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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:RO)
MONTHYEARML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A3671998-07-14014 July 1998 LER 98-002-00:on 971019,CR Emergency Air Treatment Sys Actuating Function Was Not Operable.Caused by Mispositioned Switch.Revised Procedure CPI-MON-R37.W/980714 Ltr ML17265A1921998-03-11011 March 1998 LER 98-001-00:on 980209,discovered That Boraflex Degradation in SPF Was Greater than Was Assumed.Caused by Dissolution of Boron on Boraflex Matrix,Per 10CFR50.21.Removed Spent Fuel Assemblies from Selected Degraded Storage Rack Cells ML17265A1641998-02-0606 February 1998 LER 97-007-01:on 971117,reactor Engineer Recognized That Neutron Flux Low Range Trip Circuitry for Channel Was Not in Tripped Condition as Required.Caused by Technical Inadequacies.Channel Defeat Will Be Identified ML17265A1601998-02-0606 February 1998 LER 97-006-01:on 971103,verification of B Concentration Was Not Performed Due to Misinterpretation of Event Sequence. Audible Count Rate Function Was Restored to Operable Status ML17264B1441997-12-17017 December 1997 LER 97-007-00:on 971117,NF Low Range Trip Circuitry for Channel N-44 Was Not Placed in Tripped Condition.Caused by Technical Inadequacies in Procedures.Implemented EWR 4862 to Resolve Design deficiency.W/971217 Ltr ML17264B1291997-12-0303 December 1997 LER 97-006-00:on 971103,NIS Audible Count Rate Function Was Inoperable.Caused by Misinterpretation of Event Sequence Due to Not Verifying Boron Concentration.B Verification Occurred Every 12 H Per ITS LCO Action 3.9.2.C.3.W/971203 Ltr ML17264B1271997-12-0101 December 1997 LER 97-005-00:on 971031,undetected Unblocking of SI Actuation Signal Occurred at Low Pressure Condition,Due to Faulty Bistable Which Resulted in Inadvertent SI Actuation Signal.Sias,Ci & CVI Signals Were Reset ML17264B1211997-11-24024 November 1997 LER 97-004-00:on 971024,radiation Monitor Alarm Were Noted Due to Higher than Normal Radioactive Gas Concentration Resulted in Cvi.New R-12 Alarm Setpoint Was Maintained for Duration of Refueling Outage ML17264B0461997-09-29029 September 1997 LER 97-003-01:on 970730,bistable Instrument Trip Setpoint Could Have Exceeded Allowable Value.Caused by Insufficient Existing Margin Between Trip Setpoint & Allowable Value. Held Switches in Tripped configuration.W/970929 Ltr ML17264B0111997-08-27027 August 1997 LER 97-003-00:on 970730,high Steam Flow Bistable Instrument Setpoint Plus Instrument Uncertainty Could Exceed Allowable Value in ITS Was Identified.Caused by Entry Into ITS LCO 3.0.3.Switches Placed in Tripped configuration.W/970827 Ltr ML17264A9941997-08-19019 August 1997 LER 97-002-00:on 970720,34.5 Kv Offsite Power Circuit 751 Was Lost.Caused by Automatic Actuation of B Emergency DG Due to Undervoltage on Safeguards Buses 16 & 17.Offsite Power Restored to Safeguards Buses 16 & 17.W/970819 Ltr ML17264A9911997-08-11011 August 1997 LER 96-009-02:on 960723,determined That Leak Rate Outside Containment Was Greater than Program Limit.Caused by Weld Defect.Isolated Leak & Cut Out & Replaced Leaking Pipe ML17264A8271997-03-0303 March 1997 LER 97-001-00:on 970131,discovered Service Water Temp Was Less than Specified Value.Caused by non-representative Method of Monitoring.Increased Water Temp in Screenhouse Bay to Greater than 35 Degrees F.W/970303 Ltr ML17264A8071997-01-22022 January 1997 LER 96-015-00:on 961223,discovered Thermally Induced Overpressure Transient Could Occur.Caused by Thermal Expansion of Fluid During Design Basis Accident Condition. Installed Relief Valve on Affected line.W/970122 Ltr ML17264A7471996-11-27027 November 1996 LER 96-013-00:on 961029,circuit Breakers Closed While in Mode 3 & Resulted in Condition Prohibited by TS Due to Personnel Error.Circuit Breakers for MOV-878B & MOV-878D Were re-opened.W/961127 Ltr ML17264A6051996-09-19019 September 1996 LER 96-012-00:on 960820,feedwater Transient Occurred,Due to Closure of Feedwater Regulating Valve,Causing Lo Lo Steam Generator Level Reactor Trip.Sgs Were Restored & Missing Screw in 1/P-476 Was replaced.W/960919 Ltr ML17264A6061996-09-19019 September 1996 LER 96-009-01:on 960723,leakage Outside Containment Occurred,Due to Weld Defect,Resulting in Leak Rate Greater than Program Limits.Source of Leakage Isolated from RWST by Freeze Seal,Allowing Exit from ITS LCO 3.0.3.W/960919 Ltr ML17264A5911996-09-0505 September 1996 LER 96-011-00:on 960807,improper Configuration of Circuit Breaker Occurred,Due to Undetected Internal Interference, Resulting in Automatic Start of Both Auxiliary Feedwater Pumps.Running AFW Pumps Were secured.W/960905 Ltr ML17264A5921996-09-0505 September 1996 LER 96-010-00:on 960806,latching of Main Turbine While in Mode 4 Occurred,Due to Defective Procedure,Resulting in Automatic Start of