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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B8951993-07-30030 July 1993 LER 93-008-01:on 930518,determined That Control Air Not Analyzed to Function During Seismic Event Due to Lack of Understanding Significance of Control Air Availability for Long Term DG Operation.Ufsar Will Be Updated ML20046B8961993-07-30030 July 1993 LER 93-011-00:on 921219,930209 & 0415,SW Pumps SW-P-41B, SW-P-41B & SW-P-41D Declared Inoperable,Respectively Due High Vibration.Caused by Excessive Abrasive Particles in Ocean Water.Pumps replaced.W/930730 Ltr ML20045G6641993-07-0101 July 1993 LER 93-006-01:on 930401,Train a Svc Water Inoperable Due to Corrosion Product Buildup Between Valve Stem & Packing Follower.Returned SW-V54 to Operable Status & TS 3.7.4 Action D Exited on 930402.W/930701 Ltr ML20045D6791993-06-21021 June 1993 LER 93-002-01:on 930107,determined Potential for Premature Opening of Containment Bldg Spray Sump Isolation Valves. Caused by Failure to Adequately Recognize Potential Sys Interactions.Affected Procedures Revised ML20045C5421993-06-18018 June 1993 LER 93-010-00:on 930522,SG Level Oscillations Occurred in One SG Resulting in SG Being Overfed & Causing high-high SG Water Level.Caused by Personnel Error.Power Reduced to Approx 2.5% & FW to SGs restored.W/930618 Ltr ML20045D3681993-06-18018 June 1993 LER 93-009-00:on 930520,manual Reactor Trip from 100% Power Initiated When MSIV Closed During Quarterly Testing, Resulting in Feedwater & Two Emergency Feedwater Isolations. Caused by Debris in Valves.Valves Replaced ML20045C5341993-06-16016 June 1993 LER 93-008-00:on 930518,identified That Failure of Air Supply to EDG Jacket Cooling Water Temperature Control Valves During Seismic Event Could Cause Overcooling of Edgs. Operability Determination Performed for EDGs.W/930616 Ltr ML20045B5181993-06-11011 June 1993 LER 93-007-00:on 930512,protective Devices Not Analyzed to Function During Environ Excursions Due to Unknown Cause Which Is Under Review.Operability Determination Was performed.W/930611 Ltr ML20024H1621991-05-23023 May 1991 LER 91-004-00:on 910401,steam Generator Indicated That Valve Was Not Opening Properly During Plant Restart.Caused by Differential Pressure Across Dash Plate.Dash Plate Machining Performed on Valves to Prevent Valve disk.W/910523 Ltr ML20044B2281990-07-12012 July 1990 LER 90-014-00:on 900612,discovered That Sample Pump for Steam Generator Blowdown Flash Tank Drain Radiation Monitor Not Running.Caused by Suspended Solids in Steam Generator Blowdown Sys.Solids Cleared from Flow switch.W/900712 Ltr ML20043B6741990-05-23023 May 1990 LER 90-008-01:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Air Cleanup Sys Incapable of Producing Negative Pressure.Latching Mechanism Repaired & Mods to Doors/Hardware planned.W/900523 Ltr ML20043B3551990-05-21021 May 1990 LER 90-013-00:on 900419,discovered That Containment Personnel Hatch Unsecured for Approx 28 H.Caused by Installation of Locking Plate Upside Down & Placing Lock Through Only 1 Eyelet.Instructions posted.W/900521 Ltr ML20042F5521990-05-0202 May 1990 LER 90-012-00:on 900402,transmitter Failed to Provide Pressure to Reactor Protection Sys Due to Closed Isolation Valve.Caused by Failure to Identify Valve in Procedures. Valves Manipulated to Correct positions.W/900502 Ltr ML20042E1781990-04-0606 April 1990 LER 90-006-01:on 900206,control Room Ventilation Sys Train a Radiation Monitor Went Into High Alarm Condition.Caused by Mechanical Binding of Check source.Geiger-Muller Tube Replaced & Monitor Returned to svc.W/900406 Ltr ML20042E1741990-04-0505 April 1990 LER 90-011-00:on 900306,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Failure of Geiger-Muller Tube.Monitor Removed from Svc & Tube replaced.W/900405 Ltr ML20012F5181990-04-0404 April 1990 LER 90-010-00:on 900305,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Moisture in Detector Housing.Air Intake Monitors Cleaned & Desiccant Placed in housing.W/900404 Ltr ML20012C2461990-03-12012 March 1990 LER 90-008-00:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Emergency Air Cleanup Sys Inoperable.Plant Cooldown Initiated,Latching Mechanism Repaired & Door Returned to svc.W/900312 Ltr ML20012C2481990-03-12012 March 1990 LER 90-007-00:on 900208,when Source Check Removed from Control room,RM-6506B Entered High Alarm Condition,Causing ESF Actuation of