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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
Text
RIORITY CCI'.LLTIUKTEDRll)S I'ROCI'.SSliG) 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RXDS)
ACCESSION NBR:9505220005 DOC.DATE: 95/05/08 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATXON ST MARTIN,J.T. Rochester Gas & Electric Corp.
MECREDY,R.C. Rochester Gas & Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION JOHNSON,A.R. Project Directorate I-1 (PD1-1) (Post 941001)
SUBJECT:
LER 95-003-00:on 950407,an inadvertent automatic SI actuation occurred when technician unblocked SIAS.Caused by misleading procedural dir'ection.Automatic start of engineered safeguards initiated.W/950508 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
j ENCL i SIZE:
05000244 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID 'CODE/NAME LTTR ENCL PD1-1 PD 1 1 JOHNSON,A 1 1 INTERNAL: AEOD S~/ B 2 2 AEOD/SPD/RRAB 1 1 CENT 1 1 NRR/DE/ECGB 1 1
/D EELB 1 1 NRR/DE/EMEB 1 1 NRR/DISP/PIPB 1 1 NRR/DOPS/OECB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SPSB/B 1 1 NRR/DSSA/SRXB 1 1 RES/DSIR/EIB 1 1 RGN1 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 2 2 NOAC MURPHY,G.A 1 1 NOAC POORE,W. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 N
YOTLT 'I 0 ALL"RIDS" RECIPIENTS:
PLE:KSE ISELP I:S TO REDUCE iVKSTE! CON'I ACT'I'IIE DOC!.'if!IY'I'COi'TROI.
DIS'I'RI II I UI'IOY. LIS'I'S I'OR DOCI 'ill'.X'I'S YOI.')OX"I'l DESk. ROO%1 PI-37 (EXT, 504-T083 ) TO I;LIXIIiA1'I'.YOI:R iAi!L:I'i<Oil I'.I)!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 26 ENCL 26
. ~
go~ A NO RKH"STEkDAS AIVD8'lk!C CORFOkATIOM 89 EAST AVEIVU, kCiw i,'>75k 6 4n:i,) i; ROBERT C. MECREDY vice pscs~cc~l e'u=iccr Ovesct,css May 8, 1995 U.S. Nuclear Regulatory Commission Control Desk 'ocument Attn: Allen R. Johnson PWR Project Directorate I-1 Washington, D.C. 20555
Subject:
LER 95-003, Unblocking of Safety Injection Actuation Signal While at Low Pressure Conditions, Due to Misleading Procedural Directions, Results in Inadvertent Automatic Safety Injection Actuation R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (iv), which requires a report of, "Any event or condition that resulted in a manual or automatic actuation of any engineered safety feature (ESF), including the reactor protection system (RPS)", the attached Licensee Event Report LER 95-003 is hereby submitted.
This event has in no way affected the public's health and safety.
Very trul yours, Robert C. Mecredy xc: U.S. Nuclear Regulatory Commission Mr. Allen R. Johnson (Mail Stop 14B2)
PWR Project Directorate I-1 Washington, D.C. 20555 U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Ginna USNRC Senior Resident Inspector 2 dsi/!
9'505220005 950508 PDR ADOCK 05000244 S PDR
NRC FORM 366 U.S. NUCLEAR REGULATORY COMHISSION APPROVED BY OMB NO. 3150-0104 (5.92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY 'WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
L1CENSEE EVENT REPORT (LER) FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEHENT BRANCH (HHBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, (Sce reverse for required number of digits/characters for each block) WASHIHGTON, DC 20555-0001, AHD TO THE PAPERWORK REDUCTIOH PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503.