Auxiliary Feedwater Pump.Caused by Defective Maint Procedure.Procedure revised.W/960905 Ltr ML17264A5891996-08-22022 August 1996 LER 96-009-00:on 960723,determined Leak on Piping Sys Outside Containment Greater than Program Limit.Caused by Weld Defect.Pipe & Socket Welds Were Cut Out & Replaced. W/960822 Ltr ML17264A5781996-08-0606 August 1996 LER 96-008-00:on 960707,main Feedwater Pump Breakers Opened. Caused by Change in Seal Water Differential Pressure Occurred During Sys Realignment.Afw Flow Controlled as Desired to Maintain S/G level.W/960806 Ltr ML17264A5561996-07-12012 July 1996 LER 96-007-00:on 960612,CR Operators Identified Control Rods Misaligned & Not Moving in Proper Sequence.Caused by Faulty Firing Circuit Card in Rod Control Sys.Faulty Firing Circuit Card in 1BD Power Cabinet replaced.W/960712 Ltr ML17264A5421996-06-20020 June 1996 LER 96-006-00:on 960521,discovered Containment Penetration Not in Required Status.Caused by Personnel Error.Installed Flange Inside Containment Penetration 2.W/960620 Ltr ML17264A5411996-06-17017 June 1996 LER 96-005-00:on 960516,PORC Determined Deficient Procedures Do Not Meet SRs for Testing safety-related Logic Circuits. Caused by Inadequancies in Individual Testing Procedures. Procedures Re Improved TSs revised.W/960617 Ltr ML17264A5051996-05-17017 May 1996 LER 96-003-01:on 960308,identified That Both Pressurizer PORVs Inoperable Concurrently Due to Disconnection of Flex Hose to Both PORV Actuators to Install air-sets for Benchset & Limit Switch Activities.Hpes Completed ML17264A4481996-04-0808 April 1996 LER 96-003-00:on 960308,both Pressurizer Relief Valves Inoperable.Hpes Evaluation Is Being Conducted to Determined Cause of Event.C/As:Both PORVs restored.W/960408 Ltr ML17264A4471996-04-0808 April 1996 LER 96-002-00:on 960307,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump.C/As: Thermography performed.W/960408 Ltr ML17264A4101996-03-18018 March 1996 LER 96-001-00:on 950504,inservice Test Not Performed During Refueling Outage.Caused by Inadequate Tracking of Surveillance Frequency.Valve Test Performed & Disassembled. W/960318 Ltr ML17264A2971995-12-14014 December 1995 LER 95-009-00:on 950817,surveillance Was Not Performed Due to Improper Application of TS Requirements Resulting in TS Violation.Testing of MOV-515 Was Performed on 951115.W/ 951214 Ltr ML17264A1711995-09-25025 September 1995 LER 95-008-00:on 950825,secondary Transient Occurred.Caused by Loss of B Condenser Circulating Water Pump That Resulted in Manual Rt.Returned S/G Levels to Normal Operating levels.W/950925 Ltr 1999-09-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17265A7601999-10-0505 October 1999 Part 21 Rept Re W2 Switch Supplied by W Drawn from Stock, Did Not Operate Properly After Being Installed on 990409. Switch Returned to W on 990514 for Evaluation & Root Cause Analysis ML17265A7621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Re Ginna Npp.With 991008 Ltr ML17265A7531999-09-23023 September 1999 Part 21 Rept Re Corrective Action & Closeout of 10CFR21 Rept of Noncompliance Re Unacceptable Part for 30-4 Connector. Unacceptable Parts Removed from Stock & Scrapped ML17265A7541999-09-22022 September 1999 LER 99-011-00:on 990823,small Tears Were Discovered in Flexible Duct Work Connector at Inlet of CR HVAC Sys Return Air Fan (AKF08).Caused by in-leakage Greater than That Assumed.Implemented Temporary Mod 99-029.With 990922 Ltr ML17265A7471999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Re Ginna Npp.With 990909 Ltr ML17265A7431999-08-24024 August 1999 LER 99-004-01:on 990412,discovered That Containment Recirculation Fan Chevron Separator Vanes Were Installed Backwards.Caused by Improper Assembly by Mfg.Moisture Separator Vanes Were Dismantled & Correctly re-installed ML17265A7341999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Re Ginna Npp.With 990806 Ltr ML17265A7291999-07-29029 July 1999 Interim Part 21 Rept Re safety-related DB-25 Breaker Mechanism Procured from W Did Not Pas Degradatin Checks When Drawn from Stock to Be Installed Into BUS15/03A.Holes Did Not line-up & Tripper Pan Bent ML17265A7181999-07-23023 July 1999 LER 99-007-01:on 990423,reactor Trip Occurred Due to Instrument & Control Technicians Inadvertently Pulling Fuses from Wrong Nuclear Instrument Channel.Setpoint Adjustments Were Completed by Different Crew of Technicians ML17265A7081999-07-22022 July 1999 LER 98-003-02:on 980904,actuations of CR Emergency Air Treatment Sys Was Noted Due to Invalid Causes.Caused by Various Degraded Components in CR RM Sys.