Emergency Air Cleanup Sys.Caused by Mechanical Binding.Check Source replaced.W/900312 Ltr ML20012B4491990-03-0808 March 1990 LER 90-006-00:on 900206,Train a Radiation Monitor Went Into High Alarm Condition,Resulting in Actuation of Control Room Emergency Air Cleanup & Filtration Subsystem.Caused by Mechanical Binding.Detector Tube remounted.W/900308 Ltr ML20011F4671990-02-22022 February 1990 LER 90-004-00:on 900123,wide-range Gas Monitor Process Flow Rate Value for Vent Radiation Monitor Discovered at Default Instead of Actual Value.Caused by Personnel Error.Process Flow Restored & Technician counseled.W/900222 Ltr ML20006E4591990-02-15015 February 1990 LER 90-003-00:on 900116,wide-range Gas Monitor Low Range Pump Found Inoperable.Caused by Failed Pump Diaphragm Weakened by High Flow Condition.Ruptured Pump Diaphragm Replaced & Pump Returned to Normal operations.W/900215 Ltr ML20006E1731990-02-0808 February 1990 LER 90-002-00:on 900109,discovered That Auxiliary Sample Pump Used to Satisfy Action Requirements of Tech Spec Was Not Operating.Caused by Dislodged Power Fuse.Pump Relocated & Caution Tape Installed to Protect pump.W/900208 Ltr ML20006E1801990-02-0808 February 1990 LER 90-001-00:on 900109,wide Range Gas Monitor Low Range Pump Found to Be Inoperable,Resulting in Noncompliance W/ Tech Specs.Caused by Regulator Isolation Valves Being Left in Open Position.Walkdown of Skids conducted.W/900208 Ltr ML20005E2461989-12-29029 December 1989 LER 89-014-00:on 891129,auxiliary Transformer Supply Breaker to Vital Bus E5 Tripped When Remote Manual Override Relay Energized.Caused by Procedure Inadequacies in Procedure 0S1048.01.Procedure revised.W/891229 Ltr ML20011D4381989-12-19019 December 1989 LER 89-011-01:on 890905,three Unsealed Piping Penetrations in Condensate Storage Tank Encl Identified.Caused by Failure to Transfer Sealing Requirements Into Detail Drawings.Penetrations sealed.W/891219 Ltr ML19332C8511989-11-22022 November 1989 LER 89-013-00:on 891023,discovered That Monitor Used to Satisfy Requirements of Tech Spec 3.3.3.1,Action 27 Had Been Unplugged.Caused by Personnel Error.Individual Counseled & Meeting Held W/Health Physics technicians.W/891122 Ltr ML19325F3301989-11-10010 November 1989 LER 89-012-00:on 891011,one of Two Suction Valves on RHR Train a Pump Closed,Causing Loss of All RHR Cooling Capability.Caused by Procedure Inadequacies.Procedure Revised to Specify Sequence of restoration.W/891110 Ltr ML19325C7891989-10-0505 October 1989 LER 89-011-00:on 890905,determined That Three Piping Penetrations in Condensate Storage Tank Encl Not Sealed.Root Cause Under Investigation.Penetrations Sealed & Tech Specs Surveillance Log revised.W/891005 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B8951993-07-30030 July 1993 LER 93-008-01:on 930518,determined That Control Air Not Analyzed to Function During Seismic Event Due to Lack of Understanding Significance of Control Air Availability for Long Term DG Operation.Ufsar Will Be Updated ML20046B8961993-07-30030 July 1993 LER 93-011-00:on 921219,930209 & 0415,SW Pumps SW-P-41B, SW-P-41B & SW-P-41D Declared Inoperable,Respectively Due High Vibration.Caused by Excessive Abrasive Particles in Ocean Water.Pumps replaced.W/930730 Ltr ML20045G6641993-07-0101 July 1993 LER 93-006-01:on 930401,Train a Svc Water Inoperable Due to Corrosion Product Buildup Between Valve Stem & Packing Follower.Returned SW-V54 to Operable Status & TS 3.7.4 Action D Exited on 930402.W/930701 Ltr ML20045D6791993-06-21021 June 1993 LER 93-002-01:on 930107,determined Potential for Premature Opening of Containment Bldg Spray Sump Isolation Valves. Caused by Failure to Adequately Recognize Potential Sys Interactions.Affected Procedures Revised ML20045C5421993-06-18018 June 1993 LER 93-010-00:on 930522,SG Level Oscillations Occurred in One SG Resulting in SG Being Overfed & Causing high-high SG Water Level.Caused by Personnel Error.Power Reduced to Approx 2.5% & FW to SGs restored.W/930618 Ltr ML20045D3681993-06-18018 June 1993 LER 93-009-00:on 930520,manual Reactor Trip from 100% Power Initiated When MSIV Closed During Quarterly Testing, Resulting in Feedwater & Two Emergency Feedwater Isolations. Caused by Debris in Valves.Valves Replaced ML20045C5341993-06-16016 June 1993 LER 93-008-00:on 930518,identified That Failure of Air Supply to EDG Jacket Cooling Water Temperature Control Valves During Seismic Event Could