IR 05000341/2025010

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Biennial Problem Identification and Resolution Inspection Report 05000341/2025010
ML25253A285
Person / Time
Site: Fermi 
Issue date: 09/10/2025
From: Sanchez Santiago E
NRC/RGN-III/DORS/RPB2
To: Peter Dietrich
DTE Electric Company
References
IR 2025010
Download: ML25253A285 (1)


Text

SUBJECT:

FERMI POWER PLANT, UNIT 2 - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000341/2025010

Dear Peter Dietrich:

On August 7, 2025, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your Fermi Power Plant, Unit 2 and discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations problem identification and resolution program to confirm that the station was complying with NRC regulations and licensee standards. Based on the samples reviewed, the team determined that your program complies with NRC regulations and applicable industry standards such that the Reactor Oversight Process can continue to be implemented.

The team also evaluated the stations effectiveness in identifying, prioritizing, evaluating, and correcting problems, reviewed licensee audits and self-assessments, and its use of industry and NRC operating experience information. The results of these evaluations are in the enclosure.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews, the team found no evidence of challenges to your organizations safety-conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

No findings or violations of more than minor significance were identified during this inspection.

September 10, 2025 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Elba M. Sanchez Santiago, Chief Reactor Projects Branch 2 Division of Operating Reactor Safety Docket No. 05000341 License No. NPF-43 Enclosure:

As stated cc w/ encl: Distribution via LISTSERV Signed by Sanchez Santiago, Elba on 09/10/25

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Fermi Power Plant, Unit 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 03.04)

(1) The inspectors performed a biennial assessment of the effectiveness of the licensees Problem Identification and Resolution program, use of operating experience, self-assessments and audits, and safety-conscious work environment.
  • Problem Identification and Resolution Effectiveness: The inspectors assessed the effectiveness of the licensees Problem Identification and Resolution program in identifying, prioritizing, evaluating, and correcting problems. The inspectors also conducted a five-year review of the 2-stage Target Rock Safety Relief Valves.
  • Operating Experience: The inspectors assessed the effectiveness of the licensees processes for use of operating experience.
  • Self-Assessments and Audits: The inspectors assessed the effectiveness of the licensees identification and correction of problems identified through audits and self-assessments.
  • Safety-Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

INSPECTION RESULTS

Assessment 71152B Corrective Action Program Based on the samples reviewed, the team concluded that the licensees implementation of the Corrective Action Program was generally effective and supported nuclear safety.

Effectiveness of Problem Identification:

Based on the samples reviewed, the team determined that the licensee continued to identify issues at a low threshold and appropriately entered these issues into the Corrective Action Program. The team also determined that the licensee usually entered problems into the Corrective Action Program completely and accurately.

The team noted that issues were being identified by all levels of organization and with varying degrees of safety significance. The licensee also utilized a number of Corrective Action Program support processes to identify problems, including the self-assessment and audit process and the Operating Experience Program. Some deficiencies were identified by external organizations, including the NRC, that had not been previously identified by licensee staff and were subsequently entered into the Corrective Action Program for resolution. For example, the licensee performed departmental self-assessments and Nuclear Quality Assurance (NQA) audits to identify issues in station processes. The identified deficiencies and improvement opportunities were entered into the Corrective Action Program for resolution. Similarly, the licensee screened issues from both NRC and industry operating experience and entered them into the Corrective Action Program when they were applicable to the station.

As low level, as well as safety significant issues were entered into the CAP, the team determined that the licensee was generally effective at identifying trends and taking appropriate corrective actions to prevent more significant problems from developing. In addition, the licensee used the Corrective Action Program to document instances in which previous corrective actions were ineffective or were inappropriately closed. The team did identify a potential trend in condition report (CR) generation rate decreasing over the last few years; however, the inspectors did not identify any safety or programmatic concerns with the trend.

The team performed a 5-year review of the 2-stage Target Rock Safety Relief Valves. As part of this review, the team interviewed the system engineer, and reviewed plant health reports, and selected corrective action and condition evaluation documents. The team concluded that deficiencies and concerns were identified and entered into the Corrective Action Program at a low threshold and the corrective actions were adequate and timely, commensurate with their safety significance.

Effectiveness of Prioritization and Evaluation of Issues:

Based on the samples reviewed, the team determined that licensee performance was generally effective at prioritizing and evaluating issues commensurate with the safety significance of the identified problem. In general, once a degraded or non-conforming issue was identified, the CAP process was effective in directing equipment operability / functionality review. During the Ownership Screening Committee (OSC) and Management Review Committee (MRC) meetings the team attended, licensee staff were generally thorough and intrusive in reviewing and screening issues. The team also observed healthy dialogue and good interactions among the members of the screening groups. The members came prepared and challenged each other on disposition of the identified conditions. Actions were prioritized based on the safety significance of the issues.

