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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20006E8101990-02-20020 February 1990 Special Rept Re Plans for Alternate Fire Suppression Sys Redundancy.Diesel Driven Fire Pump 122 Run Daily,Except When Out of Svc from 900126-29 ML20028C1621982-12-29029 December 1982 RO 82-15:on 821228,tiny through-wall Crack Found in Heat Affected Zone of Weld in Safety Injection Supply Line from Boric Acid Storage Tanks.Investigation in Progress ML20052J0761982-05-14014 May 1982 RO P-RO-82-7:on 820501,rod Control Sys Component Failed Causing Loss of Drive Motion for Some Rods.Caused by Failed Bridge Thyristor in Power Cabinet 1BD.Unit Brought to Hot Shutdown & Rod Control Sys Repaired on 820502 ML20009A0101981-07-0202 July 1981 Environ Event Rept 81-01:on 810604,daily Chlorination Cycle Extended for 126 Minutes.Caused by Malfunction of Timer. New Timer W/More Precise Time Control Installed W/Setting of 110 Minutes Per Day ML19340C8321980-12-0303 December 1980 RO 80-25,Revision 1:on 800904,during Investigations Re Generic Technical Activity A-12,CVM Steam Generator Mounting Bolts Found Defective.Caused by Stress Corrosion Cracking. New Steam Generator Mounting Bolts Installed & Tensioned ML19347A9651980-09-25025 September 1980 Environ Event Rept 80-03:on 800820,during Special Chlorination Program,Certain Levels of Chlorine Found Outside Circulating Water Sys That Exceeded Concentration Limits in Tech Specs 2.4.1 ML19332A8141980-09-0505 September 1980 RO 80-25:on 800904,w/unit in Refueling Shutdown,Ultrasonic Examination of Steam Generator Support Bolts Revealed Most Bolts Had Crack Indications.Several Bolts Failed When Detensioning Was Attempted.Cause Not Determined ML19326D9831980-07-16016 July 1980 RO 80-20:on 800715,w/Unit 2 at 100% Power & Unit 1 at Cold Shutdown,Main Generator Separated from Grid & One Offsite Source Was Lost,Tripping Reactor & Coolant Pumps.Caused by Severe Electrical Storm.Transformer Restored ML19320C3261980-07-0101 July 1980 RO 80-18:on 800629,steam Generator 12 Experienced Minor primary-to-secondary Leakage of About 0.006 Gallons Per Minute.Leakage Was Carefully Monitored & Showed Increase. Facility Is Shutdown.Cooldown Is Planned ML19323G9411980-06-0404 June 1980 Environ Event Rept 80-02:on 800513-14,reclaiming Ion Exchanger Out of Svc When Steam Generator Blowdown Water Discharged Into River.Sample of Outfall Revealed Ph Value Greater than 8.5.Caused by Seasonal Change of River ML19312E2141980-05-30030 May 1980 Environ Event Rept 80-01:on 800501,daily Average Discharge Temp Exceeded Ambient River Water Temp by 5.7 F While Two Cooling Towers Were Undergoing Insp,Cleaning & Repair.One Tower Returned to Svc & Electrical Load Reduced ML19309G7291980-04-30030 April 1980 RO 80-15:on 800429,volumetric Test of Facility Containment Main Airlock Showed Leakge of 600 Scc/Minute,Exceeding Tech Specs.Caused by Opening of Inner Airlock Door.Seals for Inner Door Were Replaced.Leakage Was Acceptable ML19296A6521980-01-24024 January 1980 RO-80-06:on 800123,diesel Generator D2 Tripped on High Crankcase Pressure When Crankcase Eductor Supply Pipe Came Loose.During Operability Testing of Other Diesel Generates, Jacket Coolant Hose on Water Pump Ruptured ML19291C1991980-01-15015 January 1980 Supplemental Info to RO 80-3.One Tube Defective on Steam Generator Hot Leg 21.One Tube Defective & Ten Tubes Degraded on Cold Leg 21.Hot Leg 22 to Be Inspected.Four Tubes Defective & 42 Degraded on Cold Leg 22.Cause Unknown ML19257B9051980-01-10010 January 1980 RO 80-03:during Eddy Current Insp of Steam Generator 21, Defect Discovered in One Tube.Caused by Movement of One Tube Lane Blocking Devices Against Outside Surface of Tube, 17 Inches Above Tubesheet.Tube Will Be Plugged ML19257B2561980-01-0707 January 1980 RO 80-1 