Cause Overcooling of Edgs. Operability Determination Performed for EDGs.W/930616 Ltr ML20045B5181993-06-11011 June 1993 LER 93-007-00:on 930512,protective Devices Not Analyzed to Function During Environ Excursions Due to Unknown Cause Which Is Under Review.Operability Determination Was performed.W/930611 Ltr ML20024H1621991-05-23023 May 1991 LER 91-004-00:on 910401,steam Generator Indicated That Valve Was Not Opening Properly During Plant Restart.Caused by Differential Pressure Across Dash Plate.Dash Plate Machining Performed on Valves to Prevent Valve disk.W/910523 Ltr ML20044B2281990-07-12012 July 1990 LER 90-014-00:on 900612,discovered That Sample Pump for Steam Generator Blowdown Flash Tank Drain Radiation Monitor Not Running.Caused by Suspended Solids in Steam Generator Blowdown Sys.Solids Cleared from Flow switch.W/900712 Ltr ML20043B6741990-05-23023 May 1990 LER 90-008-01:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Air Cleanup Sys Incapable of Producing Negative Pressure.Latching Mechanism Repaired & Mods to Doors/Hardware planned.W/900523 Ltr ML20043B3551990-05-21021 May 1990 LER 90-013-00:on 900419,discovered That Containment Personnel Hatch Unsecured for Approx 28 H.Caused by Installation of Locking Plate Upside Down & Placing Lock Through Only 1 Eyelet.Instructions posted.W/900521 Ltr ML20042F5521990-05-0202 May 1990 LER 90-012-00:on 900402,transmitter Failed to Provide Pressure to Reactor Protection Sys Due to Closed Isolation Valve.Caused by Failure to Identify Valve in Procedures. Valves Manipulated to Correct positions.W/900502 Ltr ML20042E1781990-04-0606 April 1990 LER 90-006-01:on 900206,control Room Ventilation Sys Train a Radiation Monitor Went Into High Alarm Condition.Caused by Mechanical Binding of Check source.Geiger-Muller Tube Replaced & Monitor Returned to svc.W/900406 Ltr ML20042E1741990-04-0505 April 1990 LER 90-011-00:on 900306,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Failure of Geiger-Muller Tube.Monitor Removed from Svc & Tube replaced.W/900405 Ltr ML20012F5181990-04-0404 April 1990 LER 90-010-00:on 900305,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Moisture in Detector Housing.Air Intake Monitors Cleaned & Desiccant Placed in housing.W/900404 Ltr ML20012C2461990-03-12012 March 1990 LER 90-008-00:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Emergency Air Cleanup Sys Inoperable.Plant Cooldown Initiated,Latching Mechanism Repaired & Door Returned to svc.W/900312 Ltr ML20012C2481990-03-12012 March 1990 LER 90-007-00:on 900208,when Source Check Removed from Control room,RM-6506B Entered High Alarm Condition,Causing ESF Actuation of Emergency Air Cleanup Sys.Caused by Mechanical Binding.Check Source replaced.W/900312 Ltr ML20012B4491990-03-0808 March 1990 LER 90-006-00:on 900206,Train a Radiation Monitor Went Into High Alarm Condition,Resulting in Actuation of Control Room Emergency Air Cleanup & Filtration Subsystem.Caused by Mechanical Binding.Detector Tube remounted.W/900308 Ltr ML20011F4671990-02-22022 February 1990 LER 90-004-00:on 900123,wide-range Gas Monitor Process Flow Rate Value for Vent Radiation Monitor Discovered at Default Instead of Actual Value.Caused by Personnel Error.Process Flow Restored & Technician counseled.W/900222 Ltr ML20006E4591990-02-15015 February 1990 LER 90-003-00:on 900116,wide-range Gas Monitor Low Range Pump Found Inoperable.Caused by Failed Pump Diaphragm Weakened by High Flow Condition.Ruptured Pump Diaphragm Replaced & Pump Returned to Normal operations.W/900215 Ltr ML20006E1731990-02-0808 February 1990 LER 90-002-00:on 900109,discovered That Auxiliary Sample Pump Used to Satisfy Action Requirements of Tech Spec Was Not Operating.Caused by Dislodged Power Fuse.Pump Relocated & Caution Tape Installed to Protect pump.W/900208 Ltr ML20006E1801990-02-0808 February 1990 LER 90-001-00:on 900109,wide Range Gas Monitor Low Range Pump Found to Be Inoperable,Resulting in Noncompliance W/ Tech Specs.Caused by Regulator Isolation Valves Being Left in Open Position.Walkdown of Skids conducted.W/900208 Ltr ML20005E2461989-12-29029 December 1989 LER 89-014-00:on 891129,auxiliary Transformer Supply Breaker to Vital Bus E5 Tripped When Remote Manual Override Relay Energized.Caused by Procedure Inadequacies in Procedure 0S1048.01.Procedure revised.W/891229 Ltr ML20011D4381989-12-19019 December 1989 LER 89-011-01:on 890905,three Unsealed Piping Penetrations