Effectiveness of Corrective Actions:

Based on the samples reviewed, the team determined that the licensee was generally effective in implementing corrective actions. In general, corrective actions for deficiencies that were safety significant were implemented in a timely manner. Problems requiring the performance of a root cause evaluation or other causal evaluation methodologies were resolved in accordance with Corrective Action Program requirements. The team sampled assignments associated with violations that were identified by the NRC previously and with licensee event reports (LERs). The team determined that the corrective actions sampled were generally effective and timely.

Assessment 71152B Self-Assessments and Audits Based on the samples reviewed, the team determined that the licensees performance of self-assessments and audits was generally effective. The licensee performed department self-assessments and quality assurance audits throughout the organization on a periodic basis. These self-assessments and audits were generally effective at identifying issues and enhancement opportunities at an appropriate threshold. The self-assessments and audits reviewed by the team identified issues that were not previously known, including issues within the Corrective Action Program itself. NQA had identified deficiencies with the licensees processes and those issues were addressed by the station using the Corrective Action Program.

Assessment 71152B The Use of Operating Experience Based on the samples reviewed, the team determined that licensees performance in the use of operating experience was generally effective. The licensee screened industry and NRC operating experience information for applicability to station. Based on these initial screenings, the licensee initiated actions in the Corrective Action Program to fully evaluate the impact, if any, to the station. When applicable, actions were developed and implemented under the Corrective Action Program to prevent similar issues from occurring. Operating experience lessons learned were communicated and incorporated into plant operations. The team observed the information being used in daily activities, such as pre-job briefs, as well as Corrective Action Program issues reviews and investigations.

Assessment 71152B Safety-Conscious Work Environment During this assessment, the team conducted focus groups and interviews, reviewed Employee Concerns Program (ECP) and Safety Culture Monitoring Panel procedures and files, examined corrective actions associated with the last SCWE inspection, and reviewed the 2024 USAA Safety Culture assessment. The team interviewed over 93 employees from the Operations, Security, Maintenance, Radiation Protection, Chemistry, NQA, and Engineering Departments. This included 15 first-line supervisors, 7 contractors, and the ECP manager.

As described in Inspection Manual Chapter, Aspects within the Cross-Cutting Areas and NUREG-2165, Safety Culture Common Language, in the area of Environment for Raising Concerns (RC), the team did not identify any significant issues with the work environment site-wide, as most interviewees (90 percent) stated they would raise any type of concern without fear of retaliation. Only 4 percent indicated hesitancy in raising nuclear safety concerns, localized to one department: Security. Specifically, 15 percent of individuals interviewed in the Security department indicated hesitancy in raising nuclear safety concerns.

This was classified as a significant precursor in the trait of RC.1 - Safety-Conscious Work Environment Policy, which could lead to a chilled work environment.

Furthermore, the team received positive feedback about the ECP representative and their accessibility as an avenue for raising concerns. While individuals expressed a willingness to submit CRs, there is a general perception that they do not consistently receive adequate feedback on the resolution of those CRs. CRs are often closed without resolving the issue, or they are assigned back to the originator for resolution, even when it is not their area of expertiseparticularly when the concerns are not directly related to nuclear safety. This was categorized as precursor in the Problem Identification and Resolution (PI) trait, specifically PI.3.

The team also noted that the Nuclear Safety Culture Monitoring Panel identified a steady increase in anonymous CR submissions. This trend raises concerns that the current work environment may be impacting the normal processes intended to surface such issues. Our review found that information from the Corrective Action Program, ECP, and other sources (e.g., Gallup) has provided opportunities for management to detect shifts in certain aspects of safety culture and SCWE. However, this information was not broken down by departments and was not trended to identify department-specific challenges.

In the area of Leadership Safety Values and Actions, the team heard that significant site-wide staffing challenges are placing tremendous strain on the organization. These challenges appeared to be attributed to attrition and delays in filling vacant positions. Staff reported that these concerns have been communicated to management multiple times; however, responses have been slow and have not fully addressed the ongoing issues. Additional concerns were shared by the Security organization, specifically related to the amount of forced overtime. The NRC team determined that this impacted LA.1, which states that leaders ensure that personnel, equipment, procedures, and other resources are available and adequate to support nuclear safety.

The team also identified concerns related to Field Presence (LA.2). Staff expressed that senior leaders are frequently absent from the field and are perceived to be consistently tied up in meetings. While they acknowledged improvements in the open-door policy and leadership presence in strategic meetings, they felt that senior leaders are failing to connect with workers at their level. One example shared involved a senior leader introducing themselves multiple times to the same individuals within a single day, suggesting a lack of familiarity and engagement with staff.

