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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket ML18153A2201998-02-0606 February 1998 LER 98-001-00:on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was submitted.W/980206 Ltr ML18153A2071998-01-13013 January 1998 LER 97-012-01:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors ML18153A2101998-01-13013 January 1998 LER 97-009-01:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status ML18153A1911997-11-26026 November 1997 LER 97-011-00:on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket ML18153A2201998-02-0606 February 1998 LER 98-001-00:on 980108,deficient Test Due to Faulty Test Equipment Resulted in TS Violation.Caused by Faulty Vibration Analyzer Cable or Loose Connection.Station Deviation Rept Was submitted.W/980206 Ltr ML18153A2071998-01-13013 January 1998 LER 97-012-01:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Two Breakers in Security Distribution Panel.Reset Affected Breakers Which Restored Power to Security Systems & Affected Doors ML18153A2101998-01-13013 January 1998 LER 97-009-01:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Caused by Inadequate Maint of Intake Canal Level Probes.Subject Probes Were Cleaned, Tested Satisfactorily & Returned to Operable Status ML18153A1911997-11-26026 November 1997 LER 97-011-00:on 971030,determined That Periodic Test Procedures for Testing Reactor Trip Bypass Breakers Did Not Test Manual Undervoltage Trip.Caused by mis-interpretation of Term in-service. Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage. ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With 990115 Ltr ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un. ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With 981214 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With 981111 Ltr ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With 981012 Ltr ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2.W/980807 Ltr ML18152B7621998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Surry Power Station,Units 1 & 2.W/980707 Ltr ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML18153A3141998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Surry Power Station,Units 1 & 2.W/980610 ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B8161998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Surry Power Station Units 1 & 2.W/980508 Ltr ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML20217P9941998-04-0707 April 1998 Safety Evaluation Granting Licensee Third 10-yr Inservice Insp Program Relief Requests SR-018 - Sr-024 ML18153A2951998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sps,Units 1 & 2.W/ 980408 Ltr ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket 1999-09-30
[Table view] |
Text
... ' *., MAR 05 '96 10:08 NLD e P.2/10 VIRGJNIA ELECTRIC ANO POWER COMPANY .
Suny Power Statum P.O. Box 31S Suny. Virginia 23883 U.S. Nuclear Regulatory Commission Serial No.: 90-377 Document Con~ol Desk Docket Ho. : 50-280 Washington, O.. C. 20555 50-281 License Ho. : DPl.-32 DPR-37 Gentlemen:
Pursuant to Surry Power Scacion Technical Speci.f1carious. Virginia Elec~ric alUi Power Company hereby submits the follOlriug Licensee Event Repo~t far Unies land 2.
REPORT NUMBER 90-004-00
'Ibis r11::yort has beeu reviewed by the Stat:Lcn Nuclear Safety and Operating I Committee and w:il1 be reviewed by Corporate N11clear Safety.
Very truly yours,
.).
~~6-(!.J1.. Kansler Station Managet:
Enclosure RECEiVED BY cc: R.egioual Admiuistrator Suite 2900 101 Mariet-ca Street, NW NOV 1 6 1990 Atlanta, Georg~a 30323
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'I I On May 22, 1990 at 1150 hcurs with Units 1 and 2 at 100% power, a fa.ult occurred on the Unit l "A" main cransformel:" as a result.of an ina.dverten~ actuation of the transfarme.r's deluge system. the fault II I-initiated a Unit 1 generator differential lockout which immediately initiated a turbine trip/re!!actor trip. The fault also resulted in the lockout of the "A11 ReserV'e Station Service Trausfomer (:RSST).
