IR 05000331/2004002
ML041140550 | |
Person / Time | |
---|---|
Site: | Duane Arnold |
Issue date: | 04/23/2004 |
From: | Burgess B NRC/RGN-III/DRP/RPB2 |
To: | Peifer M Nuclear Management Co |
References | |
IR-04-002 | |
Download: ML041140550 (57) | |
Text
ril 23, 2004
SUBJECT:
DUANE ARNOLD ENERGY CENTER NRC INTEGRATED INSPECTION REPORT 05000331/2004002
Dear Mr. Peifer:
On March 31, 2004, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Duane Arnold Energy Center. The enclosed integrated inspection report documents the inspection findings which were discussed on April 5, 2004, with Mr. J. Bjorseth and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
Based on the results of this inspection, two NRC-identified and one self-revealed findings of very low safety significance, two of which involved violations of NRC requirements, were identified. However, because these violations were of very low safety significance and because the issues were entered into the licensees corrective action program, the NRC is treating these findings as Non-Cited Violations in accordance with Section VI.A.1 of the NRCs Enforcement Policy. Additionally, licensee identified violations are listed in Section 4OA7 of this report.
If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -
Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4351; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Duane Arnold Energy Center. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA by Geoffrey Wright Acting for/
Bruce L. Burgess, Chief Branch 2 Division of Reactor Projects Docket No. 50-331 License No. DPR-49
Enclosure:
Inspection Report 05000331/2004002 w/Attachment: Supplemental Information
REGION III==
Docket No: 50-331 License No: DPR-49 Report No: 05000331/2004002 Licensee: Alliant, IES Utilities Inc.
Facility: Duane Arnold Energy Center Location: 3277 DAEC Road Palo, Iowa 52324-9785 Dates: January 1, 2004 through March 31, 2004 Inspectors: G. Wilson, Senior Resident Inspector S. Caudill, Resident Inspector J. House, Senior Radiation Specialist M. Mitchell, Radiation Specialist D. Nelson, Radiation Specialist T. Ploski, Senior Emergency Preparedness Inspector Approved by: B. Burgess, Chief Branch 2 Division of Reactor Projects Enclosure
SUMMARY OF FINDINGS
IR 05000331/2004002; 01/01/04-03/31/04; Duane Arnold Energy Center; Heat Sink
Performance, Operability Evaluations, and Event Follow-up.
This report covers a 3-month period of baseline resident inspection and announced baseline inspections on radiation protection. The inspection was conducted by Region III inspectors and the resident inspectors. Three Green findings associated with two Non-Cited Violations (NCVs)were identified. The significance of most findings is indicated by their color (Green, White,
Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
A. Inspector-Identified and Self-Revealed Findings
Cornerstone: Initiating Events
- Green.
A finding of very low safety significance was identified through a self-revealing event when the licensee failed to ensure that the E condensate demineralizer was properly reassembled following a septum replacement. The improperly assembled demineralizer resulted in a resin intrusion, which caused an increase in reactor water conductivity, and a subsequent reactor scram. The licensee repaired the E condensate demineralizer.
The finding was more than minor, since it had an actual impact on safety and resulted in a reactor scram. This finding was determined to be of very low safety significance, since it did not impact any mitigating systems capability. No violation of NRC requirements occurred. (Section 4AO3)
Cornerstone: Mitigating Systems
- Green.
A finding of very low safety significance was identified by the inspectors when the licensee failed to provide appropriate quantitative or qualitative acceptance criteria for determining that important activities were satisfactorily accomplished for the Generic Letter (GL) 89-13 heat exchanger inspections on the emergency diesel generators (EDGs). The licensee has revised their inspection procedures to include adequate acceptance criteria and documentation.