in Condensate Storage Tank Encl Identified.Caused by Failure to Transfer Sealing Requirements Into Detail Drawings.Penetrations sealed.W/891219 Ltr ML19332C8511989-11-22022 November 1989 LER 89-013-00:on 891023,discovered That Monitor Used to Satisfy Requirements of Tech Spec 3.3.3.1,Action 27 Had Been Unplugged.Caused by Personnel Error.Individual Counseled & Meeting Held W/Health Physics technicians.W/891122 Ltr ML19325F3301989-11-10010 November 1989 LER 89-012-00:on 891011,one of Two Suction Valves on RHR Train a Pump Closed,Causing Loss of All RHR Cooling Capability.Caused by Procedure Inadequacies.Procedure Revised to Specify Sequence of restoration.W/891110 Ltr ML19325C7891989-10-0505 October 1989 LER 89-011-00:on 890905,determined That Three Piping Penetrations in Condensate Storage Tank Encl Not Sealed.Root Cause Under Investigation.Penetrations Sealed & Tech Specs Surveillance Log revised.W/891005 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H2841999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Seabrook Station. with ML20212D1461999-09-17017 September 1999 SER Accepting Request to Use Proposed Alternative to Certain Weld Repair Requirements in ASME Boiling & Pressure Vessel Code ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20212B8671999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Seabrook Station. with ML20210Q7581999-08-11011 August 1999 SER Approving Proposed Merger of CES & Bec,Which Will Create New Parent Company of Canal ML20210R9781999-08-0606 August 1999 ISI Exam Rept of Seabrook Station, for RFO 6,period 3 ML20210J8681999-08-0303 August 1999 SER Approving License Transfer from Montaup Electric Co to Little Bay Power Corp & Approval of Conforming Amend for Seabrook Station Unit 1 ML20210R6001999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Seabrook Station, Unit 1.With ML20210H1151999-06-30030 June 1999 Naesc Semi-Annual Fitness-for-Duty Rept for 990101-0630 ML20209H1371999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Seabrook Station, Unit 1.With ML20195G5391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Seabrook Station, Unit 1.With ML20195C0491999-05-25025 May 1999 Offshore Intake Seal Deterrent Barrier Design ML20206E4761999-04-30030 April 1999 LER 99-S01-00:on 990408,contractor Employee Was Granted Temporary Unescorted Access to Seabrook Station Protected Area.Caused by Failure of Contractor Employee to Provide Accurate Info.Individual Access Revoked.With ML20206N1751999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Seabrook Station, Unit 1.With ML20196L2081999-04-19019 April 1999 Rev 01-07-00 to RE-21, Cycle 7 Colr ML20205K5441999-03-31031 March 1999 Decommissioning Update ML20205L8141999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Seabrook Station. with ML20205C1981999-03-24024 March 1999 Safety Evaluation Concluding That Proposed Relief Request IR-8,Rev 1,provides Acceptable Alternative to ASME Code Requirements.Recommends Authorization of Proposed Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20207F4941999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Seabrook Station. with ML20199E6731998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Seabrook Station, Unit 1.With ML20198P1831998-12-31031 December 1998 LER 98-S01-00:on 981214,incomplete pre-employment Screening Records Was Noted.Caused by Failure of Contractor Employee to Provide Accurate Info.Subject Contractor Employees Employment Was Terminated.With ML20202E8241998-12-31031 December 1998 Naesc Semi-Annual Fitness-for-Duty Rept for 980701-981231 ML20196F5741998-12-0202 December 1998 Safety Evaluation Concluding That Licensee Has Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Seabrook ML20198B8661998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Seabrook Station, Unit 1.With ML20195D0311998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Seabrook Station, Unit 1.With ML20154H5291998-10-0808 October 1998 Special Rept:On 980928,meteorological Monitoring Instrumentation Channel Inoperable for Period Greater than 7 Days.Caused by Vendor to Follow Std Industry Practice for Calibr of Instrumentation.Instruments Installed ML20154M8421998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Seabrook Generating Station,Unit 1.With ML20151V5951998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Seabrook Station, Unit 1.With ML20237B4501998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Seabrook