Approximately 10 seconds later, the Unit 2 control room operator initiated a mauual reactor trip after observing erratic control rod I Individual Rod Position Indications (IRPI). Opera~o~s performed the appropriate plant pr~cedures and quickly stabilized the units following the trips. The erratic- Unit 2 IRPI indtcations were due to voltage transients that occurred on both units' etiie~gen~y b~~e$
which were caused by the Cnit 1 generator tl:'ip, the 11 A11 RS$T lockout, and subsequent motor star~s. The #3 Eme~gency ntesel Generator automatically restored power to the Uni.t;: 1. "J" eme-rgency bus which was de-energized by the "A 11 RSST loc:kou1;. A four hour non~ergency report waa made to the Nuclear Regu.Latory Commission in accordance with 10CFR50.72.
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...--...3W'MAR "'5 '96 10:09 NLo----------------"'!""""'!1_1111!""_ _ _ _ _ _-t-'P.4/1-N"'r'. 'Cl;' '"' A U.S. NUCLIAA AEGUL.ATOIIY COlolMIUICN I
- LICENSEE EVENT REPORT (LERI TEXT CONTINUATION
- .UA6v&& 6i.ta N6. 3,so-0106
!XPIIIIGS: ":Klllrl UTIMATIO IUAOEN llliFI Rll5PONSi. TO CQ,Wll,V WTW TMIS INIIORMUION COLLECTION Ri0UE$T: 50.0 IIRS. FORWARD C:OM"'laNTS Rl!G .. AOINCi IIUROEN laSTIMATE TO TH! Al;CORDS AND Rl!POIIT5 MANAG~1"iiNT IRANCH IP,5301. U.S. NUCL~R Rl!GULATOIIV COMMISSlO."I, Yt"'$HINGTQN. 0C :OS6S, ANO TO l"HE PAPi!!RwORt.-: 51EOUCTION i'ROJ!cT Clt!Q.(11041. oi;i;1~
01' MANAGEUENT ANO 8U0Cl;T. WASHINGTON. 0C~ll$0l.
I DOCKET NUMe!R J21 ~ill NUMUR COl PAGI Cll I
Su b:'y Power Station, i.:nits l and 2 o Is I o 1o ; o I 2 l 8 I o 9 Io 1- o I o14 . J- OIO 012 OF OJ6 l.O Descrintion of the Event On May 22, 1990 at 1150 hours0.0133 days <br />0.319 hours <br />0.0019 weeks <br />4.37575e-4 months <br /> with Units l and 2 at 100% power, a fault occurred on the Unit l "A" main transformer as a result of an inadvertent actuation of the transformer's deluge system. The fault initiated a Unit l generator (EIIS-GE~,TH) differential lockout which immediately initiated a turbine trip/reactor trip. Approximately 10 seconds later, the Unit 2 control room operator initiated a manual reactor trip after observing erratic control rod Individual Rod Position Indications (!RP!) (E!!S-2I.AA).
Approximately two minutes prior to the tripst control room annunciators alerted conerol room operato~s of the actuation of the 11 A" main transformer deluge system (EI!S-KP). Plant operators were dispatched to the transfor.ner and verified that no fire existed and initiated isolation of the deluge syste~. As plant operators we~e isolating' the deluge, arcing was observed from the "A11 main transformer to the generator output isophase bus duct and t:o the "An Reserve Station Service Transformer (RSST) (EI!S-XFMR) bus bars. In addition to the generator differential lockout, the arcing initiated a. lockout of the "A" RSST, which coupled with the Uuit l gene~ator trip, resulted in de-energizing the Unit l "A" Station Service (SS) (EIIS-'EA) bus and the Unit l "J" 4160V emergency bus (EIIS-EK). The #3 Emergency Diesel Generator (EDG) (E!IS-GEN,EK) automa.t~cally started and restored power to the t1n1t l "J" bus within seconds of the "A" RSST lockout. Majo-r equipment supplied by the Unit l "A" SS bus includes the "A" Reactcr Coolant Pump (EIIS-P,AB), the "A" Main Feedwater Pump (EIIS-P, SJ) and the "A Condensate Pump (EIIS-P-KD). The "C" condensate pump automatically started when the "An condensate pump was de-energiz:;ed..
Following the iuitiation of the manual Un.:L.t 2 reactor trip, a Uuit 2 generator trip occurred as desigued 24 seconds later. The 11 A" RSST a.lsc supplies the Unit 2 "A" SS bus when the unit generator is off line.
