IR 05000341/2025002

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Integrated Inspection Report 05000341/2025002
ML25223A266
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 08/11/2025
From: Sanchez-Santiago E
NRC/RGN-III/DORS/RPB2
To: Peter Dietrich
DTE Electric Company
References
IR 2025002
Download: ML25223A266 (1)


Text

SUBJECT:

FERMI POWER PLANT, UNIT 2 - INTEGRATED INSPECTION REPORT 05000341/2025002

Dear Peter Dietrich:

On June 30, 2025, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Fermi Power Plant, Unit 2. On July 10, 2025, the NRC inspectors discussed the results of this inspection with C. Domingos, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding did not involve a violation of NRC requirements.

If you disagree with a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Fermi Power Plant, Unit 2.

August 11, 2025 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Elba M. Sanchez Santiago, Chief Reactor Projects Branch 2 Division of Operating Reactor Safety Docket No. 05000341 License No. NPF-43 Enclosure:

As stated cc: Distribution via LISTSERV Signed by Sanchez Santiago, Elba on 08/11/25

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Fermi Power Plant, Unit 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Reactor Water Cleanup System Piping Rupture Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green FIN 05000341/202500201 Open/Closed None (NPP)71152S A self-revealed Green finding was identified when the licensee failed to follow procedure MES26, Flow Accelerated Corrosion Prediction, Detection, and Correction. Specifically, a component was modeled incorrectly and operating experience/noted off-normal conditions were not utilized when selecting components for examination.

Additional Tracking Items

None.

PLANT STATUS

Unit 2 began the inspection period at rated thermal power. On May 4, 2025, a planned power reduction to approximately 86 percent power was made for a routine rod pattern adjustment.

Power was restored to 100 percent later on May 4, 2025. On June 13, 2025, a planned power reduction to approximately 70 percent was made for a routine rod pattern adjustment and surveillances. Power was restored to 100 percent on June 15, 2025. The plant remained at rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed onsite portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Division 2 emergency equipment cooling water (EECW) during emergency diesel generator (EDG) 11 maintenance window, completed the week ending April 12, 2025
(2) EDG 14 during EDG 11 maintenance window, completed the week ending April 19, 2025
(3) Division 1 residual heat removal (RHR) system, completed the week ending June 14, 2025

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) EDG 14 engine room, completed the week ending April 19, 2025
(2) Division 2 residual heat removal service water (RHRSW) pump room, completed the week ending April 19, 2025
(3) Auxiliary building cable spreading room, completed the week ending May 31, 2025
(4) Auxiliary building relay room, completed the week ending May 31, 2025

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the onsite fire brigade training and performance during an announced fire drill on the week ending April 26, 2025

71111.06 - Flood Protection Measures

Flooding Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated internal flooding mitigation protections in the: division 1 and division 2 switchgear rooms, direct current (DC) switchgear area, auxiliary building ventilation equipment areas, and division 1 and division 2 control room air conditioning rooms during the week ending April 26, 2025

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during a down power on June 13, 2025

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated training in the control room simulator associated with loss of phase for an offsite AC source, and loss of all AC power during the week ending June 15, 2025

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Scheduling and execution of combustion turbine generator (CTG) 111 maintenance activities in accordance with technical requirements, completed the week ending May 31, 2025

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Planned EDG 12 safety system maintenance outage, completed the week ending May 10, 2025
(2) Unplanned inoperability of division 1 control center heating, ventilation, and cooling system during planned division 2 RHR/RHRSW maintenance outage, completed the week ending May 17, 2025

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Reactor coolant system (RCS) and fuel cladding following reactor water cleanup system rupture and chemistry transient, completed the week ending May 3, 2025
(2) Diesel fire pump (DFP) with coolant leak, completed the week ending May 17, 2025
(3) EDG 13 starting air pressure drop, completed the week ending May 24, 2025
(4) Failure of division 2 RHR system minimum flow valve to function during a surveillance, completed the week ending May 24, 2025
(5) High pressure cooling injection (HPCI) turbine control valve pin shear, completed the week ending June 14, 2025
(6) Review of site response to industry issue documented in condition report (CR)-202546350, regarding control rod drive (CRD) collet retainer tube cracking, completed the week ending June 14, 2025

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:

Post-Maintenance Testing (PMT) (IP Section 03.01) (5 Samples)

(1) EDG 11 maintenance outage, completed the week ending April 12, 2025
(2) Standby liquid control (SLC) pump operability test after SLC pump B seal maintenance, completed the week ending April 19, 2025
(3) EECW division 1 pump and valve operability test after maintenance outage, completed the week ending May 10, 2025
(4) Piping repair following leak from reactor water cleanup system, completed the week ending May 17, 2025
(5) EDG 12 maintenance outage, to include review of foreign materials exclusion (FME)intrusion into engine, completed the week ending May 17, 2025

Surveillance Testing (IP Section 03.01) (2 Samples)

(1) EDG 14 slow start and load surveillance, completed week ending June 14, 2025
(2) SLC pump overload testing, completed the week ending June 27, 2025

Inservice Testing (IST) (IP Section 03.01) (1 Sample)

(1) Reactor core isolation cooling (RCIC) system pump operability and valve test, completed the week ending May 10,

RADIATION SAFETY

71124.03 - InPlant Airborne Radioactivity Control and Mitigation

Permanent Ventilation Systems (IP Section 03.01) (1 Sample)

The inspectors evaluated the configuration of the following permanently installed ventilation systems:

(1) Standby gas treatment filtration system

Self-Contained Breathing Apparatus for Emergency Use (IP Section 03.04) (1 Sample)

(1) The inspectors evaluated the licensees use and maintenance of self-contained breathing apparatuses.

71124.04 - Occupational Dose Assessment

Source Term Characterization (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated licensee performance as it pertains to radioactive source term characterization.

External Dosimetry (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated how the licensee processes, stores, and uses external dosimetry.

Internal Dosimetry (IP Section 03.03) (1 Sample)

The inspectors evaluated the following internal dose assessments:

(1) Dose assessments for four workers exposed to contamination during a job in the torus on April 10, 2024

Special Dosimetric Situations (IP Section 03.04) (2 Samples)

The inspectors evaluated the following special dosimetric situations:

(1)declared pregnant worker dose assessment performed from 2024 through 2025

(2) Effective dose equivalent for external radiation exposure assessments performed in

OTHER ACTIVITIES-BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

MS06: Emergency AC Power Systems (IP Section 02.05)===

(1) April 1, 2024 through March 31, 2025

MS07: High Pressure Injection Systems (IP Section 02.06) (1 Sample)

(1) April 1, 2024 through March 31, 2025 BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (1 Sample)
(1) October 1, 2024, through March 31, 2025

BI02: RCS Leak Rate Sample (IP Section 02.11) (1 Sample)

(1) April 1, 2024 through March 31, 2025

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1) October 1, 2024, through March 31, 2025 PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)
(1) October 1, 2024, through March 31, 2025

71152S - Semiannual Trend Problem Identification and Resolution Semiannual Trend Review (Section 03.02)

(1) The inspectors reviewed the licensees corrective action program to identify potential trends in the licensee's flow accelerated corrosion program that might be indicative of a more significant safety issue.

71153 - Follow Up of Events and Notices of Enforcement Discretion Event Follow Up (IP Section 03.01)

(1) The inspectors evaluated systems and operator response to an unplanned isolation of the reactor water cleanup system following a pipe rupture, completed the week ending April 26,

INSPECTION RESULTS

Reactor Water Cleanup System Piping Rupture Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green FIN 05000341/202500201 Open/Closed None (NPP)71152S A self-revealed Green finding was identified when the licensee failed to follow procedure MES26, Flow Accelerated Corrosion Prediction, Detection, and Correction. Specifically, a component was modeled incorrectly and operating experience/noted off-normal conditions were not utilized when selecting components for examination.

Description:

On April 20, 2025, while attempting to place the 'A' reactor water cleanup (RWCU)filter/demineralizer in service, multiple alarms and indications were received indicating a rupture in the RWCU system. Safety-related systems responded appropriately to the rupture, isolating the RWCU system from the reactor via the associated containment isolation valves.