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored ML17265A7131999-07-22022 July 1999 Special Rept:On 990407,radiation Monitor RM-14A Was Declared Inoperable.Caused by Failed Communication Link from TSC to Plant Process Computer Sys.Communication Link Was re-established & RM-14A Was Declaed Operable on 990521 ML17265A7031999-07-19019 July 1999 LER 99-S01-00:on 990617,determined That Temporary Unescorted Access Had Been Granted to Contractor Employee.Caused by Incomplete Info Re Circumstances of Individual Military Separation.Individual Access Was Revoked.With 990719 Ltr ML17265A7211999-07-19019 July 1999 ISI Rept for Third Interval (1990-1999) Third Period, Second Outage (1999) at Re Ginna Npp. ML17265A7021999-07-15015 July 1999 LER 99-010-00:on 990615,ventilation Isolation of Auxiliary Bldg Occurred When Auxiliary Bldg Gas Radiation Monitor R-14 Reached High Alarm Setpoint.Cr Operators Rest Auxiliary Bldg Ventilation Isolation Signal.With 990715 Ltr ML17265A7661999-06-30030 June 1999 1999 Rept of Facility Changes,Tests & Experiments Conducted Without Prior NRC Approval for Jan 1998 Through June 1999, Per 10CFR50.59.With 991020 Ltr ML17265A7011999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Re Ginna Npp.With 990712 Ltr ML17265A6851999-06-21021 June 1999 LER 99-001-01:on 990222,deficiencies in NSSS Vendor steam- Line Brake Mass & Energy Release Analysis Results in Plant Being Outside Design Bases Occurred.Caused by Deficiencies in W.Temporary Administrative Replaced.With 990621 Ltr ML17265A6761999-06-16016 June 1999 Part 21 Rept Re Defects & noncompliances,10CFR21(d)(3)(ii), Which Requires Written Notification to NRC on Identification of Defect or Failure to Comply. Relays Were Returned to Eaton for Evaluation & Root Cause Analysis ML17265A6661999-06-0202 June 1999 LER 99-009-00:on 990503,instrumentation Declared Inoperable in Multiple Channels Resulted in Condition Prohibited by Ts. Caused by Unanticipated High Frequency AC Voltage Ripple. Entered TS LCO 3.0.3.With 990602 Ltr ML17265A6681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Re Ginna Nuclear Power Plant.With 990608 Ltr ML17265A6651999-05-27027 May 1999 Interim Rept Re W2 Control Switch,Procured from W,Did Not Operate Satisfactorily When Drawn from Stock to Be Installed in Main Control Board for 1C2 Safety Injection Pump. Estimated That Evaluation Will Be Completed by 991001 ML17309A6541999-05-27027 May 1999 LER 99-008-00:on 990427,overtemperature Delta T Reactor Trip Occurred Due to Faulted Bistable During Calibr of Redundant Channel.Plant Was Stabilized in Mode 3 & Faulted Bistable Was Subsequently Replaced.With 990527 Ltr ML17265A6631999-05-24024 May 1999 LER 99-007-00:on 990423,technicians Inadvertently Pulled Fuses from Wrong Nuclear Instrument Cahnnel,Causing Reactor Trip,Due to High Range Flux Trip.Caused by Personnel Error. Labeling Scheme Improved ML17265A6601999-05-21021 May 1999 LER 99-006-00:on 990421,start of turbine-driven Auxiliary Feedwater Pump Was Noted.Caused by MOV Being Left in Open Position.Closed Manual Isolation Valve to Secure Steam to Pump.With 990521 Ltr ML17265A6591999-05-17017 May 1999 Part 21 Rept Re Relay Deficiency Detected During pre-installation Testing.Caused by Incorrectly Wired Relay Coil.Relays Were Returned to Eaton Corp for Investigation. Relays Were Repaired & Retested ML17265A6441999-05-13013 May 1999 LER 99-005-00:on 990413,undervoltage Signal of Safeguards Bus During Testing Resulted in Automatic Start of B Edg. Caused by Personnel Error.Blown Fuse Was Replaced & Offsite Power Was Restored to Safeguards Bus 17.With 990513 Ltr ML17265A6431999-05-12012 May 1999 LER 99-004-00:on 990412,discovered That Containment Recirculation Fan Moisture Separator Vanes Were Incorrectly Installed,Per 10CFR21.Caused by Improper Assembly by Mfg. Subject Vanes Were Dismantled & Correctly re-installed ML17265A6381999-05-0707 May 1999 Part 21 Rept Re Replacement Turbocharger Exhaust Turbine Side Drain Port Not Functioning as Design Intended.Caused by Manufacturing Deficiency.Turbocharger Was Reaasembled & Reinstalled on B EDG ML17265A6391999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Re Ginna Nuclear Power Plant.With 990510 Ltr ML17265A6361999-04-23023 April 1999 Part 21 Rept Re Power Supply That Did Not Work Properly When Drawn from Stock & Installed in -25 Vdc Slot.Power Supply Will Be Sent to Vendor to Perform Failure Mode Assessment.Evaluation Will Be Completed by 991001 ML17265A6301999-04-18018 April 1999 Rev 1 to Cycle 28 COLR for Re Ginna Npp. ML17265A6251999-04-15015 April 1999 Special Rept:On 990309,halon Systems Were Removed from Svc & Fire Door F502 Was Blocked Open.Caused by Mods Being Made to CR Emergency Air Treatment Sys.Continuous Fire Watch Was Established with Backup Fire Suppression Equipment ML17265A6551999-04-0909 April 1999 Initial Part 21 Rept Re Mfg Deficiency in Replacement Turbocharger for B EDG Supplied by Coltec Industries. Deficiency Consisted of Missing Drain Port in Intermediate Casing.Required Oil Drain Port Machined Open ML17265A6291999-03-31031 March 1999 Rev 0 to Cycle 28 COLR for Re