IR 05000382/1980005
| ML19323E658 | |
| Person / Time | |
|---|---|
| Site: | Waterford |
| Issue date: | 04/03/1980 |
| From: | Crossman W, Randy Hall, Mcdonald D NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | |
| Shared Package | |
| ML19323E651 | List: |
| References | |
| 50-382-80-05, 50-382-80-5, NUDOCS 8005270102 | |
| Download: ML19323E658 (6) | |
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U. S. NUCLEAR REGULATORY COMMISSION
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OFFICE OF INSPECTION AND ENFORCEMENT
REGION IV
Report No. 50-382/80-05 Docket No. 50-382 Category A2 Licensee: Louisiana Power and Light Company 142 Delaronde Street New Orleans, Louisiana 70174 Facility Name: Waterford Steam Electric Station, Unit No. 3 Inspection at: Waterford Site, Taft, Louisiana Inspection conducted: March 11-14, 1980 d
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Inspectors:
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s R.fC. Stewart',WtMT' iip'ectoK Projects Section Date (Paragraphs 1, 2, 3, & 7)
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. D. Gilbert, Reactor Inspector, Engineering Support
/ Ddte Section (Paragraph 5 &
D. G. Mcdonald, Reactor inspector, Engineering Support
'Date Section (Paragraph 4) (March 11-12, 1980 only)
Approved:
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/8 W. A. Crossman, Chief, Projects Section Date Y
' R. E. Hall, Chief, Engineering Support Section
/ ITate Inspection Summary:
Inspection on March 11-14, 1980 (Report No. 50-382/80-05)
Areas Inspected:
Routine, unannounced inspection of construction activities related to a follow-on review of in process welding activities on Reactor Coolant Pressure Boundary and other safety related piping; a follow-on l
review of Electrical Components and systems; and a status and schedule
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review of licensee action on matters previously reported under 10CFR 50.55(e).
The inspection involved forty inspector-hours by three hTC inspectors.
Results: No items of noncompliance or deviations were identified.
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DETAILS
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Persons Contacted Principal Licensee Employees
- T. Gerrets, QA Manager
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- B. Brown, QA Engineer
- C. Chatelain, QA Engineer
- B. Toups, QA Engineer L. Bass, Project QA Manager Other Personnel R. Hartnett, QA Site Supervisor, Ebasco
- L. Stinson, Site QA Program Manager, Ebasco J. Moska, QA Manager, NISCO R. King, Welder Training, Tompkins-Beckwith (T-B)
H. Miller, Welding Engineer, T-B J. Freshour, Welding Engineer, EBASCO W. Lamson, Project QC Manager, Fischbach & Moore, Inc.
The IE inspectors also interviewed other licensee and contractor personnel
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including members of the engineering and QA/QC staffs.
- Denotes those attending the exit interview.
2.
Licensee Action on Previous Inspection Findings During this inspection the IE inspector met with the licensee's QA Manager to review the status of eight (8) matters previously reported by the licensee in accordance with the requirements of 10CFR 50.55(e). The review included the current status of resolution of each of the items and scheduled dates for the final reports. No items of noncompliance or deviations were identified.
Copies of the licensee initial reports and subsequent correspondence concerning scheduled completion dates are contained in the Public Document Room and are on file in the Regional NRC office.
3.
Site Tour The IE inspectors walked through various construction and storage areas to observe construction activities in progress and to inspect the general state of cleanliness and adherence to housekeeping requirements.
- No items of noncompliance or deviations were identified.
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4.
Electrical Components and Systems
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a.
Review of Procedures
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The IE inspector reviewed the following Fischbach ano Moore procedures to determine if appropriate and adequate measures have been established to provide the necessary details required for cable terminations and splices and dielectric measurements of insulation systems for cable and
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equipment.
CP-307, Rev. 3, 1/8/79, " Cable Terminations and Splices."
CP-401, Rev. O, 1/12/79, "Hy-Pot Testing of Cable and Equipment."
CP-405, Rev, 4, 10/8/79, " Insulation Testing of Cable and Equipment."
No discrepancies with the requirements of 10CFR 50, Appendix B, IEEE Std 384-1974 or IEEE Std. 62 were noted.
b.
Observation or Work The IE inspector selected two 4160 Vac and two 125 Vdc cables that had previously been installed to determine if the installation had been accomplished in accordance with established design drawing, procedures and other documents.