on:800106,at 100% Power,Both Trains of Caustic Addition to Containment Spray Sys Found Valved Out.Caused by Valves Mistakenly Closed on 800103 During Unit 2 Cooldown for Refueling.Containment Spray Sys Operable During Period ML19260B1531979-12-0303 December 1979 Environ Event Rept 79-11 for 17 Days in Nov.Slowdown Flow in Excess of Tech Specs Required to Complete Special Chlorination Treatment Authorized by 791102 ETS Change ML19210C6831979-11-0101 November 1979 Environ Event Rept 79-10 Re Operation of Circulating Water Sys in Partial Recycle Mode W/Daily Average Blowdown Flow in Excess of 150 Cfs.Higher Flow Required to Maintain Cooling Water Inlet Temps at Less than 85 F ML19250B9621979-10-31031 October 1979 Environ Event Rept 79-09:on 791007,neutralizing Tank Batch Discharged W/Ph Greater than 8.5.Discharge Determined to Be 11.65.Caused by Improper Operation of Ph Monitor on Tank Effluent Pipe.Shift Supervisors Reinstructed ML19209B7041979-10-0303 October 1979 RO 79-27:on 791003,reactor Tripped on Low Pressurizer Pressure Followed by Safety Injection & Containment Isolation.Caused by Steam Generator Tube Leakage.Failed Tubes Will Be Plugged & Inspected ML19329F4161975-11-14014 November 1975 RO 75-02:on 750810,long Lived Halogen & Particulate One Yr Release Rate Exceeded Design Objective 3.9.2.6.Corrections Not Required Because Prairie Island Tech Spechs More Conservative than Reg Guide 1.42,Revision 1,requirements 1990-02-20
[Table view] Category:LER)
MONTHYEARML20006E8101990-02-20020 February 1990 Special Rept Re Plans for Alternate Fire Suppression Sys Redundancy.Diesel Driven Fire Pump 122 Run Daily,Except When Out of Svc from 900126-29 ML20028C1621982-12-29029 December 1982 RO 82-15:on 821228,tiny through-wall Crack Found in Heat Affected Zone of Weld in Safety Injection Supply Line from Boric Acid Storage Tanks.Investigation in Progress ML20052J0761982-05-14014 May 1982 RO P-RO-82-7:on 820501,rod Control Sys Component Failed Causing Loss of Drive Motion for Some Rods.Caused by Failed Bridge Thyristor in Power Cabinet 1BD.Unit Brought to Hot Shutdown & Rod Control Sys Repaired on 820502 ML20009A0101981-07-0202 July 1981 Environ Event Rept 81-01:on 810604,daily Chlorination Cycle Extended for 126 Minutes.Caused by Malfunction of Timer. New Timer W/More Precise Time Control Installed W/Setting of 110 Minutes Per Day ML19340C8321980-12-0303 December 1980 RO 80-25,Revision 1:on 800904,during Investigations Re Generic Technical Activity A-12,CVM Steam Generator Mounting Bolts Found Defective.Caused by Stress Corrosion Cracking. New Steam Generator Mounting Bolts Installed & Tensioned ML19347A9651980-09-25025 September 1980 Environ Event Rept 80-03:on 800820,during Special Chlorination Program,Certain Levels of Chlorine Found Outside Circulating Water Sys That Exceeded Concentration Limits in Tech Specs 2.4.1 ML19332A8141980-09-0505 September 1980 RO 80-25:on 800904,w/unit in Refueling Shutdown,Ultrasonic Examination of Steam Generator Support Bolts Revealed Most Bolts Had Crack Indications.Several Bolts Failed When Detensioning Was Attempted.Cause Not Determined ML19326D9831980-07-16016 July 1980 RO 80-20:on 800715,w/Unit 2 at 100% Power & Unit 1 at Cold Shutdown,Main Generator Separated from Grid & One Offsite Source Was Lost,Tripping Reactor & Coolant Pumps.Caused by Severe Electrical Storm.Transformer Restored ML19320C3261980-07-0101 July 1980 RO 80-18:on 800629,steam Generator 12 Experienced Minor primary-to-secondary Leakage of About 0.006 Gallons Per Minute.Leakage Was Carefully Monitored & Showed Increase. Facility Is Shutdown.Cooldown Is Planned ML19323G9411980-06-0404 June 1980 Environ Event Rept 80-02:on 800513-14,reclaiming Ion Exchanger Out of Svc When Steam Generator Blowdown Water Discharged Into River.Sample of Outfall Revealed Ph Value Greater than 