ML18139A481

From kanterella
Jump to navigation Jump to search
LER 80-041/03L-0:on 800625,pipe Stress re-analysis Indicated Baseplate Anchor Bolts on Hanger H-2 on Line 12 Inch -CC-27- 121 & Hanger H-9 on Line 12 inch-CC-33-121 Overstressed. Mods to Anchor Bolts Complete
ML18139A481
Person / Time
Site: Surry Dominion icon.png
Issue date: 07/24/1980
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
LER-80-041-03L-01, LER-80-41-3L-1, NUDOCS 8007280625
Download: ML18139A481 (2)


Text

()t;TRO.L BLOCK: 1 J__J 8 (PLEASE PRINT DR TYPE ALL REQUIRED INFORMATION)

-0, ~1~,.~j l v I~ I s l PI 8~1__,1'--l----'0-!----'0-!___,,,_I fo Io Io Io Io 1- Io Io 101, 11 1 I 1 I 1101 I I (D 7 8 9 LICENSEE CODc 14 1L5_ _,___.,_____,L---"c....,_L....,1Ce....E..i..N_;SE"'-N....LU_t-""1s_E__R-"'--'-------><--'-~25 26 LICENSE. TYPE JD 57 CAT 56 CON"T IO I, I 7 8

~
~~~ LI:J0 I oI s I o I o I oI 21 sI o/01 o I 6 J 2 1s ! s lo 1©1074 75 I 7! 2 14 Is Io80JG) 60 61 DOCKET NUMBER 68 69 EVENT DATE REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@

I o I 2 J I Pipe stress reanalysis by A.E. indicated baseplate Anchor Bolts on hanger H-2 on line IO j3 j 12 11 -CC-27-121 (Supplies Boron evaporator distillate coolers and overboard condenser IO J 4 J component cooling) and hanger H-9 on line 12 11 -CC-33-121 (takes discharge from waste Jo j s j I disposal evap. dist. cond.) are overstressed. This event is reportable in accordance Jo Js j jwith'-IE Bull'etin-79-02. The health and safety of 0 7 the public were not affected.

Io J s l 80 7 8 9 SYSTEM CAUSE CAUSE COMP. VALVE

,e CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE 0 9 8

lw I Bl@ w@ L£J@ , s , u I p , a IR 9 10 IT ~ Lu@

11 12 13 18 19 20 SEQUENTIAL OCCUR REN CE REPORT REVISION

(:::;\ LE R/RO LVENT YEAR REPORT NO. CODE TYPE NO.

\.'..V :J~~~~ I21 I 8 OJ I23 I I I 1 261 O 4 1 I/ I I28 I . 291 O 3

~ L=J ~

22 24 27 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ,:;:;.. ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS \:::) SUBMITTED FORM SUB. SUPPLIER MANUFACTURER u.J@L.Ll@

33 34

~@

35 LU 36 I 0101 01 37 Oj 40

~@

41

~

42 U.l@

43 I<< rd . oI -ii 4 I 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @

0 I Stress reanalysis calculations indicated Baseplate Anchor Bolts overstressed.

Baseplates have been modified as required.

I.:TI],L--------------------------------------------'

B 9 80 FACILITY METHOD OF r:;::;-.

STATUS  % POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION ~

Lu@ j l I 01 OJ@)._!_ _ _ NA _ _ ____. LEJ@I Architect Engineer Analysis 8 9 10 12 13 44 45 BO ACTIVITY CONTENT Q\

RELEASED OF RELEASE AMOUNT OF ACTIVITY~ LOCATION OF RELE~E @

QTI ~@) ~@I NA NA 8 9 , 10 11 44 45 BO PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION@

8 Io 9

I o1 o11J@L:J@) 12 NA 1'-3----------------------------------------JBO PERSONNEL INJURIES r,"';\

f\:UMBER DESCRIPTIONO 8

lo 9

lo jo 11 J ~ ~ ~ ~ - - - - - N _ A_ _ _~ - - ~ - - - ~ - - - - ~ - ~ - - - - '

1~ BO LOSS OF OR OAP.IAGE TO FACILITY '4J\

TYPE DESCRIPTION ~

12J@ . NA 8 9 10 80 PUBLICITY ~

NRC: USE ONLY

B 'f5zErerESCR1PT10r; ~ NA e 1111111111111!

8 S 10

.a oo 7 2sn c~,;= 68 69 80 ;:;

NA1.1E OF PREPARER J. Y. Wilson (804) 357-3] 84 0


PHONE: 1l.

C)

,_ AITACHNE~T 1 SURRY PO~'iER STATION UNI.ie DOCKET NO: 50-280 REPORT NO: 80-041/03L-0 E"VENT DATE: 6-25-80 TITLE OF REPORT: EXCESSIVE STRESS ON BASEPLATE ANCHOR BOLTE, LINES 12"-CC-27-121 AND 12"-CC-33-121

1. Description of Event:

While continuing the program of reanalysis of pipe stress data it was revealed that two (2) supports were overstressed (exceeding 50% ultimate capacity). H-2 on line 12"-CC-27-121 (Supplies Boron evaporator distillata: coolers and over-board condenser component cooling) and H-9 on line.12"-CC-33-121 (takes discharge from waste disposal evap. dist. cond.). This event is repJrtable in accordance with IE Bulletin 79-02.

2. Probable Consequences and Status of Redundant Systems:

These lines are supplied from the component coolant pumps via the component coolant heat exchanger and discharge back to the header S1J?plying the component coolant pumps. Had a rupture occurred due to overstressed hangers, the possibility for partial loss of the Component Cooling System could hav~ existed. Under the' circumstances present, the health and safety of the public were not affected.

3. Cause of Event:

The Architect Engineer encountered this problem while conducting pipe stress re-analysis. The supports did not pass the safety factor of 2 due to inclusion of the flexibility factor. However, since the safety factor analysis without flexibility was not completed, the margin of original design was not deter.rrined.

4. Immediate Corrective Action:

The isolation valve to the main component cooling line was isolated; therefore, minimizing the effects.

5. Subsequent Corrective Action:

Since modifications have been made to eliminate the overstressed condition,: no subsequent action is required.

6. Future Corrective Action:

Analysis will continue and modifications will be made to r:=.lieve any overstress condition encountered.

7. Generic Implications:

Analysis continues to discover and rectify all overstressec conditions.