ML19343B402

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LER 80-031/01T-0:on 801126,water Collected in Offgas Rad Monitor Sampling Sys,Reducing Flow.Caused by Recent Drain Mod Combined W/Pressure Variations Due to Load Change.Water Purged & Full Sample Flow re-established
ML19343B402
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 12/12/1980
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19343B401 List:
References
LER-80-031-01T, LER-80-31-1T, NUDOCS 8012230358
Download: ML19343B402 (1)


Text

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EVENT DESCRIPTION AND PROD A6LE CONSEQUENCES 9l Following a power reduction, water collected in the off-gas rad monitor j gjj sampling system reducing sample flow on 11/23/80. Even with reduced flow j y-] [ shift supervision believed the system was operable. Prompt action was l U-~] l taken to purge the system of water. Full sample flow was reestablished l M.jj L 11/2h/80 AM. Primary coolant rad monitors showed no unexpected changea l

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L I a period of time during the event. It has been determined that the water l Tg i problem was caused.by a recent drain mod combined with pressure varia- g 9l tions due to the load change. The water was purged and full sample flow j Rl reestablished by 11/2h/80 AM. The drain line will be modified. j e 9 60 1  % PGWER OTHEH S T ATUS DISC ti Di'3COVEltY OLLCHIP TION

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