In the area of Respectful Work Environment (WE), individuals expressed concerns about feeling disrespected, specifically in some coaching in the moment activities, and that leadership should talk to people, not down at them (WE1). Most of the interviewees expressed concern with trust, specifically trust in senior leadership. There were instances described when management described a change with one vision, and the implementation was completely different. Additionally, individuals viewed the increased number of anonymous condition reports as indicative of a lack of trust. (WE3). The change in senior leadership was viewed as positive, and the request to resubmit the long-standing issues via the Corrective Action Program was viewed as a hope that things will be different. While the areas of opportunity identified in this trait are not affecting individuals ability to raise nuclear safety concerns, it is considered a precursor to a decline in safety culture. All the interviewees expressed a high level of trust and confidence in their immediate supervisors.

In the area of Effective Safety Communication (CO), some interviews revealed issues with communication, specifically a lack of transparency. Comments indicated that individuals feel they need to consider how management will react to feedback before providing it, and that the rumor mill is filling the gaps in information (CO.3). Staff expressed concerns about the lack of response or feedback provided in CR closures, perceiving that management is making decisions in a vacuum and not sharing the reasoning behind some decisions, yet they ask for the rationale when staff propose ideas. Some also mentioned that responses are tailored based on the originator of the question or the manager responding, rather than being consistent and comprehensive (CO.2).

Overall, interviewees stated that morale is declining. While it may be better than last year, it is not trending upward. The NRC will continue to monitor the safety culture at Fermi and expects Fermi to implement swift corrective actions to address issues in the Security department.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On August 7, 2025, the inspectors presented the biennial problem identification and resolution inspection results to Peter Dietrich and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CARD 09-27876

2009 Configuration Design Basis Inspection (CDBI) Self

Assessment - Additional Unanalyzed HPCI/RCIC and Room

LOCA Heat Load

10/08/2009

CARD 09-28082

Key Calculation Review for DC-2849 Primary Containment

Pneumatic Supply System

10/15/2009

CARD 10-24554

HPCI and RCIC Gland Steam Leakage Higher than

Expected

06/03/2010

CARD 14-21236

Results from the BADGER Test Report Indicate 3 Fuel

Storage Rack Panels Have Boron Density Less than That

Assumed

2/17/2024

CARD 14-23790

NRC Audit - Specification 3071-226 DRILLCO Capacity

05/01/2014

CARD 15-23277

RHRSW Return From RHR HX High Temperature Alarm

Setpoints Above Piping Design Temperature

05/07/2015

CARD 16-22201

Error in Calculation of Strainer Debris Weights

03/10/2016

CARD 16-25611

2016 EQ Program Self-Assessment Deficiency: EQ Central

Files EQ1-EF2-020 and -058 Lack Formal Documentation for

the Use of Sound Reasons to the Contrary IAW with

10CFR50.49 Par. (l)

07/14/2016

CARD 16-29202

Sparging of SLC Tank and Effects on Operability Not Fully

Evaluated.

11/16/2016

CARD 17-20988

Incomplete Incorporation of TSR-36838 Rev A As-Built

Posting Against DC-0367 Vol I

2/02/2017

CARD 17-22354

AOV Thrust Calc Overly Conservative

03/22/2017

CARD 18-24672

Evaluate R1400 for (a)(1) Status

06/13/2018

CARD 19-21968

ARP 3D54 RBCCW Radn Monitor Upscale, Revised with

Insufficient Detail, Does Not Match Field Installation.

03/13/2019

CARD 19-22113

OAR Review - DC-5713 Rev F Fire Header Hydraulic Calc

Minor Error Found

03/19/2019

CARD 19-26744

Description of the RPS EPA Setpoints in the TS 3.3.8.2

Bases is Inconsistent with the UFSAR 7.2.1.1.2

09/09/2019

CARD 20-25381

SRV Insulation Found to Not Be Properly Installed

04/29/2020

71152B

Corrective Action

Documents

CARD 20-25413

Generate Work Orders to Repair SRV Insulation Identified in

04/29/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CARD 20-25381

CARD 20-25708

Air Leak on union for SRV 'R'

05/13/2020

CARD 20-28723

UNSAT SRV inspection

07/28/2020

CARD 20-28737

Missing Insulation on SRV P (B2104F013P)

07/28/2020

CARD 20-29013

SRV A Tailpipe Temperature Elevated Following RF-20

Startup

08/06/2020

CARD 20-29165

SRV 'M' Tailpipe Temperature Elevated Following RF-20

Startup

08/10/2020

CARD 20-29828

NRC Identified: Evaluate Alarm Set-Point Change for HI

Drywell Temps

09/01/2020

CARD 20-30554

Three SRVs Removed in RF-20 Found outside of As-Found

Set-Point Tolerance

09/24/2020

CARD 21-23072

Possible 50.9 Issue with SFPLI Modification

04/06/2021

CARD 21-24255

DC-6447 Voltage Issue for H21P557

05/14/2021

CARD 21-25514

21 NRC 50.59 Inspection - HPCI Strainer Evaluation in

EDP 70097 Does Not Factor Design Basis Loading

Conditions

06/22/2021

CARD 21-29019

The R3200 System Has Exceeded its Availability Criteria for

Maintenance Rule

10/11/2021

CARD 21-29328

20 MMR14 Structures Monitoring Inspection of Reactor

Building North Exterior Wall (Investigation)