Consequently. the lockout of the "A" RSST. c:ou.-pled
.t NRC F!)R . 3&MAR 05 '96 10: 09 NLD e
U.S. NUCl.fAA ltl!GULA TORY CQMllffllSlQH
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e LICENSEE EVENT REPORT ILER> l!STIUATGO 81.lROl!N PER REPONSf: TO COMPLY WTM TMIS INFORM.t.TION COLLliCTICN Af:QuiST: !50.0 HR$. FORWARO CCMM!iNTS REGARDINO BURDf.N iSTIMATE TO TH~ AEc0t'1D:i TEXT CONTINUATION ANO A1590RTS IIIANAGEMeNT IIRAfllCN 11*-SJOI. U,S. NUCl.l!AA REGULATO>IY cor,U,'IISSICN. WA5MIN<;iTON, DC =!!. ANCI TO n1e PAl'l;RWORIC lleOUCTION PROJl;CT (3150-0111'1. o,,,ci OF MANAQliMeNT ANO BUDGET, WA$i'IINGTON, DC 20=o:J.
ICOCKl;T NUllllilR IZI Lll!II NUMllll!lt 1111 PAGI 131
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Su; y Power Station, U:1its l and 2
,e,.,..1 1n lo ls f o l o Io I 2 rs I o 9 I o - Of OJ4 - o I o 01 3 OF 016 with the Unit 2 generator trip, resulted in de-energizing the Unit 2 11 A11 SS bus. Major equipment supplied f-rom this bus, including the Unit 2 "A" Reactor Coolant Pump and Unit 2 "A" Main Feedwater Pump; was de-energized. A load shedding scheme designed to shed various loads from both Units' SS buses to maintain voltage on the RSS buses was initiated. This resulted in tripping the second Unit 1 Main Feedwater Pump terminating Unit l tnain feedwater flow. How~ver. the auxiliary feed pumps had started as designed on lo~ Steam Generator (S/G) levels prior to the tripping of the second main feedwater pump and provided sufficient feedwater to the steam generators to recover level.
Following the trip, safety systems on both units functioned as designed, and beth units were stabilized. A four hour non-emergency report was made co the Nuclear ReiUlatcry Cotmnission in accordance
~ith 10CFRS0.72.
4 .0 Safetv Conseauences and !mglications During the event, the turbin~ protection and reactor protection systems for both units functioned as designed. The #3 Emergency Diesel Generator automacica.lly scarted and loaded onto the Unit 1 11 J 11 E'.mergency Bus as designed to restore power to the bus.
The loss of all Main Feed~ater ou Unit l was not significant as the Auxiliary Feedwater Pumps started and provided adequate feed~ater flow to the steam generators co maintain a heat sink for the reactor.
The two remaining Reactor Coolant Pumps en each unit continued to operate to provide forced flow through the reactor and maintain the reactor in a hot shutdown condition. There are no safety consequences associated f.l'ith the de-energization of each units' "A 11 Station Service Bus since equipmenc powered from ehese buses are not required to ensure safe reactor shutdown
_ or to mitiiate the cousequences of an accideuc.
Therefore, the health and safety of the public were not affected.