Temperature within the RWCU heat exchanger room became elevated, but remained below thresholds necessitating entry into the emergency operating procedures. The RWCU pumps tripped off by design. Between the initial rupture and a controlled pressurization of the system to help identify the leak location, areas immediately adjacent to the RWCU heat exchanger room on the second floor of the reactor building became highly contaminated with water flowing out of the room, along with the north side of the first floor of the reactor building due to leakage from above. Investigation revealed an approximate 1" thru-wall hole in the 4" return piping on the outlet of the regenerative heat exchanger. A four-foot section of pipe containing the hole was replaced, based, in part, on visual and ultrasonic examination of the upstream and downstream piping. During and after restoration of the reactor water cleanup (RCWU)system, some additional consequences of the pipe rupture were identified. For example, demineralizer resin was released into the RWCU system and that upon restoration, was transported into the reactor recirculation system, causing main steam line alarms (which subsequently cleared). The alarm required the operators to take actions to assess whether there was fuel cladding damage, which based on the indications they were able to rule out.

Additionally, a technical requirements manual (TRM) action statement was entered based on pH, conductivity, and chloride concentrations due to the resultant chemistry excursion. While not a chemistry parameter in the TRM, an increase in sulfate levels also led to discussions with industry peers and the fuel vendor regarding impacts to fuel and reactor vessel components. If the chemistry parameters had not returned to normal within the 72-hour TRM completion time a plant shutdown would have been required. Discussions with peers and the fuel vendor concluded there were no threats to continued operation.

A subsequent review by the licensee revealed flow accelerated corrosion (FAC) was the most likely cause of the rupture, pending a formal failure analysis of the pipe. On May 30, 2025, as part of an ongoing inspection sample to review the FAC program for potentially more significant issues, inspectors identified that in 2019, a corrective action document was written documenting abnormally high iron levels in water samples from the return piping of the RWCU system. Reference was made to a history of high conductivity alarms associated with high iron going back to 2011. A technical evaluation was performed, concluding FAC was likely occurring and that certain sections of piping should be inspected in the upcoming refueling outage (RF20-spring 2020). The section of piping from the outlet of the regenerative heat exchanger to sample point 51 (SP51), where the high iron was being detected, was recommended for inspection, among other piping segments. The inspectors determined this segment was particularly notable, in that iron concentrations measured elsewhere were lower, and tended to narrow down the likely location where FAC was occurring. However, the inspection was removed from RF20, with the intention to perform the inspection in a RWCU maintenance outage in September of 2020. This work was never started, as the work order was still in the planning phase as of inspector review. In RF21 (spring 2022), a decision was made based, in part, on dose considerations, to not inspect that segment. Instead, piping was replaced in another segment (also recommended by the technical evaluation for inspection)downstream of SP51 instead of between the regenerative heat exchanger outlet and SP51.

Between RF21 and the rupture, no inspections were performed between the heat exchanger and SP51, nor an updated assessment of the susceptibility of that segment to FAC. Analysis for iron concentrations from SP51 (which had been periodically monitored following the 2019 technical evaluation) ceased in December 2022. Of note, following the downstream piping replacement in RF21, two more samples were taken from SP51 in June of 2022 and December of 2022, both indicating relatively high iron concentrations. A condition report (CR)was written for the June 2022 sample, but it was closed with no action, nor forwarded to engineering for review.

The licensees flow accelerated corrosion program is governed by Procedure MES26, Flow Accelerated Corrosion Prediction, Detection, and Correction. The procedure incorporates industry recommendations for an effective FAC program, and implements one of the aging management programs required by final safety analysis report section B, Aging Management Programs and Activities. In section 3.2. the procedure outlines requirements for identifying program scope and maintaining susceptibly reviews for computer-modeled, and non-modeled, piping. In section 6.3.2, the procedure requires information such as internal and external operating experience, plant operating history, and off-normal operating conditions to be used when selecting which piping to inspect. An equipment cause evaluation performed by the licensee for the rupture concluded system/component monitoring was ineffective at detecting the degradation that led to the rupture. Further, the licensee discovered the 'T' connection just upstream of the rupture was not correctly modeled in the system (socket welds versus the assumed butt welds). Additionally, the 'T' connection contained a thermowell. Both conditions likely raised velocity and turbulence of the RWCU flow, making the immediate downstream area more susceptible to FAC, and rendered the existing modeling non-conservative for predicting wear in that location.

