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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B8951993-07-30030 July 1993 LER 93-008-01:on 930518,determined That Control Air Not Analyzed to Function During Seismic Event Due to Lack of Understanding Significance of Control Air Availability for Long Term DG Operation.Ufsar Will Be Updated ML20046B8961993-07-30030 July 1993 LER 93-011-00:on 921219,930209 & 0415,SW Pumps SW-P-41B, SW-P-41B & SW-P-41D Declared Inoperable,Respectively Due High Vibration.Caused by Excessive Abrasive Particles in Ocean Water.Pumps replaced.W/930730 Ltr ML20045G6641993-07-0101 July 1993 LER 93-006-01:on 930401,Train a Svc Water Inoperable Due to Corrosion Product Buildup Between Valve Stem & Packing Follower.Returned SW-V54 to Operable Status & TS 3.7.4 Action D Exited on 930402.W/930701 Ltr ML20045D6791993-06-21021 June 1993 LER 93-002-01:on 930107,determined Potential for Premature Opening of Containment Bldg Spray Sump Isolation Valves. Caused by Failure to Adequately Recognize Potential Sys Interactions.Affected Procedures Revised ML20045C5421993-06-18018 June 1993 LER 93-010-00:on 930522,SG Level Oscillations Occurred in One SG Resulting in SG Being Overfed & Causing high-high SG Water Level.Caused by Personnel Error.Power Reduced to Approx 2.5% & FW to SGs restored.W/930618 Ltr ML20045D3681993-06-18018 June 1993 LER 93-009-00:on 930520,manual Reactor Trip from 100% Power Initiated When MSIV Closed During Quarterly Testing, Resulting in Feedwater & Two Emergency Feedwater Isolations. Caused by Debris in Valves.Valves Replaced ML20045C5341993-06-16016 June 1993 LER 93-008-00:on 930518,identified That Failure of Air Supply to EDG Jacket Cooling Water Temperature Control Valves During Seismic Event Could Cause Overcooling of Edgs. Operability Determination Performed for EDGs.W/930616 Ltr ML20045B5181993-06-11011 June 1993 LER 93-007-00:on 930512,protective Devices Not Analyzed to Function During Environ Excursions Due to Unknown Cause Which Is Under Review.Operability Determination Was performed.W/930611 Ltr ML20024H1621991-05-23023 May 1991 LER 91-004-00:on 910401,steam Generator Indicated That Valve Was Not Opening Properly During Plant Restart.Caused by Differential Pressure Across Dash Plate.Dash Plate Machining Performed on Valves to Prevent Valve disk.W/910523 Ltr ML20044B2281990-07-12012 July 1990 LER 90-014-00:on 900612,discovered That Sample Pump for Steam Generator Blowdown Flash Tank Drain Radiation Monitor Not Running.Caused by Suspended Solids in Steam Generator Blowdown Sys.Solids Cleared from Flow switch.W/900712 Ltr ML20043B6741990-05-23023 May 1990 LER 90-008-01:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Air Cleanup Sys Incapable of Producing Negative Pressure.Latching Mechanism Repaired & Mods to Doors/Hardware planned.W/900523 Ltr ML20043B3551990-05-21021 May 1990 LER 90-013-00:on 900419,discovered That Containment Personnel Hatch Unsecured for Approx 28 H.Caused by Installation of Locking Plate Upside Down & Placing Lock Through Only 1 Eyelet.Instructions posted.W/900521 Ltr ML20042F5521990-05-0202 May 1990 LER 90-012-00:on 900402,transmitter Failed to Provide Pressure to Reactor Protection Sys Due to Closed Isolation Valve.Caused by Failure to Identify Valve in Procedures. Valves Manipulated to Correct positions.W/900502 Ltr ML20042E1781990-04-0606 April 1990 LER 90-006-01:on 900206,control Room Ventilation Sys Train a Radiation Monitor Went Into High Alarm Condition.Caused by Mechanical Binding of Check source.Geiger-Muller Tube Replaced & Monitor Returned to svc.W/900406 Ltr ML20042E1741990-04-0505 April 1990 LER 90-011-00:on 900306,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Failure of Geiger-Muller Tube.Monitor Removed from Svc & Tube replaced.W/900405 Ltr ML20012F5181990-04-0404 April 1990 LER 90-010-00:on 900305,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Moisture in Detector Housing.Air Intake Monitors Cleaned & Desiccant Placed in housing.W/900404 Ltr ML20012C2461990-03-12012 March 1990 LER 90-008-00:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Emergency Air Cleanup Sys Inoperable.Plant Cooldown Initiated,Latching Mechanism Repaired & Door Returned to svc.W/900312 Ltr ML20012C2481990-03-12012 March 1990 LER 90-007-00:on 900208,when