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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B8951993-07-30030 July 1993 LER 93-008-01:on 930518,determined That Control Air Not Analyzed to Function During Seismic Event Due to Lack of Understanding Significance of Control Air Availability for Long Term DG Operation.Ufsar Will Be Updated ML20046B8961993-07-30030 July 1993 LER 93-011-00:on 921219,930209 & 0415,SW Pumps SW-P-41B, SW-P-41B & SW-P-41D Declared Inoperable,Respectively Due High Vibration.Caused by Excessive Abrasive Particles in Ocean Water.Pumps replaced.W/930730 Ltr ML20045G6641993-07-0101 July 1993 LER 93-006-01:on 930401,Train a Svc Water Inoperable Due to Corrosion Product Buildup Between Valve Stem & Packing Follower.Returned SW-V54 to Operable Status & TS 3.7.4 Action D Exited on 930402.W/930701 Ltr ML20045D6791993-06-21021 June 1993 LER 93-002-01:on 930107,determined Potential for Premature Opening of Containment Bldg Spray Sump Isolation Valves. Caused by Failure to Adequately Recognize Potential Sys Interactions.Affected Procedures Revised ML20045C5421993-06-18018 June 1993 LER 93-010-00:on 930522,SG Level Oscillations Occurred in One SG Resulting in SG Being Overfed & Causing high-high SG Water Level.Caused by Personnel Error.Power Reduced to Approx 2.5% & FW to SGs restored.W/930618 Ltr ML20045D3681993-06-18018 June 1993 LER 93-009-00:on 930520,manual Reactor Trip from 100% Power Initiated When MSIV Closed During Quarterly Testing, Resulting in Feedwater & Two Emergency Feedwater Isolations. Caused by Debris in Valves.Valves Replaced ML20045C5341993-06-16016 June 1993 LER 93-008-00:on 930518,identified That Failure of Air Supply to EDG Jacket Cooling Water Temperature Control Valves During Seismic Event Could Cause Overcooling of Edgs. Operability Determination Performed for EDGs.W/930616 Ltr ML20045B5181993-06-11011 June 1993 LER 93-007-00:on 930512,protective Devices Not Analyzed to Function During Environ Excursions Due to Unknown Cause Which Is Under Review.Operability Determination Was performed.W/930611 Ltr ML20024H1621991-05-23023 May 1991 LER 91-004-00:on 910401,steam Generator Indicated That Valve Was Not Opening Properly During Plant Restart.Caused by Differential Pressure Across Dash Plate.Dash Plate Machining Performed on Valves to Prevent Valve disk.W/910523 Ltr ML20044B2281990-07-12012 July 1990 LER 90-014-00:on 900612,discovered That Sample Pump for Steam Generator Blowdown Flash Tank Drain Radiation Monitor Not Running.Caused by Suspended Solids in Steam Generator Blowdown Sys.Solids Cleared from Flow switch.W/900712 Ltr ML20043B6741990-05-23023 May 1990 LER 90-008-01:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Air Cleanup Sys Incapable of Producing Negative Pressure.Latching Mechanism Repaired & Mods to Doors/Hardware planned.W/900523 Ltr ML20043B3551990-05-21021 May 1990 LER 90-013-00:on 900419,discovered That Containment Personnel Hatch Unsecured for Approx 28 H.Caused by Installation of Locking Plate Upside Down & Placing Lock Through Only 1 Eyelet.Instructions posted.W/900521 Ltr ML20042F5521990-05-0202 May 1990 LER 90-012-00:on 900402,transmitter Failed to Provide Pressure to Reactor Protection Sys Due to Closed Isolation Valve.Caused by Failure to Identify Valve in Procedures. Valves Manipulated to Correct positions.W/900502 Ltr ML20042E1781990-04-0606 April 1990 LER 90-006-01:on 900206,control Room Ventilation Sys Train a Radiation Monitor Went Into High Alarm Condition.Caused by Mechanical Binding of Check source.Geiger-Muller Tube Replaced & Monitor Returned to svc.W/900406 Ltr ML20042E1741990-04-0505 April 1990 LER 90-011-00:on 900306,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Failure of Geiger-Muller Tube.Monitor Removed from Svc & Tube replaced.W/900405 Ltr ML20012F5181990-04-0404 April 1990 LER 90-010-00:on 900305,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Moisture in Detector Housing.Air Intake Monitors Cleaned & Desiccant Placed in housing.W/900404 Ltr ML20012C2461990-03-12012 March 1990 LER 