8.5.Caused by Seasonal Change of River ML19312E2141980-05-30030 May 1980 Environ Event Rept 80-01:on 800501,daily Average Discharge Temp Exceeded Ambient River Water Temp by 5.7 F While Two Cooling Towers Were Undergoing Insp,Cleaning & Repair.One Tower Returned to Svc & Electrical Load Reduced ML19309G7291980-04-30030 April 1980 RO 80-15:on 800429,volumetric Test of Facility Containment Main Airlock Showed Leakge of 600 Scc/Minute,Exceeding Tech Specs.Caused by Opening of Inner Airlock Door.Seals for Inner Door Were Replaced.Leakage Was Acceptable ML19296A6521980-01-24024 January 1980 RO-80-06:on 800123,diesel Generator D2 Tripped on High Crankcase Pressure When Crankcase Eductor Supply Pipe Came Loose.During Operability Testing of Other Diesel Generates, Jacket Coolant Hose on Water Pump Ruptured ML19291C1991980-01-15015 January 1980 Supplemental Info to RO 80-3.One Tube Defective on Steam Generator Hot Leg 21.One Tube Defective & Ten Tubes Degraded on Cold Leg 21.Hot Leg 22 to Be Inspected.Four Tubes Defective & 42 Degraded on Cold Leg 22.Cause Unknown ML19257B9051980-01-10010 January 1980 RO 80-03:during Eddy Current Insp of Steam Generator 21, Defect Discovered in One Tube.Caused by Movement of One Tube Lane Blocking Devices Against Outside Surface of Tube, 17 Inches Above Tubesheet.Tube Will Be Plugged ML19257B2561980-01-0707 January 1980 RO 80-1 on:800106,at 100% Power,Both Trains of Caustic Addition to Containment Spray Sys Found Valved Out.Caused by Valves Mistakenly Closed on 800103 During Unit 2 Cooldown for Refueling.Containment Spray Sys Operable During Period ML19260B1531979-12-0303 December 1979 Environ Event Rept 79-11 for 17 Days in Nov.Slowdown Flow in Excess of Tech Specs Required to Complete Special Chlorination Treatment Authorized by 791102 ETS Change ML19210C6831979-11-0101 November 1979 Environ Event Rept 79-10 Re Operation of Circulating Water Sys in Partial Recycle Mode W/Daily Average Blowdown Flow in Excess of 150 Cfs.Higher Flow Required to Maintain Cooling Water Inlet Temps at Less than 85 F ML19250B9621979-10-31031 October 1979 Environ Event Rept 79-09:on 791007,neutralizing Tank Batch Discharged W/Ph Greater than 8.5.Discharge Determined to Be 11.65.Caused by Improper Operation of Ph Monitor on Tank Effluent Pipe.Shift Supervisors Reinstructed ML19209B7041979-10-0303 October 1979 RO 79-27:on 791003,reactor Tripped on Low Pressurizer Pressure Followed by Safety Injection & Containment Isolation.Caused by Steam Generator Tube Leakage.Failed Tubes Will Be Plugged & Inspected ML19329F4161975-11-14014 November 1975 RO 75-02:on 750810,long Lived Halogen & Particulate One Yr Release Rate Exceeded Design Objective 3.9.2.6.Corrections Not Required Because Prairie Island Tech Spechs More Conservative than Reg Guide 1.42,Revision 1,requirements 1990-02-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G4461999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pingp.With ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20216E7151999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Pingp,Units 1 & 2. with ML20211D3981999-08-24024 August 1999 Safety Evaluation Supporting Requested Actions to Licenses DPR-42 & DPR-60,respectively ML20211C2531999-08-0404 August 1999 Unit 1 ISI Summary Rept Interval 3,Period 2 Refueling Outage Dates 990425-990526 Cycle 19 971212-990526 ML20210Q4891999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pingp,Units 1 & 2. with ML20211B5971999-07-31031 July 1999 Cycle 20 Voltage-Based Repair Criteria 90-Day Rept ML20209J1131999-07-15015 July 1999 Safety Evaluation of Topical Rept NSPNAD-8102,rev 7 Reload Safety Evaluation Methods for Application to PI Units. Rept Acceptable for Referencing in Prairie Island Licensing Actions ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML20209F9811999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Prairie