10/21/2021

CARD 21-29364

Revise EP-304-01

10/21/2021

CARD 22-00260

Water alarm Manhole 16949, Pump Run Light Lit

2/23/2022

CARD 22-25711

Unable to Raise RPV Level with Div 1 Core Spray Keep-Fill

IAW 43.401.100 ILRT

04/27/2022

CARD 22-26034

EP-101, Classification of Emergencies Needs Clarification

Based on 20-32952 and EPFAQ 2015-006

05/05/2022

CARD 22-26422

SRVs B2104F013 M, D, F, and J have elevated Tail Pipe

Temperatures

05/17/2022

CARD 22-26474

Four SRVs (M, D, F, J) indicative of weeping

05/20/2022

CARD 22-28201

Three SRVs removed in RF-21 Found outside of As-Found

Set-Point Tolerance

07/26/2022

71152B

Corrective Action

Documents

CARD 22-29803

FERMEX 2022 - Opportunities to Improve Dispatch

Timeliness of DCRTs

09/22/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CARD 22-30029

NRC Design Basis Assurance Inspection (DBAI) Re-Exit

Finding

09/30/2022

CARD 22-31399

EDG LO Sampling Not Aligned with Renewed License

11/28/2022

CARD 22-32154

PST Perform 28.508.04 Emergency Equipment Monthly

Inspection

2/28/2022

CARD 23-20646

Investigate Drywell Cooling Time for Dedicated Shutdown

Scenario

01/24/2023

CR-2023-30014

Lack of transparency from senior leadership team

05/05/2023

CR-2023-30106

TR.2 Area of Concern: Line and Training Managers Have

Not Fully Analyzed Some Gaps in the Oversight Of Training

Programs and Developed Actions to Address Underlying

Behaviors

05/10/2023

CR-2023-30342

License Renewal - Indication on CST Fourth Level Wall

Panel Below Minimum Design Thickness

05/19/2023

CR-2023-30437

HPCI Inboard Torus Suction Isolation Valve Abnormal Stroke

05/23/2023

CR-2023-31630

MDCT D Fan Tripped

07/18/2023

CR-2023-31935

NQA Audit 23-0107 Finding - Repeated Gaps with

Radioactive Material (RAM) Management and Survey Map

Documentation

07/27/2023

CR-2023-32105

ILT 2023 Throughput did not meet expectations, Root Cause

08/03/2023

CR-2023-32208

1D58 - STM LK DET RCIC LOGIC POWER FAILURE and

1D62 - STM LK DET HPCI LOGIC POWER FAILURE

Received Simultaneously

08/09/2023

CR-2023-32454

DW Leak identification - RCS leakage from B Reactor Recirc

Sample Line

08/20/2023

CR-2023-32488

NQA Audit 23-0108 Recommendation - Evaluate Emergency

Preparedness Drill Objectives Rated Unsat or Marginal

from 2021 through 2023 for Trends

08/22/2023

CR-2023-32802

Diesel Fire Pump Fail to Start

09/04/2023

CR-2023-33018

28.501.02 - FIRE SUPPRESSION WATER SYSTEM VALVE

LINEUP VERIFICATION past critical

09/12/2023

CR-2023-33390

Zone 14 - DC MCC - Fire Alarm light lit with no Fire Alarm

09/29/2023

CR-2023-33907

Components Prematurely Removed From 24.425.01

10/23/2023

71152B

Corrective Action

Documents

CR-2023-34053

Uncontrolled Material Discovered in the Safeguards

10/27/2023

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Information (SGI) Room

CR-2023-34093

NRC Violation - 2023 CYBER SECURITY INSPECTION:

Failure to meet Defense-in-Depth Protective Strategies per

NEI 08-09 Section E.6 Controls

2/22/2023

CR-2023-34253

Procedure Non-Adherence SEP-AD4-02

11/06/2023

CR-2023-34258

Vendor Assigned to Access Authorization Notified Fermi 2 of

An Internal Investigation.

11/06/2023

CR-2023-34344

NRC Violation - Integrated Inspection: Inoperable MDCTs

Following Modification to the Brake Control Circuit.