Source Check Removed from Control room,RM-6506B Entered High Alarm Condition,Causing ESF Actuation of Emergency Air Cleanup Sys.Caused by Mechanical Binding.Check Source replaced.W/900312 Ltr ML20012B4491990-03-0808 March 1990 LER 90-006-00:on 900206,Train a Radiation Monitor Went Into High Alarm Condition,Resulting in Actuation of Control Room Emergency Air Cleanup & Filtration Subsystem.Caused by Mechanical Binding.Detector Tube remounted.W/900308 Ltr ML20011F4671990-02-22022 February 1990 LER 90-004-00:on 900123,wide-range Gas Monitor Process Flow Rate Value for Vent Radiation Monitor Discovered at Default Instead of Actual Value.Caused by Personnel Error.Process Flow Restored & Technician counseled.W/900222 Ltr ML20006E4591990-02-15015 February 1990 LER 90-003-00:on 900116,wide-range Gas Monitor Low Range Pump Found Inoperable.Caused by Failed Pump Diaphragm Weakened by High Flow Condition.Ruptured Pump Diaphragm Replaced & Pump Returned to Normal operations.W/900215 Ltr ML20006E1731990-02-0808 February 1990 LER 90-002-00:on 900109,discovered That Auxiliary Sample Pump Used to Satisfy Action Requirements of Tech Spec Was Not Operating.Caused by Dislodged Power Fuse.Pump Relocated & Caution Tape Installed to Protect pump.W/900208 Ltr ML20006E1801990-02-0808 February 1990 LER 90-001-00:on 900109,wide Range Gas Monitor Low Range Pump Found to Be Inoperable,Resulting in Noncompliance W/ Tech Specs.Caused by Regulator Isolation Valves Being Left in Open Position.Walkdown of Skids conducted.W/900208 Ltr ML20005E2461989-12-29029 December 1989 LER 89-014-00:on 891129,auxiliary Transformer Supply Breaker to Vital Bus E5 Tripped When Remote Manual Override Relay Energized.Caused by Procedure Inadequacies in Procedure 0S1048.01.Procedure revised.W/891229 Ltr ML20011D4381989-12-19019 December 1989 LER 89-011-01:on 890905,three Unsealed Piping Penetrations in Condensate Storage Tank Encl Identified.Caused by Failure to Transfer Sealing Requirements Into Detail Drawings.Penetrations sealed.W/891219 Ltr ML19332C8511989-11-22022 November 1989 LER 89-013-00:on 891023,discovered That Monitor Used to Satisfy Requirements of Tech Spec 3.3.3.1,Action 27 Had Been Unplugged.Caused by Personnel Error.Individual Counseled & Meeting Held W/Health Physics technicians.W/891122 Ltr ML19325F3301989-11-10010 November 1989 LER 89-012-00:on 891011,one of Two Suction Valves on RHR Train a Pump Closed,Causing Loss of All RHR Cooling Capability.Caused by Procedure Inadequacies.Procedure Revised to Specify Sequence of restoration.W/891110 Ltr ML19325C7891989-10-0505 October 1989 LER 89-011-00:on 890905,determined That Three Piping Penetrations in Condensate Storage Tank Encl Not Sealed.Root Cause Under Investigation.Penetrations Sealed & Tech Specs Surveillance Log revised.W/891005 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B8951993-07-30030 July 1993 LER 93-008-01:on 930518,determined That Control Air Not Analyzed to Function During Seismic Event Due to Lack of Understanding Significance of Control Air Availability for Long Term DG Operation.Ufsar Will Be Updated ML20046B8961993-07-30030 July 1993 LER 93-011-00:on 921219,930209 & 0415,SW Pumps SW-P-41B, SW-P-41B & SW-P-41D Declared Inoperable,Respectively Due High Vibration.Caused by Excessive Abrasive Particles in Ocean Water.Pumps replaced.W/930730 Ltr ML20045G6641993-07-0101 July 1993 LER 93-006-01:on 930401,Train a Svc Water Inoperable Due to Corrosion Product Buildup Between Valve Stem & Packing Follower.Returned SW-V54 to Operable Status & TS 3.7.4 Action D Exited on 930402.W/930701 Ltr ML20045D6791993-06-21021 June 1993 LER 93-002-01:on 930107,determined Potential for Premature Opening of Containment Bldg Spray Sump Isolation Valves. Caused by Failure to Adequately Recognize Potential Sys Interactions.Affected Procedures Revised ML20045C5421993-06-18018 June 1993 LER 93-010-00:on 930522,SG Level Oscillations Occurred in One SG Resulting in SG Being Overfed & Causing high-high SG Water Level.Caused by Personnel Error.Power Reduced to Approx 2.5% & FW to SGs restored.W/930618 Ltr ML20045D3681993-06-18018 June 1993 LER 93-009-00:on 930520,manual Reactor Trip from 100% Power Initiated When MSIV Closed During Quarterly Testing, Resulting in Feedwater & Two Emergency Feedwater Isolations. Caused by Debris