Island Nuclear Generating Plant,Units 1 & 2.With ML20196F4081999-06-23023 June 1999 Revised Pages 71,72 & 298 to Rev 7 of NSPNAD-8102, Prairie Island Nuclear Power Plant Reload Safety Evaluation Methods for Application to PI Units ML20195G5181999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Prairie Island Nuclear Generating Plant,Units 1 & 2.With . Page 3 in Final Rept of Incoming Submittal Was Not Included ML20207B5931999-05-26026 May 1999 SER Accepting Licensee Proposed Alternative to ASME Code for Surface Exam (PT) of Seal Welds on Threaded Caps for Unit 1 Reactor Vessel Head Penetrations for part-length CRDMs ML20196L2501999-05-13013 May 1999 Rev 0 to PINGP Unit 1 COLR Cycle 20 ML20206L6191999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pingp,Units 1 & 2. with ML20205N1081999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pingp,Units 1 & 2. with ML20205Q5101999-03-15015 March 1999 Inservice Insp Summary Rept Interval 3,Period 1 & 2 Refueling Outage Dates 981109-1229 Cycle 19,970327-981229 ML20207J6951999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Prairie Island Nuclear Generating Plant ML20202J7711999-02-0404 February 1999 Simulator Certification Rept for Prairie Island Plant Simulation Facility,1998 Annual Rept ML20202G3761999-01-31031 January 1999 Non-proprietary Rev 7 to NSPNAD-8102-NP, Prairie Island Nuclear Power Plant Reload SE Methods for Application to PI Units ML20207L2811999-01-31031 January 1999 Revised Monthly Operating Repts for Jan 1999 for Pingp,Units 1 & 2 ML20202J1731999-01-22022 January 1999 Safety Evaluation Concluding That NSP Proposed Alternative to Surface Exam Requirements of ASME BPV Code for CRD Mechanism Canopy Seal Welds Will Provide Acceptable Level of Quality & Safety ML20206P7861998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Prairie Island Nuclear Generating Plant.With ML20205H0561998-12-31031 December 1998 Northern States Power Co 1998 Annual Rept. with ML20198J6441998-12-17017 December 1998 Rev 0 to PINGP COLR Unit 2-Cycle 19 ML20206N2731998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Prairie Island Nuclear Generating Plant,Units 1 & 2.With ML20196D7341998-11-20020 November 1998 Third Quarter 1998 & Oct 1998 Data Rept for Prairie Island Isfsi ML20155K6301998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Prairie Island Nuclear Generating Plant,Units 1 & 2.With ML20154H4061998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Prairie Island Nuclear Generating Plant.With ML20202J7991998-09-30030 September 1998 Non-proprietary Version of Rev 3 to CEN-629-NP, Repair of W Series 44 & 51 SG Tubes Using Leaktight Sleeves,Final Rept ML20198P0571998-09-0303 September 1998 Rev 1 to 95T047, Back-up Compressed Air Supply for Cooling Water Strainer Backwash Valve Actuator ML20153B0761998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Prairie Island Nuclear Generating Plant.With ML20237A3961998-08-11011 August 1998 Safety Evaluation on Westinghouse Owners Group Proposed Insp Program for part-length CRDM Housing Issue.Insp Program for Type 309 Welds Inadequate from Statistical Point of View ML20237A8171998-08-0505 August 1998 SER Related to USI A-46 Program GL 87-02 Implementation for Prairie Island Nuclear Generating Plant,Units 1 & 2 ML20236X8531998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Prairie Island Nuclear Generating Plant ML20236R6481998-07-15015 July 1998 Metallurgical Investigation & Root Cause Assessment of Part Length CRDM Housing Motor Tube Cracking at PINGP Unit 2 - Preliminary Summary Rept ML20236R0771998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Prairie Island Nuclear Generating Plant ML20249A5751998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Prairie Island Nuclear Generating Plant