90-008-00:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Emergency Air Cleanup Sys Inoperable.Plant Cooldown Initiated,Latching Mechanism Repaired & Door Returned to svc.W/900312 Ltr ML20012C2481990-03-12012 March 1990 LER 90-007-00:on 900208,when Source Check Removed from Control room,RM-6506B Entered High Alarm Condition,Causing ESF Actuation of Emergency Air Cleanup Sys.Caused by Mechanical Binding.Check Source replaced.W/900312 Ltr ML20012B4491990-03-0808 March 1990 LER 90-006-00:on 900206,Train a Radiation Monitor Went Into High Alarm Condition,Resulting in Actuation of Control Room Emergency Air Cleanup & Filtration Subsystem.Caused by Mechanical Binding.Detector Tube remounted.W/900308 Ltr ML20011F4671990-02-22022 February 1990 LER 90-004-00:on 900123,wide-range Gas Monitor Process Flow Rate Value for Vent Radiation Monitor Discovered at Default Instead of Actual Value.Caused by Personnel Error.Process Flow Restored & Technician counseled.W/900222 Ltr ML20006E4591990-02-15015 February 1990 LER 90-003-00:on 900116,wide-range Gas Monitor Low Range Pump Found Inoperable.Caused by Failed Pump Diaphragm Weakened by High Flow Condition.Ruptured Pump Diaphragm Replaced & Pump Returned to Normal operations.W/900215 Ltr ML20006E1731990-02-0808 February 1990 LER 90-002-00:on 900109,discovered That Auxiliary Sample Pump Used to Satisfy Action Requirements of Tech Spec Was Not Operating.Caused by Dislodged Power Fuse.Pump Relocated & Caution Tape Installed to Protect pump.W/900208 Ltr ML20006E1801990-02-0808 February 1990 LER 90-001-00:on 900109,wide Range Gas Monitor Low Range Pump Found to Be Inoperable,Resulting in Noncompliance W/ Tech Specs.Caused by Regulator Isolation Valves Being Left in Open Position.Walkdown of Skids conducted.W/900208 Ltr ML20005E2461989-12-29029 December 1989 LER 89-014-00:on 891129,auxiliary Transformer Supply Breaker to Vital Bus E5 Tripped When Remote Manual Override Relay Energized.Caused by Procedure Inadequacies in Procedure 0S1048.01.Procedure revised.W/891229 Ltr ML20011D4381989-12-19019 December 1989 LER 89-011-01:on 890905,three Unsealed Piping Penetrations in Condensate Storage Tank Encl Identified.Caused by Failure to Transfer Sealing Requirements Into Detail Drawings.Penetrations sealed.W/891219 Ltr ML19332C8511989-11-22022 November 1989 LER 89-013-00:on 891023,discovered That Monitor Used to Satisfy Requirements of Tech Spec 3.3.3.1,Action 27 Had Been Unplugged.Caused by Personnel Error.Individual Counseled & Meeting Held W/Health Physics technicians.W/891122 Ltr ML19325F3301989-11-10010 November 1989 LER 89-012-00:on 891011,one of Two Suction Valves on RHR Train a Pump Closed,Causing Loss of All RHR Cooling Capability.Caused by Procedure Inadequacies.Procedure Revised to Specify Sequence of restoration.W/891110 Ltr ML19325C7891989-10-0505 October 1989 LER 89-011-00:on 890905,determined That Three Piping Penetrations in Condensate Storage Tank Encl Not Sealed.Root Cause Under Investigation.Penetrations Sealed & Tech Specs Surveillance Log revised.W/891005 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B8951993-07-30030 July 1993 LER 93-008-01:on 930518,determined That Control Air Not Analyzed to Function During Seismic Event Due to Lack of Understanding Significance of Control Air Availability for Long Term DG Operation.Ufsar Will Be Updated ML20046B8961993-07-30030 July 1993 LER 93-011-00:on 921219,930209 & 0415,SW Pumps SW-P-41B, SW-P-41B & SW-P-41D Declared Inoperable,Respectively Due High Vibration.Caused by Excessive Abrasive Particles in Ocean Water.Pumps replaced.W/930730 Ltr ML20045G6641993-07-0101 July 1993 LER 93-006-01:on 930401,Train a Svc Water Inoperable Due to Corrosion Product Buildup Between Valve Stem & Packing Follower.Returned SW-V54 to Operable Status & TS 3.7.4 Action D Exited on 930402.W/930701 Ltr ML20045D6791993-06-21021 June 1993 LER 93-002-01:on 930107,determined Potential for Premature Opening of Containment Bldg Spray Sump Isolation Valves. Caused by Failure to Adequately Recognize Potential Sys Interactions.Affected Procedures Revised ML20045C5421993-06-18018 June 1993 