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Cable # 30500A-SA 3-1C/250 MCM 4160 Vac 4KV Switchgear 3A35 to HPSI Pump "A" Dwg. # B288/530500 Rev. 22-1 Q.C. Check List 307-30500A-SA (2) Cable # 30535A-SB 3-IC/250 MCM 4160 Vac 4KV Switchgear 3A35 to LPSI Pump "B" Dwg. # B288/SM30535 Rev. 16 Q.C. Check List 307-30535A-SB (3) Cable # 32486A-SA 2-1C/#4 125 Vdc 125 Vdc Power Distribution Panel to MCC 3A3125 Tie Breaker Dwg. # B288/S32486 Rev. 17 QC Check List 307-32486A-SA (4)
Cable # 32487A-SA 2-1C/#4 125 Vdc 125 Vdc Power Distribution Panel to'MCC 3A135 Tie Breaker Dwg. # B288/S32487 Rev. 17 QC Check List 307-32487A-SA
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In addition to the above, the IE inspector noted a hold tag and conditional release on the following 480 Vac MCC module.
480 Vac MOV Control Flow Control Valve 3AC-TMG46A MCC-3A313S F & M Hold Tag CR-8041 Conditional Release E-93 Inspection h port 317-28-02 No items of noncompliance or deviations were ident'fied.
c.
Review of Records The IE Inspector reviewed the records for the cables and MOV controls identified in item b above.
The record review did not identify any areas where the QA program and procedures were not being adequately implemented.
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No items of noncompliance or deviations were identified.
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Reactor Control Element Drive Mechanism The IE inspector observed NISCO welding an upper canopy seal, Weld Number 35 on Drawing 3015-022, for the Control Element Drive Mechanism.
Seal welding was being accomplished with the automatic gas tungsten-are welding process using certified weld wire type ER NICRFE-5 (Heat No. H-66-75-07069A)
and qualified welders (1003, 1029 and 1037) as specified in weld procedure specification NPS 43.5.2.
The material text report and welder qualification reco-ds were reviewed and found to be consistent with the requirements in Section III of ASME B&PV Code.
No items of noncompliance or deviations were identified.
6.
Reactor Coolant and Other Safety-Related Piping a.
Review of Procedures The IE inspector selectively reviewed Tompkins - Beckwith welding procedures and supporting procedure qualification reports for welding reactor coolant and other safety-related piping for compliance with the ASME B&PV Code, Sections III and IX, 1974 Edition through summer 1976 Addenda. The documents reviewed included:
Document Title WPS 1.1 Gas Tungsten-Arc welding Revision W-9 and Shielded Metal-Arc
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Welding of Carbon l
Steel Materials
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Document Title WPS 8.1 Gas Tungsten-Arc Welding and Revision W-5 Shield Metal-Arc Welding (PQR WP 8.1-8.1A)
of Stainless Steel Material WPS 1.14 Consumable Insert, Revision W-0 Gas Tungsten-Arc
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(PQR WP 1.5-1.5D)
Welding and Shielded Metal-Arc Welding of Carbon Steel Materials, Preheat 50 degrees F Minimum and Postweld Heat Treatment Procedure TBP-26 Visual Inspection Revision H Procedure Procedure TBP-30 Preheating and Interpass Revision B Temperature Procedure Procedure TBP-7 Welder Qualification Revision H Procedure Procedure TBP-32 Tools-Color Coding For Use on Revision A Stainless Steel b.
Observation of Work The IE inspector observed the Tompkins - Beckwith activities at various stages of weld joint completion.
The traveler (Q2+5 MS-1C-10 F/E) for Main Steam field weld FW-1 was reviewed for adequacy of welding preheat and postweld heat treatment specified for a weld thickness of 1.250 to 2.062 inches.
The requirements were consistent with the qualified welding procedure and section NC of the ASME B&PV Code. Welding of Safety Injection Piping was observed being performed on two field welds designated FW-1 on travelers Q1-SI-IC-20 E and Q2-SI-IC-102 F/E.
The welding material and qualification of welders were consistent with requirements of WPS 8.2.
Three welds in the component cooling piping, designated SW-18 on Traveler Q3-CC-LW3-CC-17 F/E and FW-1 on Travelers Q3-CC-1C-972 E and Q3-CC-1C-973 E, were observed and the welding materials traced to the certified material test reports.
Welding materials were consistent with requirements of WPS 1.8 for SW-18 and WPS 1.7 for FW-1.
The weld reinforcement on two feedwater pipe welds, FW-2 and FW-3 of Traveler Q3-FW-1C-862 F/E was inspected and found consistent with visual inspection Procedure TBP-26 requirements.
The in process testing of three welders was observed by the IE inspector. The welders were using the electrode, pipe material, welding process and welding position specified on the welder per-formance test record.
The three welder performance tests specified radiographic inspection for final acceptance but were unavailable for evaluation at the time of the inspection.
In the areas inspected, no discrepancies with the requirements of ASME B&PV Code Section IX were noted.
No items of noncompliance or deviations were identified.
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7.
Exit Interview The IE inspectors met with licensee representatives (denoted in paragraph 1) at the conclusion of the inspection on March 11, 1980.
The IE inspectors summarized the purpose and the scope of the inspection and
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the findings.
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