Station ML20236R1781998-06-30030 June 1998 Naesc Semi-Annual Fitness-for-Duty Rept for 980101-0630 ML20236M3591998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Seabrook Station, Unit 1 ML20237A4871998-06-0303 June 1998 North Atlantic Seabrook Station 1998 Exercise on 980603 ML20248M2951998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Seabrook Station, Unit 1 ML20247G2641998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Seabrook Station ML20247H3171998-04-27027 April 1998 Rev 1 to Seabrook Station SGs B & C Isi,May/June 1997 ML20216F8891998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Seabrook Station 05000443/LER-1998-002, Re Potential Safety Injection Pump Runout Conditions Identified on 980113.LER 98-002-00 Retracted1998-03-20020 March 1998 Re Potential Safety Injection Pump Runout Conditions Identified on 980113.LER 98-002-00 Retracted ML20216H9211998-03-13013 March 1998 Fitness for Duty Program Performance Data Personnel Subject to 10CFR26 ML20248L2811998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Seabrook Station, Unit 1 ML20197A7531998-02-27027 February 1998 Safety Evaluation Accepting License Request for Relief from ASME Code,Section IX Requirements Re Inservice Insp of RHR Heat Exchanger Nozzle Welds & Reactor Vessel Closure Head Nuts ML20202G3701998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Seabrook Station ML20198G0271997-12-31031 December 1997 Commonwealth Energy Sys 1997 Annual Rept ML20248L7711997-12-31031 December 1997 Western Massachusetts Electric 1997 Annual Rept. Supporting Info,Encl ML20198G1021997-12-31031 December 1997 Baycorp Holdings 1997 Annual Rept ML20198N7021997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Seabrook Station, Unit 1 ML20198G0351997-12-31031 December 1997 Eastern Edison Co 1997 Annual Rept ML20198G0681997-12-31031 December 1997 Taunton Municipal Lighting Plant 1997 Annual Rept ML20248L7671997-12-31031 December 1997 North Atlantic 1997 Annual Rept ML20198F9511997-12-31031 December 1997 United Illuminating Co 1997 Annual Rept ML20236M9561997-12-31031 December 1997 Amended Public Service of New Hampshire 1997 Annual Rept 1999-09-30
[Table view] |
Text
-
y Seab k NH 03874 f
= Telephone (603)474-9521 Energy Service Corporation
( Facsimile (603)474-2987 Ted C. Feigenbaum l
I Senior Vice President and ;
Chief Nuclear Officer i l NYN-93106 1
l J uly 30,1993 United States Nuclear Regulatory Commission Washington, D.C. '20555 {
i Attention: Document Control Desk ;
Reference:
Facility Operating License No. NPF-86, Docket No. 50-443
Subject:
Licensee Event Report (LER) 93-01100: " Voluntary LER 93-011, Service ,
Water Pumps SW-P-41B, SW-P-41C and SW-P-41D" i Gentlemen:
Enclosed please find Licensec Event Report (LER) No. 93 011-00 for Seabrook Station. This submittal documents events which occurred on December 19,1992, February ,
9,1993 and April 15,1993. l Should you require further information regarding this matter, please contact Mr. -
James M. Peschel, Regulatory Compliance Manager at (603) 474-9521 extension 377 i
i Very truly yours, l p^ -. i
- w. ~
l Ted C. Feigenbau l
TCF:MLM/act f
Enclosures:
NRC Forms 366/366A f f
l i
l ,
i l
1 i
f.)60C2L l
f nyI '
_ a member of the Northeast Utilities system / I l
9308060392 930730 PDR ADOCK 05000443 E ,h,'/fu .
8i l
t l
S PDR # t
I
~~
United States Nuclear Regulatory Commission July 30,1993 Attention: Document Control Desk Page two -
i ec: Mr. Thomas T. Martin Regional Administrator l U.S. Nuclear Regulatory Commission l Region I _[
475 Allendale Road King of Prussia, PA 19406 ;
Mr. Albert W. De Agazio, Sr. Project Manager Project Directorate I-4 Division of Reactor Projects U.S. Nuclear Regulatory Commission Washington, DC 20555 Mr. Noel Dudley NRC Senior Resident Inspector f P.O. Box 1149 ';
Seabrook, NH 03874 ,
i INPO i
Records Center 700 Galleria Parkway ,
Atlanta, GA 30339-5957 l
~
NRC fDRM 366 U.S. NUCLEAR RLGULATORY Ct#911SS10 APPROVED BY OMB NO. 3150-0104 (5 97) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH I " E$ "
LICENSEE EVENT REPORT (LER) $Agg"lNu$ EDLgDING g[G BIhlN 5 TE l)
THE 1hf0RMAT10N AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISS]DN, (See reverse f or re::uired nunber of digits / characters for each block) WASHINGTON, DC ?0555-0001, AND TO THE PAPERWORK REDUC 110N PROJE CT (3150-0104), OFF]CE Of MANAGEMENT AND BUDGET, WASHINCTON, DC 20503.
