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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B8951993-07-30030 July 1993 LER 93-008-01:on 930518,determined That Control Air Not Analyzed to Function During Seismic Event Due to Lack of Understanding Significance of Control Air Availability for Long Term DG Operation.Ufsar Will Be Updated ML20046B8961993-07-30030 July 1993 LER 93-011-00:on 921219,930209 & 0415,SW Pumps SW-P-41B, SW-P-41B & SW-P-41D Declared Inoperable,Respectively Due High Vibration.Caused by Excessive Abrasive Particles in Ocean Water.Pumps replaced.W/930730 Ltr ML20045G6641993-07-0101 July 1993 LER 93-006-01:on 930401,Train a Svc Water Inoperable Due to Corrosion Product Buildup Between Valve Stem & Packing Follower.Returned SW-V54 to Operable Status & TS 3.7.4 Action D Exited on 930402.W/930701 Ltr ML20045D6791993-06-21021 June 1993 LER 93-002-01:on 930107,determined Potential for Premature Opening of Containment Bldg Spray Sump Isolation Valves. Caused by Failure to Adequately Recognize Potential Sys Interactions.Affected Procedures Revised ML20045C5421993-06-18018 June 1993 LER 93-010-00:on 930522,SG Level Oscillations Occurred in One SG Resulting in SG Being Overfed & Causing high-high SG Water Level.Caused by Personnel Error.Power Reduced to Approx 2.5% & FW to SGs restored.W/930618 Ltr ML20045D3681993-06-18018 June 1993 LER 93-009-00:on 930520,manual Reactor Trip from 100% Power Initiated When MSIV Closed During Quarterly Testing, Resulting in Feedwater & Two Emergency Feedwater Isolations. Caused by Debris in Valves.Valves Replaced ML20045C5341993-06-16016 June 1993 LER 93-008-00:on 930518,identified That Failure of Air Supply to EDG Jacket Cooling Water Temperature Control Valves During Seismic Event Could Cause Overcooling of Edgs. Operability Determination Performed for EDGs.W/930616 Ltr ML20045B5181993-06-11011 June 1993 LER 93-007-00:on 930512,protective Devices Not Analyzed to Function During Environ Excursions Due to Unknown Cause Which Is Under Review.Operability Determination Was performed.W/930611 Ltr ML20024H1621991-05-23023 May 1991 LER 91-004-00:on 910401,steam Generator Indicated That Valve Was Not Opening Properly During Plant Restart.Caused by Differential Pressure Across Dash Plate.Dash Plate Machining Performed on Valves to Prevent Valve disk.W/910523 Ltr ML20044B2281990-07-12012 July 1990 LER 90-014-00:on 900612,discovered That Sample Pump for Steam Generator Blowdown Flash Tank Drain Radiation Monitor Not Running.Caused by Suspended Solids in Steam Generator Blowdown Sys.Solids Cleared from Flow switch.W/900712 Ltr ML20043B6741990-05-23023 May 1990 LER 90-008-01:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Air Cleanup Sys Incapable of Producing Negative Pressure.Latching Mechanism Repaired & Mods to Doors/Hardware planned.W/900523 Ltr ML20043B3551990-05-21021 May 1990 LER 90-013-00:on 900419,discovered That Containment Personnel Hatch Unsecured for Approx 28 H.Caused by Installation of Locking Plate Upside Down & Placing Lock Through Only 1 Eyelet.Instructions posted.W/900521 Ltr ML20042F5521990-05-0202 May 1990 LER 90-012-00:on 900402,transmitter Failed to Provide Pressure to Reactor Protection Sys Due to Closed Isolation Valve.Caused by Failure to Identify Valve in Procedures. Valves Manipulated to Correct positions.W/900502 Ltr ML20042E1781990-04-0606 April 1990 LER 90-006-01:on 900206,control Room Ventilation Sys Train a Radiation Monitor Went Into High Alarm Condition.Caused by Mechanical Binding of Check source.Geiger-Muller Tube Replaced & Monitor Returned to svc.W/900406 Ltr ML20042E1741990-04-0505 April 1990 LER 90-011-00:on 