FAcILITY NAME (1) R.E. Ginna Nuclear Power Plant DOCKET NUHBER (2) PAGE (3) 05000244 10F 12 TITLE (4) Unblocking of Safety Injection Actuation Signal While at Low Pressure Conditions, Due to Hisleading Procedural'Directions, Results in Inadvertent Automatic Safety Injection Actuation EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)
SEQUENTIAL REVISION FACILITY HAME DOCKET NUMBER MONTH DAY YEAR YEAR HONTH DAY YEAR NUMBER NUHBER 04 07 95 95 -003-- 00 05 08 FACILITY NAME DOCKET NUMBER OPERATING N
THIS REPORT IS SUBHITTED PURSUANT TO THE RE(jUIREHENTS OF 10 CFR 5: (Check one or mor e) (ll)
HODE (9) 20.402(b) 20.405(c) 50.73(a)(2)(iv) 73. 71(b)
POWER 20.405(a )(1)(i) 50.36(c)('I) 50.73(a)(2)(v) 73.71(c) 000 LEVEL (10) 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii) OTHER 20.405(a)(1)(iii) 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) (Specify in 20.405(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) Abstract below and in Text, 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x) NRC Form 366A)
LICENSEE CONTACT FOR THIS LER (12)
NAME John T. St. Hartin - Technical Assistant TELEPHONE NUMBER (Include Area Code)
(315) 524-4446 COHPLETE ONE LINE FOR EACH COHPONENT FAILURE DESCRIBED IN THIS REPORT (13)
REPORTABLE REPORTABLE CAUSE SYSTEH COHPONENT HANUFACTURER CAUSE SYSTEM COHPONENT HANUFACTURER TO NPRDS TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED MONTH DAY YEAR YES SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE). DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e:, approximately 15 single-spaced typewritten lines) (16)
On April 7, 1995 at approximately 0900 EDST, with the plant in the cold shutdown mode for the annual refueling and maintenance outage, an inadvertent automatic Safety Injection Actuation occurred when a technician unknowingly unblocked the Safety Injection Actuation Signal with pressurizer pressure and steam line pressure less than the setpoint for Safety Injection Actuation.
Immediate corrective action was to monitor the automatic start of engineered safeguards features components and secure unneeded equipment.
The underlying cause of the inadvertent automatic Safety Injection Actuation was due to misleading procedural direction. This event is NUREG-1022 Cause Code (D).
Corrective action to preclude repetition is outlined in Section V.B.
NRC FORM 366 (5-92)
NRC FORM 366A U.S. NUCLEAR REGULATORY COHHISS ION APPROVED BY OHB NO. 3150.0104 (5.92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COHPLY WITH THIS INFORMATIOH COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS HANAGEHENT BRANCH TEXT CONTINUATION (MHBB 7714), U.S. NUCLEAR REGULATORY COMHISSION, WASHINGTON, DC 20555-0001, AHD TO THE PAPERWORK REDUCTION PROJECT (3150.0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAHE (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 M
2 OF 12 95 -- 003 pp TEXT (If more space is required, use additional copies of HRC Form 366A) (17)
PRE-EVENT PLANT CONDITIONS:
The plant was in the cold shutdown mode for the annual refueling and maintenance outage. The reactor coolant system (RCS) temperature was approximately 100 degrees F, and the RCS was depressurized. RCS loop levels were at approximately 80 inches, which is a partially drained condition with water level four inches below the reactor vessel flange.
On April 6, 1995, calibrations of individual instrument channels associated with Reactor Protection System (RPS) Channel 3 were started for Nuclear Instrument System (NIS) channel N-43 (using calibration procedure CPI-BISTABLES-N43), pressurizer (PRZR) pressure channel P-431 (using calibration procedure CPI-PT-431), and RCS Average Temperature channel T-403 (using calibration procedure CPI-TAVG-403). These channels were defeated in accordance with procedures. The calibration steps of CPI-PT-431 had been completed, but the P-431 channel could not be reinstated because reinstatement activities also required the completion of calibrations of N-43 and T-403, which were not yet completed. Therefore, procedure steps for reinstating P-431 were not performed at this time.
The calibrations of N-43 and T-403 were completed on April 7'by teams of Instrument and Control (I&C) technicians. An I&C technician working in the Control Room was ready to reinstate the individual instruments associated with RPS Channel 3 (N-43, P-431, and T-403).
He had also been requested to support the IGC technicians assigned to calibrate PRZR pressures by defeating and reinstating pressure channels. The IIC technicians assigned to PRZR pressures were in the Containment Building (CNMT) and requested the IIC technician in the Control Room to defeat P-429, associated with RPS Protection Channel
- 1. The IEC technicians in CNMT and in the Control Room discussed the sequence of defeating and reinstating, and concluded that expeditious to defeat the P-429 channel and proceed with calibration it was more of PT-429, than to wait for reinstatement of N-43, P-431, and T-403 before defeating P-429.
HRC FORH 366A (5 92)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AHD RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 UM M 3 OF 12 95 -- 003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
On previous calibrations that week, and as part of the. pre-job briefings on April 7, the IEC technicians were advised that they could perform work associated with more than one protection channel at a time at this plant mode. Therefore, they concluded that acceptable to defeat P-429 first, and proceeded with the defeat of P-it was 429.
