IR 05000387/1979026
| ML17138A972 | |
| Person / Time | |
|---|---|
| Site: | Susquehanna |
| Issue date: | 10/11/1979 |
| From: | Gallo R, Mcgaughy R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17138A971 | List: |
| References | |
| 50-387-79-26, 50-388-79-14, NUDOCS 7912060200 | |
| Download: ML17138A972 (14) | |
Text
U.
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NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT
REGION I
50-387/79"26 Report No.
50-388/79-14 50-387 Docket No.
50-388 CPPR" 101 License No.
CPPR-102 Priority Category Licensee:
Penns 1 vani a Steam Electri c Stati on 2 North Ninth Street Allentown Penns lvani a 18101 Facility Name:
Sus uehanna Steam Electric Station Inspection At:
Salem Townshi Penns lvania Inspection Conducted:
Jul 30-Au ust 31 1979 Inspectors:
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.
M. Gallo, si~t Reactor Inspector Pr I// / /~
date Approved by:
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n R.
M. McGaughy '
ef, Projects Section RC8ES Branc date
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date I
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1979 I
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9-337/79-2 p
p tion and welding of reactor coolant pressure boundary and other piping; instal-lation and storage of safety-related components; Circular 79-10; ACR/PGCC rework ASME certification system requirements; procedures and work in progress for the Reactor Pressure Vessel Recirculation System nozzle modification.
The inspector also performed plant tours and reviewed licensee actions on previously identified items.
The inspection involved 65 inspectors-hours, including 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> during off shift by the NRC Resident Inspector.
Results:
No items of noncompliance were identified.
Region I Form 167 (August 1979)
F060
Unit 2 Ins ection on Jul 30-Au ust 31 1979 Re ort No. 50-388/79-14 R
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tion and welding of reactor coolant pressure boundary and other piping; Circul'ar 79-10; ASME certification system requirements.
The inspector also performed plant tours and reviewed licensee actions on previously identified items.
The inspection involved 9 inspector-hours by the NRC Resident Inspector.
Results:
No items of noncompliance were identifie DETAILS Persons Contacted Penns lvania Power and Li ht Com an Note L.
R.
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G.
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R.
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Ballard, Site QAE Beckley, Site QAE Brignole, Senior Project Engineer-Construction Burvis, Site QAE Carroll, Site QAE L. Denson, Assistant Project Construction Manager H. Featenby, Project Construction Manager Gorski, Resident Engineer Green, Resident NQA La Zarowitz, Resident Engineer F. Oldenhage, Resident Engineer Petrokonis, Project Engineer - Construction R. Sabol, Manager, Nuclear Quality Assurance A. Schwarz, Senior Project Engineer - Construction
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Bechtel Cor oration G.
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G.
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Bel 1, Bechtel QAE A. Drucker, Electrical QAE Colker, Lead Pipe/Mechanical Engineer Gelinas, QC Lead Engineer Piping/Mechanical Henke, Welding Superintendent Khandar, Mechanical QAE Konjura, Mechanical QAE Lamb, Assistant Lead Welding QCE Lilligh, Project QAE Minor, Project Field Engineer O'ullivan, Assistant Project Field Engineer Ott, Lead Welding QCE L. Ricks, Mechanical QAE Ross, Lead Welding Engineer Schrader, Project Field QCE Stout, Assistant Project Field QCE Turnbow, Field Construction Manager Engineer 1,
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3 General Electric Com an -Nuclear Ener Business Grou NEBG E.
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A. Gustafson, Site Manager C. Walker, QA/QC Representative
General Electric Com an -Installation and Service En ineerin IPSE G. Bragan, Site Manager
'.
Kong, Project Manager Recirculation System Nozzle Modification Peabod Testin Com an M. Mhalen, NDE Supervisor Notes 1 - Denotes those present at the exit interview August 3, 1979 2 - Denotes those present at the exit interview August 10, 1979 3 - Denotes those present at the exit interview August 31, 1979 The inspector also interviewed other PP8L employees, as well as employees of Bechtel, Peabody Testing Company and General Electric Company.
2.
Plant Tours - Units 1 and
The inspector observed work activities in progress, completed work and plant status in several areas of the plant during general inspection of the plant.
The inspector examined work for any obvious defects or non-compliance with regulatory requirements or license conditions.
Particular note was taken of presence of quality control inspectors and quality con-trol evidence such as inspection records, material identification, non-comforming material identification, housekeeping and equipment preserva-tion.
The inspector interviewed craft personnel, supervision and quality inspection p'ersonnel as such personnel were available in the work areas.