Corrective Actions: The licensee entered the issue into the corrective action program, replaced the affected pipe, and reviewed the program in light of the pipe failure to check for any adjustments needed for upcoming component inspection scope.

Corrective Action References: CR 202547014

Performance Assessment:

Performance Deficiency: Procedure MES26, Flow Accelerated Corrosion Prediction, Detection, and Correction, implements the FAC program at the plant. Contrary to MES26 section 3.2, a susceptibility review, identifying susceptible modeled and non-modeled piping, was not maintained. Specifically, the model assumed the piping joint just upstream of the rupture location was a butt-welded connection versus a socket-welded connection with a thermowell, resulting in a non-conservative corrosion model for the piping. Additionally, as required by MES26 section 6.3.2, the plant's operating history and noted off-normal operating conditions were not utilized in the component examination selection process. Specifically, a 2019 engineering technical evaluation, driven by unusually high iron concentrations in chemistry samples, recommended the piping between the regenerative heat exchanger outlet and SP51 be examined because of FAC concerns. The piping was not examined prior to rupture in 2025. Failing to meet the requirements of MES26 constituted a performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Equipment Performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, the performance deficiency resulted in a high-energy line break in the secondary containment (reactor building), resulting in a containment/reactor isolation of the RWCU system. Further, the rupture caused a pressure wave in the RWCU system, dislodging filter/demineralizer resin into the system and severely clogging a filter used during system warmup and flushing. Ultimately, upon restoration, the resin entered the reactor causing high radiation conditions in the main steam system and alarm response by the operations staff to assess for fuel cladding damage. The resultant chemistry excursion caused entry into a TRM 72-hour shutdown action statement as well, and consultation with the fuel vendor regarding potential impacts of high sulfates on the fuel and reactor components.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power.

Specifically, utilizing Exhibit 1, section B, the high-energy line break did not result in a plant scram nor loss of mitigation equipment needed to achieve a stable shutdown condition.

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance.

Enforcement:

Inspectors did not identify a violation of regulatory requirements associated with this finding.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On July 10, 2025, the inspectors presented the integrated inspection results to C. Domingos, Site Vice President, and other members of the licensee staff.
  • On May 8, 2025, the inspectors presented the radiation protection inspection results to C. Domingos, Site Vice President, and other members of the licensee staff.

THIRD PARTY REVIEWS The inspectors reviewed a World Association of Nuclear Operators report that was issued to the site during the inspection period.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

6M7215357

Emergency Equipment Cooling Water System Division II

Drawings

6M7215734

Emergency Diesel Generator System Functional Operating

Sketch

23.127

Reactor Building Closed Cooling Water/Emergency

Equipment Cooling Water System

153

23.205 Att. 1A

Division I RHR Initial Valve Lineup

23.205 Att. 8A

Division I RHR LPCI Standby Lineup Verification

Procedures

23.307

Emergency Diesel Generator System

139

71111.04

Work Orders

69156730

Perform 24.307.17 Sec-5.1 EDG 14 Start and Load Test -

Slow Start

06/09/2025

FPAB28

Relay Room, Zone 8, Elevation 613'6"

FPAB2M11

Auxiliary Building, Cable Spreading Room, Zone 11,

Elevation 630'

FPRHR114EDG

RHR Complex, EDG 14 Room, El. 590'0"

FPRHR151

RHR Complex, Division II Pump Room Zone 51, El. 590'0"

LPFP9402321

Fire Drill/Evaluation

71111.05

Procedures

MOP10001

Fire Brigade Drill Record Form

EF2PRA011

Internal Flood Walkdown Summary Notebook

71111.06

Engineering

Evaluations

EF2PRA012

Internal Flood Analysis Notebook

Miscellaneous

SSOP2022464

License Operator Requalification Simulation Lesson Plan

71111.11Q

Procedures

2.000.03

Power Operation 25% to 100% to 25%

109

CR202436104

CTG 111 Failed to Achieve Base Load and Failed PMT

2/05/2024

Corrective Action

Documents

CR202441956

Standby Diesel Generator (Aggreko) Output Voltmeter

Reading Extremely Low

09/02/2024

Miscellaneous

27331

R1100 Get Well Plan

MMR APP D

Guidelines For Determining Fictional Failures (FFs) and

Maintenance Preventable Functional Failures (MPFFs)