I AClll1Y NAML (1) Scabrook Station DOOR.f i NUMMR (2) PAGE(3) 50-443 1 OF 4 TITtE (4) Voluntary LER for Senice Water Pumps SW-P-418. SW-P-41C and SW-P-41D IVIN1 DAll (5) [ [ R NUMHI R (6) RI P0HI DAll (7) Olltf R I ACillill.S INV0l VID (8) l MONTH DAY YE AR YE AR NUMBE R NUMBER MONTH DAY YEAR 05000
' #" "" UU # "
12 19 92 93 --
11 --
00 07 30 93 0 00 i OPIRAllNG y IHl$ RE P0HI IS MMH H D PURWNI 10 M RIQM Mt NTS M 10 G R D (M one or nm) (H )
MODC (9) 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b) '
POWLR 20.405(a)(1)( t ) 50.35(c)(1) 50.73(a)(2)(v) 73.71(c)
(EVEL (10) 20.405(a)(1)(ii) 50.3b(c)(2) 50.73(a)(2)(vit) X OlHLR 20.405(a)(1)(iii) 50.73(a)(2)(i) 50.73(a)(2)(vitt)(A) (Specify in 20.405(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(vtii)(B) A tract b ow 20.405(a)(1)(v) 50.73(a )(2)( iii) 50.13(a)(2)(x) NRC form 366A) l i101NSI[ CONIACI IOR litiS IIR (12)
NAME TELEPHONL NUMBLR (Include Area t' ode)
Mr. James M. Peschel, Regulatory Compliance Manger (603) 474-9521 extension 37/2 COMPtiIF ONI IIN! IOR lADI COMPONINI IAllURE DISCRIBID IN THIS REPORI (13)
CAUSE SYSTEM COMPONENT MANUFACTURER gf3 CAUSE SYSTEM COMPONENT MANUTACTURER ,
B BI P J105 Yes a
SUPPil_MI NI AL RI POR1 IIPI CilD (14) [ XP[ CUD _. MONTH DAY YEAR Yi S SuliMISSIDN ;
(If yes, corplete EXPECTED SUBMISSION DATE). X N DATE (15) l AH51RACI (Limit to 1400 spaces, i.e., approxinately 15 single-spaced typewritten lines) (16)
This LER is being submitted as a voluntary LER by North Atlantic Energy Corporation (North Atlamic).
At various times during a four month period, three of the four ocean Seniw Water (SW) Pumps were declared inoperable due to high sibration. The pump high vibration conditions occurred m the following order: SW-P-41C, December 19, 1992; j SW P-41D, February 9,1W3, and SW-P-41B, April 15, 1993. Ai! four ocean SW Pumps (SW-P-41A through SW-P-41D) are
- Model No. H5056, two stage vertical pumps manufactured by the Johnston Pump / General Valve Co.
There were no adverse safety consequences as a result of these events.
The root cause of the high vibration condition for SW-P-41B, SW-P-41C and SW-P-4]D was due to excessive abrasive particles ;
present in the ocean water. The abrasive particles produced accelerated wear of the shaft bearing journals. Contributing to i the excessive sibration was the significantly out of balance impellers in each pump.
North Atlantic has replaced / rebuilt all three SW pumps. The replacement! rebuilt pumps were successfully tested and remain in senice to date.
l l
4 NGC FDRM 35C (5-92)
I l
l CLC 10RM 36SA U.S. NUCLEAR REGULA10RY COPMISSICJ APPROVED BY OMB HO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN FER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO I LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, TEXT CONTINUATION WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
i l f ACit IlY NAML (1) IXXXLI NUMBER (2) t ER NUMBER (6) PAGE (3)
YEAR SEQUENilAL REVISION "U" " "
Seabrook Station 50-443 93 2 Of 4 '
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TLXi (11 more space is required, use additiona l copies of NRC form 366A) (17)
HACKGROUND INFORM ATION The Seabrook Station Senice Water (SW) System consists of two, independent and redundant parallel flow trains, each '
l supplying cooling water to a primary component cooling water heat exchanger, a diesel generator jacket water cooler, the !
secondary component cooling water heat exchangers and the condenser water box priming pump seal water heat exchangers.
l Under normal conditions, flow is supplied by pumps taking suction from a common bay of the SW Pumphouse. If transfer to ,
the Cooling Tower (CT) occurs, senice water is obtained from the CT Basin using the CT Pumps. The SW System utilizes six pumps. Four pumps are in the ocean portion of the system and two pumps are in the CT portion of the system. Each pump ,
is capable of handling 100% of the SW System heat loads following a design basis accident. The SW System Limiting 1 Condition for Operation Action Requirements and Smveillance Requirements are specified in Seabrook Station Technical l Specifications 3/4.7.4 and 3/4.7.5.