No items of noncompliance were identified.
3.
Licensee Action on Previous Ins ection Findin s a 0 (Closed)
Unresolved Item (387/78-16-02):
Incomplete Material Specifications The licensee has developed and is implementing a program to review all suppliers quality documentation prior to system turnover.
This review is being conducted in accordance with Field Procedure FP-G-21, Revision 0.
Documentation Review Record Serial No.
1643 includes the lack of the hardness test results for the 90'lbow in pipe spool DCA-110-2"4.
The material certification for the E 308-16 filler metal heat No.
740654A does not include the results of fillet weld tests because this test is optional in accordance with SFA 5.4 and not required by ASME Section III Article NB-2400.
The inspector had no further ques-tions on this matter at this tim (Closed)
Unresolved Item (387/78-16-04):
Indications in recircula-tion system safe end welds'.
(Note:
This item was incorrectly iden-tified as 78-16-03 in the original report.)
Subsequent to the preservice inspection of the N2 nozzle safe ends the licensee committed to replace the recirculation system inlet nozzle safe ends and thermal sleeves.
PP8L letter PLA-350, dated May 4, 1979, documents the modifications.'he modification requires the removal of the nozzle safe ends and the safe end to safe end extension weld in question.
The ten Unit 1 safe ends have been removed.
The modified safe end design does not incorporate a safe
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end extension.
The licensee has contracted to destructively examine a safe end to safe end extension weld to verify the ultrsonic test-ing conducted during preservice inspection.
The inspector had no further questions on this matter at this time.
(Closed) Unresolved Item (387/79-04-02):
Containment Liner Plate Melding The licensee has issued Field Procedure FP-M-l, Revision 6 which incorporates controls for the inspection of welding on the contain-ment liner plate.
The revised procedure requires that guality Con-trol Personnel be notified prior to welding attachments to or remov-ing attachments from the liner plate.
The procedure requires inspec-tion of the liner plate adjacent to the attachments to verify the absence of injurious defects.
It also provides reference to Specifi-cation C-50 for rework criteria and includes criteria for initiating a nonconformance report.
The inspector discussed the above requirements with the gC engineer responsible for inspection of the liner plate attachment welding.
The FACE was familiar with the revised field procedure and stated that responsible field personnel were notifying gC in accordance with the field procedure.
The inspector had no further questions on this matter at this time.
(Closed)
Unresolved Item (387/79-19-02):
Radiograph Records One view of the radiograph for weld DBA-108-1-FM8 had been rejected.
The reshoot of view 10-11 had not been properly requested and view 11-0 had been mistakenly reshot.
Nonconformance Report No.
3888 was issued to document the acceptance of the weld without complete radiographic coverage.
The inspector reviewed the radiograph for view 10-11 of DBA-108-1-FM8 and identi-fied no further discrepancie The inspector reviewed the radiograph records for the five additional Class 1 welds with reshot radiographs.
No additional unradiographed areas were identified. Additional radiographs examined included:
DLA-102-1-FM 14 OLA-102-1-FM 3 DCA-108-1"FM 9 OCA-107-1-FM 2 DCA-103-1-FM 7.
The inspector discussed the above finding with the appropriate Bechtel equality Control Engineer and the authorized nuclear inspec-tor.
The inspector had further questions on this matter at this time.
4.
Reactor Coolant Pressure Boundar and Safet -Related Pi in Weldin The following activities were examined to determine that they were being performed in accordance with the ASME Section III and IX Codes, PSAR Appendix D, the Bechtel guality Assurance Manual Section III, Site Spe-cifications M 204, M 207, drawings H-198 and M-199, Bechtel Field Proce-dure FP-M-3, GE Specifications 24A4628 and Peabody Testing Procedure IPRT"100"39"03.
a.
Meldin
- Unit 2 Melding of:
SP-DCA-H79-20-BM5 SP"DCA-M79-26"BM5 FCI-P-44-FM1 The inspector verified selected detailed drawings, welding procedures, base and filler materials as specified, welder qualification, quality control documentation, weld appearance, welding variables such as gas flow and amperage and nondestructive testing activities as appropriate.
No items of noncompliance were identified.
b.
Nondestructive Testin
- Unit 2 Radiographic Inspection Records for Meld Nos.
SP-DCA"M79"20"BM5 SP-DCA-N79-26"BM5
The inspector verified conformance to the applicable radiographic testing procedure and the specified technique.
No items of noncompliance were identified.
c.
Post Weld Heat Treatment - Unit 1 The inspector observed the post weld heat treatment of weld DBB-118-1-FM 2.