MMR APP E

Maintenance Rule SSC Specific Functions

71111.12

Procedures

MMR APP F

Maintenance Rule Performance Criteria

71111.13

Engineering

Evaluations

TEE1108078

Removal of RHR Complex Pump Room Roof Plugs Under

LCO 3.0.9

F

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Miscellaneous

Shift Manager Daily Alignment Meeting Package

05/13/2025

MMR APP H

Maintenance Rule Conduct Manual OnLine Core Damage

Risk Management Guidelines

MMR12

Maintenance Rue Conduct Manual Equipment Out of

Service Risk Management

20A

ODE20

Protected Equipment

Procedures

ODE20, ATT. 17

Protected Equipment Form EDG 12 Safety System Outage

Calculations

DC6336 Vol 1

EDG Starting Air System Sizing Basis

B

24680

Self-Assessment Finding: Non-Conservative EDG Starting

Air Operability Criterion

05/24/2012

23976

Control Rod 1031 Failed to Withdrawal

09/09/2023

23185

Pert 21 60Day Interim Report Notification: Failure of the

CRD Collet Retainer Tube/Outer Tube Weld (SC2301)

04/28/2023

CR202440147

Control Rod 2227 Difficult to Move

06/12/2024

CR202443587

Control Rod 2227 Difficult to Move

11/09/2024

CR202444216

Coolant Leak from Diesel Fire Pump

2/092024

CR202535153

Diesel Fire Pump Needs Coolant Topped Off

03/12/2025

CR202545556

Tie Pin for HPCI Control Valve Rod Linkage Broke While

Disassembling

2/10/2025

CR202546070

Failure Analysis Findings for HPCI Pilot Valve Pin

03/06/2025

CR202546350

SIL 139 Revision 1, Control Rod Drive Collet Retainer Tube

Cracking

03/19/2025

CR202546731

Coolant Leak From Diesel Fire Pump (DFP)

04/07/2025

CR202547132

Numerous MCR Alarms Received After Placing RWCU

Pump in Service

04/26/2025

CR202547149

Fuel Warranty Limit Exceeded for Reactor Water Sulfates

04/26/2025

CR202547692

EDG 13 Air Receiver Check Valves Leak By

05/19/2025

CR202547693

EDG 13 Starting Air Pressure Drop > 30 psig During Slow

Start Surveillance 24.307.16

05/19/2025

71111.15

Corrective Action

Documents

CR202547714

Division 2 RHR Min Flow Valve E1150F007B (RHR DIV2

PUMPS 'B' and 'D' MIN FLO MOV) did Not Automatically

Open When Securing Torus Cooling

05/20/2025

Corrective Action

Documents

Resulting from

Inspection

CR202547061

NRC Identified - Coolant Residue on DFP Coolant System

Piping

04/23/2025

66336C

Gov Control System

10/03/1969

66375 D

HPCI DIL Relay Assem-Remove Servo

10/07/1969

6M7212043

Diagram High Press Coolant Injection SYS Barometric

CNDR (HPCI) Reactor Building

AJ

6M7212083

Diagram Residual Heat Removal (RHR) Division 2

Drawings

6M72157082

HPCI Turbine Lube Oil/Control Oil Functional Operating

Sketch

L

Engineering

Changes

T13213

Residual Heat Removal System

04/18/2024

9609887

E4101C002 - Servo for Woodward Governor

07/08/1987

Engineering

Evaluations

FPEE240003

Evaluation of Surveillance Frequencies Extensions for Fire

Protection Equipment

DBD-E1100

Residual Heat Removal System (RHR)

G

EDP37362

RHR and Core Spray Strong Pump/Weak Pump Interaction

B

Nuclear

Generation

Memorandum

To: M. Kirschenheiter From: I. Finney; Latent Issue Review:

Control Rod Drive System

2/28/2019

Miscellaneous

VMB1160.1

[CONFIDENTIAL] Installation, Operation, and Maintenance

Driver Manual

35.202.009

HPCI Steam Turbine - General Maintenance

35.206.001

RCIC Steam Turbine Maintenance

35.206.005

RCIC Turbine Trip Throttle Valve General Maintenance

46.202.001

HPCI Turbine Governor Control System Calibration

54.000.03

Control Rod Scram Insert Time Test

74.000.19

Chemistry Routine Surveillances

74.00018

Chemistry Shiftly, 72Hour, and Situational Surveillances

76.000.34

Reactor Coolant Analysis

Procedures

CHS-PRI06

Fermi 2 - Chemistry Specifications

71111.15

Work Orders

68147634

Neil Req'd - Clean and Lube External Portions of Control

and Stop Valves and Lid

2/06/2025

71111.15

Work Orders

950023227

Div 2 RHR Min Flow Valve E1150F007B did Not Auto Open

as Expected

05/21/2025

Calculations

DC6309 VOL 1

Design-Basis of EDG Fuel Oil and Day Tank Level-

Requirements and Setpoints

B

24860

EDG12 2 and 10 Piston/Liners Have Indications of Wear

09/16/2023

2547350

FME Cover Became Entangled in EDG12 Upper Torsional

Damper

05/06/2025

CR202546696

Work Will Not Complete As Scheduled

04/04/2025

CR202546737

NQA - Documentation of Inspection Result Per MES83101

of the Coatings for R3000A005 (EDG11 Expansion Tank)

04/07/2025

CR202546745

TDX Time Delay Relay Failed AsFound Testing

04/07/2025

CR2025469793

Significant Wear on EDG 11 and 10 Upper Piston

04/09/2025

CR202547029

Leak in RWCU Heat Exchangers Room

04/20/2025

CR202547053

RWCU HX Room Transient Temperature Excursion of

168F EX Impact Assessment

04/22/2025

CR202547056

RWCU Inspection Results

04/23/2025

Corrective Action

Documents

CR202547089

G3300F033 RWCU Blowdown FCV Not Operating as

Expected

04/24/2025

Drawings

6M7212046

Diagram Reactor Water Clean-Up Reactor Building

23.307

Emergency Diesel Generator System

139

24.139.02

SLC Pump and Check Valve Operability Test

24.307.14

Emergency Diesel Generator 11 - Start and Load Test

71111.24

Procedures

24.307.17

Emergency diesel generator 14 - Start and Load Test

24.307.45

Emergency Diesel Generator 11 - Fast Start Followed by

Load Reject

34.307.001

Emergency Diesel Generators - Inspection and Preventive

Maintenance

2.139.01

Standby Liquid Control System Associated Isolation Device

Test

IST Program

Description

Inservice Testing Program Fourth Ten-Year Interval

IST Program Pump

Basis

Inservice Testing Program for Pumps and Valves Part 12:

IST Program Basis

71111.24

Procedures

IST Program Relief

Requests

Inservice Testing Program for Pumps and Valves Part 7:

IST Program Relief Requests

IST Pump Scope

Table

Inservice Testing Program for Pumps and Valves Part 3:

IST Pump Scope Table

IST Pump Testing

Program

Inservice Testing Program for Pumps and Valves Part 2:

IST Pump Testing Program

MMA11

Post-Maintenance Testing Guidelines

MWC10

Work Package Preparation

VME81.1

Operations and Maintenance Technical Manual-

Emergency Diesel Generators

67464736

Inspect Air Start Distributors, Pilot Valves and Springs

04/08/2025

293649

Perform 24.139.02 SLC Pump and Check Valve Operability

Test

04/15/2025

68558615

Perform 24.206.01 RCIC System Pump Operability and

Valve Test at 1000 PSIG

05/12/2025

69029447

Perform 42.139.01 SLC Pump "A" Associated Isolation Test

Device

06/24/2025

950019607

Perform 24.207.08 SEC5.1 DIV 1 EECW PUMP & VALVE

OPERABILITY TEST

05/01/2025

Work Orders

950019686

Leak at RWCU Regenerate HX

04/21/2025

CR202435708

Reactor Services & Radiation Protection Need to

Implement Airborne Contamination Mitigation Actions Prior

to DW Head and Rx Head Disassembly Activities

01/18/2024

CR202438114

PAPR Failure in HRA/HCA

04/09/2024

CR202444310

RP RET SCBA Qualifications Below Threshold in XX33

2/13/2024

CR202545627

Evaluate the Required Pounds per Square Inch (PSI) of

Training SCBA Cylinders

2/14/2025

Corrective Action

Documents

CR202546076

NQA Audit 250101 Recommendation-Improvement of

HEPA Vacuum Issue/Return Log

03/06/2025

MSA Training Certificate of Accomplishments

Various

Annual SCBA Flow Tests

Various

24032703601

Laboratory Report - Compressed Air/Gas Quality Testing

03/27/2024

24102216501

Laboratory Report - Compressed Air/Gas Quality Testing

10/22/2024

25011706504

Laboratory Report - Compressed Air/Gas Quality Testing

01/17/2025

65.000.768 Att 1

MSA FireHawk M7 SCBA Inspection Record

Various

71124.03

Miscellaneous

65.000.769 Att 1

MSA AirHawk SCBA Inspection Record

Various

Miscellaneous

u019411

Fermi 2 - Radiation Protection Respirator Qualification

Report

04/15/2025

65.000.738

Filling of Breathing Air Cylinders

65.000.757

Filling Control Room Emergency Breathing Air System

65.000.768

Inspection of MSA FireHawk M7 Self-Contained Breathing

Apparatus

65.000.769

Inspection of MSA AirHawk Self-Contained Breathing

Apparatus

65.000.770

Inspection of MSA Ultra Elite AP Respirator

Procedures

65.000.771

Inspection of PremAire Cadet Escape Respiratory

Equipment

71124.03

Self-Assessments NPRP240079

Quick Hit Self-Assessment: NRC Inspection 71124.03-

InPlant Airborne

2/13/2024

Calculations

24006 CDRM WB

Multi Calculations

EDEX

Calculations of EDEX for Workers in 2024

Various

CR202335303

Scheduled Work in RP Rad Health Not Performed due to

Inadequate Staffing

2/29/2023

CR202436344

Dose Alarm Received While Performing Main Steam Line

Plug Maintenance

2/16/2024

CR202437062

Safety Concern Due to RP Procedure Change

03/21/2024

CR202438147

Dosimetry Records Not Vaulted According to MGA07

04/10/2024

CR202438195

Individuals With Potential Uptakes

04/11/2024

CR202439872

Individual Reported to Davis-Besse Nuclear Power Station

With Contamination on Boots

05/28/2024

Corrective Action

Documents

CR202545289

An Abundance of Individuals Undergoing Inprocessing

Never Pick Up their DLR from Dosimetry and/or Do Not

Require a DLR

01/28/2025

DLR/Secondary Dosimetry Comparison Resolution Form

Various

NPRP180203

Adjustment of Self Reading Dosimeter Doses to More

Consistently Compare to Individual DLR Results

11/09/2018

NPRP240002

Scaling Factor Report & Waste Stream Sample results from

GEL Laboratories, LLC, Dated November 21, 2023

01/18/2024

71124.04

Miscellaneous

NPRP240033

Prospective Evaluation of Fermi 2 Internal Dose

05/07/2024

NPRP240076

Scaling Factor Report & Waste Stream Sample Results

from GEL Laboratories, LLC, Dated August 16, 2024

11/15/2024

NPRP250012

Evaluation of Impact of Current Radionuclide Mix on RP

Instruments

03/25/2025

Miscellaneous

NVLAP LAB

CODE 1005180

Certificate of Accreditation to ISO/IEC 17025:2017

Various

65.000.267

Whole Body Count Protocol and Evaluation of Bioassay

Results

11.1

Procedures

66.000.248

Calibration of Self Reading Dosimeters

PM2024041115

Post Decon Survey of Bay 12 - 15:00

04/11/2024

PM202404111

Operator Uptake Investigation - 02:45

04/11/2024

PM2024041110

Updated Bottom of Torus Survey - 11:00

04/11/2024

Radiation

Surveys