in Valves.Valves Replaced ML20045C5341993-06-16016 June 1993 LER 93-008-00:on 930518,identified That Failure of Air Supply to EDG Jacket Cooling Water Temperature Control Valves During Seismic Event Could Cause Overcooling of Edgs. Operability Determination Performed for EDGs.W/930616 Ltr ML20045B5181993-06-11011 June 1993 LER 93-007-00:on 930512,protective Devices Not Analyzed to Function During Environ Excursions Due to Unknown Cause Which Is Under Review.Operability Determination Was performed.W/930611 Ltr ML20024H1621991-05-23023 May 1991 LER 91-004-00:on 910401,steam Generator Indicated That Valve Was Not Opening Properly During Plant Restart.Caused by Differential Pressure Across Dash Plate.Dash Plate Machining Performed on Valves to Prevent Valve disk.W/910523 Ltr ML20044B2281990-07-12012 July 1990 LER 90-014-00:on 900612,discovered That Sample Pump for Steam Generator Blowdown Flash Tank Drain Radiation Monitor Not Running.Caused by Suspended Solids in Steam Generator Blowdown Sys.Solids Cleared from Flow switch.W/900712 Ltr ML20043B6741990-05-23023 May 1990 LER 90-008-01:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Air Cleanup Sys Incapable of Producing Negative Pressure.Latching Mechanism Repaired & Mods to Doors/Hardware planned.W/900523 Ltr ML20043B3551990-05-21021 May 1990 LER 90-013-00:on 900419,discovered That Containment Personnel Hatch Unsecured for Approx 28 H.Caused by Installation of Locking Plate Upside Down & Placing Lock Through Only 1 Eyelet.Instructions posted.W/900521 Ltr ML20042F5521990-05-0202 May 1990 LER 90-012-00:on 900402,transmitter Failed to Provide Pressure to Reactor Protection Sys Due to Closed Isolation Valve.Caused by Failure to Identify Valve in Procedures. Valves Manipulated to Correct positions.W/900502 Ltr ML20042E1781990-04-0606 April 1990 LER 90-006-01:on 900206,control Room Ventilation Sys Train a Radiation Monitor Went Into High Alarm Condition.Caused by Mechanical Binding of Check source.Geiger-Muller Tube Replaced & Monitor Returned to svc.W/900406 Ltr ML20042E1741990-04-0505 April 1990 LER 90-011-00:on 900306,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Failure of Geiger-Muller Tube.Monitor Removed from Svc & Tube replaced.W/900405 Ltr ML20012F5181990-04-0404 April 1990 LER 90-010-00:on 900305,actuation of Control Room Emergency Air Cleanup & Filtration Subsystem Occurred.Caused by Moisture in Detector Housing.Air Intake Monitors Cleaned & Desiccant Placed in housing.W/900404 Ltr ML20012C2461990-03-12012 March 1990 LER 90-008-00:on 900209,latching Mechanism for Door Entering Containment Encl Bldg Failed,Rendering Emergency Air Cleanup Sys Inoperable.Plant Cooldown Initiated,Latching Mechanism Repaired & Door Returned to svc.W/900312 Ltr ML20012C2481990-03-12012 March 1990 LER 90-007-00:on 900208,when Source Check Removed from Control room,RM-6506B Entered High Alarm Condition,Causing ESF Actuation of Emergency Air Cleanup Sys.Caused by Mechanical Binding.Check Source replaced.W/900312 Ltr ML20012B4491990-03-0808 March 1990 LER 90-006-00:on 900206,Train a Radiation Monitor Went Into High Alarm Condition,Resulting in Actuation of Control Room Emergency Air Cleanup & Filtration Subsystem.Caused by Mechanical Binding.Detector Tube remounted.W/900308 Ltr ML20011F4671990-02-22022 February 1990 LER 90-004-00:on 900123,wide-range Gas Monitor Process Flow Rate Value for Vent Radiation Monitor Discovered at Default Instead of Actual Value.Caused by Personnel Error.Process Flow Restored & Technician counseled.W/900222 Ltr ML20006E4591990-02-15015 February 1990 LER 90-003-00:on 900116,wide-range Gas Monitor Low Range Pump Found Inoperable.Caused by Failed Pump Diaphragm Weakened by High Flow Condition.Ruptured Pump Diaphragm Replaced & Pump Returned to Normal operations.W/900215 Ltr ML20006E1731990-02-0808 February 1990 LER 90-002-00:on 900109,discovered That Auxiliary Sample Pump Used to Satisfy Action Requirements of Tech Spec Was Not Operating.Caused by Dislodged Power Fuse.Pump Relocated & Caution Tape Installed to Protect pump.W/900208 Ltr ML20006E1801990-02-0808 February 1990 LER 90-001-00:on 900109,wide Range Gas Monitor Low Range Pump Found to Be Inoperable,Resulting in Noncompliance W/ Tech Specs.Caused by Regulator Isolation Valves Being Left in Open Position.Walkdown of