900306,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Failure of Geiger-Muller Tube.Monitor Removed from Svc & Tube replaced.W/900405 Ltr ML20012F5181990-04-0404 April 1990 LER 90-010-00:on 900305,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Moisture in Detector Housing.Air Intake Monitors Cleaned & Desiccant Placed in housing.W/900404 Ltr ML20012C2461990-03-12012 March 1990 LER 90-008-00:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Emergency Air Cleanup Sys Inoperable.Plant Cooldown Initiated,Latching Mechanism Repaired & Door Returned to svc.W/900312 Ltr ML20012C2481990-03-12012 March 1990 LER 90-007-00:on 900208,when Source Check Removed from Control room,RM-6506B Entered High Alarm Condition,Causing ESF Actuation of Emergency Air Cleanup Sys.Caused by Mechanical Binding.Check Source replaced.W/900312 Ltr ML20012B4491990-03-0808 March 1990 LER 90-006-00:on 900206,Train a Radiation Monitor Went Into High Alarm Condition,Resulting in Actuation of Control Room Emergency Air Cleanup & Filtration Subsystem.Caused by Mechanical Binding.Detector Tube remounted.W/900308 Ltr ML20011F4671990-02-22022 February 1990 LER 90-004-00:on 900123,wide-range Gas Monitor Process Flow Rate Value for Vent Radiation Monitor Discovered at Default Instead of Actual Value.Caused by Personnel Error.Process Flow Restored & Technician counseled.W/900222 Ltr ML20006E4591990-02-15015 February 1990 LER 90-003-00:on 900116,wide-range Gas Monitor Low Range Pump Found Inoperable.Caused by Failed Pump Diaphragm Weakened by High Flow Condition.Ruptured Pump Diaphragm Replaced & Pump Returned to Normal operations.W/900215 Ltr ML20006E1731990-02-0808 February 1990 LER 90-002-00:on 900109,discovered That Auxiliary Sample Pump Used to Satisfy Action Requirements of Tech Spec Was Not Operating.Caused by Dislodged Power Fuse.Pump Relocated & Caution Tape Installed to Protect pump.W/900208 Ltr ML20006E1801990-02-0808 February 1990 LER 90-001-00:on 900109,wide Range Gas Monitor Low Range Pump Found to Be Inoperable,Resulting in Noncompliance W/ Tech Specs.Caused by Regulator Isolation Valves Being Left in Open Position.Walkdown of Skids conducted.W/900208 Ltr ML20005E2461989-12-29029 December 1989 LER 89-014-00:on 891129,auxiliary Transformer Supply Breaker to Vital Bus E5 Tripped When Remote Manual Override Relay Energized.Caused by Procedure Inadequacies in Procedure 0S1048.01.Procedure revised.W/891229 Ltr ML20011D4381989-12-19019 December 1989 LER 89-011-01:on 890905,three Unsealed Piping Penetrations in Condensate Storage Tank Encl Identified.Caused by Failure to Transfer Sealing Requirements Into Detail Drawings.Penetrations sealed.W/891219 Ltr ML19332C8511989-11-22022 November 1989 LER 89-013-00:on 891023,discovered That Monitor Used to Satisfy Requirements of Tech Spec 3.3.3.1,Action 27 Had Been Unplugged.Caused by Personnel Error.Individual Counseled & Meeting Held W/Health Physics technicians.W/891122 Ltr ML19325F3301989-11-10010 November 1989 LER 89-012-00:on 891011,one of Two Suction Valves on RHR Train a Pump Closed,Causing Loss of All RHR Cooling Capability.Caused by Procedure Inadequacies.Procedure Revised to Specify Sequence of restoration.W/891110 Ltr ML19325C7891989-10-0505 October 1989 LER 89-011-00:on 890905,determined That Three Piping Penetrations in Condensate Storage Tank Encl Not Sealed.Root Cause Under Investigation.Penetrations Sealed & Tech Specs Surveillance Log revised.W/891005 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B8951993-07-30030 July 1993 LER 93-008-01:on 930518,determined That Control Air Not Analyzed to Function During Seismic Event Due to Lack of Understanding Significance of Control Air Availability