LER 93-010-00:on 930522,SG Level Oscillations Occurred in One SG Resulting in SG Being Overfed & Causing high-high SG Water Level.Caused by Personnel Error.Power Reduced to Approx 2.5% & FW to SGs restored.W/930618 Ltr ML20045D3681993-06-18018 June 1993 LER 93-009-00:on 930520,manual Reactor Trip from 100% Power Initiated When MSIV Closed During Quarterly Testing, Resulting in Feedwater & Two Emergency Feedwater Isolations. Caused by Debris in Valves.Valves Replaced ML20045C5341993-06-16016 June 1993 LER 93-008-00:on 930518,identified That Failure of Air Supply to EDG Jacket Cooling Water Temperature Control Valves During Seismic Event Could Cause Overcooling of Edgs. Operability Determination Performed for EDGs.W/930616 Ltr ML20045B5181993-06-11011 June 1993 LER 93-007-00:on 930512,protective Devices Not Analyzed to Function During Environ Excursions Due to Unknown Cause Which Is Under Review.Operability Determination Was performed.W/930611 Ltr ML20024H1621991-05-23023 May 1991 LER 91-004-00:on 910401,steam Generator Indicated That Valve Was Not Opening Properly During Plant Restart.Caused by Differential Pressure Across Dash Plate.Dash Plate Machining Performed on Valves to Prevent Valve disk.W/910523 Ltr ML20044B2281990-07-12012 July 1990 LER 90-014-00:on 900612,discovered That Sample Pump for Steam Generator Blowdown Flash Tank Drain Radiation Monitor Not Running.Caused by Suspended Solids in Steam Generator Blowdown Sys.Solids Cleared from Flow switch.W/900712 Ltr ML20043B6741990-05-23023 May 1990 LER 90-008-01:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Air Cleanup Sys Incapable of Producing Negative Pressure.Latching Mechanism Repaired & Mods to Doors/Hardware planned.W/900523 Ltr ML20043B3551990-05-21021 May 1990 LER 90-013-00:on 900419,discovered That Containment Personnel Hatch Unsecured for Approx 28 H.Caused by Installation of Locking Plate Upside Down & Placing Lock Through Only 1 Eyelet.Instructions posted.W/900521 Ltr ML20042F5521990-05-0202 May 1990 LER 90-012-00:on 900402,transmitter Failed to Provide Pressure to Reactor Protection Sys Due to Closed Isolation Valve.Caused by Failure to Identify Valve in Procedures. Valves Manipulated to Correct positions.W/900502 Ltr ML20042E1781990-04-0606 April 1990 LER 90-006-01:on 900206,control Room Ventilation Sys Train a Radiation Monitor Went Into High Alarm Condition.Caused by Mechanical Binding of Check source.Geiger-Muller Tube Replaced & Monitor Returned to svc.W/900406 Ltr ML20042E1741990-04-0505 April 1990 LER 90-011-00:on 900306,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Failure of Geiger-Muller Tube.Monitor Removed from Svc & Tube replaced.W/900405 Ltr ML20012F5181990-04-0404 April 1990 LER 90-010-00:on 900305,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Moisture in Detector Housing.Air Intake Monitors Cleaned & Desiccant Placed in housing.W/900404 Ltr ML20012C2461990-03-12012 March 1990 LER 90-008-00:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Emergency Air Cleanup Sys Inoperable.Plant Cooldown Initiated,Latching Mechanism Repaired & Door Returned to svc.W/900312 Ltr ML20012C2481990-03-12012 March 1990 LER 90-007-00:on 900208,when Source Check Removed from Control room,RM-6506B Entered High Alarm Condition,Causing ESF Actuation of Emergency Air Cleanup Sys.Caused by Mechanical Binding.Check Source replaced.W/900312 Ltr ML20012B4491990-03-0808 March 1990 LER 90-006-00:on 900206,Train a Radiation Monitor Went Into High Alarm Condition,Resulting in Actuation of Control Room Emergency Air Cleanup & Filtration Subsystem.Caused by Mechanical Binding.Detector Tube remounted.W/900308 Ltr ML20011F4671990-02-22022 February 1990 LER 90-004-00:on 900123,wide-range Gas Monitor Process Flow Rate Value for Vent Radiation Monitor Discovered at Default Instead of Actual Value.Caused by Personnel Error.Process Flow Restored & Technician counseled.W/900222 Ltr ML20006E4591990-02-15015 February 1990 LER 90-003-00:on 900116,wide-range Gas Monitor Low Range Pump Found Inoperable.Caused by Failed Pump Diaphragm Weakened by High Flow