Skids conducted.W/900208 Ltr ML20005E2461989-12-29029 December 1989 LER 89-014-00:on 891129,auxiliary Transformer Supply Breaker to Vital Bus E5 Tripped When Remote Manual Override Relay Energized.Caused by Procedure Inadequacies in Procedure 0S1048.01.Procedure revised.W/891229 Ltr ML20011D4381989-12-19019 December 1989 LER 89-011-01:on 890905,three Unsealed Piping Penetrations in Condensate Storage Tank Encl Identified.Caused by Failure to Transfer Sealing Requirements Into Detail Drawings.Penetrations sealed.W/891219 Ltr ML19332C8511989-11-22022 November 1989 LER 89-013-00:on 891023,discovered That Monitor Used to Satisfy Requirements of Tech Spec 3.3.3.1,Action 27 Had Been Unplugged.Caused by Personnel Error.Individual Counseled & Meeting Held W/Health Physics technicians.W/891122 Ltr ML19325F3301989-11-10010 November 1989 LER 89-012-00:on 891011,one of Two Suction Valves on RHR Train a Pump Closed,Causing Loss of All RHR Cooling Capability.Caused by Procedure Inadequacies.Procedure Revised to Specify Sequence of restoration.W/891110 Ltr ML19325C7891989-10-0505 October 1989 LER 89-011-00:on 890905,determined That Three Piping Penetrations in Condensate Storage Tank Encl Not Sealed.Root Cause Under Investigation.Penetrations Sealed & Tech Specs Surveillance Log revised.W/891005 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217H2841999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Seabrook Station. with ML20212D1461999-09-17017 September 1999 SER Accepting Request to Use Proposed Alternative to Certain Weld Repair Requirements in ASME Boiling & Pressure Vessel Code ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20212B8671999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Seabrook Station. with ML20210Q7581999-08-11011 August 1999 SER Approving Proposed Merger of CES & Bec,Which Will Create New Parent Company of Canal ML20210R9781999-08-0606 August 1999 ISI Exam Rept of Seabrook Station, for RFO 6,period 3 ML20210J8681999-08-0303 August 1999 SER Approving License Transfer from Montaup Electric Co to Little Bay Power Corp & Approval of Conforming Amend for Seabrook Station Unit 1 ML20210R6001999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Seabrook Station, Unit 1.With ML20210H1151999-06-30030 June 1999 Naesc Semi-Annual Fitness-for-Duty Rept for 990101-0630 ML20209H1371999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Seabrook Station, Unit 1.With ML20195G5391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Seabrook Station, Unit 1.With ML20195C0491999-05-25025 May 1999 Offshore Intake Seal Deterrent Barrier Design ML20206E4761999-04-30030 April 1999 LER 99-S01-00:on 990408,contractor Employee Was Granted Temporary Unescorted Access to Seabrook Station Protected Area.Caused by Failure of Contractor Employee to Provide Accurate Info.Individual Access Revoked.With ML20206N1751999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Seabrook Station, Unit 1.With ML20196L2081999-04-19019 April 1999 Rev 01-07-00 to RE-21, Cycle 7 Colr ML20205K5441999-03-31031 March 1999 Decommissioning Update ML20205L8141999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Seabrook Station. with ML20205C1981999-03-24024 March 1999 Safety Evaluation Concluding That Proposed Relief Request IR-8,Rev 1,provides Acceptable Alternative to ASME Code Requirements.Recommends Authorization of Proposed Alternative Pursuant to 10CFR50.55a(a)(3)(i) ML20207F4941999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Seabrook Station. with ML20199E6731998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Seabrook Station, Unit 1.With ML20198P1831998-12-31031 December 1998 LER 98-S01-00:on 981214,incomplete pre-employment Screening Records Was Noted.Caused by Failure of Contractor Employee to Provide Accurate Info.Subject Contractor Employees Employment Was Terminated.With ML20202E8241998-12-31031 December 1998 Naesc Semi-Annual Fitness-for-Duty Rept for 980701-981231 ML20196F5741998-12-0202 December 1998 Safety Evaluation Concluding That Licensee Has Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Seabrook ML20198B8661998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Seabrook Station, Unit 1.With ML20195D0311998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Seabrook Station, Unit 1.With ML20154H5291998-10-0808 