for Long Term DG Operation.Ufsar Will Be Updated ML20046B8961993-07-30030 July 1993 LER 93-011-00:on 921219,930209 & 0415,SW Pumps SW-P-41B, SW-P-41B & SW-P-41D Declared Inoperable,Respectively Due High Vibration.Caused by Excessive Abrasive Particles in Ocean Water.Pumps replaced.W/930730 Ltr ML20045G6641993-07-0101 July 1993 LER 93-006-01:on 930401,Train a Svc Water Inoperable Due to Corrosion Product Buildup Between Valve Stem & Packing Follower.Returned SW-V54 to Operable Status & TS 3.7.4 Action D Exited on 930402.W/930701 Ltr ML20045D6791993-06-21021 June 1993 LER 93-002-01:on 930107,determined Potential for Premature Opening of Containment Bldg Spray Sump Isolation Valves. Caused by Failure to Adequately Recognize Potential Sys Interactions.Affected Procedures Revised ML20045C5421993-06-18018 June 1993 LER 93-010-00:on 930522,SG Level Oscillations Occurred in One SG Resulting in SG Being Overfed & Causing high-high SG Water Level.Caused by Personnel Error.Power Reduced to Approx 2.5% & FW to SGs restored.W/930618 Ltr ML20045D3681993-06-18018 June 1993 LER 93-009-00:on 930520,manual Reactor Trip from 100% Power Initiated When MSIV Closed During Quarterly Testing, Resulting in Feedwater & Two Emergency Feedwater Isolations. Caused by Debris in Valves.Valves Replaced ML20045C5341993-06-16016 June 1993 LER 93-008-00:on 930518,identified That Failure of Air Supply to EDG Jacket Cooling Water Temperature Control Valves During Seismic Event Could Cause Overcooling of Edgs. Operability Determination Performed for EDGs.W/930616 Ltr ML20045B5181993-06-11011 June 1993 LER 93-007-00:on 930512,protective Devices Not Analyzed to Function During Environ Excursions Due to Unknown Cause Which Is Under Review.Operability Determination Was performed.W/930611 Ltr ML20024H1621991-05-23023 May 1991 LER 91-004-00:on 910401,steam Generator Indicated That Valve Was Not Opening Properly During Plant Restart.Caused by Differential Pressure Across Dash Plate.Dash Plate Machining Performed on Valves to Prevent Valve disk.W/910523 Ltr ML20044B2281990-07-12012 July 1990 LER 90-014-00:on 900612,discovered That Sample Pump for Steam Generator Blowdown Flash Tank Drain Radiation Monitor Not Running.Caused by Suspended Solids in Steam Generator Blowdown Sys.Solids Cleared from Flow switch.W/900712 Ltr ML20043B6741990-05-23023 May 1990 LER 90-008-01:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Air Cleanup Sys Incapable of Producing Negative Pressure.Latching Mechanism Repaired & Mods to Doors/Hardware planned.W/900523 Ltr ML20043B3551990-05-21021 May 1990 LER 90-013-00:on 900419,discovered That Containment Personnel Hatch Unsecured for Approx 28 H.Caused by Installation of Locking Plate Upside Down & Placing Lock Through Only 1 Eyelet.Instructions posted.W/900521 Ltr ML20042F5521990-05-0202 May 1990 LER 90-012-00:on 900402,transmitter Failed to Provide Pressure to Reactor Protection Sys Due to Closed Isolation Valve.Caused by Failure to Identify Valve in Procedures. Valves Manipulated to Correct positions.W/900502 Ltr ML20042E1781990-04-0606 April 1990 LER 90-006-01:on 900206,control Room Ventilation Sys Train a Radiation Monitor Went Into High Alarm Condition.Caused by Mechanical Binding of Check source.Geiger-Muller Tube Replaced & Monitor Returned to svc.W/900406 Ltr ML20042E1741990-04-0505 April 1990 LER 90-011-00:on 900306,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Failure of Geiger-Muller Tube.Monitor Removed from Svc & Tube replaced.W/900405 Ltr ML20012F5181990-04-0404 April 1990 LER 90-010-00:on 900305,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Moisture in Detector Housing.Air Intake Monitors Cleaned & Desiccant