Condition.Ruptured Pump Diaphragm Replaced & Pump Returned to Normal operations.W/900215 Ltr ML20006E1731990-02-0808 February 1990 LER 90-002-00:on 900109,discovered That Auxiliary Sample Pump Used to Satisfy Action Requirements of Tech Spec Was Not Operating.Caused by Dislodged Power Fuse.Pump Relocated & Caution Tape Installed to Protect pump.W/900208 Ltr ML20006E1801990-02-0808 February 1990 LER 90-001-00:on 900109,wide Range Gas Monitor Low Range Pump Found to Be Inoperable,Resulting in Noncompliance W/ Tech Specs.Caused by Regulator Isolation Valves Being Left in Open Position.Walkdown of Skids conducted.W/900208 Ltr ML20005E2461989-12-29029 December 1989 LER 89-014-00:on 891129,auxiliary Transformer Supply Breaker to Vital Bus E5 Tripped When Remote Manual Override Relay Energized.Caused by Procedure Inadequacies in Procedure 0S1048.01.Procedure revised.W/891229 Ltr ML20011D4381989-12-19019 December 1989 LER 89-011-01:on 890905,three Unsealed Piping Penetrations in Condensate Storage Tank Encl Identified.Caused by Failure to Transfer Sealing Requirements Into Detail Drawings.Penetrations sealed.W/891219 Ltr ML19332C8511989-11-22022 November 1989 LER 89-013-00:on 891023,discovered That Monitor Used to Satisfy Requirements of Tech Spec 3.3.3.1,Action 27 Had Been Unplugged.Caused by Personnel Error.Individual Counseled & Meeting Held W/Health Physics technicians.W/891122 Ltr ML19325F3301989-11-10010 November 1989 LER 89-012-00:on 891011,one of Two Suction Valves on RHR Train a Pump Closed,Causing Loss of All RHR Cooling Capability.Caused by Procedure Inadequacies.Procedure Revised to Specify Sequence of restoration.W/891110 Ltr ML19325C7891989-10-0505 October 1989 LER 89-011-00:on 890905,determined That Three Piping Penetrations in Condensate Storage Tank Encl Not Sealed.Root Cause Under Investigation.Penetrations Sealed & Tech Specs Surveillance Log revised.W/891005 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H2841999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Seabrook Station. with ML20212D1461999-09-17017 September 1999 SER Accepting Request to Use Proposed Alternative to Certain Weld Repair Requirements in ASME Boiling & Pressure Vessel Code ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20212B8671999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Seabrook Station. with ML20210Q7581999-08-11011 August 1999 SER Approving Proposed Merger of CES & Bec,Which Will Create New Parent Company of Canal ML20210R9781999-08-0606 August 1999 ISI Exam Rept of Seabrook Station, for RFO 6,period 3 ML20210J8681999-08-0303 August 1999 SER Approving License Transfer from Montaup Electric Co to Little Bay Power Corp & Approval of Conforming Amend for Seabrook Station Unit 1 ML20210R6001999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Seabrook Station, Unit 1.With ML20210H1151999-06-30030 June 1999 Naesc Semi-Annual Fitness-for-Duty Rept for 990101-0630 ML20209H1371999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Seabrook Station, Unit 1.With ML20195G5391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Seabrook Station, Unit 1.With ML20195C0491999-05-25025 May 1999 Offshore Intake Seal Deterrent Barrier Design ML20206E4761999-04-30030 April 1999 LER 99-S01-00:on 990408,contractor Employee Was Granted Temporary Unescorted Access to Seabrook Station Protected Area.Caused by Failure of Contractor Employee to Provide Accurate Info.Individual Access Revoked.With ML20206N1751999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Seabrook Station, Unit 1.With ML20196L2081999-04-19019 April 1999 Rev 01-07-00 to RE-21, Cycle 7 Colr ML20205K5441999-03-31031 March 1999 Decommissioning Update ML20205L8141999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Seabrook Station. with ML20205C1981999-03-24024 March 1999 Safety Evaluation Concluding That Proposed Relief Request IR-8,Rev 1,provides Acceptable Alternative to ASME Code Requirements.Recommends Authorization of Proposed Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20207F4941999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Seabrook