Ginna Npp. ML17265A6241999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Ginna Station.With 990409 Ltr ML17265A6141999-03-31031 March 1999 LER 99-003-00:on 990301,two Main Steam non-return Check Valves Were Declared Inoperable Due to Exceedance of Acceptance Criteria.Caused by Changes in Methodology & Matls.Packing Gland Torque Will Be Adjusted.With 990331 Ltr ML17265A6131999-03-29029 March 1999 LER 99-002-00:on 990227,discovered That Surveillance Had Not Been Performed at Frequency,Per Ts.Caused by Personnel Error.Procedure O-6.13 Will Be Evaluated for Enhancement Documentation of Completion of ITS Srs.With 990329 Ltr ML17265A6061999-03-24024 March 1999 LER 99-001-00:on 990222,plant Was Noted Outside Design Basis.Caused by Deficiencies in NSSS Vendor Slb Mass & Energy Release.Placed Temporary Administrative Restriction 40 Degrees F Max on Screenhouse Bay Temp ML17265A5661999-03-0101 March 1999 Rev 26 to QA Program for Station Operation. ML17265A5961999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Ginna Nuclear Power Plant.With 990310 Ltr ML17265A5371999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Re Ginna Nuclear Power Plant.With 990205 Ltr ML17265A5951998-12-31031 December 1998 Rg&E 1998 Annual Rept. ML17265A5001998-12-21021 December 1998 Rev 26 to QA Program for Station Operation. ML17265A4951998-12-21021 December 1998 LER 98-005-00:on 981120,loss of 34.5 Kv Offsite Power Circuit 751,resulted in Automatic Start of B Edg.Caused by Faulted Cable Splice.Performed Appropriate Actions of Abnormal Procedure AP-ELEC.1.With 981221 Ltr ML17265A4931998-12-17017 December 1998 LER 98-004-00:on 971030,determined That Improperly Performed Surveillance Resulted in Condition Prohibited by Ts.Caused by Procedure non-adherence.Appropriate Calibr Procedures Were Properly Performed with 24 H of Condition Discovery ML17265A4761998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Re Ginna Nuclear Power Plant.With 981210 Ltr ML17265A4691998-11-25025 November 1998 LER 98-003-01:on 980904,actuations of CR Emergency Air Treatment Systems (Creats) Occurred.Caused by Radon build-up During Temp Inversion.Creats Actuation Signal Was Reset & Normal Ventilation Was Restored to CR ML17265A4531998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Re Ginna Nuclear Power Plant.With 981110 Ltr ML17265A4271998-10-0505 October 1998 LER 98-003-00:on 980904,actuations of CR Emergency Air Treatment Sys Occurred.Caused by Radon build-up During Temp Inversion.Air Samples Were Taken & Determined That Source of Radiation Was Naturally Occurring Radon.With 981005 Ltr ML17265A4291998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Re Ginna Nuclear Power Plant.With 981009 Ltr 1999-09-30
[Table view] |
Text
ACCELERATED DOCUMENT DISTRISUT105 SYS'j.'j 'M REGULRT% INFORMATION DISTRIBUTIO&STEN (RIDE)
ACCESSION NBR:9305140080 DOC.DATE: 93/05/04 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G 05000244 AUTH. NAME AUTHOR AFFILIATION BACKUSFW.H. Rochester Gas & Electric Rochester Gas & Electric Corp. Corp.'ECREDY,R.C.
RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 93-002-00:on 930404,during 1993 SG eddy current exam, d determined 1% of total tubes in SG A & B degraded. Caused by IGA & IGSCC within tube sheet crevice region. Tubes welded using tube sheet sleeve.W/930504 DISTRIBUTION CODE: IE22T NOTES:License Exp date COPIES RECEIVED:LTR ltr.
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
in accordance with 10CFR2,2.109(9/19/72).
l lENCL SIZE: /G 05000244 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD1-3 LA 1 1 PD1-3 PD 1 1 JOHNSONFA 1 1 INTERNAL: ACNW 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRIL/RPEB 1 1 NRR/DRSS/PRPB 2 2 1 1 NRR/DSSA/SRXB 1 1 RE FIL 02 1 1 RES/DSIR/EIB 1 1 RG ILE 01 1 1 EXTERNAL: EG&G BRYCEFJ.H '
2 2 L ST LOBBY WARD 1 NRC PDR 1 1 NSIC MURPHY,G.A 1 1 NSIC POOREFW. 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTEI CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 30 ENCL 30
'l ROCHESTER GAS AND ELECTRIC CORPORATION 4 89 EAST AVENUE, ROCH STER N.Y.; ""649.0001 ROBERT C. MCCREDY TEr.ErssiONE Vrre Presidenr AREA coDE7)8 546 2700 Cinna Nuclear Produerion May 4, 1993 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Subject:
LER 93-002, Steam Generator Tube Degradation Due To IGA/SCC, Causes Quality Assurance Manual Reportable Limits to be Reached R.E. Ginna Nuclear Power Plant Docket No. 50-244 In accordance with 10 CFR 50.73, Licensee Event Report System, item (Other), and the Ginna Station Quality Assurance Manual Appendix B, which requires that, "If the number of tubes in a generator falling into categories (a) or (b) below exceeds the criteria, then results of the inspection shall be considered a Reportable Event pursuant to 10 CFR 50.73," the attached Licensee Event. Report LER 93-002 is hereby submitted.