October 1998 Special Rept:On 980928,meteorological Monitoring Instrumentation Channel Inoperable for Period Greater than 7 Days.Caused by Vendor to Follow Std Industry Practice for Calibr of Instrumentation.Instruments Installed ML20154M8421998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Seabrook Generating Station,Unit 1.With ML20151V5951998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Seabrook Station, Unit 1.With ML20237B4501998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Seabrook Station ML20236R1781998-06-30030 June 1998 Naesc Semi-Annual Fitness-for-Duty Rept for 980101-0630 ML20236M3591998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Seabrook Station, Unit 1 ML20237A4871998-06-0303 June 1998 North Atlantic Seabrook Station 1998 Exercise on 980603 ML20248M2951998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Seabrook Station, Unit 1 ML20247G2641998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Seabrook Station ML20247H3171998-04-27027 April 1998 Rev 1 to Seabrook Station SGs B & C Isi,May/June 1997 ML20216F8891998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Seabrook Station 05000443/LER-1998-002, Re Potential Safety Injection Pump Runout Conditions Identified on 980113.LER 98-002-00 Retracted1998-03-20020 March 1998 Re Potential Safety Injection Pump Runout Conditions Identified on 980113.LER 98-002-00 Retracted ML20216H9211998-03-13013 March 1998 Fitness for Duty Program Performance Data Personnel Subject to 10CFR26 ML20248L2811998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Seabrook Station, Unit 1 ML20197A7531998-02-27027 February 1998 Safety Evaluation Accepting License Request for Relief from ASME Code,Section IX Requirements Re Inservice Insp of RHR Heat Exchanger Nozzle Welds & Reactor Vessel Closure Head Nuts ML20202G3701998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Seabrook Station ML20198G0271997-12-31031 December 1997 Commonwealth Energy Sys 1997 Annual Rept ML20248L7711997-12-31031 December 1997 Western Massachusetts Electric 1997 Annual Rept. Supporting Info,Encl ML20198G1021997-12-31031 December 1997 Baycorp Holdings 1997 Annual Rept ML20198N7021997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Seabrook Station, Unit 1 ML20198G0351997-12-31031 December 1997 Eastern Edison Co 1997 Annual Rept ML20198G0681997-12-31031 December 1997 Taunton Municipal Lighting Plant 1997 Annual Rept ML20248L7671997-12-31031 December 1997 North Atlantic 1997 Annual Rept ML20198F9511997-12-31031 December 1997 United Illuminating Co 1997 Annual Rept ML20236M9561997-12-31031 December 1997 Amended Public Service of New Hampshire 1997 Annual Rept 1999-09-30
[Table view] |
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P.O. Box 300 '
NOdh =
seedrook. "H 03874 Telephone (603)474-9521
[C Facsimile (603)474-2987
' Energy Service Corporation Ted c. Feigenbaum -
Senior Vice President and Chief NuclearOfficer NYN-93087 -
June 18,1993 United States Nuclear Regulatory Commission Washinct on, D.C. 20555 Attention: Document Control Desk
Reference:
Facility Operating License No. NPF-86, Docket No. 50-443
Subject:
Licensee Event Report (LER) 93-10 00: " Engineered Safety Features Actuation- Feedwater Isolation" Gentlemen:
Enclosed is Licensee Event Report (LER) No. 93-10-00 for Seabrook Station. This submittal documents an event which was discovered on May 22,1993. This event is being reported pursuant to 10CFR50.73(a)(2)(iv).
Should you require further information regarding this matter, please contact Mr.
James M. Peschel, Regulatory Compliance Manager at (603) 474 9521 extension 3772. ,
Very truly yours,
[fC Ted C. Feigenba m TCF:EWM/cwm ,
Enclosures:
NRC Forms 366/366A i
2200C7 9306230270 930618 E a member of the Northeast Utilities system
.PUR
-S ADOCK 05000443 Td PDR. y /
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=. __. ,
9 United States Nuclear Regulatory Commission June-18,1993 -
Atterition: Document Control Desk Page two ,
.I cc: Mr. Thomas T. Martin )
Regional Administrator ,
United States Nuclear Regulatory Commission l Region 1 _.'
475 Allen' dale Road King of Prussia, PA 19406-Mr. Albert W. De Agazio, Sr. Project Manager Project Directorate I-4 -1 Division of Reactor Projects j U.S. Nuclear Regulatory Commission Washington, DC 20555 Mr. Noel Dudley .