Station. with ML20199E6731998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Seabrook Station, Unit 1.With ML20198P1831998-12-31031 December 1998 LER 98-S01-00:on 981214,incomplete pre-employment Screening Records Was Noted.Caused by Failure of Contractor Employee to Provide Accurate Info.Subject Contractor Employees Employment Was Terminated.With ML20202E8241998-12-31031 December 1998 Naesc Semi-Annual Fitness-for-Duty Rept for 980701-981231 ML20196F5741998-12-0202 December 1998 Safety Evaluation Concluding That Licensee Has Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Seabrook ML20198B8661998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Seabrook Station, Unit 1.With ML20195D0311998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Seabrook Station, Unit 1.With ML20154H5291998-10-0808 October 1998 Special Rept:On 980928,meteorological Monitoring Instrumentation Channel Inoperable for Period Greater than 7 Days.Caused by Vendor to Follow Std Industry Practice for Calibr of Instrumentation.Instruments Installed ML20154M8421998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Seabrook Generating Station,Unit 1.With ML20151V5951998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Seabrook Station, Unit 1.With ML20237B4501998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Seabrook Station ML20236R1781998-06-30030 June 1998 Naesc Semi-Annual Fitness-for-Duty Rept for 980101-0630 ML20236M3591998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Seabrook Station, Unit 1 ML20237A4871998-06-0303 June 1998 North Atlantic Seabrook Station 1998 Exercise on 980603 ML20248M2951998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Seabrook Station, Unit 1 ML20247G2641998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Seabrook Station ML20247H3171998-04-27027 April 1998 Rev 1 to Seabrook Station SGs B & C Isi,May/June 1997 ML20216F8891998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Seabrook Station 05000443/LER-1998-002, Re Potential Safety Injection Pump Runout Conditions Identified on 980113.LER 98-002-00 Retracted1998-03-20020 March 1998 Re Potential Safety Injection Pump Runout Conditions Identified on 980113.LER 98-002-00 Retracted ML20216H9211998-03-13013 March 1998 Fitness for Duty Program Performance Data Personnel Subject to 10CFR26 ML20248L2811998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Seabrook Station, Unit 1 ML20197A7531998-02-27027 February 1998 Safety Evaluation Accepting License Request for Relief from ASME Code,Section IX Requirements Re Inservice Insp of RHR Heat Exchanger Nozzle Welds & Reactor Vessel Closure Head Nuts ML20202G3701998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Seabrook Station ML20198G0271997-12-31031 December 1997 Commonwealth Energy Sys 1997 Annual Rept ML20248L7711997-12-31031 December 1997 Western Massachusetts Electric 1997 Annual Rept. Supporting Info,Encl ML20198G1021997-12-31031 December 1997 Baycorp Holdings 1997 Annual Rept ML20198N7021997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Seabrook Station, Unit 1 ML20198G0351997-12-31031 December 1997 Eastern Edison Co 1997 Annual Rept ML20198G0681997-12-31031 December 1997 Taunton Municipal Lighting Plant 1997 Annual Rept ML20248L7671997-12-31031 December 1997 North Atlantic 1997 Annual Rept ML20198F9511997-12-31031 December 1997 United Illuminating Co 1997 Annual Rept ML20236M9561997-12-31031 December 1997 Amended Public Service of New Hampshire 1997 Annual Rept 1999-09-30
[Table view] |
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' P.O. Box 300 -
NOdh =
Seabrook ws O3874 Telephone (603)474 9521 j[h [ Facsimile (603)474 2987 Energy Service Corporation Ted C. Feigenbaum Senior Vice President and Chief Nuclear Officer NYN- 93099 July 1,1993 United States Nuclear Regulatory Commission Washington, D.C. 20555 Attention: Document Control Desk
References:
(a) Facility Operating License No. NPF-86, Docket No. 50-443 ,
(b) North Atlantic Letter NYN 93065 dated April 30,1993," Licensee Event Report (LER) 93-006-00: Train A Service Water Inoperability," T.C.