This event has in no way affected the public's health and safety.
Very ruly yours, Robert C. Mecredy xco U.S. Nuclear Regulatory Commission Region 475 I
Allendale Road King 'of Prussia, PA 19406 Ginna USNRC. Senior Resident Inspector 4 OAArg.
9305140080 930504 PDR ADQCK 05000244 J'p JD lpP
i NRC FORA 366 U.S. NUCLEAR REGULATORY COMMISSION
~ (6$ 9) APPROVEO OMB NO. 31504)104 EXPIRES: 4130l92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUESTI 50.0 HRS, FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (F630), V.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON. DC 20503.
FACILITY NAME (11 DOCKET NUMBER (2I PAGE 3 R.E. Ginna Nuclear Power Plant 0 5 0 0 0 24 4 1 OFO 9 Steam Generator Tube Degradation Due To 'lGA/SCC, Causes. Quality Assurance Manual Reportable Limits to be Reached EVENT DATE IS) LER NUMBER (6) R EPO RT DATE (7) OTHER FACILITIES INVOLVED (6)
MONTH DAY YEAR YEAR ctsS BEGUBNTIAL REVISION MONTH DAY YEAR FACILITYNAMES DOCKET NUMBER(S)
NUMBER iNS NUMBER 0 5 0 0 0 0 4 4 9 393 0 0 2 0 0 0 504 9 3 0 5 0 0 0 THIS REPORT IS SUBMITTED PURSUANT T 0 THE RLGUIREMENTS OF 10 CF R ('): (Cnecti one or more of tne followinpl (11)
OPERATING MODE (9) 20A02(B) 20A05(c) 60.73(o l (2)(iv) 73.71(B)
POWER 20A06( ~ )(1)(i) 60.36(c) (I ) 60.73( ~ )(2)(v) 73.71(cl LEYEL 0 0 0 20.405(o) l1) liil 50.36(c) l2) 60.73(o) (2)(vii) X OTHER ISpeciyyin AOttrect farrow end ln Teat. HRC Form 20A05( ~ llllliiil 60.7 3( ~ ) (2)(il 60,73(ol(2) (viiil(A) 366A) 20A05(e)(1)(Ivl 60.73(o)(2) liil 50,73(ol(2) (villi(BI 20.405( ~ )(1)(v) 60.73(ol(2) (ill) 50.73( ~ ) l2) l a)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER Wesley H. Backus.- AREA CODE Technical Assistant to the Operations Hanager 3 35 524 -44 46 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFAC.
TVRER REPORTABLE R%6+3:44Ry'N@'S CAUSE SYSTEM COMPONENT MANUFAC.
TVRER EPORTABI.E TO NPRDS Yg~E)IIT~ne" I, 4
AB TB G H 1 H SUPPLEMENTAL REPORT EXPECTED (14) MONTH kwM!DAY YEAR EXPECTED SUBMISSION DATE (15)
YES (/I yeA complete EXPECTED SVBMISSIDH DATEI X NO ABSTRACT (Limit to tetXJ tpecet, ie., epproalmetely fifteen tinple.rpece rypewritten lineri (16)
During the 1993 Annual Refueling and Maintenance Outage, subsequent to the eddy current examination performed 122 tubes in the on both the "A" and "B" "A"
Westinghouse Series 44 Steam Generators, steam generator and 171 tubes in the "BLS steam generator required corrective action due to tube degradation.
"AL) and "B" steam The immediate cause of the event was that the generator tube degradation was in excess of the Ginna Quality Assurance Manual Reportability Limits.
The underlying cause of the tube degradation is a common steam generator problem of a partially rolled tube sheet crevice with recurring intergranular attack/stress corrosion cracking (IGA/SCC) attack on and Primary Water Stress Corrosion Cracking (PWSCC) steam generator tubing. (This event is NUREG-1022 (X) cause code)
Corrective action taken was to either sleeve or plug the affected tubes with accepted industry repair methods.
NRC Form 366 (6$ 9)
l LJ
NRC FOAM 366A US. NUCLEAA REGULATORY COMMISSION (669) APPROVED 0MB NO. 31500104 EXPIRES: 4/30/92 LICENSEE EYE REPORT ILER) E ATEO BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATIOIV COLLECTION REOUESTI 500 HRS. FORWARD TEXT CONTINUATION COMMENTS REGARDING BUADEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BAANCH (F430), U.S. NUCLFAR REGULATORY COMMISSION, WASHINGTON, OC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (315041041. OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, OC 20503.
FACILITY NAME (1) DOCKET NUMBER (21 LEA NUMBER (6) PAGE (3)
YEAR SEOUBNTIAL 'PPI REVISION NUMBER ~SI NUMBBR R.E. Ginna Nuclear Power Plant TEXT IIImove s/rsce Is nq)rr/rer/, Iree edv//I/arrsl NAC Farm 3664's/ (12) 05000244 .9 3 0 0 2 00 02 oF0 9 PRE-EVENT P COND TIONS The plant was in the cold/refueling shutdown condition for the Annual Refueling and Maintenance Outage. Reactor Coolant System (RCS) was depressurized and RCS temperature was approximately 644F. Steam Generator (S/G) eddy current examination was in progress.