NRC Senior Resident Inspector P.O. Ilox 1149 Seabrook,' NH 03874 ,
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INPO Records Center 700 Galleria Parkway Atlanta, GA 30339-5957 i F
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i OtC IORM 366 U.S. NUCtLAR REGUI AIORY COPHISSION APPROULD B7 OMD CD. 3150-0104 i (5-92) EXPlRES 5/31/95 i 1
ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
LICENSEE EVEN'I, REPORT (LER) FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCd (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION.
(See reverse for required number of digits / characters for each block) WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OfflCE OF ,
MANAGEMFNT AND BUDGET, WASHINGTON, DC 20503. !
~
I ACILilY N/ME (1) DOCKL1 NUMBLR (2) PAGE (3)
Seabrook Station 05000443 1 OF 5 Till t' (4)
Engineered Safety Features Actuation- Feedwater Isolation (Vf MI DAll (5) tfR NUMBfR (6) RfPORI DAlf (7) OlHIR f ACit ITIES INV0t Vf D (8)
MONTH DAY YEAR YEAR NUMBER NUMPER MONTH DAY YEAR 05000 FA M I M NAML NET ""
05 22 93 93 10 00 06 18 93 O 0O OPERATING y IHIS RFPORT IS SUBMIlllD PURSUANI 10 THE REQUIRIMINIS Of 10 CFR %: (Check one or more) (11)
MODE (9) 20.402(b) 20.405(c) X 50.73(a)(2)(iv) 73.71(b)
POWER 20.405(a)(1)(1) 50.36(c)(1) 50.73(a)(2)(v) 73.71(c)
I4 LEVEL (10) 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) OTHER 20.405( a)(1)( t il) 50.73(a)(2)(i) 50.73(a)(2 )(v iii)( A) (Specify in low 20.40$(a)(1)(iv) 50.73(a)(2)(li) 50.73(a)(2)(viii)(B) /[jt ct 20.405(a)(1)(v) 150.73(a)(2)(iii) 50.73(a)(2)(x) NRC Form 366A)
TIC [N5FI ONIACI FOR THIS 1IR (12)
NAME lELEPHONE NUMBER (include Area Code)
Mr. James M. Peschel, Regulatorf# Compliance Mgr. (603) 474-9521 Ext. 3772 COMPIElf ONI IINI F OR F ACH COMPONI NT F Alt VRf Df SOtlBf D IN THIS RFPORI (13)
CAUSL SYSTLM COMPONfNT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER 0
MONTH l SUPPlf MINIAl RfIVtT IXPf CIID (14) EXPECTED DAY YF AR YLS SUDMISSION (If yes, complete EXPECTED SUBMISSION DATE). X NO DATE (15) ,
"5BSIRACI (Limit to 1400 spaces, i.e. approximately 15 single-spaced typewritten lines) (16)
During a plant startup (approximately 14 percent power) on May 22,1993, at approximately 1000 EDT, Steam Generator (SG) !
level oscillations occurred in one SG resulting in the SG being overfed and causing a high-high SG watt r level. This caused a I feedwater isolation to all four SG's and additionally caused a turbine trip signal. Operator response to the event prevented a l reactor trip and reactor power was reduced to approximately 2.5% At 1154 EDT, North Atlantic made a four-hour !
notiGeation to the NRC pursuant to 10 CFR 50.72(b)(2)(ii) since this event constituted an ESF actuation. ;
I There were no adverse safety consequences as a result of this event. A'l equipment functioned as designed and all operator j actions v ere determined to be appropriate to ensure the safety of the plant and the public.
l The root cause for this esent was determined to be personnel error on the part of the feed station operator. Specifically, the l feed station operator knew the steps involved to successfully transfer to the main feedwater regulating valves (FRV's) but did l not properly anticipate and interpret the SG level conditions with respect to existing plant conditions. The extreme sensitivity of the FRV's was not fully realized, as shown by the 'A' FRV being opened approximately 6 percent initially.
Immediate corrective actions, as a result of the Feedwater Isolation, were to reduce power to approximately 2.5% and restore feedwater to the SGs which prevented a reactor trip. Long term corrective actions include: procedure enhancements; low power operator training; an evaluation of simulator enhancements with regard to low power and feedwater operations; and pre-shift bricGngs for low power evolutions.
T E TGrR 369 UW
Y FCRM 366A U.S. NUCLEAR REGULATORY C0pellSSIC~J AIPROVED BY OMB NO. 3150-0104 EXPIRES 5/31/95 l (5-92) l ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH I
, THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO I LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, TEXT CONTINUATION WASHINGTON, REDUCTION PROJECTDC 20555-0001, (3150-0104), OFFICEANDOf TO THE P MANAGEMENT AND BUDCET, WASHINGTON, DC 20503.