,__,.."i"!AR NN:1!C Mi;Jllll.111 05 '96 10: 10 NL.IJ l&.ael:*
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- u.s. IIIUCL IAA At:G UU.TOltV COMM ISSION -
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l E$TIMATEg IILll'IOl;N ~!ail lli;SPCNU TO C()Ml'~V WTIOI nus LICENSEE EVENT REPORT (LER) il\lFQRll,l,4.TION COLLl;CTION AE(ll.J!Si': SO.O HAS. FOl'IWAAO
,;QMl,li;NTS REOAACIING 8UR01;1\1 ESTlll,IATli TC TWE RECORCS TEXT CONTINUATION 41110 FIEPORT$ MANAGSMi;NT BRANCH IP*SlQl, U.$. t.uet.l!AR Ri<iULATOAY COMMISSION. Wl'-SHINGTON, OC mM. ANO TO THli IIAi>iRWOfh( REOUCTION PAOJEl;'r (J150<)I04J. 0/IFIC! r OF MANAGl!M!NT .a.NO BUDGET, W*>>tll\lGTON. OC: 2~03. f FA::11.:
$1 NAMI !11 ry ?ower Station, ~nits 1 and Z Ooet(i.T Nu~e111 1:z1 L~R NUMc1u1 101
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!he arcing which occurred on the Unit l main tranafc?:1ner has been attributed to the actuation of the 11 A" main deluge system which contained corrosion product contaminants. The distance between the "A" RSST bus bars a.nd the 11 A" Main Transformer 230KV leads is in confonnance with electrical codes and standards.
However, the proximity of these conductors is believed to have been a contributing factcr to the loss of the 11 11 A RSST.
Approximately 20 to 30 minutes prior* to the actuat.ion of the transformer deluge system, a construction employee inadvertently bumped the weather enclosure cabinet for the Unit 1 transformers' deluge manual pull stations. The employee verified the pull staeion had not actuated immediately after he bumped the cabinet. However, following the event, the manual pull station was discovered in the actuated position.
The pull stations are maintained in the de-actuated positicn by a glass rod which holds the pull lever in the upright position. The pull station is actuated by pulling down the lever which breaks the glass. The pull station will also fail to the actuated position if the glass fails. It 1s surmised that the glass failedt and the pull station actuated 20 to 30 minutes after the enclosure was bumped~
The Unit 2 !RPis are powered from the Unit 2 semi-vital bus, which in turn was po~ered from the Unit 2 11 J 11 emergency bus. The transformer that supplies power to the IRP!s 1s designed to maintain its output voltage with+ 0.5% when the input voltage is within+ 10%. Following the Unit l t~1p, a. voltage.
transient ;cc:urred on both units emergency buses. due to the fault and subsequent large motor starts. The voltage transient on the Unit 2 tt.rn eiuergency bus exceeded the + 10%. This was sufficient to cause significant fluctuations in the IRPis which prompted the Unit 2 operator to trip ehe Unit 2 rea~tor. (Refer
- to Attachment l for break.er pos*it1ons.)
4.0 !mmediate Corrective Action(s)
Operators followed appropriate plant procedures to quickly stabilize the units following the respective reactor trips. Also, the Shift Technical Advisor L..--1~------------------------**-----*-
NRC IIOl'I
~~~~~~~~~~~~*.
~MAR 05 '96 10: 10 NLD A u.s. NUCUAR REQULATCRV C:OMWIU"'N LICENSEE EVENT REPORT (LER)
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Su. y Power Station, Units land 2 o Is ! o I o ! o I 21 s 10 9 Io 1- o I 01 41- oIo oIs oi:
monitored the critical safety function status trees to ensure specific plant parameters were noted and that those parameeers remained within safe bounds.
5.0 Additional Corrective Action(s)
All main and station service transformer deluge systems were flowed in accordance with periodic test procedures.
The fire protection manual pull stations for the Unit land Unit 2 transicrtllers have been replaced with pull stations which are less susceptible to inadvertent actuation.
The "A" Ma.in 'transformer was inspected following the trip and no preexisting conditions which could have caused the arcing were found.
The High Voltage bushing en the output on the Unit l 11 A" Main transformer, whic.~ was damaged. by the arcing, has been replaced.
A lightning arrestor on the "A" RSST damaged by the arcing has been r~placed. In additiont slight damage to the 4160V bus bars from the 11 A" RSST was repaired.
6.0 Action(s) Taken to Prevent Recurrence tn addition ca the corrective actious described above.
evaluacicns of enhancemencs to the IRP! system and ita power supply are being conducted. An evaluation will be pe~fo~ed to determine the feasibility of enhancing the separation bet.ween the "A" Main Transformer* a.nd the "A" Reserve Station Service bus bars. In the interim, the deluge system to the "A" Main Transformer has been isolated based on engineering g,~idance, and an evaluation of t~e deluge system is being conducted.