The calibration procedure that Operations perform (CPI-PT-429) initial conditions specified an operability check of the other PRZR pressure channels (but only F).
if Temperature was less than 350 degrees F.
RCS temperature was above 350 degrees Thus, the IIC technician in the Control Room marked this step as "Not'pplicable"
("N/Au) and did not request that the Control Room operators perform operability checks of the other PRZR pressure channels. The IEC technician continued with the defeat of P-429.
As part of the calibration procedure, the IIC technician had to obtain permission from the Shift Supervisor for the defeat of P-429.
The Control Room operators were aware that IEC would be performing activities associated with more than one RPS protection channel, knew that 'the calibration steps of CPI-PT-431 had been completed, and assumed that the P-431 channel had been reinstated the previous day.
Therefore, the Control Room operators gave the IEC technician permission to defeat channel P-429. The I&C technician proceeded to defeat channel P-429 using CPI-PT-429.
II. DESCRIPTION OF EVENT:
A. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
April 6, 1995: I&C starts calibrations using CPI-BISTABLES-N43, CPI-PT-431, and CPI-TAVG-403.
April 6, 1995: IRC completes calibration of P-431, but does not reinstate the P-431 PRZR pressure channel.
April 7, 1995, 0830 EDST: IIC completes calibrations of N-43 and T-403.
April 7, 1995, 0845 EDST: IRC obtains permission to defeat P-429 PRZR pressure channel.
NRC FORM 366A (5-92)
NRC FORH 366A U.S. NUCLEAR REGULATORY COHHISS ION APPROVED BY OMB NO. 3150 ~ 0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REOUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS HANAGEMENT BRANCH TEXT CONTINUATION (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAME (1) DOCKET NUHBER (2) LER NUHBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 4 OF 12 95 003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
April 7, 1995, 0900 EDST: Event date and time.
April 7, 1995, 0900 EDST: Discovery date and time.
April 7, 1995, 0908 EDST: Safety Injection Actuation and Containment Isolation signals are reset.
April 7, 1995, 0915 EDST: Containment Ventilation Isolation signal is reset.
April 7, 1995, 0930 EDST: Pre-event cold shutdown conditions are restored.
B. EVENT:
The plant was in the cold shutdown mode for the annual refueling and maintenance outage. The RCS temperature was approximately 100 degrees F, and the RCS was depressurized. RCS loop levels were at approximately 80 inches, which is a partially drained condition with water level four inches below the reactor vessel flange.
On April 7, 1995, two IRC technicians were in the CNMT for performance of annual calibration of PRZR pressure transmitters.
Another I&C technician was in the Control Room and was assigned to perform the defeating and reinstating of the PRZR pressure channels, as requested by the technicians in CNMT. The I&C technician in the Control Room was defeating channel P-429 using calibration procedure CPI-PT-429. At approximately 0900 EDST, the IEC technician in the Control Room placed the Safety Injection (SI) Unblock Bistable Proving Switch (BSPS) for P-429 to the tripped state.
The SI Actuation Signal (SIAS),is provided with a block signal which prevents a SIAS from occurring for low PRZR pressure and for low steam line pressure. At this time SIAS was blocked, which is a normal configuration when PRZR pressure is intentionally reduced below the SIAS setpoint.
NRC FORH 366A (5-92)
NRC FORH 366A U.S. NUCLEAR REGULATORY COHHISSION APPROVED BY OMB NO. 3150-0104 (5.92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COHPLY WITH THIS INFORHATION COLLECTION REQUEST: 50.0 NRS.
FORWARD COMMENTS REGARDING BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE INFORHATION AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (HNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001 AND TO THE PAPERWORK REDUCTION PROJECT (3110-0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAHE (1) DOCKET NUHBER (2) LER NUHBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 M
5 OF 12 95 003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
With the SI Unblock BSPS for channel P-431 state from calibrations completed the previous day, the logic to still in the tripped block SI from low pressure signals was the SIAS was automatically unblocked as soon as the P-429 BSPS still present. However, was placed in the tripped state. PRZR pressure and pressures in both the "A" and "B" steam generators (S/G) were below the setpoint for automatic SI Actuation, resulting in automatic SI Actuation from 2/3 Logic for PRZR pressure less than 1750 PSIG and from 2/3 Logic for S/G pressure less than 514 PSIG.