Placed in housing.W/900404 Ltr ML20012C2461990-03-12012 March 1990 LER 90-008-00:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Emergency Air Cleanup Sys Inoperable.Plant Cooldown Initiated,Latching Mechanism Repaired & Door Returned to svc.W/900312 Ltr ML20012C2481990-03-12012 March 1990 LER 90-007-00:on 900208,when Source Check Removed from Control room,RM-6506B Entered High Alarm Condition,Causing ESF Actuation of Emergency Air Cleanup Sys.Caused by Mechanical Binding.Check Source replaced.W/900312 Ltr ML20012B4491990-03-0808 March 1990 LER 90-006-00:on 900206,Train a Radiation Monitor Went Into High Alarm Condition,Resulting in Actuation of Control Room Emergency Air Cleanup & Filtration Subsystem.Caused by Mechanical Binding.Detector Tube remounted.W/900308 Ltr ML20011F4671990-02-22022 February 1990 LER 90-004-00:on 900123,wide-range Gas Monitor Process Flow Rate Value for Vent Radiation Monitor Discovered at Default Instead of Actual Value.Caused by Personnel Error.Process Flow Restored & Technician counseled.W/900222 Ltr ML20006E4591990-02-15015 February 1990 LER 90-003-00:on 900116,wide-range Gas Monitor Low Range Pump Found Inoperable.Caused by Failed Pump Diaphragm Weakened by High Flow Condition.Ruptured Pump Diaphragm Replaced & Pump Returned to Normal operations.W/900215 Ltr ML20006E1731990-02-0808 February 1990 LER 90-002-00:on 900109,discovered That Auxiliary Sample Pump Used to Satisfy Action Requirements of Tech Spec Was Not Operating.Caused by Dislodged Power Fuse.Pump Relocated & Caution Tape Installed to Protect pump.W/900208 Ltr ML20006E1801990-02-0808 February 1990 LER 90-001-00:on 900109,wide Range Gas Monitor Low Range Pump Found to Be Inoperable,Resulting in Noncompliance W/ Tech Specs.Caused by Regulator Isolation Valves Being Left in Open Position.Walkdown of Skids conducted.W/900208 Ltr ML20005E2461989-12-29029 December 1989 LER 89-014-00:on 891129,auxiliary Transformer Supply Breaker to Vital Bus E5 Tripped When Remote Manual Override Relay Energized.Caused by Procedure Inadequacies in Procedure 0S1048.01.Procedure revised.W/891229 Ltr ML20011D4381989-12-19019 December 1989 LER 89-011-01:on 890905,three Unsealed Piping Penetrations in Condensate Storage Tank Encl Identified.Caused by Failure to Transfer Sealing Requirements Into Detail Drawings.Penetrations sealed.W/891219 Ltr ML19332C8511989-11-22022 November 1989 LER 89-013-00:on 891023,discovered That Monitor Used to Satisfy Requirements of Tech Spec 3.3.3.1,Action 27 Had Been Unplugged.Caused by Personnel Error.Individual Counseled & Meeting Held W/Health Physics technicians.W/891122 Ltr ML19325F3301989-11-10010 November 1989 LER 89-012-00:on 891011,one of Two Suction Valves on RHR Train a Pump Closed,Causing Loss of All RHR Cooling Capability.Caused by Procedure Inadequacies.Procedure Revised to Specify Sequence of restoration.W/891110 Ltr ML19325C7891989-10-0505 October 1989 LER 89-011-00:on 890905,determined That Three Piping Penetrations in Condensate Storage Tank Encl Not Sealed.Root Cause Under Investigation.Penetrations Sealed & Tech Specs Surveillance Log revised.W/891005 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H2841999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Seabrook Station. with ML20212D1461999-09-17017 September 1999 SER Accepting Request to Use Proposed Alternative to Certain Weld Repair Requirements in ASME Boiling & Pressure Vessel Code ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20212B8671999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Seabrook Station. with ML20210Q7581999-08-11011 August 1999 SER Approving Proposed Merger of CES & Bec,Which Will Create New Parent