The finding was more than minor because it potentially affected the licensees ability to ensure that the safety-related heat exchangers on the EDGs would be available, reliable, and capable of responding to initiating events to prevent undesirable consequences. The finding was of very low safety significance because the as-found and as-left conditions of the heat exchangers did not reveal any actual concerns with the operability of the EDGs. An NCV of 10 CFR 50, Appendix B, Criterion V, was identified for the failure to have adequate acceptance criteria and documentation for the EDGs heat exchanger inspections. (Section 1R07)
- Green.
A finding of very low safety significance was identified by the inspectors when the licensee failed to ensure proper design control was maintained when the residual heat removal service water (RHRSW)/emergency service water (ESW) pit level indicating switches (LIS) 4935A and LIS4935B were downgraded to non safety-related components. When the LISs were downgraded, safety-related and non safety-related circuits were cross connected without appropriate isolation devices. The licensee rededicated the LISs as safety-related components.
The finding was more than minor because it potentially affected the availability and reliability of the river water system to make-up to the RHRSW/ESW pit in response to specific initiating events that would result in undesirable consequences. The finding was of very low safety significance because there is a safety-related hand switch that could be used to open the make-up valves. An NCV of 10 CFR 50, Appendix B, Criterion III, was identified for the failure to maintain design control when the RHRSW/ESW pit LISs were downgraded.
(Section 1R15)
Licensee-Identified Violations
Violations of very low safety significance, which were identified by the licensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program.
These violations and the licensees corrective action tracking numbers are listed in Section 4OA7 of this report.
REPORT DETAILS
Summary of Plant Status
Duane Arnold Energy Center operated at or near full power for the entire assessment period except for brief down-power maneuvers to accomplish rod pattern adjustments and to conduct planned surveillance testing activities with the following exception:
- On January 2, 2004, power was returned to 100 percent from 50 percent capacity after completing maintenance, which began on December 31, 2003, to replace the B reactor feed pumps lubricating oil heat exchanger.
REACTOR SAFETY
Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity, and
1R04 Equipment Alignment
.1 Partial Walkdown
a. Inspection Scope
The inspectors performed four partial walkdowns of accessible portions of trains of risk-significant mitigating systems equipment. The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure. The inspectors reviewed the equipment alignment to identify any discrepancies that could impact the function of the system and potentially increase risk. Redundant or backup systems were selected by the inspectors during times when the trains were of increased importance due to the redundant trains of other related equipment being unavailable.
Inspection activities included, but were not limited to, a review of the licensees procedures, verification of equipment alignment, and an observation of material condition, including operating parameters of in-service equipment. Identified equipment alignment problems were verified by the inspectors to be properly resolved.
The inspectors selected the following equipment trains to verify operability and proper equipment line-up for a total of four samples:
- B Control Rod Drive (CRD) System with the A CRD System Out-Of-Service (OOS) for maintenance during the week ending January 17, 2004;
- B Residual Heat Removal (RHR) System with portions of the A RHR System OOS for maintenance during the week ending January 31, 2004;
- High Pressure Coolant Injection (HPCI) System with Reactor Core Isolation Cooling (RCIC) OOS for maintenance during the week ending February 21, 2004; and
b. Findings
No findings of significance were identified.
.2 Complete Walkdown
a. Inspection Scope
During the week ending January 10, 2004, the inspectors performed a complete system alignment inspection of the Residual Heat Removal Service Water (RHRSW) system for a total of one sample. This system was selected because it was considered both safety-significant and risk-significant in the licensees probabilistic risk assessment. The inspection consisted of the following activities:
- a review of plant procedures including selected Abnormal Operating Procedures (AOPs) and Emergency Operating Procedures (EOPs), drawings, and the Updated Final Safety Analysis Report (UFSAR) to identify proper system alignment;
- a review of outstanding or completed temporary and permanent modifications to the system;
- a review of control room operator log entries from January 10, 2003, through January 5, 2004, to identify potential system issues; and
- electrical and mechanical walkdowns of the system to verify proper alignment, component accessibility, availability, and current condition.