The inspector verified that approved procedures post weld heat treatment procedures provided for requirements such as:
heating and cooling rates; monitoring and recording of metal temperatures; holding temperature and time.
A Bechtel audit finding was identified relative to this post weld heat treatment.
The audit finding is documented in Field Audit 13-4-2 OAF-1 concerning the requirements for guality Control inspection of post weld heat treatment.
Docu-ments reviewed by the inspector included:
Bechtel gA Manual Section III Subsection 5100 and Appendix 3, WD-1 Procedure Specification for Post Meld Heat Treatment of Field Melds - PHT-501, Revision
An unresolved item regarding the placement of thermocouples is identified in Inspection Report 50-387/79-28.
No items of noncompliance were identified.
d.
Meldin Material Control The inspector examined the control of weld filler metal by GE I&SE relative to the Recirculation System Nozzle Modification.
Documen" tation and site practices were examined 'to verify that purchasing, receiving, identification, storage, certification testing and issue were accomplished in accordance with the GE I&SE gA Manual 18XA7005 and GE I&SE Procedures SRSE 1-7, 1-31, and 1-33.
The inspector reviewed documentation for two heats of filler metal.
Those heats were:
Heat No.
3544T382 4282R308L
~Te ERNiCr-3 308L The ferrite number for the above 308L material did not appear on the vendor material test certification 'form held at the site.
GE I&SE personnel confirmed th'at the ferrite number was in accordance with SRSE 1-31 and obtined a revised certificatio No items of noncompliance were identified.
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5.
Recirculation S stem Nozzle Modification - Unit 1 The inspector reviewed procedures and observed work in progress relative to the Recirculation System nozzle modification.
The procedures and work were examined to verify conformance with ASME Section III thru Summer 1976 Addenda and Section XI 1974 edition for General Electric Installation and Service Engineering (GE I&SE) work; and ASME Section III thru Winter 1972 Addenda for Bechtel work; and commitments in PAL letters, to the NRC, PLA-291 dated September 25, 1978 and PLA-350 dated May 4, 1979.
Procedures reviewed included:
GE IPSE Procedures:
SRSE 1-13, Revi 1-14, Revision 1-16, Revision 1-18, Revision 1-19, Revision 1-24, Revision 1-25, Revision 1-28, Revision 1-37, Revision sion 2j
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0; 2; and
GE IPSE Nonconformance Reports Nos. 13-17 The inspector observed work in progress and verified conformance to applicable procedures:
SRSE l-ll, 1-37, and Bechtel FCI-M-174.
Specific work evolutions observed included:
Cutting and Machining of Recirculation System Nozzles:
N2B N2J N2D N2K During the work in progress, the licensee's contractor has identified discrepancies.
The conditions noted are documented in accordance with applicable gA Manual Requirements including:
Welding of mockup of thermal sleeve to jet pump Welding of mockup of buildup on the external jet pump riser pipe spool No items of noncompliance were identifie.
Reactor Coolant Pressure Boundar and Safet -Related Pi in Units 1 and
a.
Pi in Work in Pro ress - Units 1 and
The inspector examined work activities relative to the hydrostatic pressure test of Emergency Service Mater Piping Supplying Spray Pond Network 8"1.
The inspector verified:
test pressure was per design documents, qC coverage of the test, inspection and test documenta-tion, test instrument calibration.
Documentation reviewed by the inspector included:
Bechtel Drawings M112 and M199 Specification M214 Revision
Pressure Test Report - Release No.
1927 gCI T-l.00, Revision
No items of noncompliance were identified.
b.
Pi in S stem Installation Verification - Unit 1 The inspector examined one partially completed piping run and yeri-.
fied that it was. installed in accordance with approved drawings;..-
The piping run examined was the Reactor Water Cleanup line from the Regenerative Heat Exchanger to the Main Feedwater lines.
The inspector verified conformance to FSAR Section 5.4.8 and draw-ings D88-122-2 and M-144.
No items of noncompliance were identified.
7.
Pi e Fittin s Manufactured
. from Unacce table Material - IE Circular No. ?9"10 On May 10, 1979, the Tube Turns Division of Chemetron Corporation reported to the NRC that potentially defective four inch elbows of ASTM A-234 MPB material Lot W6719 had been provided to certain Nuclear Power Plants.
IE Circular No. 79-10 advised all construction permit holders to review their pipe fitting receiving documents to determine if the potentially defective elbows had been received.
The licensee has reviewed the appropriate documentation for Susquehanna and has determined no material from Lot M6719 has been received at the site.