DESCRIPTION OP EVENT A. DATES AND APPROXIMATE TIMES OF MAZOR OCCURR19lCES:
o April 4, 1993, 1800 EDST: Event date and time.
o April 4, 1993, 1800 EDST: Discovery date and t.ime.
o April 6, 1993, 1300 EDST: Oral notification made to the NRC Office of Nuclear Reactor Regulation (NRR).
o April 7, 1993, 2128 EDST: Steam Generator repairs completed.
o April 19, 1993: A Special Report was sent to the USNRC.
B. LRGFNT During the 1993 Annual Refueling and Maintenance Outage, an eddy current examination was performed in both the "A" and "B" Restinghouse Series 44 design recirculating steam generators.
The purpose of the eddy current examination was to assess any corrosion or mechanical damage that may have occurred during the cycle since the 1992 examin-ation.
NRC Farm 366A (64)9)
1 NRC FORM 366A U S. NUCLEAR REGULATORY COMMISSION 164)9) APPROVED OMB NO. 31500104 EXPIRES: 4/30/92 ATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVE REPORT ILER) E INFORMATION COLLECTION REOUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH IF@30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT 131500104), OFFICE OF MANAGEMENTAND BUDGET. WASHINGTON. DC 20503.
FACILITY NAME (1) DOCKET NUMBER 12) LER NUMBER )6) PAGE 13)
YEAR gq>> SEOVENTIAL NUM>>44 ~Ay REVISION x.% NUM>>84 R.E. Ginna Nuclear Power Plant o s o o o 24 4 / 3 002 0 0 3 OF 0 9 TEXT ///14>>i>> <<>>c>> /4 nqvkaf, >>4>> atdtdon>>/NRC %%dnn 3664'4/ ()7)
The examination was performed by personnel from Rochester Gas and Electric (RG&E) and Allen Nuclear Associates, Inc. (ANA). All personnel were trained and qualified in the eddy current examination method and have been certified to a minimum of Level I for data acquisition and Level II for data analysis.
The initial eddy current examination "B" steam generators of the "A" and utilizing a was performed standard bobbin coil technique with data acquisition being performed with the EDDYNET Acquisition System.
The frequencies selected were 400, 200, 100, and 25 KHz.
Additional eddy current examinations of the "A" and "B" steam generators were performed utilizing the Zetec 3-coil Motorized Rotating Pancake Coil (MRPC) probe to examine the roll transition region, selected crevices and support plates. The frequencies used for these examinations were 400, 300, 100, and 25 KHz.
The inlet or hot leg examination program plan was generated to provide the examination of 100% of each open unsleeved steam generator tube from the tube end through the first tube support plate, along with 20%
of these tubes being selected and examined for their full length (20% random sample as recommended in the Electric Power Research Institute (EPRI) guidelines) with the bobbin coil. In addition, 20% of each type of sleeve was examined and the remaining tube examined full length. All Row 1 and Row 2 U-Bend regions were Coil examined with the Motorized Rotating Pancake (MRPC) between the g6 tube support plate hot side and the g6 tube support plate cold side from the cold leg side.
NRC Form 366A )))69)
NRC FOAM 366A U.S, NUCLEAR REGULATORY COMMISSION (64)9) APPROVED 0 M 6 NO. 31504)(04 EXPIRES: 4/30/92 E ATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVE REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P4)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31504)104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON. DC 20503.
FACILITY NAME (1) DOCKET NUMBER (21 LER NUMBER (6) PAGE (3)
REVISION YEAR <5+j SEQUENTIAL NUMBER NUMBER R.E. Ginna Nuclear Power Plant o s o o o 2 4 4 9 3 002 0 0 0 4 QF 0 9 TEXT Ilfmore Epeoe lr rer)eked, Iree er/I/lr/one/NRC %%dnrr 3664'4/ (12)
Results of the above examinations indicated that 122 tubes in the "AEE steam generator required action (i,.e. 121 tubes that were found to have "new" tubesheet crevice indications, and one tube that was obstructed by a foreign object.) 171 tubes in the "B" steam generator required action (i.e. 123 new repairs, plus 48 previously plugged tubes.) Corrective actions were therefore taken for 122 tubes in the "A" steam generator, and for 171 tubes in the "B" steam genera-tor.
On April 4, 1993 at approximately 1800 EDST, with the RCS depressurized and temperature at approximately 644F, final review of the 1993 Steam Generator eddy current examination results was completed. Results of this review indicated that more than one percent of the total tubes inspected are degraded (i.e.
imperfections greater than the repair limit).
Because of the above, the r'esults of the inspection are considered a reportable event pursuant to 10 CFR 50.73 per Appendix "B" of the Ginna Station Quality Assurance Manual.
On April 6, 1993, at approximately 1300 EDST oral notification was made"B" to the NRC Office of NRR pursuant to Appendix of the Ginna Station Quality Assurance Manual.
On April 19, 1993, a Special Report listing the number of tubes required to be plugged or sleeved in each Steam Generator, was reported to the NRC, pursuant to Appendix "B" of the Ginna Station Quality Assurance Manual.
C 'NOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRZBUTED TO THE EVENT:
None.