The inspectors also reviewed selected issues documented in Corrective Action Plans (CAPs) to determine if they had been properly addressed in the licensees corrective action program. The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure.
b. Findings
No findings of significance were identified.
1R05 Fire Protection
.1 Quarterly Fire Zone Inspections
a. Inspection Scope
The inspectors walked down nine risk-significant fire areas to assess fire protection requirements. The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure. The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and had implemented adequate compensatory measures for OOS, degraded or inoperable fire protection equipment, systems or features. The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events, the potential to impact equipment which could initiate or mitigate a plant transient, or the impact on the plants ability to respond to a security event. The inspection activities included, but were not limited to, the control of transient combustibles and ignition sources, fire detection equipment, manual suppression capabilities, passive suppression capabilities, automatic suppression capabilities, compensatory measures, and barriers to fire propagation.
The inspectors selected the following areas for review for a total of nine samples:
During the week ending February 21, 2004:
- Area Fire Plan (AFP) 1, North Corner Rooms;
- AFP 2, South Corner Rooms;
- AFP 18, North Turbine Building Ground;
- AFP 19, South Turbine Building Ground;
- AFP 21, North Turbine Operating Deck; and
- AFP 22, South Turbine Operating Deck.
During the week ending February 28, 2004:
- AFP 12, Reactor Building Decay Tank;
- AFP 26, Control Building; and
- AFP 27, Control Building Heating, Ventilation and Air-Conditioning.
b. Findings
No findings of significance were identified.
.2 Annual Fire Drill Observation
a. Inspection Scope
On January 14, 2004, the inspectors conducted an annual observation of the licensees fire brigade response activities during a drill which simulated a fire in the Cable Spreading Room. The inspectors evaluated the readiness of personnel to fight fires by verifying that protective clothing/turnout gear was properly donned; self-contained breathing apparatus equipment was properly worn and used; fire hose lines were capable of reaching all necessary fire hazard locations, the lines were laid out without flow constrictions, the hoses were simulated being charged with water, and the nozzles were pattern (flow stream) tested prior to entering the fire area; the fire area was entered in a controlled manner; sufficient fire fighting equipment was brought to the scene by the fire brigade; the fire brigade leader's directions were thorough, clear, and effective; communications with plant operators and between fire brigade members were efficient and effective; the fire brigade checked for fire victims and for fire propagation into other plant areas; effective smoke removal operations were simulated; fire fighting pre-plan strategies were used; and the drill scenario was followed and the drill objectives met. The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure.
b. Findings
No findings of significance were identified.
1R06 Flood Protection Measures
a. Inspection Scope
The inspectors performed an annual review of the flood protection barriers and procedures for coping with internal flooding in the HPCI Room for a total of one sample.
The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure. The inspection focused on verifying that flood mitigation plans and equipment were consistent with design requirements and risk analysis assumptions. The inspection activities included, but were not limited to, a review and/or walkdown to assess design measures, seals, drain systems, contingency equipment condition and availability of temporary equipment and barriers, performance and surveillance tests, procedural adequacy, and compensatory measures. The inspection was conducted during the week ending January 24, 2004.
b. Findings
No findings of significance were identified.
1RO7 Heat Sink Performance (71111.07)
a. Inspection Scope
The inspectors performed an annual review of the licensees inspection and testing of the A and B emergency diesel generator (EDG) heat exchangers for a total of two samples. The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure. The inspection focused on potential deficiencies that could mask the ability to detect degraded performance, identification of any common cause issues that had the potential to increase risk, and ensuring that the licensee was adequately addressing problems that could result in initiating events that would increase risk. The inspection activities included, but were not limited to, a review of the licensees observations as compared against acceptance criteria, the correlation of scheduled testing and the frequency of testing, and the impact of instrument inaccuracies on test results. The inspectors also verified that test acceptance criteria considered differences between test conditions, design conditions, and testing criteria.