Feigenbaum to USNRC
Subject:
Supplemental Licensee Event Report (LER) 93-06-01; " Train A Service Water Inoperability" '!
Gentlemen:
Enclosed please find Licensee Event Report (LER) No. 93-06-01 for Seabrook Station. This submittal provides supplemental information regarding previous occurrences of the event, root cause determination, and corrective actions.
Should you require further information regarding this matter, please contact Mr-James M. Pe:;chel, Regulatory Compliance Manager at (603) 474-9521 extenden 3772.
Very tr yours, /
g fgds,- tr Ted C. Fei enbaum TCF:MDO/act
Enclosures:
NRC Forms 366/366A i
130064 j
9307150023 930701 }
PDR g
ADOCK 05000443-PDR D@)a member of the Northeast Utilities L. system
i
. United Sta'tes Nucler.r Regulatory Commission July 1,1993 ,
4 Attention: Document Control Desk Page two Mr. Thomas T. Martin
- cc: ,
Regional Administrator United States Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Mr. Albert W. De Agazio, Sr. Project Manager Project Directorate I-4 Division of Reactor Projects U.S. Nuclear Regulatory Commission ,
Washington, DC 20555 Mr. Noel Dudley NRC Senior Resident Inspector
- P.O. Box 1149 Seabrook, nil 03874 INPO -
Records Center +
700 Galleria Parkway Atlanta, GA 30339-5957 P
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l 1
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NRC FORM 366 U.S. NUCLEAR REGULATORY CDP 9tlSSIC APPROULD IlY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH LLfCTl " "f "E$
LICENSEE EVENT REPORT (LER) $ARD f0 I"f "
S EcAR9xNG BURDlN kS Ti THE INFORMATION AND RECORDS MANAGEMENT BRANCH "k
(MNBB 7714), U.S. NUCLEAR REGUL ATORY COMMISS10N, (See reverse for required nunber of digits / characters for each block) WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE Of MANAGEMENT AND BUDGET, WASHINGTON, DC 20503, FACILITY NAME (1) DOCKLT NUMBER (2) PAGE (3)
Seabrook Station 05000443 1 OF 3 TillE(4) '
Train A Service Water Inoperability EVENI DATE (5) llR NUMillR (6) RIPORI DALE (1) OIHIR FACILIIIf 5 INV0t Vf D (8)
SEQUENTIAL REVISION MONTH DAY YEAR YEAR NUMBER NUMBER MONTH DAY YEAR 05000 FACILITY NAME DOCKET UMBE 4 1 93 93 -- 006 -- 01 7 01 93 OPERATING y IHIS REPORI IS SUHMllllD PURSUANI 10 THE RIQUIREMINIS Of 10 CFR 9: (Check one or more) (11)
MODE (9) 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73.71(b)
POWER 20.405(a)(1)(1) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c) 100 LEVEL (10) 20.405(a)(1)(11) 50.36(c)(2) 50.73(a)(2)(vii) OIHER 20.405(a)(1)(lit) X 50.73(a)(2)(1) 50.73(a)(2)(viii)(A) (Specify in trac ow 20.405(a)(1)(iv) 50.73(a)(2)(li) 50.73(a)(2)(viii)(B) 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) NRC Form 366A) llCIMSIf CONIACT FOR THIS lf R (12)
NAME lELEPHONE NUMBER (Include Area Code)
Mr. James M. Peschel, Regulatory Compliance Mngr. (603)474-9521 ext. 3772 COMPIEll DNE t INF IOR LAOf COMPONINI I AltuRF DESCRIHED IN THIS Rf PORI (13)
E E 0 CAUSE SYSTEM COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER p p 3 SUPPilMINIAI RIPORT EXPICIID (14) EXPECTED MONTH DAY YE AR YES SullMISSION (If yes, complete EXPECTED SUBMISSION DATE). X NO DATE(15)
ABSTRACI (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On April 1,1993, while performing surveillance testing, the Train A Cooling Tower Pump discharge valve could not be fully closed utilizing the motor operator attached to the valve. When this valve is not fully closed an interlock prevents starting of the associated train's Senice Water (SW) pumps and Cooling Tower Pump [BI). The pumps would not start automatically follow'mg a Loss of Offsite Power with the valve not fully closed and therefore, the pumps were declared inoperable.