ML20247G7011998-05-31031 May 1998 Metallurgical Investigation & Root Cause Assessment of Part Length CRDM Housing Motor Tube Cracking at Prairie Island Nuclear Generating Plant,Unit 2 ML20248M0561998-05-31031 May 1998 Rev 5 to CEN-620-NP, Series 44 & 51 Design SG Tube Repair Using Tube Rerolling Technique ML20247E2671998-05-0505 May 1998 Rev 0 to Pingp,Units 1 & 2,Pressure & Temp Limits Rept (Effective Until 35 Efpy) ML20247G2921998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Prairie Island Nuclear Generating Plant ML20217M6901998-04-29029 April 1998 Safety Evaluation Accepting Methodology for Relocation of Reactor Coolant Sys P/T Limit Curves & LTOP Sys Limits Proposed by NSP for Pingp,Units 1 & 2 ML20216C6361998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Prairie Nuclear Generating Plant Units 1 & 2 ML20216H0341998-03-31031 March 1998 Cycle-19 Voltage Based TSP Alternate Repair Criteria 90-Day Rept ML20217D2041998-03-13013 March 1998 Rev 1 to 28723-A, Intake Canal Liquefaction Analysis Rept for Pingp,Welch,Mn ML20236P9801998-03-12012 March 1998 Rev 0 to 97FP02-DOC-01, Compliance Review of 10CFR50,App R, Section Iii.O RCP Lube Oil Collection Sys ML20248L3931998-03-10010 March 1998 ISI Summary Rept Interval 3,Period 1 & 2 Refueling Outage Dates 971018-971212 Cycle 18,960303-971212 ML20216D0911998-03-0606 March 1998 Rev 0 to Prairie Island Generating Plant,Units 1 & 2, Pressure & Temp Limits Rept 1999-09-30
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p .sB NSED NORTHERN STATES P O W E Fv COMPANY M f N N E A PO LI S. MIN N E SCTA SS409 December 3,1980 Mr J G Keppler Office of Inspection & Enforcement ,
U S Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137
Dear Mr Keppler:
PRAIRIE ISLAND NUCLEAR GENERATING PLANT Docket No. 50-282 License No. DPR-42 Supplement to Licensee Event Report 80-25 (Rev 1)
Defective Steam Generator Bolting -- ...
Attached are three copies of a followup report containing additional information related to Licensee Event Report 80-25.
Yours ve ry t ruly, 0*
e
.s L 0 Mayer, PE Manager of Nuclear Suppo:t Services ti LOM/DHM/bd cc: Director, IE, USNRC (40) ;
l Director, MIPC, USNRC (3) r-NRC Resident Inspector .3 g
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- n
- J W Ferman l
Attachment
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80121706.40 g DEC 101980
i Attachment December 3, 1980 Director, IE III, USNRC 1
NORTHERN STATES POWER COMPANY PRAIRIE ISLAND NUCLEAR GENERATING PLANT R0-80-25 Supplemental Report Defective Steam Generator Bolting 1
Identification of Occurrence De fe ct iva Vascomax 250 CVM steam generator mounting bolts. Twenty eight of the 48 mounting bolts on #11 and #12 Steam Generators were found defective.
As a result, Unit 2 was shutdown for mounting bolt inspection; this inspec-tion revealed three defective bolts in #22 Steam Generator.
Conditions Prior to Occurrence Unit I was in refueling shutdown and Unit 2 was at 100% steady-state power.
Method of Discovery and Description 1 On September 4, 1980 maintenance personnel began to detension the Unit 1 Vascomax 250 CVM Steam Generator mounting bolts. During investigations initiated by the NRC related to Generic Technical Activity A-12 we learned that the bolts were installed with a pre-load. The bolts were to be l detensioned from approximately 1550 ft lbs to 115 ft lbs to eliminate this i
j condition. The firs t two bolts on which detensioning was attempted f ailed l
just below the head at the thread relief.
Ultrasonic testing of the remaining 46 mounting bolts on the Unit I steen gene ra t ors indicated 26 additional bolts with 'no, or weak, back reflection.
During bolt removal and replacement 25 of these bolts failed. One bolt was cracked below the head at the thread relief. Of the 28 defective bolts,1,4 were found in each generator.
