ML18153D096

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LER 92-009-00:on 920713,automatic ESF Actuation Signal Occurred,Causing Auxiliary Feedwater Sys motor-operated Valves to Receive Open Signal.Caused by Failure of 25A9 Breaker to Trip.Svc Water Leak isolated.W/920812 Ltr
ML18153D096
Person / Time
Site: Surry Dominion icon.png
Issue date: 08/12/1992
From: Kansler M
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
92-536, LER-92-009-02, LER-92-9-2, NUDOCS 9208190138
Download: ML18153D096 (5)


Text

e 10CFR50.73

. Surry Power Station P.O.Box:315 Surry, Virginia 23883 August 12, 1992 U. S. Nuclear Regulatory Commission Serial No.: 92-536 Document Control Desk SPS:MDK

. Washington, D. C. 20555 Docket No.: 50-281 License No.: DPR-37

Dear Sirs:

Pursuant to Surry Power Station Technical Specifications, Virginia Electric and Power Company hereby submits the following Licensee Event Report applicable to Surry Power Station Unit 2.

REPORT NUMBER 50-281/92-009-00 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be forwarded to the Management Safety Review Committee for its review.

Very truly yours,

. . Kansler Station Manager Enclosure cc: Regional Administrator 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323 M. W. Branch NRC Senior Resident Inspector Surry Power Station 9208190138 920812 180044.

PDR ADOCK 05000281 S PDR

NRC FORM 366 US. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 (6-89)

EXPIRES: 4130/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN LICENSEE EVENT REPORT (LER) ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), U.S.

NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.

FACILITY NAME (1) DOCKET NUMBER (2) PAGE 3 Surry Power Station, Unit 2 05000281 OF O 4 TITLE (4)

EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)

SEQUENTIAL REVISION FACILITY NAMES DOCKET NUMBER(S)

MONTH MONTH DAY YEAR NUMBER NUMBER 0

0 7 139292 0 0 9 0 0 0 8 5 0 0 0 OPERATING MODE (9) 73.71(b) 20.405(a) (1) (i) S0.36(c)(1) 50.73(a)(2)(V) 73.71(c)

OTHER 1Spocify in Abstr"'1 20.405(a)(1 )(ii) S0.36(c)(2) S0.73(a)(2)(viQ .

be!ow and in Tm:t NRC Form 366A) 20.405(a)(1 )(iii) 50.73(a)(2)(1) S0.73(a)(2)(viii)(A) 20.405(a)(1 )(iv) 50.73(a)(2)(11) 50.73(a)(2)(viii)(B) 20.405(a)(1)(v) 50.73(a)(2)(iii) S0.73(a)(2)(x)

LICENSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NUMBER M. R. Kansler, Station Manager AREA CODE 804357 REPORTABLE TO NPRDS X EA B K R EXPECTED MONTH DAY YEAR SUBMISSION YES (II yes. complete EXPECTED SUBMISSION DATE) DATE (15)

ABSTRACT (Limit to 1400 spaces. i.e., approximately fifteen single-space typewritten &nos) (16)

At 2328 hours0.0269 days <br />0.647 hours <br />0.00385 weeks <br />8.85804e-4 months <br /> on July 13, 1992; with Unit 1 at IOO% power and Unit 2 at cold shutdown, an automatic Engineered Safety Feature (ESF) actuation signal occurred causing the Unit 2 auxiliary feedwater system motor operated valves to receive an open signal. The ESF signal was generated when the "2A" station service bus was deenergized removing electrical power from the "A" condensate pump, causing low suction pressure to the main feedwater pumps. The low suction pressure generated an ESF Signal to start the motor driven auxiliary feedwater pumps and open the auxiliary feedwater motor operated valves. A four-hour non emergency report was made to the NRC in accordance with IO CFR 50.72.