Technical Specification 3.7.4, Service Water System, does not permit plant operation with 3 pumps within one loop inoperable and thus Technical Specification 3.0.3 was entered. The valve failed to close due to a corrosion product buildup between the vah'e stem and packing follower.
Subsequent investigation has determined that on two previous occasions, maintenance was performed on the Train A Cooling I
Tower Pump Discharge Valve which resulted in the inoperability of the Train A SW pumps. . The maintenance was performed on October 23,1990 and May 31,1991. On both of these occasions Technical Specification Action 3.7.4d was entered for one Cooling Tower Senice Water Pump inoperable. The maintenance that was performed did not involve a failure of the valve to close due to corrosion product buildup or over-torquing the packing gland.
There were no adverse safety consequences as a result of the event. Train B SW was OPERABLE and in operation for each I of the occasions that Train A SW was inoperable.
NRC FORM 366 (5-92)
NRC toali 366A U.S. NUCLI AR RLGULA10R7 COMMISSIC^] APPROVLD liY ONU NO. 3150-0104
'(5-92) EXPIRES 5/31/95 ESilMATED BURDEN PER RESPONSE TO COMPLY Wi1H IHIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE 10 LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECOR05 MANAGEMENT BRANCH (MNBB 7714), U.S. NUCtE AR REGULATORY COMMISSION, TEXT CONTINUATION WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE Of MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACIL11Y NAME (1) DOCKLI NUMBlR (?) llR NUMBIR (6? PAGE (3) ygg SEQUENTIAL REVISION Seabrook Station " "
05000443 93 2 OF 3
-- 0 0 6 --
TLK1 (I( Inore space is requfred, use additionai coples of MC l'orm 36M) (l1)
The Service Water (SW) System [Bl] at Seabrook Station is comprised of two redundant trains. Each train has two pumps which supply cooling water from the ocean and one pump which supplies cooling water from a mechanical draft cooling tower.
Operation of any one of the six pumps (2 trains of 3 pumps) is adequate to mitigate the consequences of a design basis event.
On April 1,1993 SW Train A valve testing was being performed. Part of the testing involves transferring SW supply from the ocean to the cooling tower and back to the ocean so that the open and close times for Train A Cooling Tower Pump Discharge Valve, SW-V54, can be measured. At 0300 of the same day, while measuring SW-V54's close time, the valve stopped before the fully closed position was reached. Operators reestablished SW cooling from the cooling tower by opening SW-V54 and sent personnel to investigate the cause of the failure. At 0318 the three pumps within Train A SW were declared to be inoperable because neither the LCO or ACTION requirements for Technical Specification 3.7.4, Service Water System, could be met. Technical Specification 3.03 was entered at this time. At 0330 of the same day SW-V54 was closed manually and SW was transferred back to the ocean cooling supply. Once SW cooling was esteblished from the ocean the two ocean SW pumps were declared to be OPERABLE, Technical Specification 3.03 was exited and Technical Specification 3.7.4 ACrlON d was entered for the Cooling Tower Pump being inoperable.