I DESCRIPTION OF EVENT Three of the four ocean Service Water (SW) Pumps were declared inoperable due to high vibration at various times between December 1992 to April 1993. The pump failures occurred in the following order: SW-P-41C, December 19,1992; SW-P-41D, February 9,1993, and SW-P-418, April 15,1993. All four ocean SW Pumps (SW-P-41A through SW-P-41D) are Model No.
H5056, two stage vertical pumps manufactured by the Johnston Pump / General Valve Co.
During Seabrook Station's second refueling outage, between September 23, 1992 and October 8,1992, Senice Water Pumps SW-P-41C and SW-P-41D were removed for routine inspection, overhaul, and rebuilt at Seabrook by Station Maintenance personnel. SW-P-41C maintenance consisted of replacing the bowl assembly (including 2 impellers), shafting, bearings and columns with spare parts. SW-P-41D maintenance consisted of reusing the same bowl assembly (including 2 impellers) and replacing the shafting, bearings and columns with spare parts. Post-maintenance testing for both pumps showed normal conditions and operating parameters to be within acceptable limits.
On December 12-13, 1992, a severe ocean storm caused excessive debris and seaweed to enter the Circulating Water (CW) and SW Pumphouses. Senice Water Pumps SW-P-41C and SW-P-41D were operating during the majority of the storm. The unusual amount of debris (scaweed) eventually caused a loss of CW flow to the condensers resulting in a manual reactor trip (LER 92-025-00). l On December 19,1992, SW-P-41C began experiencing high vibration. Vibration signatures indicated that the vibration was excessive (overall vibration was > 1.0 in/sec). The pump was declared inoperable due to high vibration. At the time the pump was declared inoperable, it had accumulated approximately 204 total running hours.
On February 9,1993, SW-P-41D showed signs of higher-than-normal vibration. Vibration signatures indicated that vibration was excessive (spikes up to 1.9 in/sec). As a result, the pump was declared inoperable. At this time, the pump had accumulated approximately 500 total running hours.
On April 15,1993, SW-P-41B showed signs of higher-than normal vibration. Vibration signatures taken during the Technical Specification Operability Surveillance Test were high, although within the limits. Additional vibration analyses were performed, and SW-P-41B was declared inoperable due to high intermittent vibration spikes up to 1 in/sec. At this time, the pump had accumulated approximately 4921 total running hours.
.- .g NRC f 0RM 36fA U.S. MUCLLAR RLGut A10RY CtP911SS]Cd APPROVLD BY OMB NO. 3150-0104 (5-92) EXPlRES 5/31/95 ESTIMATED B'JRDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. 6 FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INF ORMAT10N AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, TEXT CONTINUATION WASHINGTON, DC 20555-000), AND TO THE PAPERWORK ,
REDUCTION PROJECT (3150-0104), OfflCE Of MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
IACitITY NAMI (1) DOCKl1 NuMBIR (?) LIR NUMDfR (6) PAGE (3)
SEQUENTIAL REVISION YEAR NUMBER NUMBER Seabrook Station 50-443 93 00 3 OF 4
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CORRECTIVE ACTIONS SW-P-41 C l Service Water Pump S%-P-41C was inspected and tested to determine the cause of the vibration. Adjustments were made in an effort to reduce sibration. The vibration could not be reduced and the root cause could not be determined. Therefore, this pump was reinoved from senice and replaced with the original pump which had been removed during OR02. The final assembly consisted of the old column sections, lineshafts, bearings and a new bowl assembly. The replacement pump was successfully tested and remains in service to date. Balance quality of the two impellers currently installed is unknown. The two impullers taken from SW-P-41C pump were returned to the manufacturer who found them significantly out of balance.
The impellers were rebalanced and returned to Seabrook Station. ;
i SW-P-41 D Service Water Pump SW-P-41D was removed and replaced with a rebuilt pump. The rebuilt pump consisted of new shafts and bearings, as well as the original bow' sembly, columns and impeller.= that were removed from SW-P-41C. The impellers were rebalanced by the manufacturer pri o .o installation. The rebuilt pump was successfully tested and remains in service to i date. The two impellers removed from SW-P-41D were returned to the manufactarer who found them significantly out of balance. The impellers were rebalanced and returned to Seabrook Station.