The inspection was conducted during the week ending February 28, 2004.
b. Findings
Introduction The inspectors identified a finding of very low safety significance (Green) and an associated Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, relating to the failure to provide appropriate quantitative or qualitative acceptance criteria for Generic Letter (GL) 89-13 heat exchanger inspections in the procedure for inspecting the EDG heat exchangers.
Description During the week of February 28, 2004, the inspectors reviewed preventive work orders (PWOs) for the periodic inspections of the A and B EDGs jacket water, lubricating oil, and scavenging air heat exchangers. The inspectors noted that the work instructions lacked explicit inspection acceptance criteria, and the data sheets only contained the word sat for the as-found condition. Without detailed as-found information, previous comparison results, or explicit acceptance criteria, the inspectors could not identify what was being used to validate the cleaning and inspection frequencies associated with GL 89-13 heat exchanger inspections. The failure to have appropriate criteria or documentation for heat exchanger cleanliness had the potential to impact plant safety by affecting the ability of the associated mitigating system to perform its intended function. The inspectors questioned licensee management, the system engineer, and the program engineer regarding the work order documentation and acceptance criteria.
All acknowledged that the work orders contained neither detailed as-found documentation nor explicit acceptance criteria. As a result of the inspectors questioning, the licensee has revised the EDG heat exchanger inspection procedures to provide explicit acceptance criteria and a thorough written assessment of the as-found condition of the heat exchangers. The inspectors concluded that the as-found documentation and the acceptance criteria lacked sufficient detail for an adequate assessment of heat exchanger performance. The inspectors determined that, although the procedure did not contain adequate acceptance criteria and documentation of the as-found condition, the as-left conditions did not reveal any actual concerns with the operability of the heat exchangers. Therefore, this finding was determined to be of very low safety significance.
Analysis The inspectors determined that the failure to have adequate acceptance criteria for the GL 89-13 heat exchanger inspections was a performance deficiency. Since a performance deficiency existed, the inspectors reviewed this issue against the guidance contained in Appendix B, Issue Screening, of Inspection Manual Chapter (IMC) 0612, Power Reactor Inspection Reports. In particular, the inspectors compared this finding to the findings identified in Appendix E, Examples of Minor Issues, of IMC 0612 to determine whether the finding was minor. Following that review, the inspectors concluded that the guidance in Appendix E was not applicable for the specific finding.
The inspectors determined that the finding was more than minor because the failure to ensure proper heat exchanger performance has the potential to impact safety and effects the equipment performance attribute of the Mitigating Systems cornerstone. In this case, the finding potentially affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
As a result, the inspectors reviewed this issue in accordance with IMC 0609, A, Significance Determination of Reactor Inspection Findings for At-Power Situations, using the Mitigating Systems worksheet. Since the failure to have adequate acceptance criteria for the EDG heat exchanger inspections did not result in a loss of function per GL 91-18, did not represent the actual loss of a safety function, did not exceed the Technical Specification (TS) Allowed Outage Time (AOT), did not represent an actual loss of safety function for a non-TS train, and was not risk-significant due to seismic, fire, flooding or severe weather concerns, it screened as Green.
Enforcement 10 CFR 50 Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that instructions, procedures or drawings include appropriate quantitative or qualitative acceptance criteria for determining that important activities have been satisfactorily accomplished. Contrary to the above, on or before February 28, 2004, the licensee failed to have adequate acceptance criteria and documentation for visual inspections of the EDG heat exchangers, which are Appendix B systems. Specifically, the licensee did not provide proper criteria for determining whether heat exchanger performance would remain satisfactory until the next inspection. The licensee has since revised the relevant procedures to include more thorough acceptance criteria and documentation. Because of the findings very low safety significance and because it was entered into the corrective action program, the NRC is treating this issue as an NCV (NCV 5000331/2004002-01), in accordance with Section VI.A.1 of the NRCs Enforcement Policy. This issue was entered into the licensees corrective action program as CAP 30954.