Company of Canal ML20210R9781999-08-0606 August 1999 ISI Exam Rept of Seabrook Station, for RFO 6,period 3 ML20210J8681999-08-0303 August 1999 SER Approving License Transfer from Montaup Electric Co to Little Bay Power Corp & Approval of Conforming Amend for Seabrook Station Unit 1 ML20210R6001999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Seabrook Station, Unit 1.With ML20210H1151999-06-30030 June 1999 Naesc Semi-Annual Fitness-for-Duty Rept for 990101-0630 ML20209H1371999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Seabrook Station, Unit 1.With ML20195G5391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Seabrook Station, Unit 1.With ML20195C0491999-05-25025 May 1999 Offshore Intake Seal Deterrent Barrier Design ML20206E4761999-04-30030 April 1999 LER 99-S01-00:on 990408,contractor Employee Was Granted Temporary Unescorted Access to Seabrook Station Protected Area.Caused by Failure of Contractor Employee to Provide Accurate Info.Individual Access Revoked.With ML20206N1751999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Seabrook Station, Unit 1.With ML20196L2081999-04-19019 April 1999 Rev 01-07-00 to RE-21, Cycle 7 Colr ML20205K5441999-03-31031 March 1999 Decommissioning Update ML20205L8141999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Seabrook Station. with ML20205C1981999-03-24024 March 1999 Safety Evaluation Concluding That Proposed Relief Request IR-8,Rev 1,provides Acceptable Alternative to ASME Code Requirements.Recommends Authorization of Proposed Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20207F4941999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Seabrook Station. with ML20199E6731998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Seabrook Station, Unit 1.With ML20198P1831998-12-31031 December 1998 LER 98-S01-00:on 981214,incomplete pre-employment Screening Records Was Noted.Caused by Failure of Contractor Employee to Provide Accurate Info.Subject Contractor Employees Employment Was Terminated.With ML20202E8241998-12-31031 December 1998 Naesc Semi-Annual Fitness-for-Duty Rept for 980701-981231 ML20196F5741998-12-0202 December 1998 Safety Evaluation Concluding That Licensee Has Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Seabrook ML20198B8661998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Seabrook Station, Unit 1.With ML20195D0311998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Seabrook Station, Unit 1.With ML20154H5291998-10-0808 October 1998 Special Rept:On 980928,meteorological Monitoring Instrumentation Channel Inoperable for Period Greater than 7 Days.Caused by Vendor to Follow Std Industry Practice for Calibr of Instrumentation.Instruments Installed ML20154M8421998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Seabrook Generating Station,Unit 1.With ML20151V5951998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Seabrook Station, Unit 1.With ML20237B4501998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Seabrook Station ML20236R1781998-06-30030 June 1998 Naesc Semi-Annual Fitness-for-Duty Rept for 980101-0630 ML20236M3591998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Seabrook Station, Unit 1 ML20237A4871998-06-0303 June 1998 North Atlantic Seabrook Station 1998 Exercise on 980603 ML20248M2951998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Seabrook Station, Unit 1 ML20247G2641998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Seabrook Station ML20247H3171998-04-27027 April 1998 Rev 1 to Seabrook Station SGs B & C Isi,May/June 1997 ML20216F8891998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Seabrook Station 05000443/LER-1998-002, Re Potential Safety Injection Pump Runout Conditions