F AClll1Y NAME (1) DOCKET NUMBER (2) LER NUMBER (6? PAGE (3)
SEQUENilAL REVISION YEAR Scabrook Station NUMBER NUMBER 05000443 93 00 2 OF 5 10 TEXT (if more space is required, ese t'-itional copfes of NRC form 366A) (t7)
Description of Event During a plant startup (approximately 14 percent power) on May 22,1993, at approximately 1000 EDT, Steam Generator (SG) level oscillations occurred in one SG, resulting in the SG being overfed and causing a high-high SG water level. This caused a fcedwater isolation to all four SG's and additionally caused a turbine trip signal. Operator response to the event prevented a reactor trip and reactor power was reduced to approximately 2.5%.
The plant was in the process of starting up following the unit trip that occurred on May 20,1993 (See LER 93-09). The turbine was off-line on the turning gear at the time of the event. The main turbine was reset and was in the process of shell and chest warming. The shift assumed the watch during the evening of May 22, 1993 and were continuing the steps of main plant evolution, (MPE), procedure OS1000.02, Plant Startup from Hot Standby to Minimum Load. An additional control room operator was available to augment the crew as feed station operator during planned low power feedwater operations.
The USS directed the primary control room operator to increase power using control rods. This action was taken primarily to increase feed flow and move away from the low power conditions to a point where SG 1evel control sensitivity to feed flow changes would be less severe. This order was acknowledged by the primary operator and rods were withdrawn a couple of steps.
The feed station operator recognized that the Feedwater Regulating Bypass Valves were 80% open and were near the upper end of their control range. The feed station operator asked the USS for permission to start transferring feed flow from the Feedwater Regulating Bypass Valves to the Feedwater Regulating Valves (FRV's). The USS then directed the feed station operator to commence transferring feedflow from the Feedwate r Regulating Bypass Valves to the FRV's by starting with the ' A' SG. This direction was acknowledged by the feed station operator.
The feed station operator, in attempting to open the 'A' FRV slightly, held the valve open pushbutton too long, which resulted in opening the FRV approximately 6 percent. The extreme sensitivity of the FRV's was not realized, as shown by the 'A' FRV being opened approximately 6 percent initially. Shortly afterwards, the feed station operator took manual control of feedwater flow to the other 3 SGs and attempted to open their respective FRV's slightly to compensate for the inventory changes that would result from the earlier power increase. The feed station operator was under the impression that, in the process of transferring the 'A' SG from the bypass to the FRV, it would also be necessary to take manual control of the feedwater flow to the other 3 SGs to compensate for inventory changes due to the power increase and changes in feed flow distribution when swapping from the bypass valve to the FRV on one SG. The feed station operator did not inform the USS of his actions on the 'B', 'C', and 'D' SGs.
hRC f DiiH 366A T5-92)
INRC' FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST:
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TEXT CONTINUATION NUCLEAR REGULATORY COMMISSION WASHINGTON, DC 20555-0001, AND TO TIIE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.
FACILITY MAME (1) DOCKET NUMBER LER NUMBLR (6) PAGE (3)
YEAR SEQUENTIAL REVIS10 Seabrook Station 05000443 93 00 3 OF 5 0
TEXT (if more space is required, use additional copies of NRC form 366A) (t?)
(Continued)
The MPE procedure, OS1000.02, provides a method for plant startup through 22 percent power. The procedure specifically addresses feedwater temperature, limitations on the Feedwater Regulating Bypass Valves, power stabilization for enhanced feedwater level control, and turbine generator operations. The transfer of feedwater flow control from the Feed Regulating Bypass Valves to the Main Feed Regulating Valves was attempted with the turbine generator on the turning gear, therefore there was effectively no feedwater heating. The USS proceeded with the unit startup despite not having feedwater preheating due to the concern of feedwater instability at low power levels. This lack of feedwater preheating, was not discussed with the shift or feedwater station operator. The sequence of bringing all four main feedwater regulating valves off of their closed seats, coupled with the earlier power increase, induced oscillations in all four SG's.
The oscillations were made worse by cold feedwater temperatures and rapidly progressed to the point at which the feed station operator requested assistance.
The USS assigned a second operator to the feed station. Before the oscillations could be brought under control, the 'B' SG narrow range indicated level reached the F-14 setpoint (86% narrow range level) and a Feedwater Isolation occurred. Although the Feedwater Isolation was not avoided, the combined effort of two experienced feed station operators, (both had been through the power ascension low power feed control training and had successfully been involved with several startups as feed station operators), did prevent a reactor trip due to low SG level.
At 1154 EDT, North Atlantic made a four-hour notification to the NRC pursuant to 10 CFR 50.72(b)(2)(ii) since this event constituted an ESF actuation.