At the time the auxiliary feedwater motor operated valves received an open signal, Unit 2 was in cold shutdown with the Residual Heat Removal (RHR) System in service. The auxiliary feedwater system was not required to be operable for the affected Unit. In responding to an event on non-safety related equipment in the turbine building, the operating team had identified the need to deenergize the "2A" station service bus and were aware that the auxiliary feedwater motor operated valves would open. When the "2A" bus was deenergized, the "A" condensate pump breaker tripped on undervoltage, a low pressure condition was sensed at the feed water pumps and the auxiliary feedwater MOV s received an open signal as designed.

Steam generator levels remained normal throughout the event with ample heat sink available. Core cooling was provided by the RHR system. At no time during the event was the auxiliary feedwater system required. Therefore, the health and safety of the public were not affected. _ This event is being reported pursuant to IO CFR 50.73(a)(2)(iv), for an automatic actuation of an ESF.

NRC Form 366 (6-89)

NRC FORM 366A US. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 (6-89) EXPIRES: 4/30/92 ESTIMATED BURDEN PER*RESPONSE TO COMPLY WITH THIS INFORMATION LICENSEE EVENT REPORT (LER) COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN TEXT CONTINUATION ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), U.S.

NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPI.RWORK REDUCTION PROJECT (3150-0104). OFFICE OF MANAGEMENT AND

FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE(3)

