ML19210E362

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LER 79-034/03L-0:on 791101,during Surveillance Testing, Standby Liquid Control Pump Relief Valve Operated Below Tech Spec Limit.Caused by Setpoint Drift on Jmsk Crosby Valve. Valve Readjusted within Tech Spec Limit
ML19210E362
Person / Time
Site: Peach Bottom Constellation icon.png
Issue date: 11/28/1979
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
LER-79-034-03L-01, LER-79-34-3L-1, NUDOCS 7912040405
Download: ML19210E362 (1)


Text

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Mr. Doyce H. Grice, Director .

No.

Office of Inspection (, Enforcement, Region l 3 79 3h/3L o U.S. Nuc lear Regulatory Corrinission 631 Park Avenuc King of Prussio, PA 1 % 06 Dc .n Mr. Gricrt This LER refers to the setpoint drift of the standby liquid control pump relief vr.1ve. The governing Tech Speo is h.h. A.2. A U. S NtJCL E AR RE GUL A1oHY cOVW5510N LICENSEE LVENT REPORT coNinol etocic l l l l l l

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[nI4) L which is below the required minimim sot _t.ing of 1h00 PSIG. Redundant t

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[T{K] [ The cause was setpoint drift on model JWK Crosby valve which Q] [_ wa_s _ readjusted, retested, and returned to service. Test resulta were i gp[ within Tech Spec limits.

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