The inspector reviewed Bechtel JAR F-505 relative to this circular and had no further questions on this matter.
No items of noncompliance were identifie.
Com liance with ASME Certification S stem Re uirements Units 1 and
The inspector reviewed the licensee's gA Program to verify that the licensee satisfies the requirements of ASME Section III, Article NA-3000.
The inspector reviewed the Bechtel gA Manual Section III to verify the following:
(1) the licensee's contractor has provided for a construction
.organization that assumes the responsibilities and duties of certificate holders defined in Article NA-3000 of ASME Section III; (2) the licensee's contractor and the licensee hold valid Certificate of Authorization for the work being performed; (3) that the NPT and NA certificate holder, Bechtel, has been issued a site extension; and (4) that the activities being performed by the NPT and NA certificate holder include all, but do not exceed, the responsibilities defined in the appropriate sections of NA 3000.
Documentation reviewed by the inspector during this inspection included:
FSAR Table 3.2-3 Bechtel gA Manual Section III ASME Certificates of Authorization, as follows:
N-1541 PAL authorization to complete Form N-3 for Unit 1 N-1542 PP8L authorization to complete Form N-3 for Unit 2 N-881-2 Bechtel authorization to use the NA symbol for Susque-hanna Units 1 and
N-882-2 Bechtel authorization to use the NPT symbol for Sus-quehanna Units 1 and
ASME letter, dated June 22, 1979, to Bechtel extending expiration dates for NA and NPT symbols N-881-2 and N-882-2 No items of noncompliance were identified.
9.
Accident Involvin Unit 1 Core S ra Pum Motor 1P-206A On July 30, 1979 at approximately 3:30 p.m.
Core Spray Pump Motor 1P206A fell approximately 40 feet onto a concrete floor in a Unit 1 truck bay.
The motor fell as the result of the failure of the 7/8 inch diameter sling used for'lifting the motor.
An Equipment Installation Plan had been prepared, in accordance with Field Procedure FP-M-2, Revision 1, for the installation of four core spray pump motor A description of the accident and probable causes for the sling failure are discussed in the Bechtel accident report transmitted to PAL by Bechtel letter BCLPC-6567 dated August 21, 1979.
NCR-4269 documents the disposition of the damaged motor.
The inspector will review the imple-mentation of Field Procedure FP-M-2 regarding the handling of safety-related equipment during a future inspection.
No items of noncompliance were identified.
10.
ACR/PGCC Rework a.
HYPOT Testin of General Electric Cables GE Field Disposition Instruction (FDI) MJGO Revision 3 requires the completion of AC HYPOT testing of all conductors in each GE cable inspected in accordance with the FDI.
Field Deviation Disposition Request (FDDR) No.
KR1-548, Revision 10, modified the HYPOT testing to require the performance of a DC HYPOT test and if necessary the AC test.
The stated reason for the change was that "many of the cables fail the AC test but pass the DC test.
This is because of capacitive reactance in the cables."
The inspector requested that the licensee provide a justification for the use of DC HYPOT testing where operating circuits are AC.
This item is unresolved pending evaluation by the licensee and review by the NRC (387/79-26-01).
b.
Deficienc in Am henol Connectors and Cutler Hammer E-30 Switches Bechtel MCAR 1-37 identifies two deficiences identified by site gC personnel during routine surveillance of work on ACR/PGCC panels.
The first deficiency concerns the failure of female pins to seat properly in amphenol connectors.
The relative position of the pins varies after mating and unmating of the connectors.
This is parti-cularly noted if the female pins have been removed and reinserted into the connector dielectric.
C.
The second deficiency concerns cutler hammer push-button switches installed in ACR benchboards.
Ten of 189 switches do not retract when manual depression is removed.
Resolution of MCAR 1-37 will be reviewed during a subsequent NRC inspection.
No items of noncompliance were identified.
Cable Ins ection On August 23, 1979, the inspector attended a meeting with representa-tives of PP8L, Bechtel, General Electric and the NRC regarding the application of a sampling plan to the inspection of electrical con-ductors in GE supplied cables.
The.sampling plan is described in FDI MJGO, Revision ll.
Unresolved Items Unresolved items are matters about which more information is required to ascertain whether they are acceptable items, items of n'oncompliance, or deviation.
An unresolved item disclosed during the inspection is discussed in par agraph 10. a.
.12.
Exit Interviews At periodic intervals during the course of this inspection, meetings were held with facility management (dates and attendees are denoted in Detail 1)
to discuss inspection scope and findings.