ML070920308

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Special Report 3-SR-2007-001, Report of Boron Deposit at Control Element Drive Mechanism Vent
ML070920308
Person / Time
Site: Palo Verde Arizona Public Service icon.png
Issue date: 03/22/2007
From: Hesser J
Arizona Public Service Co
To:
Document Control Desk, NRC/NRR/ADRO
References
102-05671-JHH/TNW/JAP/DFH, EA-03-009 3-SR-2007-001
Download: ML070920308 (3)


Text

NRC Revised Order EA-03-009 L A M

A subsidiary of Pinnacle West Capital Corporation John H. Hesser Mail Station 7605 Palo Verde Nuclear Vice President Tel (623) 393-5553 PO Box 52034 Generating Station Nuclear Engineering Fax (623) 393-6077 Phoenix, Arizona 85072-2034 102-05671 -JHH/TNW/JAP/DFH March 22, 2007 ATTN: Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555-0001

Subject:

Palo Verde Nuclear Generating Station (PVNGS)

Unit 3 Docket No. STN 50-530 Special Report 3-SR-2007-001 Report of Boron Deposit at Control Element Drive Mechanism Vent

Dear Sirs:

Attached please find Special Report 3-SR-2007-001 prepared and submitted by AriZona Public Service (APS) pursuant to NRC Revised Order EA-03-009, dated February 20, 2004.Section IV.D of the Order requires licensees to perform certain visual inspections to identify potential boric acid leaks from pressure-retaining components above the Reactor Pressure Vessel head.Section IV.E of the Order requires licensees to submit reports detailing the inspection results within sixty (60) days after returning plants to operation.

This special report details the results of visual inspections performed at PVNGS Unit 3 subsequent to a reactor shutdown on January 27, 2007 for a short notice outage. The visual inspections were performed in accordance with the Boric Acid Corrosion Prevention Program which APS implements to identify and prevent boric acid corrosion of reactor pressure boundary components.

In accordance with 10 CFR 50.4(b)(1), copies of this report are being provided to the Region IV Administrator and the Palo Verde NRC Senior Resident Inspector.

A member of the STARS (Strategic Teaming and Resource Sharing) Alliance Callaway

  • Comanche Peak
  • Diablo Canyon Palo Verde South Texas Project
  • Wolf Creek

Special Report 3-SR-2007-001 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Page 2 No commitments are being made to the NRC by this letter.

If you have questions regarding this submittal, please contact James Proctor, Section Leader, Compliance, at (623) 393-5730.

Sincerely, JHHITNW/JAP/DFH/gt Attachment cc:

B. S. Mallett NRC Region IV Regional Administrator M. B. Fields NRC NRR Project Manager M. T. Markley NRC NRR Project Manager G. G. Warnick NRC Senior Resident Inspector for Palo Verde Assistant General Counsel for Materials Litigation and Enforcement Rulemaking and Adjudication Staff

Attachment Palo Verde Nuclear Generating Station (PVNGS) Unit 3 Special Report No. 3-SR-2007-001 Boron Deposit Found at Control Element Drive Mechanism Vent Docket No. STN 50-530 Reporting Requirement:

The NRC Revised Order EA-03-009, "Interim Inspection Requirements for Reactor Pressure Vessel Heads at Pressurized Water Reactors," dated February 20, 2004,Section IV.D requires that certain visual inspections be performed to identify potential boric acid leaks from pressure-retaining components above the reactor pressure vessel head.

Additionally,Section IV.E of the NRC Order requires that licensees submit reports detailing the inspection results performed per section IV.D within sixty (60) days after returning the plant to operation if a leak or boron deposit was found during the inspection.

Background:

On January 27, 2007, Palo Verde Unit 3 was shutdown for a short notice outage. The unit was returned to service on January 31, 2007. Subsequent to the reactor shutdown, routine visual inspection was performed in accordance with the Boric Acid Corrosion Prevention Program (PVNGS procedure 70TI-9ZC01). PVNGS implemented the Boric Acid Corrosion Prevention Program to prevent boric acid corrosion of reactor pressure boundary components and to ensure the provisions of USNRC Generic Letter No. 88-05, "Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary Components in PWR Plants" were met.

Report Detailing Inspection Results:

During boric acid walk-downs on January 27, 2007, one, not previously reported, Unit 3 boric acid residue site was identified above the RPV head. The site was located on the Versa Vent for control element drive mechanism (CEDM) number 69. The site did not exhibit evidence of an active leak, nor did the boric acid residue contact the RPV head or related insulation and no carbon steel was affected.

The dry residue on Versa Vent number 69 was cleaned during the outage and a Work Order was generated in accordance with the corrective action program to rework the Versa Vent. Unit 3 was returned to operation (Mode 1) on January 31, 2007.