NRC Form 366A (64)9)
NRC FORM 3SSA US. NUCLEAR REGULATORY COMMISSION (669) APPROVED OMB NO. 3150d')04 EXPIRES: 4/30/92 LICENSEE EVE REPORT (LER) E ATED BURDEN PER AESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION AEOUESTI SOA) HRS. FOAWARD TEXT CONTINUATION REGARDING BURDEN ESTIMATE TO THE RECORDS 'OMMENTS ANO REPORTS MANAGEMENT BRANCH (F430). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PAO/ECT (3)50d)04). OFFICE OF MANAGEMENTAND BUDGET, IVASHINGTON,OC 20503.
FACILITY NAME (1) DOCKET NUMBER (2)
LER NUMBER (6) PAGE (3)
YEAR @~ SEQUENTIAL NUMSER r,.~IS REVISION NUMSER R.E. Ginna Nuclear Power Plant o s o o o 2 44 9 3 002 0 0 0 5 OF 0 9 TEXT /// moro EPEco /I ror/o)od, IIEP odd/dooo/ HRC Form 30549/ (17)
D OTHER SYSTEMS OR SECONDARY FONCTIONS AFFECTED:
None.
METHOD OF DISCOVERY The event was apparent after the final review of the "A" and "B" steam generator eddy current examination results.
OPERATOR ACTION Control Room operators completed the notifications and evaluations required by the A-25.1 (Ginna Station Event Report), submitted for the event by the Steam Generator examination and repair supervision.
SAFETY SYSTEM RESPONSES:
None.
III CAUSE 0 EVI2ÃT A IMMEDIATE CAUSE The immediate cause of the event was that the "A" and "B" steam generator tube degradation was in excess of the Ginna Station Quality Assurance Manual Reportable Limits.
B ROOT CAUSE:
The results "of" the" examination indicate that Inter-granular Attack (IGA) and Intergranular Stress Corrosion Cracking (IGSCC) continue to be active within the tubesheet crevice region on the inlet side of each steam generator. As in the, past, IGA/SCC is much more prevalent in the "B" steam generator with 103 new crevice indications reported in 1993. In the "A" steam generator, 41 new crevice indications were reported in 1993.
NRC Form 368A (04)9)
NRC FORM 366A US. NUCLEAR REGULATORY COMMISSION (64)9) APPROVED OMB NO. 31500104 EXPIRES: 4/30/92 LICENSEE EVE REPORT ILER) E ATEO BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION ANO REPORTS MANAGEMENT BRANCH (F430). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (3(504)(04). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON. DC 20503.
FACILITY NAME (l) DOCKET NUMBER (2)
LER NUMBER (6) PAGE (3)
- ~<Q7j SEQUENTIAL ,"SN'EVISION NUMSER N% NUMSER R.E. Gonna Nuclear Power Plant 0 s 2 4 4 0 0 2 0 0 60F 09 0 0 o TEXT /// mare g>>ce /4 mr/Idred. o>> edd/done/HRC Fomr 35649/ l)7)
In 1992, 118 new crevice indications were reported in the "B(l steam generator, and 34 new crevice indications were reported in the "A" steam generator. Comparison of 1992 and 1993 results does not suggest any signi-ficant change in the rate of tube degradation due to IGA/SCC.
The majority of the inlet tubesheet crevice corrosion indications are IGA/SCC of the Mill Annealed Inconel 600 tube material. This form of corrosion is believed to be the result of an alkaline environment forming in the tubesheet crevices. This environment has developed over the years as deposits and active species, such as sodium and phosphate, have reacted, changing a neutral or inhibited crevice into the aggressive environment that presently exists.
Along with IGA/SCC in the crevices, Primary Water Stress Corrosion Cracking (PWSCC) at the roll transi-tion continued to be active during the last operating cycle. This mechanism was first addressed in 1989 and this year there were 20 roll transition (PWSCC) indications in the "Bsl steam generator and 80 roll transition (PWSCC) indications in the "A" steam generator. These numbers include tubes that may have PWSCC in combination with IGA or SCC in the crevice.
Comparing the number of roll transition indications reported in 1992 with the number of these indications reported in 1993, results reveal that significantly fewer roll transition indications were reported in 1993. However, the number of these indications reported in 1992 was unusually high, and represents a data anomoly due to the first-time use of the MRPC technique for examining 1004 of the roll transition and tubesheet crevice region.
large number of pre-existing roll It is believed that a transition indica-tions were first detected by MRPC in 1992, and had not been detected by previous standard bobbin coil techniques. The use of the MRPC probe for examining the roll transition region was continued in 1993.
NR C Form 366A (64)9)
NRC FORM 366A US;NUCLEAR REGULATORY COMMISSION (649) APPROVED OMB NO. 31504104 E X P I R ES: 4/30/92 E ATEO BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVE REPORT (LER) INFORMATION COLLECTION REQUEST: 508) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (F430), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31504)104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR @i: SEQUENTIAL NUMBER
.~ REVISION
'&%5 NUMBER R.E. Ginna Nuclear Power Plant o s o o o 2 4 4 9 3 0 2 0 0 0 7 QF 0 9 TEXT /// Ruuu 4/>>ce /4 rapkaL u>> udder>>l//RC Form 35642/ (12)
ANALYSZS OP EVENT This event is reportable in accordance with 10 CFR 50.73, Licensee Event Report item (Other) and the Ginna Station Quality Assurance Manual Appendix "B" which requires that, "Xf the number of tubes in a generator falling into categories (a) or (b) below exceeds the criteria, then results of the inspection shall be considered a reportablein event pursuant to 10 CFR 50.73." The tube degradation the "A" and "B" steam generators exceeded the criterion of (b) which states, "more than 1 percent of the total tubes inspected are degraded (imperfections greater than the repair limit)". This repair limit is defined as, than "Steam Generator tubes that have imperfections greater 40 percent through wall, as indicated by eddy current, shall be repaired by plugging or sleeving."
