ML18136A433

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LER 80-001/03L-0:on 800101,w/unit at Cold Shutdown,Snubber 1-WFPD-HSS-14 Found W/Empty Reservoir & Declared Inoperable Per Tech Spec.Caused by Leakage Around Pipe Nipple Threads on Valve Block & Extended Seal Washers.Snubber Replaced
ML18136A433
Person / Time
Site: Surry Dominion icon.png
Issue date: 01/22/1980
From: Stewart W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18136A432 List:
References
LER-80-001-03L, LER-80-1-3L, NUDOCS 8001250498
Download: ML18136A433 (2)


Text

NRC FORM 366 u. s~ NUCLEAR REGULATO (7-7..,71 . "'°'

.NSEE EVENT REPORT .*.

CONTROL BLOCK: L I--'-----1.--1--L.__-L..___JI 1 . 6 G) (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

!IE] I VI Al s I p I s I 7 8 9 LICENSEE CODE 1 101 14 15

°I OI - I OIO I OIO IO I- IO IO 1014 11 11 I 1 ! 1 101 LICENSE NUMBER 25 26 LICENSE TYPE 30 I I© 57 CAT 58 CON'T CilJJ 7 8

~~~~~  !.:_JG) I o I s I o I o I o I 2 I s I o101 01 11 01 11 Bl 01@1 01 11 31 o! sl olG) 60 61 DOCKET NUMBER 68 . 69 EVENT DATE 74 75 REPORT DATE 80
  • EVENT DEs*cR IPTi oN *.o.No PRosAs*i::E col'ilsEauENc~s@:.

[II3J I With the unit at cold shutdown, Snubber 1-WFPD-HSS-14 was found with an empty

[QJ2J reservoir. The snubber was declared inoperable as per the basis for Technical Spec-.

[Q]I] fication 4. 17 and reportable per Technical Specification 6. 6. 2. b. (2). The inoperabi- -I

((I[] bility of the snubber had no effect* upon the health or safety of the general public

[)))) because the unit was in cold shutdown.

CIT[]

7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

[ill] I c1 HI@ LI@ ~@ I s I uI p I O I RI T 1@ LE.J ~@

7 8 9 10 11 12 13 1a 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION

@ LEA/RO ['.VENT YEAR REPORT NO; CODE TYPE NO.

REPORT NUMBER I 8J O I l::::.I I 0 l O 1* 11 1......-1 I O 13 I ~ . L=J L2J 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN {22) ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS M SUBMITTED FORM SUB. SUPPLIER MANUFACTURER L:J@L_j@

33 34

~@

35 L:J I 0 1°1 °1 I 36 37 '40 L:J@

41

~ Li I L l 3 I l I 9 I@

42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @

j The empty reservoir was due to leakage from around the pipe nipple threads on the o::::m I valve block and seal washers on the ~mubber Is bleed screws. The immediate corrective

[II}] 1 action taken was to replace the snubber with an operable one.

[IIT]

7 8 9 80 FACILITY METHOD OF ~

STATUS  % POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION

[2E) l_j@-1 01 Oj OJ@)_!_NA_ _ _ __ l.2:j~!...__Op~e_r_at_o_r~W._a_l_kd_o_wn~~~~~~~~~~I 7 8 9 10 12 13 44 45 46 80 ACTIVITY CONTENT Q\

RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE @

[iJI]. ~ @) l:.J@1.-I__NA_ _ _ _ _ ___, '----------'-------- _j NA

. 80 7 8 9 10 11 44 45 PERSONNEL EXl'OSURES ~

NU'e!BER. (;":;\ TYPE DESCRIPTION~

ITE1 I OI I OJl:J@'--__NA ____________________--,--__.

7 8 9 11 12 13 80 .**

PERSONNEL INJURIES ~

QNU~BER DESCRIPTION 41

~ I I I O l@._________________________*_J 7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION

'43'

~

~

7 8 9

~{S)L--~NA~~~~~~~~~~~~~~~~~~~~~~~~~~~~___,

10 80 PUBLICITY Q LI C} CY NRC USE ONL y ISS.LJEDQ DESCRIPTION~ 8 0 Q 12 5 0 7 / 0 * "'

ITI£] ~6'--_NA _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ____. II II IIIIII II I~

1 8 g 1o 68 69 80.;;;

0 NAME OF PREPARER w T, Stewart PHONE: (gQ4)357 3184 a..

Cl

ATTACHMENT, PAGE 1 of 1 SURRY POWER STATION, UNIT 1 DOCKET NO: 50-280 REPORT NO: LER-80/001/03L-0 EVENT DATE: 1-1-80 TITLE OF REPORT: Snubber l-WFPD-HSS-14 Leaking Reservoir Seal

1. DESCRIPTION OF EVENT With the unit at cold shutdown, Snubber l-WFPD-HSS-14 was found with an empty reservoir. The snubber was replaced and disassembled to determine the cause of leakage. The snubber was declared inoperable as per the basis for Technical Specification 4.17. This event is reportable per Technical Specification 6. 6. 2. b. (2).
2. PROBABLE CONSEQUENCES OF EVENT:

The inoperability of the Main Feed System Snubber, l-WFPD-HSS-14, had no effect upon the health and safety of the general public because the unit was in cold shutdown and the Main Feed System was not being used.

3. CAUSE OF EVENT:

The cause was found to be leakage around pipe nipple threads on the valve block and extended seal washers on the snubber's bleed screws.

4. Il1MEDIATE CORRECTIVE ACTION:

_The immediate corrective action taken was to replace the snubber with an operable one. All other snubbers on the 47' level in containment were inspected and none were found with low fluid levels.

5. SCHEDULED CORRECTIVE ACTION:

None.

6. ACTION TAKEN TO PREVENT RECURRENCE:

Periodic testing of snubbers will be performed in accordance with Technical Specification 4.17.

7. GENERIC IMPLICATIONS:

Since this is considered to be a random event, no generic implications exist.