On the evening of September 4, 1980 Unit 2 was shut down to inspect the mounting bolts in #21 and #22 steam generators. On #22 steam generator three mounting bolts were found to be defective.
l l
l L
December 3, 1980 Page Designation of the Apparent Cause of the Occurrence It is known that maraging high strength steels are highly susceptible to stress corrosion cracking in the presence of moisture, high tensile stress, and elevated temperature. Elements that contribute to stress corrosion cracking were found to exist: *
- 1) The thread relief located below the bolt head created a stress riser.
- 2) The bolts when installed during construction were torqued to approximately 1550 ft 1bs.
- 3) Westinghouse's metallurgical investigation revealed the presence of zine and chlorine. -
- 4) Approximately 50 percent of the support adapter holes did not line up with the holes in the support so some binding was present.
- 5) It appears a bottoming tap may not have been utilized on all the steam generator support bolt holes. This may have resulted in stress levels in the bolts higher than originally cons ide red . .
- 6) There was evidence of valve leakage in the vicinity of some bolting which provided a source of moisture.
Westinghouse R & D Center performed visual metallographic and f ractographic examination of the cracks, chemical evaluation of bolt material and crack deposits, and sechanical property tests. The results of the Westing-house findings are as follows:
- 1) The cracks were circumferential and were initiated at the outer f surf ace around the thread relief below the bolt head where a stress
' concentration due to the head-to-shank radius is likely to be present.
I
- 2) The fractures contained points of multiple origin along the outer circumference of the thread relief region. The fractures were relatively flat, although highly irregular in a few cases. ,
- 3) In almost all cases, cracking was extensive with the apparent service fracture covering in excess of 90% of the bolt section. The l
l fractures were he3vily oxidized in most cases.
l
- 4) Micro structural studies of the bolt material by light optic and l
electron transmission microscopopy showed no apparent abnormalities in the micro structure.
t
- 5) Scanning electron fractography of the fractured surf aces revealed that fracture occurred primarily by transgranular cleavage, except for small islands of dimpled rupture where the bolt was fractured during removal, t
December 3, 1980 Page 6) Chemical evaluations of the fracture surf aces by EDAX analysis revealed, in addition to the principal alloying elements, the presence of zine and chlorine. Both elements are known to lower the stress corrosion resistance of the bolt material in the presence of moisture.
- 7) Tensile testing of a sound bolt resulted in a yield strength of 260.9 Ksi.
- 8) Hardness readings taken on a sectioned bolt head revealed Rockwell "Rc" numbers ranging from 48 to 53.
- 9) The fracture toughness tests revealed a room temperature value of 98.9 Ksi. ,
- 10) The results of the chemical analysis of the bolt material showed that the chemistry is within the specification requirement for 18% Ni (250) Vascomax Material.
- 11) Estimates of the load to which the bolts were subjected to during service showed that cracking occurred at a substantially lower stress level (60 to 80 Ksi) than the load bearing capacity of the bolt material (yield stress of 260 Ksi).
The following dif ferences existed between the Unit 1 & 2 steam generator mounting bolts:
- 1) On Unit 1, the steam generator mounting bolts are located under the mirror insulation and on Unit 2 they are outside the insulation.
This results in a temperature dif ference between Unit 1 and Unit 2 mounting bolts of approximately 150 F.
- 2) The thread relief for the bolts for the Unit 2 mounting bolts is located approximately 1/2" away from the bolt head instead of just below the bolt head in the Unit 1 mounting bolts.
- 3) The initial torque data shows the Unit 1 bolts were torqued to approximately 1550 ft 1bs and the Unit 2 bolts were torqued to approximately 1400 ft 1bs.
- 4) The Unit 2 mounting bolts were supplied with washers and the Unit 1 bolts were not.
- 5) The mounting bolts. on Unit 2 broke loose for detensioning at approximately 2500 f t 1bs. r,me of the bolts on Unit 1 could not be detensioned at loads esi imated to be in excess of 4000 f t lbs and had to be burned out.
$ December 3, 1980 Page Analysis of Occurrence As a result of the steam generator mounting bolt f ailures, no radioactive material was released, no other equipment was af fected, no adminis trative controle were violated, no extra personnel exposure occurred (except for the bolt replacement), and normal plant operation was not affected.