Identified on 980113.LER 98-002-00 Retracted1998-03-20020 March 1998 Re Potential Safety Injection Pump Runout Conditions Identified on 980113.LER 98-002-00 Retracted ML20216H9211998-03-13013 March 1998 Fitness for Duty Program Performance Data Personnel Subject to 10CFR26 ML20248L2811998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Seabrook Station, Unit 1 ML20197A7531998-02-27027 February 1998 Safety Evaluation Accepting License Request for Relief from ASME Code,Section IX Requirements Re Inservice Insp of RHR Heat Exchanger Nozzle Welds & Reactor Vessel Closure Head Nuts ML20202G3701998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Seabrook Station ML20198G0271997-12-31031 December 1997 Commonwealth Energy Sys 1997 Annual Rept ML20248L7711997-12-31031 December 1997 Western Massachusetts Electric 1997 Annual Rept. Supporting Info,Encl ML20198G1021997-12-31031 December 1997 Baycorp Holdings 1997 Annual Rept ML20198N7021997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Seabrook Station, Unit 1 ML20198G0351997-12-31031 December 1997 Eastern Edison Co 1997 Annual Rept ML20198G0681997-12-31031 December 1997 Taunton Municipal Lighting Plant 1997 Annual Rept ML20248L7671997-12-31031 December 1997 North Atlantic 1997 Annual Rept ML20198F9511997-12-31031 December 1997 United Illuminating Co 1997 Annual Rept ML20236M9561997-12-31031 December 1997 Amended Public Service of New Hampshire 1997 Annual Rept 1999-09-30
[Table view] |
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t .
- n NRC FORM 366 U.S. NUCLEAR REGULATORY COPMISSIC3 APPROVED BY OMB NO. 3150-0104
($-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH NF OL 0 HR LICENSEE EVENT REPORT (LER) $ARD TION REgUEST THE INFORMATION AND RECORDS MANAGEMENT BRANCH l (MNBB7714),U.S.NUCLEARREGULATORYCOMMISSION, 1 (Seereverseforrequirednumberofdigits/charactersforeachblock) ggN, C 0555-0001 D TO TH RW0g MANAGEMENT AND BUDGET. WASHINGTON, DC 20503.
FACILITYNAME(1) DOCKET NUMBER (2) PAGE(3) l SEABROOK STATION 05000443 1 OF 4 l TITLE (4)
MANUAL REACTOR TRIP DUE TO INADVERTENT MSIV CLOSURE ~
EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
SEQUENTIAL REVISION MONTH DAY YEAR YEAR MONTH DAY YEAR NUMBER NUMBER 05000 FAM NAME DOCKET "
05 20 93 93 --
09 --
00 06 18 93 0 000 OPERATING y THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 6: (Check one or more) (11)
MODE (9) 20.402(b) 20.405(c) X 50.73(a)(2)(iv) 73.71(b)
POWER 20.405(a)(1)(1) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c) 100 LEVEL (10) 20.405(a)(1)(ti) 50.36(c)(2) 50.73(a)(2)(vii) OTHER
- 20.405(a)(1)(iii) 50.73(a)(2)(1) 50.73(a)(2)(viii)(A) (Specify in trac low l iM g 20.405(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B)
WP 20.405(a)(1)(v) 50.73(a)(2)(ill) 50.73(a)(2)(x) NRC Form 366A)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONENUMBER(IncludeAreaCode)
Mr. James M. Peschel, Regulatory Compliance Manager (603)474-9521 ext.3772 COPFLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER R0 E 0 P X SB FSV E095 Y '
si!,
a SUPPLFK NTAL REPORT EXPECTED (14) EXPECTED MONTH DAY YEAR i Y !
X (ESIf yes, complete EXPECTED SUBMISSION DATE). NO SUBMISSION 9 15 93 DATE(15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On May 20, 1993, at 0437 EDT, a manual reactor trip from 100 percent power was initiated when a main steam [SB] isolation valve (MSIV) closed during MSIV quarterly testing. The trip was followed by a Feedwater Isolation and two Emergency Feedwater actuations. This event was reported to the NRC at 0553 EDT as an immediate notification pursuant to 10CFR50.72(b)(2)(ii),actuationoftheReactorProtectionSystem(RPS)andEngineered SafetyFeature(ESF) System.
