ML19341A255

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LER 80-031/03L-0:on 801218,reactor Core Isolation Cooling Inboard Steam Supply Isolation Valve Did Not Automatically Close.Caused by Valve Closing Torque Switch on Type Smb Limitorque Operator for Valve MO3-13-15 Being Open
ML19341A255
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 01/13/1981
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
LER-80-031-03L, LER-80-31-3L, NUDOCS 8101220468
Download: ML19341A255 (1)


Text

Mr. Boyc 2 H. Gri:r, Dir:ctor No. -**

3-80-31/3L Of fice of Inspectie- & Enforcement, Region 1 U.S. Nuclear Regulatory Cormiission ._ _ _. _ _ _ - - _ - - _

p King of Prussia, PA 19406

Dear Mr. Grier:

2 ThigiLER ccacems failure of a RCIC steam supply isolation valve to close Mhen recaired chiring shutdown. Governir.g Technical Specification is 3 5.D.C ,. n U

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, U. S. NUCLE AR REGULATORY CoMM;$5loN

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(PLE ASE PRIN* M TYPE ALL REQUIRED INFORMATION)

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v ,3 i i steam supply isolation valve did not automatically ciose as required. I o64i I Applicable Tech Spec is 3.5.D.1. 'PA outboard steam surely valve closed I o i t, j l automatically as required. Tne valves nomally automatically close when I

,cil main steam pressure decreases below 105 PSIG. The low pressure isclation I 9Tl l logic was totally operable. I 0 18 ] l I es 6'

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4) 43 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS iioil The valve closing torque switch on the type SMB Limiteraue operater I i li1 i for valve Mo3-13-15 was found open. The switch was'rerlaced. I i>il Valve operation and response to an isolation signal were satisfactorily I

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