2/08/2023

CR-2023-35161

Improper Oil Viscosity and Oil Type

2/19/2023

CR-2024-35333

Numerous Fire Protection Surveillances going Unperformed

Due Poor Change Management And Lack Of Training

01/02/2024

CR-2024-35386

Revised Security NRC Baseline Inspection Procedures

01/04/2024

CR-2024-35411

Fatigue Management - Work Hours Not Entered into FRMS

01/05/2024

CR-2024-35422

Diesel Fire Pump Coolant Level Issue

01/06/2024

CR-2024-35449

DFP Coolant level low

01/08/2024

CR-2024-35596

Security CLO - Failure to coordinate Protected Area barrier

manipulation with CAS

01/16/2024

CR-2024-35783

Condenser Tube Leaks and SF6 Testing, Root Cause

07/18/2024

CR-2024-35844

28.504.08 Cannot Be Performed as Written

01/23/2024

CR-2024-36020

NRC SCWE Inspection Observation-Perception of

Production over Safety (Radiation Safety)

CR-2024-36022

NRC SCWE Inspection Observation-Site over reliance on

RP

CR-2024-36023

NRC SCWE Inspection Observation-Long Term Contractor

Support

CR-2024-36106

Issues with FRMS Software Calculations

2/06/2024

CR-2024-36149

NRC Violation - 4Q2023: Division 1 Emergency Equipment

Cooling Water/Service Water (EECW/EESW) Heat

Exchangers Found Above Operability Limit

03/07/2024

CR-2024-36156

NRC Violation - 4Q2023: Failure to Identify Conditions

Adverse to Quality Associated with Gear Reducer Foot

Supports for the Mechanical Draft Cooling Towers

04/09/2024

CR-2024-36261

NRC KPI for Security Equipment Unavailability Reaches

2/13/2024

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Critical Margin Threshold

CR-2024-36293

NQA - Methods for Calibration Validation of Containment

High Range Radiation Monitors Appear to Not Meet Station

Design or Regulatory Requirements.

2/14/2024

CR-2024-36363

OSSF SPING Not Restored to Functional Status within 30

Days.

2/17/2024

CR-2024-36436

Procedure Enhancement 24.204.06 LPCI P&V

2/21/2024

CR-2024-36581

Entry into TRLCO 3.0.3 required for Appendix R Alternate

Shutdown Auxiliary Systems (2C1-2 Spare Battery Charger)

2/28/2024

CR-2024-36632

HHS Lab Rejected Specimen

2/29/2024

CR-2024-36700

NOS - Apparently Incorrect Conversion Factors for Off Gas

Radiation Monitor B Calibration.

03/04/2024

CR-2024-37085

NRC Identified Hose Hanging Over Handrail of HPCI Hatch.

03/21/2024

CR-2024-37127

Inadequate Corrective Actions to Sustain Excellence in the

Fire Protection Program

03/22/2024

CR-2024-37148

Automatic RPS Scram on High RPV Pressure While

Attempting to Lower Generator MW to 55 MWe per

2.000.04

03/23/2024

CR-2024-37198

NQA RF22 Monitoring - Junior RP Technician Did Not Verify

Daily Source Check of Canberra Tennelec as Required by

65.000.146

03/24/2024

CR-2024-37245

Foreign Material Dropped in Suppression Pool.

03/25/2024

CR-2024-37411

MOP05-200 Identifies Core Spray as a WICA System

Inconsistently

03/28/2024

CR-2024-37844

Fatigue Management - 10 CFR 26 Subpart I Work Hour Rule

Violations

04/04/2024

CR-2024-38029

Div-1 CCHVAC Chiller Trip

04/08/2024

CR-2024-38133

FFD Procedure Revision

04/10/2024

CR-2024-38195

Individuals with Potential Uptakes.

04/11/2024

CR-2024-38264

Lower Retaining Nut Loosened on C11A-K4A Relay Prior to

Reinstallation.

04/12/2024

CR-2024-38698

24.321.04 DEDICATED SHUTDOWN PANELS H21-P627

AND H21-P628-OPERABILITY TEST Procedure

enhancement

04/23/2024

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CR-2024-38856

G343R609 RWCU Pump Disch Flow Indication Reading 100

GPM with Pumps Shutdown

04/26/2024

CR-2024-38999

E5150F007 tripped thermal overloads while stroking open

04/29/2024

CR-2024-39110

EDG Fuel Delivery Additives Not Properly Verified Prior to

On-Site Chem Testing and Fuel Offload

05/01/2024

CR-2024-39164

Purge Trouble and Chiller Surging Div-1 CCHVAC

05/02/2024

CR-2024-39230

AOP Entry due to Trip of the East CRD Pump

05/04/2024

CR-2024-39570

SRVs B2104F013A, B, H Have Elevated Tail Pipe

Temperatures

05/13/2024

CR-2024-39746

SRVs B2104F013P & R Have Elevated Tailpipe

Temperatures

05/21/2024

CR-2024-39872

Individual Reported to Davis Besse Nuclear Power Station

with Contamination on Boots.