Fluor Power Services performed an evaluation of the saf ety margin available due to the degraded bolt ing. The evaluation indicated that the Vascomax 250 CVM bolts reach a maximum allowable stress in the SSE, taking into account dead we igh t , pressure, and thermal considerations, of 11.8 percent of the specified bolt minimum yield strength. On #11 and #12 Steam Generators one bolt for each steam generator was unavailable for shear load, due to failure in the Heli Coil. Fourteen bolts for each steam generator were unavailable' to assume tension load. Based on the as-found condition of the
. S/G mounting bolts, the remaining 14 bolts would have held the steam generator during an SSE.
Fluor Power Services safety evaluation indicated that the Vascomax 250 CVM bolts reach a maximum allowable stress during the design basis LOCA, taking into account dead weight, pressure, and thermal considerations, of approx-imately 41.4 percent of the specified bolt minimum yield strength. The remaining bolts, 96 percent available for shear load and 41.7 percent available for tensile loads, may have prevented support f ailure during the
- design basis LOCA condition and would have been adequate for less severe LOCA conditions.
The re f o re , the consequences from the standpoint of the public health and safety were minimal.
NOTE: Westinghouse and Fluor Power Services are working on-reanalysis of the loads the mounting bolts actually see. It appears the actual bolt loadings during the SSE and LOCA conditions will be considerable sma lle r .
On #22 Steam Generator the three defective bolts were located in one support pad. Westinghouse analysis indicated it was acceptable to operate
- l with the remaining three Vascomax 250CVM bolts in that pad. To increase l
the safety margin on that pad, a bolt was removed f rom two other legs and i
installed in that pad. All other Unit 2 bolts were de-tensioned and the I
unit was returned to service.
Corrective Action l
l The following actions were taken in Unit I to prevent recurrence of mounting bolt failures:
- 1) The new steam generator mounting bolts were installed and tensioned to 50 f t lbs with a maximum specified tension of 115 f t lbs.
- 2) The mouating holes in the' steam generator were cleaned with low l
[
halogen or sulfur material.
l l
December 3,1980 Page 5
- 3) The bolts were installed with a certified lubricant with independent chemical contamination tests.
- 4) The exposed bolt head and surrounding area were seal coated with a high temperature silicone paint.
- 5) The steam generator support adapter plates bolt holes were machined so the adapter holes will line up with the steam generator support holes .
- 6) The steam generator support holes were retapped. as necessary with a bottoming tap.
- 7) The new bolts have rolled threads in lieu of machined threads.
- 8) The thread relief on the new bolts is very gradual and located approximately one inch from the bolt head.
- 9) The bolts will continue to be ultrasonically inspected in accordance with our inservice inspection program.
As a result of the above modifications, Prairie Island's steam generator mounting bolts should now be classified in Group III in NUREG-0577.
Failure Data
Description:
1 1/2" - 12 UNF-2A Vascomax 250 CVM steam generator mounting bolts Material Manufacturer: VASCO (a Teledyne Company)
Machined By: Welding and Steel Fabrication Co., Inc.
Future Action During the 1981 refueling of Unit 2 the Vascomax 250 CVM steam generator mounting bolts will be replaced with the new improved Vascomax 250 CVM bolts as described above. The bolts that are removed will be examined for signs of stress corrosion cracks.
I Prepared by: George Lenertz, Production Engineer Prairie Island Nuclear Generating Plant I
, ,,..m.
NRC FO M 366 U. S. NUCLE AR REGULATORY COMMISSION (7 77)
LICENSEE EVENT REPORT (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
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l RELE ASED OF RELE ASE I I li 161 7 8 9 U @ l l@l to 11 44 l
45 80 h PERSONNEL EXPOSURES NUP.*B E R TYPE DESCRIPTION >
II! 7l { l { l PERSONNE L INJURIES
! NUv8ER DESCRIPflON I
li ta l l I I l@l12 80 7 8 9 11 LOSS OF OR DAVAGE TO FACILITY t TYPE DESCRIPTION
!l !9I 80 l 7 8 9 10 PU8 uciTY NRC USE ONLY
- DESCRIPTION ISSUED l llllllllllllI*;
l l2loll l l 68 69 80 5 7 8 3 10 NAME OF PREPARER PHONE:
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