Safety Conseauences There were no adverse safety consequences as a result of this event. All equipment functioned as designed and the operator actions in response to the event were determined to be appropriate to ensure the safety of the plant and the public. At no time during this event was there any impact on the health and safety of plant employees or the public.
Root Cause it is recognized that SG level control and feedwater regulating valve transfer at low power is sensitive and difficult evolution. Ilowever, the use of a dedicated feed station operator and training have been proven to i
TRC t URM 3bbA T5 WT-
E FORM 366A U.S. MUCLEAR REGULATORY COMMISSION APPROVLD BY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY
. WITH THIS INFORMATION COLLECTION REQUEST:
50.0 HRS. FORWARD COMMENTS REGARDING LICENSEE EVENT REPORT (LER) BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S.
TEXT CONTINUATION NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT , OFFICE OF MANAGEMENT AND (3150-0104)HINGTON, BUDGET, WAS DC 20503.
IACitIIY NAME (1) DOCKET NUMBER tfR NUMBER (6) PAGE (3)
YEAR SEQUENilAL REVIS10 Seabrook Station 05000443 93 00 4 OF 5 10 LEX 1 (if more space is required, use additional copies of MRC f orm 366A) (11)
(Continued) be extremely successful in the past. The root cause for this event was determined to be personnel error on the part of the feed statian operator. Specifically, the feed station operator knew the steps involved to successfully transfer to the FRV's but did not properly anticipate and interpret the SG level conditions with respect to existing plant conditions. The extreme sensitivity of the FRV's was not realized as shown by the
'A' FRV being opened approximately 6 percent initially.
Several contributing factors were identified that if corrected or improved may have supported the feed station operator during this evolution. These factors are as follows:
- 1. The time span between the first valve opening and the power increase was not entirely consistent with the power / steam generator level stability guidance in the main plant evolution procedure.
- 2. The MPE and operating procedure did not include or reference appropriate portions of the Westinghouse power ascension feedwater control training or lessons learned from previous successful performance of this evolution.
- 3. Incomplete communication existed as the feed station 'erator did not announce to the crew that he was taking manual control of the other three FRV's.
Corrective Actions Immediate corrective actions, in response to the Feedwater Isolation, were to reduce plant power to approximately 2.5% and restore feedwater flow to the steam generators. Long term corrective actions to prevent reoccurrence include the following:
- 1. The normal operating procedure used for transferring the Feedwater Regulating Valves Dypass to the Main Feedwater Regulating Valves will be revised to provide additional guidance on plant parameters to monitor when initiating and completing the transfer.
- 2. Operator training will be provided in the simulator on the revised procedure and low power operations.
- 3. The simulator design will be reviewed for enhancements that could improve simulator response during low power operations aad feedwater station operations.
- 4. The guidelines for pre-shift crew briefing will be reviewed to ensure that low power feedwater system l
! operations are adequately addressed.
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l MRC'f0RM 366A U.S. NUCLEAR RECHLAIORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES 5/31/95 (5 92)
ESTIMATED DURDEN PER RFSPONSE TO COMPLY
. WITH THIS INFORMATION COLLECTION REQUEST.
50.0 HRS. FORWARD COMMENTS REGARDl!(G LICENSEE EVENT REPORT (LER) BURDEN ESTIMATE TO THE INFORMATION aND b.S.
TEXT CONTINUATION RECORDS MANAGEMENT NUCLEAR REGULATORY BRANCH (MNBB COMMISSION WASHlh 7714),GTON, DC 20555-000), AND TO IIIE PAPERWORK REDUC 110N PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, OC 70503.
FACIllIY NAME (1) DOCKET NUMHFR t[R NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVIS10 Seabrook Station 05000443 93 00 5 OF 5 0
1LK1 (11 more space is required, use additional copies of NRC form 366A) (11)
Plant Conditions At the time of this event the plant was in MODE 1, at 14 percent power, with a Reactor Coolant System temperature of 558 degrees Fahrenheit and pressure of 2235 psig.
Similar Events This is the second occurrence where a high-high level in a SG resulted in a Feedwater Isolation that involved operator action. LER 92-017 documents an event which occurred on September 7,1992 with the plant in MODE 1. During a routine shutdown to begin a refueling outage while at approximately 12 percent power SG level oscillations led to one SG being overfed, initiating a Feedwater Isolation. The root cause for this event was determined to be incomp.ete communication, in that the operations crew did not effectively communicate and coordinate actions that were taking place on rod control, feedwater control, and turbine control. The Feedwater Isolation described in this LER differed in that it occurred during a plant startup and was induced by operator action while the Feedwater Isolation of LER 92-017 was induced by the plant.
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