An assessment was performed considering the safety con-sequences and implications of this event with the following results and conclusions:
There were no safety consequences or implications resulting from the steam generator tube degradation in excess of the Quality Assurance Manual Reportable Limits because:
o The degraded tubes were identified and repaired prior to any significant leakage or steam generator tube rupture occurring.
Even assuming a complete severance of a steam generator tube at full power, as stated in the R.E. Ginna Nuclear Power Plant Updated Final Safety Analysis Report (Ginna/UFSAR)'section 15.6.3, (Steam Generator Tube Rupture), the sequence of recovery actions ensures early termination of primary to secondary leakage with or without offsite power available thus limiting offsite radiation doses to within the guidelines of 10 CFR 100.
Based on the above, it health and safety was assured at all times.
can be concluded that the public's NRC Form 366A (669)
'I NRC FORM 366A US. NUCLEAR REGULATORY COMMISSION
)689) APPROVED OMB NO. 31500104
~ EXPIRES: 4/30/92 LICENSEE EVE REPORT (LER) ATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 500 HRS. FORWARD TEXT CONTINUATION COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH IF@30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PRO/ECT 131504)104), OFFICE OF MANAGEMENTAND BUDGET. WASHINGTON, DC20503.
FACILITYNAME n) DOCKET NUMBER 12)
LER NUMBER (6) PAGE 131 YEAR SEQUENTIAL . REVISION NVMSER NUMBER R.E. Gonna Nuclear Power Plant TEXT illmare <<wee /4 ra)rdred, o s o o o 2 4 4 3 002 0 0 0 8 QF 09 Iree eddldaae/kRC Farm 3664'4/ I IT)
V. CO CTXVE ACTION A ACTION TAKEN TO RETURN AFFECTED SYSTEMS TO PRE-EVENT NORMAL STATUS o Of the 122 tubes repaired in the "A" steam generator, 51 tubes were repaired using a Combustion Engineering 27" welded sleeve in the hot leg, plus 62 tubes were repaired using a Babcock and Wilcox explosively welded tubesheet sleeve in the hot leg. All of the above tubes will remain in'ervice. The remaining 9 tubes were removed from service by plugging both the hot and cold leg tube ends. A total of 194 tubes in the "A" steam generator are currently plugged and 668 tubes are sleeved.
0 Of the 171 tubes repaired in the "B" steam generator, 153 tubes were repaired using a Babcock and Wilcox explosively welded tube sheet sleeve in the hot leg. All of the above tubes will remain in service. The remaining 18 tubes were removed from service by plugging both the hot and cold leg tube ends. A tota'l of 284 tubes in the "B" steam generator are currently plugged and 1286 tubes are sleeved.
All the above repairs on the "ALE and "B" steam generators were completed on April 7, 1993 at approxi-mately 2128 EDST.
B . ACTION TAKEN OR PLANNED TO PREVENT RECURRENCE:
The occurrence/presence of IGA, SCC, and PWSCC is a common PWR steam generator problem. Utilities with susceptible tubing and partially rolled crevices must deal with this recurring attack on steam generator tubing.
NRC Form 366A (PIB)
NRC FORM 366A UA. NUCLEAR REGULATORY COMMISSION (64)9) APPROVED OMB NO. 31504)104 EXPIRES: 4/30/92 LICENSEE EVE REPORT (LER) E ATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P4)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (31504)(04). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2)
LER NUMBER (6) PAGE (3)
YEAR PI:y, SEOUENTIAL @X REVISION NUMBER R.E. Ginna Nuclear Power Plane o s o o o 2 4 4 002 0 9 or- 0 9 TEXT llfmare 4/>>ae /4 Iertu/rer/ u>> er/d/I/ane/ JVRC Farm 36643) (17)
R.E. Ginna Nuclear Power Plant will continue, careful monitoring of both primary RCS and secondary side .
water chemistry parameters.
These water chemistry parameters will continue to be evaluated against accepted industry guidelines in order to minimize harmful primary and/or secondary side environments.
Degraded steam generator tubes shall be sleeved or plugged in accordance with the inservice inspection program and accepted industry repair methods.
VI. ADDITIONAL INFORMATION A. FAILED COMPONENTS:
The degraded components are: Inconel 600 Mill Annealed U-Bend tubes having an outside diameter of 0.875 inches and a nominal wall thickness of 0.050 inches. These tubes were manufactured by Huntington Alloy Company.
B. PREVIOUS LERs ON SIMILAR EVENTS:
A similar LER event historical search was conducted with the following results: The crevice indications are similar to those reported in A0-74-02, A0-75-07, R0-75-013, and LERs76-008, 77-008, 78-003, 19-006, 79 022P 80 0036 81 009P 82 003l 82 022/ 83 013/ 89 001,90-004, 91-005, and 92-005.
C. SPECIAL COMMENTS For a more indepth report, refer to the Special Report "Summary Examination Report for the 1993 Steam Generator Eddy Current Inspection at R.E. Ginna Nuclear Power Station", Revision 1, dated April 20, 1993.
As a note of interest, RG&E has ordered new steam generators for R.E. Ginna Nuclear Power Plant to be installed in 1996.
NRC Fomr 366A (64)9)
1 '