Automatic SI Actuation caused automatic actuation of CNMT Isolation (CI) and CNMT Ventilation Isolation (CVI) .
All operable Engineered Safeguards Features (ESF) components were observed to function properly, with the exception of valve position indication for MOV-852B (RHR Discharge to Reactor Vessel Deluge valve). 'he valve position indication for MOV-852B did not indicate full travel to the open position. However, subsequent investigation confirmed that the valve did, in fact, travel to the "full open" position. All safeguards busses remained energized from off-site power.
Due to plant conditions, several ESF components were not operable at the start of this event. The "B" D/G was inoperable for annual manufacturer inspection and overhaul. All three SI pumps were rendered inoperable (start switch in "pull-stop") to comply with Ginna Technical Specifications (TS) requirements for low temperature RCS over-pressure protection. Therefore, the "B" D/G did not start "and no SI pumps started. No injection flow from the SI pumps to the RCS occurred.
Initially one Residual Heat Removal (RHR) pump was in service.
The second RHR pump started due to the SIAS. MOV-852A and MOV-852B (valves for reactor vessel deluge from RHR pumps) opened to allow for RHR flow to the top of the reactor vessel, as well as continuing RHR flow via the normal shutdown cooling flowpath.
The total RHR flow was being controlled by flow control valve FVC-626, so no substantial increase in RHR flow occurred. The RCS remained stable at the initial conditions during this event and also during subsequent restoration actions. No disturbance of primary system conditions was noted. The second RHR pump was secured at approximately 0920 EDST.
NRC FORH 366A (5-92)
NRC FORM 366A U.S. NUCLEAR REGULATORY COHHISSION APPROVED BY OHB NO. 3150-0104 (5.92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTIOH REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS MANAGEHENT BRANCH TEXT CONTINUATION (MHBB 7714), U.S. NUCLEAR REGULATORY COMHISSION, WASHINGTON, DC 20555-0001, AHD TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503.
fACILITY NAHE (1) DOCKET NUHBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 NUMB 6 OF 12 95 -- 003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO THE EVENT:
PRZR pressure activities completed channel P-431 was on April 6, 1995, still defeated from calibration and was inoperable at the start of the event.
D. OTHER SYSTEMS OR SECONDARY FUNCTIONS AFFECTED:
None E. METHOD OF DISCOVERY:
This event was immediately apparent due to numerous Main Control Board Annunciator alarms in the Control room.
F. OPERATOR ACTION:
The Control Room operators responded to the Annunciator alarms, and noted that the standby RHR pump had started and that Motor Control Center (MCC) 1G had tripped. They diagnosed that automatic SI Actuation had occurred, and verified that all previously operable ESF components functioned properly. No immediate actions were required for the RCS, since reactor vessel water level and RHR flow indications remained stable.
After determining the cause of the inadvertent automatic SIAS, the Control room operators reset the SIAS and CI and CVI signals.
Unneeded equipment was secured. All CI valves and CVI components (which changed position due to the SIAS) were returned to their positions prior to the event. Pre-event conditions were restored.
Subsequently, the Control Room operators notified higher supervision and the NRC. The Shift Supervisor notified the NRC Operations Center within four hours, per 10CFR50.72 (b) (2) (ii) .
NRC FORH 366A (5-92)
NRC FORM 366A U.S. NUCLEAR REGULATORY COHHISSION APPROVED BY OHB NO. 3150-0104 (5.92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AHD RECORDS 'HANAGEHENT BRANCH TEXT CONTINUATION (HNBB 7714), U.ST NUCLEAR REGULATORY COMMISSION, WASHINGTON'C 20555 0001 i AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MAHAGEMENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAHE (1) DOCKET NUHBER (2) LER NUHBER (6) PAGE (3)
SEQUENT IAL REVISION R.E. Ginna Nuclear Power Plant 05000244 NUM 7 OF 12 95 -- 003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
G. SAFETY SYSTEM RESPONSES:
All safety systems and components that were operable responded as designed, except that the valve position indication for MOV-852B did not indicate full travel to the open position. All other operable ESF components were observed to function properly after the automatic SIAS.
III.
CAUSE OF EVENT:
A. IMMEDIATE CAUSE:
The immediate cause of the inadvertent automatic SI Actuation was both from 2/3 logic from PRZR pressure and from 2/3 logic from S/G pressure with SIAS unblocked.