During MSIV quarterly testing, the MSIVs are alternately stroked to ten percent closed and then reopened. However, one MSIV failed to return to the open position when the ten )
percent limit was reached, and instead continued to close. The reactor was manually tripped when the narrow range level in the affected steam generator was twenty-two percent and decreasing. l There were no adverse safety consequences as a result of this event.
The cause of the MSIV malfunction was determi.ied to be debris lodged in a hydraulic solenoid valve that allowed the hydraulic pressure keeping the MSIV open to bleed off, resulting in the MSIV drifting closed.
NRC FORM 366 (5-921 9306280289 930618 PDR ADOCK 05000443 s PDR
.i O
~
FJC f0RM 366A U.s. NUCLEAR REGULATORY CO MISSION APPROVED BY O M NO. 3150-0104 (S.92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH 50.0 HRS.
THis INFORMATION COLLECTION" REgEST:
LICENSEE EVENT REPORT (LER) NNFOM A ECORDs MANAGEM BRAN TEXT CONTINUATION gNkDN2'0555-0 1 AND T H $
REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUIEER (2) LER NUfEER (6: PAGE (3)
YEAR SEQUENTIAL REVISION SEABROOK STATION "
05000443 2 OF 4 93 -- 09 -- 00 TEXT (If more space is required, use additional copies of NRC form 366A) (17)
Description of Event On May 20, 1993, at 0437 EDT, plant operators initiated a manual reactor trip from 100 percent power when a main steam isolation valve (MSIV) closed during the performance of MSIV quarterly testing.
Seabrook Station is a four loop Westinghouse plant, with an MSIV in each of the four main steam lines. Each MSIV is controlled by a hydraulic / pneumatic actuator that uses nitrogen '
to maintain pressure on top of an operating piston (which tends to close the MSIV) and hydraulic pressure on the bottom of the operating piston to keep the valve open. There are two hydraulic solenoid operated valves that are used to vent the hydraulic pressure to a reservoir to close the valves. There are two trains of hydraulic control for each MSIV to increase reliability. MSIV operability is verified once per quarter during power operation by cycling each valve through ten percent of valve travel with both trains of hydraulic control using a test panel on the main control board. '
The train A test of the four MSIVs had been performed earlier on the shift with all MSIVs !
cycling properly. Two minor discrepancies, low nitrogen pressure on MSIV A and loose i limit switches on MSIV B, were noted. The train B test of MSIV A and C were then l completed satisfactorily (MSIV B was not tested using train B due to the loose limit i switches). However, when MSIV D was tested, the Senior Control Room Operator noted that '
the valve failed to stop at ten percent closed. The MSIV's continued closure was verified by indications of steam generator level shrinkage, steam flow reduction from steam generator D, and a delta temperature deviation alarm in the affected reactor coolant loop.
Attempts to stop the valve from closing were unsuccessful. Approximately four minutes after the start of the MSIV D test, with steam generator D narrow range level at twenty-I two percent and decreasing, the Unit Shift Superintendent ordered a manual trip of the reactor.
The decision to trip the reactor, and the response to the reactor trip and the subsequent recovery actions by plant operators, were determined to be correct. Primary plant system response was normal with ex FeedwaterSystem(EFW)[BA]pectedEngineeredSafetyFeature(ESF)actuations(Emergency actuation on Steam Generator LO-LO level and Feedwater System
[SJ] Isolation in response to low Reactor Coolant System temperature). During the response to the reactor trip, the Unit Shift Supervisor (USS) ordered the Senior Control Room Operator (SCRO) to reopen the feedwater isolation valves, as required by the applicable Emergency Response Procedure (ES-0.1, Reactor Trip Response). However, the SCR0 did not hear this order, and the USS continued with ES-0.1, verifying the startup l feed pump was running with greater than 14 percent level in the steam generators, and then !
securing the emergency feedwater pump. With feedwater secured, steam generator levels !
decreased to the LO-L0 level setpoint and a second EFW actuation occurred.
At 0553 EDT on May 20, 1993 North Atlantic made a four-hour notification to the NRC l- pursuantto10CFR50.72(b)(2)(ii).
l l
6 NRC FORM $66A U.s. NUCLEAR REGULA10RY COPNISSION APPROVED Hf OMB NO. 3150-0104 l l
(5-92) ,
EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH 50.0 HRS.