1 l SW-P-41 B Senice Water Pump SW-P-41B was removed and replaced with a rebuilt pump. The rebuilt pump consisted of a spare bowl assembly and r: balanced impellers. The columns and shafts were also replaced. The replacement pump was successfully tested and remains in senice to date. The two impellers removed from SW-P-41B were returned to the manfacturer who found them signWeantly out of balance. The impellers were rebalanced and returned to Seabrook Station. i l
l ADDtT10NA1, INIORM ATION The SW pump specification states: (1) all pumps shall be tested at the factory to check balance, and (2) operation and 0 performance in accordance with the Hydraulic Institute Standards for Centrifugal, Rotary and Reciprocating Pumps. Johnston UPump has stated that all pump impellers are balanced and documented by company programs and procedures before the
! performance test is implemented. In July 1976, United Engineers & Constructors Inc. conducted a site surveillance at the ,
Johnston Pump facility. The surveillance was to verify all applicable acceptance criteria using a Quality control vendor l Surveillance Check Plan (OCVS) before shipping the pumps to Seabrook. The OCVS did not identify or require verification j of impeller balancing documentation. Johnston Pump has recently been requested to provide pump impeller balancing !
documeritation for the Seabrook Station SW pumps. Johnston Pur p has reviewed their records and is currently unable to locate this information.
The SW Pumps will be modified by applying a chrome oxide coating to the bearing areas of the shafts and by replacing the existing rubber cutless lineshaft bearings with composite type bearings.
Vibration monitoring will be performed more frcquently following a major storm in order to better detect the onset of acy abnormal conditions. These vibration signatures will be carefully examined and the rotating speed vibration ecmponent trended to detect the onset of degradation.
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MRC FORM 3%A U.S. NUCLi>Jt REGULA1GRY COMMISSION APPROULD DV OMB CD. 3150-0104 (592) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURL)EN ES11 MATE 10 LICENSEE EVENT REPORT (LER) THE INf0RMA110N AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHING 10N, DC 20555-0001, AND TO THE PAPERWORK REDUC 110N PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
IACitITY MAM O) 00CK11 NUMBl'R (2) Lt R NUMBt R (6L PACE (3)
YEAR SEQUENTIAL REVI5 ION Seabrook Station 50-443 93 4 OF 4
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The SW Pump failure information has been evaluated by North Atlantic Engineering for reportability pursuant to 10CFR21.
Their evaluation of the information found the events not reportable under the provisions of 10CFR21.
To date no significant degradation of the SW Pump 41A has been identified. SW-P-41A is monitored each time it is run and the appropriate maintenance actions will be taken if degradation is noted.
ROOT CAUSE SW. P-41 C .
SW-P-41C was evaluated for the cause of high vibration by Pump & Vibration Consultants, Inc. (PVC). The PVC evaluation concluded that the most probable cause of failure of SW-P-41C was due to excessive abrasive particles present in the water during the December storm. The abrasive particles produced accelerated wear of the shaft bearing journals. This caused the excessive vibration to occur due to the impeller out-of-balance. Since the shaft bearing journals in this type of pump are lubricated by the fluid being pumped, (ocean water in this case) any abrasive material in the water is passed through the bearings resulting in abnormal bearing wear. Additionally, the pump impellers were significantly out-of-balance. This contributed to the pump being removed from senice and declared inoperable.
SW-P-41 D The root cause of failure of SW-P 41D was attributed to excessive abrasive particles present in the ocean water during the December storm. North Atlantic determined the root cause of failure of SW-P-41D to be the same as that of SW-P-41C because of the identical, as-found condition of the pumps and the fact that both pumps were operating during the December storm. SW-P-41C and SW-P-41D had identical wear patterns on the bearing journals. The impellers of SW-P-41D were significantly out-of-balance.
SW- P-41 H The root cause failure for SW-P-41D was attributed to excessive abrasive particles present in the ocean water during the numerous 1492-1993 winter storms. North Atlantic determined the root cause of failure of SW-P-41B to be the same as that of SW-P-41C and SW.P-41D because of the identical, as-found condition of the pumps. SW-P-41B had identictd wear patterns on the bearing journals as SW-P-41C and SW-P-41D. The SW-P-41B impellers were significantly out-of-balance.
PIANT CONDITIONS At the time of each event, the plant was in MODE 1 and operating at 10Ec power.
S AI ETY CONSEOUENCES No adverse safety consequences resulted from the inoperability of the three SW pumps. The SW System remained operable and capable of fulfilling its design basis function during each pump inoperable event. The SW System was maintained operable by transferring heat loads to the CT by existing station procedures. Although the four ocean SW Pumps were declared inoperable, they we.re maintained available for use. If needed these pumps could have been put back into service within approximately ten minutes.
PREVIOUS OCCURRENCES There have been no other previous occurrences / events of this type.
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