05/28/2024

CR-2024-39996

EDG 13 Overvoltage Trip String Monitor Light Out

06/02/2024

CR-2024-40139

Security Loggable Event - Loss of Vital Area Keys

06/07/2024

CR-2024-40149

Div 2 Battery Room Higher than Max Design Temp Limit

06/08/2024

CR-2024-40664

Missed Hourly Firewatch rounds in the Aux Bldg.

07/01/2024

CR-2024-40826

FermEX Submittal Not Completed per the Requirements of

10CFR50, Appendix E, IV, F.2.b

07/10/2024

CR-2024-41183

Leak from T4100-F375 Instrument Line

07/26/2024

CR-2024-41313

Four SRV Pilots Removed in RF-22 Found outside of

As-Found Set-Point Tolerance.

08/01/2024

CR-2024-41471

DIV 1 Control Air Dryer Differential Pressure High

08/08/2024

CR-2024-41473

RHR Pump "A" Motor Upper Thrust Bearing Low out of

Standstill

08/09/2024

CR-2024-41569

Employee with Expired Fitness for Duty (FFD) Training and

Active Badge

08/14/2024

CR-2024-41615

Licensee-Identified Violation - NRC report 2Q2024:

Individual entered Locked High Radiation Area without

proper dosimetry

10/09/2024

CR-2024-41616

Licensee-Identified Violation - NRC report 2Q2024: Gaps in

M&TE Program Compliance Over Last 4 Years Resulting in

Presumed Lost Test Equipment and Other Issues.

05/14/2025

71152B

Corrective Action

Documents

CR-2024-41634

Licensee-Identified Violation - NRC report 2Q2024:

10/29/2024

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

E5150F007 - Non-Conservative Gear Ratio Discrepancy

Resulting in Negative Analytical Torque Margin

CR-2024-41787

Installed Material does Not Meet Dedication Requirements

08/26/2024

CR-2024-41837

FERMEX 2024 Critique Item-Dosimeters for TSC and OSC

08/28/2024

CR-2024-41876

RERP Exercise 08/27/2024 - Dose Discrepancies

Encountered

08/28/2024

CR-2024-41900

28.502.10 Scheduled for WW 2435 and will Not Be Able to

Be Performed Prior to Going past Critical.

08/29/2024

CR-2024-42165

EDG13 Lube Oil Level High

09/12/2024

CR-2024-42192

Blown Fuse E41F2B in H21-P081

09/12/2024

CR-2024-42273

Preplanned Loss of Security UPS Availability for Removal

and Replacement

09/17/2024

CR-2024-42371

Trend of Lowering EDG 13 Jacket Coolant Expansion Tank

Level

09/21/2024

CR-2024-42530

NRC Identified Operability Quality for CR-2024-40402 did

Not Provide Enough Detail to Explain Bases for Operability.

09/27/2024

CR-2024-43107

Tailgating event/ Security Rules Violation

10/22/2024

CR-2024-43113

2F-5A Pos 2B-R M Contactor Stationary and Moveable

Contacts Found with Excessive Pitting

10/22/2024

CR-2024-43174

Identify Common Causes of Recent NRC Violations and

Findings

10/24/2024

CR-2024-43380

SCWE: Concerning Exponential Trend in Anonymous CRs

Under the Current Senior Leadership Team

CR-2024-43443

Trend Only - Compensatory Measures established at PAP

and RHR

11/04/2024

CR-2024-43993

24 RP Pre-NRC 71124.03 Self-Assessment

Recommendation - Evaluate Risk of Emergency Air

Breathing Compressor Being Located outside the PA

11/26/2024

CR-2024-44059

Div 1 EECW Heat Exchanger A has Loose Clamping Bolt

2/02/2024

CR-2024-44090

Procedure 64.120.040 CONTAINMENT AREA HIGH

RANGE RADIATION MONITOR-DIVISION 1 CALIBRATION

Not Usable for Calibration

2/03/2024

CR-2024-44182

Replacement of All Site SCBAs, Cylinders and Confined

Space Respirators.

2/06/2024

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CR-2024-44278

RP Department Gap in Radiological Risk Recognition.

2/12/2024

CR-2024-44703

Temporary Loss of CCTV call up cameras

2/23/2024

CR-2024-44750

10D67 Div 2 48/24V Battery 2IB Trouble in alarm with

Normal Charger Parameters

2/29/2024

CR-2025-31643

Rollup of aggregate RHR Hydramotor Problems

07/11/2023

CR-2025-44994

East Main Turbine Bypass Valve Spurious Opening

01/13/2025

CR-2025-45311

Revise EP-101 Enclosure A (EAL Classification Matrix)

01/29/2025

CR-2025-45347

NRC Violation - 4Q2024: Failure to Establish Required

Firewatch with RB SW Quad Fire Detectors Non-Functional.

