ML19350F102

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LER 81-031/03L-0:on 810518,reactor Coolant Temp Exceeded Tech Spec Limit Before Shutdown Cooling,Secured to Permit Maint of Valve MO-17,could Be re-established.Caused by Lack of Timely Coordination Between Operations & Maint Personnel
ML19350F102
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 06/17/1981
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
LER-81-031-03L, LER-81-31-3L, NUDOCS 8106240214
Download: ML19350F102 (1)


Text

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Mr. Soyce M. Grier, O f rector Office of Inspection f, Enforcement, Region I P00RORIISL /

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Dear Mr. 3riert N eW% ,

This LER concerns reactor coolant temperature exceeding 21 '#,g .

primary containment integrity. Governing Tech Spec is 3.7.A.2. Q ,,

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r a . .. ... car tvesf osscaiatioN Aho P909 5LE c0NsEOVENcts h ITTTI LWith the unit shutdown for maintenance, shutdown cooling was secu. nd to f gI permit maintenance of valve MO 17, shutdown cooling suction isolation I r3,i [ valve. Operator ordered restoration of shutdown cooling due to increasing i i3,,; i reactor coolant tem erature. Reactor coolant tem erature exceeded 212 F i

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