potential safety implications exist. The review will include partial ESF actuations and integrated system operation under normal and accident conditions.
- 3. North Atlantic Operations management has reviewed this event, to include the placement of components in their safeguards configuration, with the operating crews.
- 4. Select personnel from Licensing, Operations, Technical Support, and Engineering have participated in a Station Operating Experience Review seminar.
Previous Occurrences This is the first event of this type at Seabrook Station.
At the time of the event the plant was in Mode 1 at 100% power.
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