B. INTERMEDIATE CAUSE:
The intermediate cause of automatic SIAS being unknowingly unblocked was placing the SI Unblock BSPS for P-429 to the tripped state with the same BSPS for P-431 already in the tripped state. This was a procedural error and was a direct result of an error in an approved procedure. Calibration procedure CPI-PT-429 had misleading information, in that a step was to be marked "N/A" if RCS temperature was less than 350 degrees F.
step "N/A" allowed the I&C technician to trip the P-429 BSPS Marking this without requesting that the Control Room operators verify that the same BSPS was not tripped in the other PRZR pressure channels. With this step marked "N/A", there was no for IEC to notify the Control Room operators that P-431requirement was still defeated when permission was obtained from the Control Room operators to perform the defeat of P-429.
NRC FORM 366A (5-92)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150.0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDIHG BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MNBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 8 OF 95 003 pp 12'EXT (If more space is required, use additional copies of NRC Form 366A) (17)
A contributing factor was that the IKC technicians were not aware that SIAS would automatically unblock when two PRZR pressure channels were defeated at the same time. The IEC technicians also believed that Unblock of SI was not a concern at these plant conditions, and were unaware of'the consequences of unblocking SI at these plant conditions. Another contributing factor was that the Control Room operators were made aware that I&C would be performing activities associated with more than one RPS channel, but did not ask which specific channels would be defeated simultaneously.
These actions were both cognitive and procedural errors and were the direct result of an error in an approved procedure. There were no unusual characteristics of the work location (Control Room) that contributed to the error.
C. ROOT CAUSE:
The underlying cause of the misleading information in calibration procedure CPI-PT-429 was the addition of wording that identified operability requirements based upon TS Table 3.5-2, Item 1, when the procedure was upgraded. One of the standards for the procedure upgrade was to more accurately identify the TS issues associated with calibrations.
The underlying cause of the imprecise valve position indication for MOV-852B was the sequence of actuation of valve limit switch rotors. Limit switch contacts on one rotor actuated to deenergize the valve motor before limit switch contacts on a different rotor actuated to extinguish the green light (which is intended to extinguish just prior to the valve reaching the fully open position).
This event is NUREG-1022 Cause Code (D), "Defective Procedure" ~
This event does not meet the NUMARC 93-01, "Industry Guideline for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants", definition of a "Maintenance Preventable Functional Failure", since there was no functional failure.
NRC FORM 366A (5-92)
NRC FORH 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150 ~ 0104 (5-92) EXPIRES 5/31/95 ESTIHATED BURDEN PER RESPONSE TO COMPLY WITH THIS IHFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDING BURDEN ESTIHATE TO LICENSEE EVENT REPORT (LER) THE INFORHATION AND RECORDS HANAGEMENT BRANCH TEXT CONTINUATION (HNBB 7714), U.S. NUCLEAR REGULATORY COHHISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF HANAGEMENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAHE (1) DOCKET NUHBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 NUM 9 OF 12 95 003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
IV. ANALYSIS OF EVENT:
This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report System, item (a) (2) (iv), which requires a report of, "Any event or condition that resulted in a manual or automatic actuation of any engineered safety feature (ESF), including the reactor protection system (RPS)". The inadvertent automatic SI Actuation is an automatic actuation of an ESF.
An assessment was performed considering both the safety consequences and implications of this event with the following results and conclusions:
There were no operational or safety consequences or implications attributed to the inadvertent automatic SI Actuation because:
The plant was in the cold shutdown mode with high head SI pumps rendered inoperable in accordance with TS. The RHR system was aligned for decay heat removal, and S/G nozzle dams were in place.
With SI pumps inoperable, the RCS was not subjected to over-pressure conditions when operable ESF components started.
The Refueling Water Storage Tank was not aligned to the suction of the RHR pumps. Therefore, there was no addition of water inventory to the RCS.
RCS temperature continued to be maintained stable via the RHR system. Therefore, reactivity was not affected by RCS temperature changes.
The Service Water System, Component Cooling Water System, and Spent Fuel Cooling System all remained in service during this event.
With Spent Fuel Cooling remaining in service, removal of decay heat from the Spent Fuel Pool was assured.
HRC FORH 366A (5-92)
NRC FORH 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORHATIOH COLLECTION REQUEST: 50.0 HRS.