03/19/2025

CR-2025-45386

E5150F025 RCIC Turb Steam Drain Pot Inboard Isolation

Valve Stroke Time Outside IST Limit

01/31/2025

CR-2025-45531

RB SPING Not Restored to Functionally Capable within 30

Days as Required by ODCM

2/07/2025

CR-2025-45537

EDM Truck Would Not Start during Weekly Testing

2/08/2025

CR-2025-45552

EITER -Owner Controlled Area Notification System (OCANS)

Speaker Tower #1 and #3 Not Functioning Properly

2/10/2025

CR-2025-45569

3D56 Testability Logic CH A/B RPS/PWR Failure due to

Gross Failure on C11-N601D (SDV Water Level)

2/11/2025

CR-2025-45604

RERP Emergency Management Performance Evaluation

(EMPE) Drill - Objective K5.3 UNSAT for TSC - TSC

Emergency HVAC

2/27/2025

CR-2025-45678

During February 11, 2025 Emergency Management

Performance Evaluation (EMPE), Objective I.3.6 was UNSAT

for the TSC

2/17/2025

CR-2025-45781

CAS and SAS Intercom not functioning as designed

2/21/2025

CR-2025-45863

Missing / unaccounted for equipment

2/25/2025

CR-2025-45914

During February 11, 2025 Emergency Management

Performance Evaluation (EMPE), Objective E1.6 was SAT

with Significant Comments for the EOF

2/27/2025

CR-2025-45949

Failed Calibration of M&TE, AG-058-M, Heise HQS-2 0-100

PSIA Pressure Module on Q Work Performed Between

2/20/2023 and 8/06/2023 by Work Group Mechanical

Maintenance

2/28/2025

71152B

Corrective Action

Documents

CR-2025-46173

Evaluate D.C. Cook Security Event

03/11/2025

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CR-2025-46327

Security Industry Operation Experience Applicability

Review - Vogtle and Callaway Protective Strategy NRC

Violations

03/18/2025

CR-2025-46429

Fermi Security OE Applicability Review - Palo Verde SIED

25-003: Negligent Discharge during Dry Fire Manipulations

03/24/2025

CR-2025-46529

Failed Calibration of M&TE, AG-045-M, Heise HQS-2 0-20

PSIA Pressure Module on Q Work Performed Between

2/19/2024 and 3/19/2025 by Work Group RADPROI

03/28/2025

CR-2025-46871

Cleanliness Within Both Divisions of RHR Complex

Unsatisfactory

04/12/2025

CR-2025-47014

Isolation of RWCU when Returning RWCU F/D-A to Service

04/20/2025

CR-2025-47114

Lead Shielding Installed on G3300F033 Without Completing

65.000.303 and WI-RE-10

04/25/2025

CR-2025-47490

When did the Fermi Motto Become More with less

CR-2025-47649

Failed Calibration of M&TE, PG-962-M and PG-725-M on "Q"

Work Performed between 03/29/2024 to 09/29/2024 and

03/30/2024 to 09/30/2024 Work by Group IANDC

05/16/2025

CR-2025-47749

Fatigue Management - SAP Files for FRMS Not Being

Processed

05/22/2025

CR-2025-47768

Division 2 Control Air Compressor (CAC) Loading Very

Slowly

05/23/2025

CR-2025-47853

Loss of Video Capture in CAS/SAS

05/28/2025

CR-2025-47984

Lead Curtains Fell off of X-Ray Machine #2

06/04/2025

CR-2025-48063

TSC Conditions Do Not Support RERP Drill Scheduled for

6/10/2025

06/08/2025

CR-2025-49070

25 NRC PI&R Inspection Observation

07/25/2025

CR-2025-49072

25 NRC PI&R Inspection Observation

07/25/2025

CR-2025-49134

25 NRC PI&R Inspection Feedback on SCWE Interviews

with Individual Contributors Across Site

07/29/2025

CR-2025-49161

25 NRC PI&R Inspection: Discrepancy with Web Based

Training Due Dates

07/30/2025

CR-2025-49164

25 NRC PI&R Inspection - Inspector Feedback

07/30/2025

Corrective Action

Documents

Resulting from

Inspection

CR-2025-49186

25 NRC PI&R Inspection: Enhancement Required to

Guidance for Issuance of M&TE Under MMA05, Tool and

07/31/2025

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

M&TE Issue, Control and Return.