THIS INFORMATION COLLECTION REgEST:
LICENSEE EVENT REPORT (LER) $ F0 A ECORDS NAGE BRAN REGULAT R OMP TEXT CONTINUATION [M g g g . j.S. NUCLE REDUCTION PROJECT (3150-0104), OFFICE OF l MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER MUMBER (6? PAGE (3)
SEQUENTIAL REVISION YEAR SEABROOK STATION "" " " "
05000443 93 0 3 OF 4 ,
-- 09 -- l TEXT (If more space is required, use additional C.Tles of MRC forin 366A) (11)
Safety Conseauences There were no adverse safety consequences as a result of this event. Plant equipment functioned as designed and operator actions were determined to be correct. At no time during the event was there any impact on the health and safety of plant employees or the ;
public.
1 Root Cause The root cause of this event was determined to be debris lodged in one of the hydraulic solenoid valves that align the hydraulic portion of the MSIV operating piston with the ,
hydraulic reservoir. This debris caused the solenoid valve to stay in mid position during '
the ten percent closure test, permitting the hydraulic fluid to drain from the bottom of the operating cylinder. As the hydraulic pressure in the operating piston fell below the nitrogen pressure on top of the operating cylinder, the MSIV closed. A supplement to this report will be provided when the mechanism for introducing the debris is determined.
The root cause of the second EFW actuation was detern ined to be incomplete communication between the Unit Shift Supervisor and the control board operator regarding the reopening i of the feedwater isolation valves. ;
Corrective Actions j The hydraulic solenoid valves on MSIV D were replaced and the MSIV was tested satisfactorily. The minor discrepancies on MSIV A and MSIV B (low nitrogen pressure and loose limit switches, respectively) have been corrected. In addition, a Human Performance Evaluation was performed for the trip and for the events leading to the second EFW actuation.
The following additional actions are being taken:
- 1. The failed solenoids from MSIV D are being evaluated to determine what mechanism introduced the debris and produced their failure mode.
- 2. A logic change to the slow closure circuit is being developed so that the MSIV does not momentarily transfer from slow to fast closure before reopening during the partial closure test.
- 3. Emergency Response Procedure ES-0.1 will be revised to list the feedwater Isolaticn valve numbers.
- 4. Other Emergency Response Procedures will be reviewed for the use of specific valve numbers while performing evolutions. Precedure changes will be issued as applicable.
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NRC.f0RM'366A U.S. NUCLEAR REGULATORY COP 9tlSS10N APPROVED BY OMB NO. 3150-0104 (3-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
LICENSEE EVENT REPORT (LER) h0!"Yrfr0N!$fi A EC PDS P NAGE i BRAN TEXT CONTINUATION [Fjjyg.th'S'05SS_9 D 2 NUCLE REGULAT R 0 REDUCTION PROJECT (3150-0104),
g OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY KAME (1) DOCKET NUMBER (2) LER NUMBER (6L PAGE (3)
YEAR SEQUENTIAL REVISION SEABROOK STATION """ " "
05000443 93 0 4 OF 4
-- 09 --
TEXT (if more space is required, use additional copfes of hRC Fonn 366A) (11)
- 5. The decibel level and frequency for control board alarms will be evaluated to determine if they have been set too high, thereby contributing unnecessarily to the environmental noise level in the control room.
- 6. The lessons learned from this event will be discussed with all operating crews.
Plant Conditions At the time of this event, the plant was in Mode 1, at 100 percent power, with a Reactor Coolant System temperature of 587 degrees Fahrenheit and a pressure of 2235 psig.
Related Events This is the first event at Seabrook Station where MSIV testing anomalies resulted in a reactor trip.
This is the third event at Seabrook Station where incomplete communication among the operations crew contributed to a Reactor Protection System / Engineered Safety Features actuation. The previous occurrences were reported in LER 92-017 and LER 93-01, 1
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