1'"'~.8/1~~--------_,,.
e LICEN$EE EVENT REPORT ILEA)
IJ.$, JfUC:UAR IUiGIII.A TOIIV COMMISSION * >>~Yl!D o,,,1 ..o. 3150 ,0,04 eXPIAEiS: 4 ~
QT1MATEO IIURCIEN Pill! RliSIIOHII! TO CQl,Ull,V WTM Tl,f1S IN¢0Ri..it.TION COLLECTION FIEOIJ!S'f: ~O.CI MAS. ,ORWARO CQIIIIMli ..TS fll!GAAOING UURt'EN li5TIMATE TO THE Rl!CORC5
'v TEXT CONTINUATION ANO AU¢R1S P,,tANAGEMlil\lT ~ANCM iP*9JOI, U.S. NUCUAR REGU!.Al'O>!V COMMISSION. WA/;>UNGTON. CC 20555. ANO TO 1'ME PA,.l;RWORK RECUCTION PAOJl!CT c:111i0-01041. CFFICI 01' MA~EMiNT I.NO 8UQGET. WASHIH<iTOH, CC 20803.
FAC!&:.IT NAMII (1 I DOCICliT IIWMllill 121 1.!fl JfUMHII Ill I
S~ ~Y Po~er Station, Units land 2 o 1s Io Io Io I 218 I o 910 - o f Oj 4 -, o 10 0 J6 0~ OJ 6 T&xT Ill. ~-
- IW'//llff, 11* .ulfiDMi /liRC Fann J!illA -., ill) 7.0 Similar Events LER 1*89-44: "Manual Reactor 1'rip/Turb1ne Trip Initiated Following Less of Power to Semi-Vital Bus c:au1:1ed by a Fa.ult on 11 A" RSST". This event: occurred due to roofing material blowing off the turbine building roof and faulting the "A" RSST.
a.o Manufacturer/Model Number(s)
General Electric Single Phase, 60 cycle 1 Class FOA (Manual GEK*l64l2).
Moloney LTC (Load Tap Changer) Transformer, Type MA, Design X-760.
ji
~* *~ MAR 05 '96 10:11 NLD e Breaker e P,9/10 Position Prior 'ro Event LER 280-90-004 Attachment 1 From cffsite ciistribution From offsite disl:l'ibution Figure l Bus 6 34.S KV 6
RSST 34.SKV i 4160V . . RSST
- 262
,.1SF1 4160V 4160V Emetg. Bus limerg. Sus 2SHS lH 2H 0
4160V
'1:2rv SOOI<V 22KV 1SJ7 L. To Unir 1 Emergency Gu.ssos Cl02 Unit 1 Unit2 Cenenstar Generator Les;end
-J-. Transformer
-r-"
Op,m '4160 V & Up D Braaker 480 120 Closed 4160 V &: Up Breaker To480V To Unit2 Emergenq and 12.0VUPS ) 480 V &:: below
- Semi-Vital Brabr Bus (Vital BuSSflJ
P.10/10 MAR 05 '96 10:12 NLD e
Breaker Position After Event Ul and U2 Generator Output Breakers Open LER 280...90-004 Attachment 1 From offsite distribution Fram oifsite distribution Figure 2 34.SKV 111ill(
4160V 4160V 1SH8 Emerg.6us Emerg. Bus 1H 2H
,f 41611V 2~ lil!W'5-81111 4160V
~
2SJ7 15J7 To Unit l E~ncy Busse, C102 Unit 1 Unit2 Gerwracor Ganeratot
~ I 2J-1480V Emorgcnc:y Bus lJM Open 4160 V &c Up D Bn=aker 480 120 Closed 4160 V & Up Braker To480V io Unit2 Emergency and 120VU'PS ) 480 V &; beJow Scmi*Vital Breaker 8u:1 (Vital Su~s,