CR-2025-49241

25 NRC PI&R Inspection - NRC Identified - Improper

Closure of CARC CR-2025-45678 Related to EMPE

Objective I.3.6 UNSAT for the TSC

08/04/2025

CR-2025-49346

25 NRC PI&R Inspection - NRC Feedback on CAP

CARDs 20-29828 and 22-30029

08/07/2025

Engineering

Evaluations

EFA-E41-24-002

Evaluation of E4100F067 Hydraulic Piston Seal

ECP Investigations

24

Safety Culture Monitoring Panel Presentation and Minutes

for 2025

Spring Gallup Survey

25

Station Trend Reports for Q1, Q2 and Q3

25

OSC Meeting Package

07/24/2025

MRC Meeting Package

07/29/2025

OSC Meeting Package

07/23/2025

341-2024-001

Automatic RPS SCRAM on High RPV Pressure While

Attempting to Lower Generator Output During RF-22

05/15/2024

341-2024-002

Primary Containment Isolation Valve Declared Inoperable

for a Period Prohibited by Plant Technical Specifications

05/16/2024

CSCCD-

G41K187A

Spent Fuel Pool (SFP) Level Primary Channel Signal

Processor

CSCCD-

G41R601A

Spent Fuel Pool (SFP) Level Primary Channel Remote

Indicator - Control Room

G41R601A-S

Calibration Specification Sheet - Spent Fuel Pool Water

Level Indicator

A

MGA16

Fatigue Management

Revision 15

NOS-24-0017

24 Nuclear Safety Culture Assessment (NSCA) Report

11/24/2024

Miscellaneous

NRC-25-0018

Annual Radioactive Effluent Release Report and

Radiological Environmental Operating Report

04/28/2025

20.300.SBO

Loss of Offsite and Onsite Power

23.139

Standby Liquid Control System

EP-101

Classification of Emergencies

71152B

Procedures

FBP-8

FERMI 2 Management Observation Program

Revision 12

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

FBP-82

Fostering a Healthy Nuclear Safety Culture

Revision 20

MCE03

Chemistry Sampling and Analysis

MGA12

FERMI Employee Concerns Program

Revision 7

MQA11

Corrective Action Program

MQA11-100

Operability Determination Process

MQA11-200

Quality Assurance Conduct Manual

Implementing Procedure

Revision 2

MQA11-300

Screening and Assignment

MQA11-400

Corrective Action Program Condition Disposition

MQA11-500

Non-Corrective Action Program Condition Disposition

MQA11-600

Root Cause Evaluations

23-0100

Operations, Emergency Operating Procedures, and Fire

Protection Program Reports

2/27/2023

23-0107

Nuclear Quality Assurance Audit of the Radiation Protection

Program

08/18/2023

23-0108

Nuclear Quality Assurance Audit of the Emergency

Preparedness Program

09/26/2023

23-07

Oversight Station Assessment Report

11/01/2023

23-1001

22 Mid-Cycle Recommendation Surveillance

03/24/2023

24-0101

Security Audit Report

03/11/2024

24-0105

Nuclear Quality Assurance audit of the Evaluation and

Corrective Action, and Operating Experience Programs

08/09/2024

24-0106

Nuclear Quality Assurance Audit of the Radiation Protection,

Radiological Effluents Monitoring, and Radioactive Material,

Transfer & Disposal Programs

08/16/2024

24-0107

Training and Qualifications of Unit Program Audit Report

09/09/2024

24-04

Oversight Station Assessment Report Final

11/01/2024

24-1002

Nuclear Quality Assurance Surveillance of Emergency

Preparedness Program

09/26/2024

NAPI-25-0003

Problem Identification and Resolution (PI&R) Formal

Self-Assessment

06/16/2025

Self-Assessments

NARP-24-0078

Pre-Inspection Readiness QHSA - EAL and Emergency Plan

Changes

08/01/2024

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

NARP-24-0100

NRC Inspection Readiness Assessment: Exercise Evaluation

71114.01 & Performance Indicator Verification 71151

07/30/2024

NPOP-23-0086

Quality of OJT/TPE Training

11/12/2023

NPOP-24-0017

Fire Protection Implementation

11/28/2023

NPRP-24-0003

QHSA: Radioactive Gaseous and Liquid Effluent Treatment

System

01/16/2024

NPRP-24-0079

Quick Hit Self-Assessment: NRC Inspection 71124.03 - In-

Plant Airborne

2/13/2024

NSSE 25-0020

Security Training (IP 71130.07) Security Plan Changes

(IP 71130.09)

05/02/2025

Self-Assessments

NSSE-24-0029

Force-On-Force (IP 71130.03)

09/20/2024

66491878

Perform 44.030.272 ECCS RX Stm Dome Pres RHR/CSS

Inject, Div 2, CHNL B, Xmtr Cal

04/05/2024

67598569

G33R609 - Replace Indicator

04/29/2024

68531328

Troubleshoot and Repair Close Seal In Ckt on E4150-F042

03/19/2024

71152B

Work Orders

68688424

Perform 24.202.01 HPCI Pump / Flow Test & Valve Stroke at

25 PSIG

05/15/2025