ML19344F073

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LER 80-018/03L-0:on 800802,during Surveillance Test on PCIS Normally Open Valves W/Unit at Full Power,Reactor Water Cleanup Sys Return Isolation Valve MO-3-12-68 Failed to Close Using Control Switch.Cause Not Determined
ML19344F073
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 09/01/1980
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
LER-80-018-03L, LER-80-18-3L, NUDOCS 8009120369
Download: ML19344F073 (1)


Text

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Dear Mr. Gricr:

This IER concerns the failure of the reactor water cleanup system uturn isolation valve, MO-3-12-68, to close during surveillance testing.

The coverning Technical Specifications are 3 7.D.1 and 3 7.D.2.

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