FORWARD COMHENTS REGARDING BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORHATION AND RECORDS HANAGEHENT BRANCH TEXT CONTINUATION (MNBB 7714), U.S. NUCLEAR REGULATORY COHMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF HANAGEMENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 UM 95 -- 00 10 OF 12 003 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
~ The RHR cooling capability remained in service and RCS integrity was maintained. Therefore, heat removal from the reactor was assured.
~ Flow through MOV-852B was not limited due to valve position. The valve was, in fact, "full open", despite the indication.
Based on the above, safety was assured at all times.
it can be concluded that the public's health and V. CORRECTIVE ACTION:
A. ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS:
PRZR pressure channel P-431 BSPS was reinstated (removed from the trip mode), thus terminating the SI Unblock logic, and allowing the Control Room operators to again block SIAS.
After the cause of the event was identified, the SIAS, CI, and CVI signals were reset. Unneeded ectuipment was secured.
MOV-852B was stroke-tested to the full open position.
All CI valves and CVI components (which changed position due to the SIAS) were returned to their positions prior to the event. Pre-event conditions were restored.
B. ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
A Training Work Request (TWR) has been initiated to evaluate the training for I&C technicians relating to SIAS initiation.
Pre-outage training the need to include for IEC technicians will be evaluated for ESF and RPS logic.
Calibration procedures have been reviewed to identify those that have the same misleading information as CPI-PT-429.
Procedures have been changed to remove the misleading information.
NRC FORM 366A (5-92)
NRC FORH 366A U.S. NUCLEAR REGULATORY COHHISSION APPROVED BY OHB NO. 3150-0104 (5-92) EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDIHG BURDEH ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS MANAGEHENT BRANCH TEXT CONTINUATION (HNBB 7714), U.S. NUCLEAR REGULATORY COHMISSIOH, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET WASHINGTON DC 20503.
FACILITY NAME (1) DOCKET NUHBER (2) LER NUHBER (6) PAGE (3)
YEAR SEQUENTIAL REVI,SION R.E. Ginna Nuclear Power Plant 05000244 UM 11 OF 12 003 00 TDT (If more space is required, use additional copies of NRC Form 366A) (17)
Methods to visually indicate to Control Room operators which instrument channels are being tested or are defeated will be evaluated.
The limit switch positions for MOV-852B were adjusted to ensure that the limit switch contacts to extinguish the green light actuate before the limit switch contacts that deenergize the valve motor. Limit switch actuation was reviewed for other MOVs, and this was determined to be case. an'solated VI. ADDITIONAL INFORMATION:
A. FAILED COMPONENTS:
None B. PREVIOUS LERs ON SIMILAR EVENTS:
A similar LER event historical search was conducted with the following results:
LER 84-006 described an automatic actuation of SIAS. During plant heatup, PRZR pressure was increased above the automatic setpoint for unblocking SI, with S/G pressure still below the SIAS setpoint, due to operator error. The corrective action to prevent recurrence was to revise operating procedures for plant heatup. This action would not have prevented LER 95-003.
LER 85-004 described an automatic actuation of SIAS. The BSPS for one channel of SI actuation was in the tripped state. During a separate activity, an instrument bus was inadvertently deenergized, causing another bistable to trip, resulting in the logic for SIAS. The corrective action to prevent recurrence was to revise procedures to prevent the inadvertent loss of power to instrument busses'his action would not have prevented LER 95-003.
NRC FORH 366A (5-92)
, ARM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVEO BY OMB NO. 3150 ~ 0104 (5.92) EXPIRES 5/31/95 ESTIMATED BURDEH PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS.
FORWARD COMMENTS REGARDIHG BURDEN ESTIMATE TO LICENSEE EVENT REPORT (LER) THE INFORMATION AND RECORDS MANAGEMENT BRANCH TEXT CONTINUATION (MHBB 7714), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001, AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET WASHIHGTOH DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL REVISION R.E. Ginna Nuclear Power Plant 05000244 UM NUMB 12 OF 12 95 003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (17)
LER 89-003 described an automatic actuation of SIAS. Simulated signals (above the SIAS setpoint) were inserted into two PRZR pressure channels, causing SIAS. The corrective action to prevent recurrence was to provide clearer direction to test technicians when simulating signals. This action would not have prevented LER 95-003.
C. SPECIAL COMMENTS:
None NRC FORM 366A (5-92)
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