The interlock which prevents the SW pumps from starting whcn SW-V54 is not fully closed has two purposes. First it prevents starting the Cooling Towei Pump when its discharge valve is not fully closed and second, it prevents the ocean SW pumps from filling the Cooling Tower with seawater. The three Train A SW pumps were declared to be inoperable because they were not capable of starting automatically following a Loss of Offsite Power (LOP) after the Emergency Diesel Generators re-energize the emergency busses. In addition, Technical Specification Surveillance Requirement 4.7.4b.2) also requires that the SW pumps be capable of starting automatically. Once SW V54 was closed manually, the ocean SW pumps became OPERABLE because they were now capable of starting automatically.
Subsequent investigation has determined that on two previous occasions, maintenance was performed on SW-V54 which resulted in the inoperability of the Train A SW pumps. The maintenance was performed on October 23,1990 and May 31, 1991 On both of these occassions Technical Specification Action 3.7.4d was incorrectly entered for one Cooling Tower Service Water Pump inoperable while Technical Specification 3.03 should have been entered. The maintenance that was performed was not associated with a failure of the valve to close due to corrosion product buildup or over-torquing the packing gland.
There were no occasions where maintenance was performed on the B Train Cooling Tower Pump Discharge Valve (SW-V25),
which resulted in the inoperability of Train B SW.
Root Cause The valve failed to close due to corrosion product buildup between the valve stem and packing follower. This caused increased friction between the valve stem and packing follower which resulted in a higher loading on the valves motor operator. The increased loading on the valve stem prematurely actuated a torque switch which stopped the valve prior to full stroke completion.
A contributing cause for the valve's failure is procedure inadequacy. The torque value specified for the valve's packing gland fastener caused over-torquing of the valve's packing during installation. This caused increased friction and resulting valve stem loading and contributed to the premature actuation of the torque switch.
~i E FORM 366A (5-92)
NRC FGtM 366A U.S. NUClLAR REGULA10RY CurtilSSICQ APPROVLD BY OMO NO. 3150-0104
'(5'-92)' EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REOUESTt 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, TEXT CONTINUATION WASHINGTON, DC 20555-000), AND TO THE PAPERWORK RE0UCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
F ACILI1Y NAME (1) DoCKEl NUMBER (?) if R NUMULR (6: PAGE (3)
SEQUENTIAL REVISION YEAR Seabrook Station """ """ "
05000443 93 0 3 OF 3
-- 0 0 6 --
TLKl (If wre space is required, use additional copies of MC Form 366A) (11)
An additional Root Cause, related to the subsequent investigation, is attributed to personnel error. Specifically that control room personnel failed to identify the need to limit work activities on SW-V54.
Corrective Action L SW-V54 was returned to OPERABLE status and Technical Specification 3.7.4 ACTION d. exited at 0523 on 4/2/93.
- 2. The diagnostic surveillance frequency for SW-54 will be changed from each refueling to quarterly for the next two quarters.
- 3. A new maximum packing gland fastener torque value for the 24 inch Service Water butterfly valves will be established.
- 4. An Engineering Evaluation will be performed to evaluate recommendations made by the valve vendor. These recommendations will be applied to other valves if applicable.
- 5. Diagnostic testing, to measure opening and closing torque, is scheduled to be completed on 24 inch Service Water motor operated valves during the next refueling outage.
- 6. The Repetitive Task Sheets associated with the Cooling Tower Pump Discharge Valves will be revised to reflect work limitations during applicable Modes.
- 7. A Standing Operating Order will be developed and issued discussing the limitations of working on the Cooling Tower Pump Discharge Valves.
- 8. The event will be discussed with the operators as part of Requalification Training.
Safety Consetiuences There were no adverse safety consequences as a result of this event. The operation of only one train of SW is adequate to mitigate the consequences of a design basis event. Train H SW was operable for each of the occasions that Train A SW was inoperable.
Previous Occurrences This is the second event where personnel error has been the cause of the failure to recognize that maintenance activities would result in equipment inoperability and a condition prohibited by the Technic:d Specifications. A previous occurrence was reported by North Atlantic in LER 92 07 00. On that occassion work activities were permitted which resulted in the inoperability of the Train A Containment Enclosure Emergency Air Cleanup System at the same time that the Train II Emergency Diesel Generator was inoperable.
At the time of the event the plant was in Mode 1 at m0% power.
NRCFORM366A($-92)