PM202504304

Characterization of RWCU Piping Removed From RWCU

HX Room. to Be Sent Out for Analysis

04/30/2025

71124.04

Self-Assessments NPRP240080

Quick Hit Self-Assessment: NRC Inspection 71124.04-

Occupational Dose Assessment

2/13/2024

CR202437903

NRC identified: Locked High Radiation Area Controls Not in

Accordance With Technical Specifications

04/05/2024

CR202441609

NRC Violation-2Q2024: Locked High Radiation Area

Controls Not in Accordance with Technical Specifications

08/15/2024

Corrective Action

Documents

Resulting from

Inspection

CR202548223

NRC Identified - November 2024 and December 2024 EDG

Performance Indicator (Unavailability) Report

Discrepancies

06/13/2025

Fermi 2 - HPCI Performance Indicators

Various

Fermi 2 - EDG MSPI and WANO Performance Indicators

Various

MSPI Derivation Report - High Pressure Injection System

Unreliability Index

03/2025

MSPI Derivation Report - High Pressure Injection System

Unavailability Index

03/2025

MSPI Derivation Report - AC Power System Unreliability

Index

03/2025

MSPI Derivation Report - AC Power System Unavailability

Index

03/2025

Fermi II Reactor DEI Chemistry Data Report

Various

Activity Released by Release Point and Isotopes

Various

71151

Miscellaneous

24 Annual Radioactive Effluent Release Report

Procedures

24.000.02

Eight-Hour - Mode 1, 2, 3 - Control Room RCS Operation

Leakage

Various

23626

AsFound Accelerated Corrosion Inside Valve Body of

N22F413

09/09/2023

2130533

Increased Inleakage to Sump D017

11/29/2021

2130971

FAC and Erosion Control Program Investigation Related to

2130533, Increased Inleakage to Sump D017

2/13/2021

26453

Cycle Isolation Monitoring: Elevated Temperature Noted on

North Reactor Feed Pump Min Flow Valve Following

Startup

05/19/2022

27151

Cycle Isolation Monitoring: Elevated Temperature Noted on

N3039F620 MTG MSR Reheater Steam Supply Drain

09/03/2023

27373

High Soluble Iron in RWCU Effluent Sample

06/23/2022

CR202310162

23 INPO Materials Review Visit: Recommendation for

Flow Accelerated Corrosion Program

09/14/2023

CR202331926

Self-Assessment Recommendation: TMIS -230035 -

Update Information in PEP19 Appendix I

07/27/2023

CR202334588

Evaluate EPRI ASME Code Reconciliation for FAC

Programs

11/20/2023

CR202435639

LRI OE Review: Flow Accelerated Corrosion Program:

Refueling Outage Path Delay Due to Valve Repairs

01/17/2024

CR202547014

Isolation of RWCU When Returning RWCU F/DA to

Service

04/20/2025

CR202547035

Programmatic Weakness Involving the Conduct of FME

Steering Committee Meetings

04/21/2025

CR202547054

Trend of Poor Initial FME High Risk Plan Quality -

Requesting Performance Gap Analysis

04/22/2025

CR202547100

FME Program Gap: Completion of Loss of Integrity Actions

04/24/2025

CR202547176

Passive Component Degradation Trend: Flow Accelerated

Corrosion and Erosion Control and Service Water Piping

Corrosion/Erosion Control

04/28/2025

CR202547914

WO for Proposed RWCU Piping Replacement Needed

05/30/2025

CR202548038

NQA - Ready to Work Challenges Identified Reviewing

Sample of P1 and -100 Work Orders

06/05/2025

71152S

Corrective Action

Documents

CR202548091

NSRG 2501XX: NSRG Engineering Subcommittee Action

- Passive Component Degradation Trend

06/09/2025

Engineering

Evaluations

PEP19 Appendix A

FAC Program Susceptibility Review

FAC-

RF22SCOPE

Technical Basis for RF22 FAC Program Inspection and

Replacements Scopes IAW MES26 Requirements

09/26/2022

Nuclear

Generation

Memorandum

To: Sean T. Howell From: J.D. Wines - 2023 Quick Hit Self-

Assessment Report for Materials Review Visit Readiness

07/28/2023

Miscellaneous

PEP19

Flow Accelerated Corrosion Program Notebook

Procedures

MES26

Flow Accelerated Corrosion Prediction, Detection, and

Correction

65374361

Cycle Isolation Monitoring: Elevated Temperature Noted on

North RFP Min Flow Valve

04/21/2024

Work Orders

66444817

FAC 40, 41, 42, and 43 - RF22 - Perform Erosion/Corrosion

Inspection of Main Steam Piping

03/25/2024

Corrective Action

Documents

CR202547014

Isolation of RWCU When Returning RWCU F/DA to

Service

04/20/2025

71153

Miscellaneous

DBD-G3300

Reactor Water Cleanup System

D