REVISION Surry Power Station Unit 2 YEAR

~~~i~~j SEQUENTIAL NUMBER ttr NUMBER ol sl o I ol 0 l2lsl1 9 I2 - 0 I 0 I 9 - 0 I 0 0 I 2 OF O I 4 TEXT (II mere space ls required, use oddiional NRC Ferm 366A'*J .(17)

1.0 DESCRIPTION

OF THE EVENT On July 13, 1992 with Unit 1 at 100% power and Unit 2 at cold shutdown with the residual heat removal (RHR) system [EIIS-BP] in service, the Unit 2 auxiliary feedwater system (AFW) [EIIS-BA]

motor operated valves (MOVs) received an open signal as the result of planned actions taken to correct the failure of a circuit breaker to trip on a non-safety related chiller.

  • The turbine building operator was performing a routine swapover of the mechanical refrigeration units in the chilled water system

[EIIS-KM]. The Unit 2 mechanical refrigeration unit continued to run when the local stop circuitry was activated. One result of the chiller malfunction was a leak in the service water supply line to the chill~r unit. The service water leak was isolated. Attempts by a Senior Reactor Operator (SRO) to trip the chiller unit's breaker (25A9) located in a switchgear room were unsuccessful. The breaker could not be racked out due to the mechanical interlock preventing engagement of the racking tool when the breaker contacts are closed.

_The SRO determined thai the associated.station service bus "2A" [EIIS-EA] feeder breaker (25Al) should be tripped and its control and trip fuses pulled. Bus loading was reviewed and it was identified by the SRO that the "A" condensate pump would trip, resulting in a loss of condensate recirculation flow and a low suction pressure signal to the main feedwater pumps. The SRO also identified that the low suction pressure to the main feedwater pumps generate a main feedwater pump trip signal and initiate an automatic start signal for the motor driven auxiliary feedwater pumps and an open signal to the auxiliary feedwater motor operated valves (MOVs).

Discussions between the SRO and the Unit 2 SRO *confirmed that maintaining condensate flow was not necessary and could be secured under existing plant conditions. Both motor driven AFW pump control switches were in their normal pull-to-lock position for plant conditions. The SROs concurred that the resultant low suction pressure at the main feedwater pumps would result in an automatic open signal to the auxiliary feedwater MOV s, an Engineered Safety Feature (ESP) actuation [EIIS-JE].

When the "2A" station service bus and its associated loads were deenergized, the "A" condensate*

pump tripped as expected due to the undervoltage condition. The Auxiliary Feedwater MOVs received an automatic signal to open as expected, and benchboard indication as observed by the Unit 2 SRO, confirmed the MOY's opened. Actuation of an ESP system component is reportable in accordance with 10 CPR 50.73(a)(2)(iv).

NRC Ferm 366A (6-89)

NRG FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 (6-89) EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION LICENSEE EVENT REPORT (LER) COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN TEXT CONTINUATION ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), U.S.

NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.

FACILITY NAME (1) DOCKET NUMBER (21 LER NUMBER (6) PAGE(3)

REVISION YEAR i :~~; SEQUENTIAL NUMBER

~$]~~

~::::::::: NUMBER Surry Power Station Unit 2 oI s I o I o I 0 I 2 I 811 9 I2 - 0 I 0 I 9 - 0 I 0 013 rn: 014 TEXT (II more space lo required, use addllonal N.RC Fam 366A'*l (17) 2.0 SIGNIFICANT SAFETY CONSEQUENCES AND IMPLICATIONS This event resulted in no negative safety consequences or implications. At no time did actual plant conditions warrant an ESF actuation. Unit 2 was in the cold shutdown condition prior to the event occurring. The auxiliary feedwater system was not required to be operable for the affected unit.

Auxiliary feed water crosstie capability to and from the opposite unit remained available. The actions

~en to open the main feeder breaker and deenergize the "2A" station service bus were planned and nec~ssary to protect plant secondary equipment from damage and assure personnel safety was maintained. Core cooling was maintained through use of the RHR system. The service water system leak was processed. by the turbine building sump pumps and isolated by operator action. The health and safety of the public were not affected.

3.0 CAUSE OF THE EVENT This event resulted from a failure of the 25A9 breaker to trip. A worn toggle assembly caused binding on the mechanical linkage mechanism preventing the breaker from tripping open.

4.0 IMMEDIATE CORRECTIVE ACTIONS The "2A" Station Service bus loading was reviewed by the SRO tasked with deenergizing the "2A" bus. The associated 480 volt buses (2Al and 2A2) were crosstied to the remaining energized buses

  • prior to deenergizing the "2A" bus. Breaker 25Al, the "2A" station service bus feeder breaker, was tripped open, racked out, and the control fuses were removed. The 25A7 breaker was tripped, preventing backfeed to. the 2A bus through the 4160/480v transformer. The service water leak was isolated by securing the associated pump (2-SW-P-4B) and locally closing manual valves (1-SW-460 and 2-SW-414).

5.0 ADDITIONAL CORRECTIVE ACTIONS Station Work Order 129506 repaired breaker 02-EPH-BKR-25A. The service water piping leak has been repaired.

6.0 ACTIONS TO PREVENT RECURRENCE A Root Cause Evaluation Team (RCE) has been established to investigate this event.

Recommendations will be implemented as appropriate.

NRC Form 366A (6-89)

"G ----------------1 NRC FORM 366A

  • U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3150-0104 (6-89) EXPIRES: 4130/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION LICENSEE EVENT REPORT (LER) COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN TEXT CONTINUATION ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), u~s.

- -* NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104). OFFICE OF MANAGEMENT AND BUDGET, WASHiNGTON, DC 20503.

FACILITY NAME (1) OCX:KET NUMBER (21 LER NUMBER (6) PAGE(3)

REVISION Surry Power Station Unit 2 YEAR

~flt~ SEQUENTIAL NUMBER iim NUMBER oIs I o I ol o I 2 Is I 1 9 I 2 - 0 I 0 I *9 - 0 I 0 014 OF 014 TEXT (If more space is required, use addilonal NRC Form 366A's) (17) 7.0 SIMILAR EVENTS The following Licensee Event Reports involved unplanned ESF
:lctuations. of auxiliary feed water pumps and/or MOVs.

LER 89-022 (Unit 2), dated 7-3-89; LER 86-009 (Unit 1); dated 2-25°86; LER 86-010 (Unit 1), dated 2-27-86.

8.0 ADDITIONAL INFORMATION MANUFACTURER/MODEL NUMBER:

Manufacturer: Asea Brown Boveri Model Number: 5HK250 Serial Number: 44252C3-6-11C NRC Form 366A (6-89)