Corrective actions included the development of detailed cleanliness criteria and thorough documentation for the as-found condition of the EDG heat exchanger inspections.
1R11 Licensed Operator Requalification Program
a. Inspection Scope
During the week ending January 17, 2004, the inspectors observed a training crew performance on Simulator Exercise Guide (SEG) 2004C1-01 for a total of one sample.
The scenario included a loss of uninterruptible power supply and an Anticipated Transient Without Scram (ATWS). The inspectors used the documents listed in the to accomplish the objectives of the inspection procedure. The inspection assessed the licensees effectiveness in evaluating the requalification program, ensuring that licensed individuals operate the facility safely and within the conditions of their license, and evaluated licensed operator mastery of high-risk operator actions. The inspection activities included, but were not limited to, a review of high risk activities, emergency plan performance, incorporation of lessons learned, clarity and formality of communications, task prioritization, timeliness of actions, alarm response actions, control board operations, procedural adequacy and implementation, supervisory oversight, group dynamics, interpretations of technical specifications, simulator fidelity, and licensee critique of performance.
The crew performance was compared to licensee management expectations and guidelines as presented in the following documents:
- Administrative Control Procedure (ACP) 110.1, Conduct of Operations, Revision 1;
- ACP 101.01, Procedure Use and Adherence, Revision 24; and
- ACP 101.2, Verification Process and SELF/PEER Checking Practices, Revision 5.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors reviewed three systems to assess maintenance effectiveness. The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure. The inspectors reviewed areas to assess maintenance effectiveness, including maintenance rule activities, work practices, and common cause issues. Inspection activities included, but were not limited to, the licensee's categorization of specific issues including evaluation of performance criteria, appropriate work practices, identification of common cause errors, extent of condition, and trending of key parameters. Additionally, the inspectors reviewed implementation of the Maintenance Rule (10 CFR 50.65) requirements, including a review of scoping, goal-setting, performance monitoring, short-term and long-term corrective actions, functional failure determinations associated with reviewed condition reports, and current equipment performance status.
The inspectors performed the following maintenance effectiveness reviews for a total of three samples:
C a function-oriented review of the Control Rod Drive (CRD) system because it was designated as risk-significant under the Maintenance Rule, during the week ending January 31, 2004; C a function-oriented review of the Standby Liquid Control (SBLC) system because it was designated as risk-significant under the Maintenance Rule, during the week ending February 7, 2004; and C a function-oriented review of the Instrument Air system because it was designated as risk-significant under the Maintenance Rule, during the week ending March 20, 2004.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors reviewed the licensees evaluation of plant risk, scheduling, and configuration control. The inspectors also evaluated the performance of maintenance associated with planned and emergent work activities to determine if they were adequately managed. In particular, the inspectors reviewed the program for conducting maintenance risk safety assessments and to ensure that the planning, assessment and management of on-line risk was adequate. The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure. The inspectors also reviewed that actions to address increased on-line risk during these periods, such as establishing compensatory actions, minimizing the duration of the activity, obtaining appropriate management approval, and informing appropriate plant staff, were accomplished when on-line risk was increased due to maintenance on risk-significant structures, systems, and components (SSCs).
The following activities were reviewed for a total of seven samples:
- The inspectors reviewed the maintenance risk assessment for work planned during the weeks of January 17, January 31, February 14, February 21, March 13, March 20, and March 27, 2004.
b. Findings
No findings of significance were identified.
1R14 Personnel Performance During Non-Routine Plant Evolutions and Events
.1 Control Rod Sequence Exchange
a. Inspection Scope
During the week of February 28, 2004, the inspectors observed portions of the licensees planned power reduction and various surveillance test procedures. The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure. The inspectors observed operator performance in the control room during portions of both the power reduction and subsequent power escalation. In addition, the inspectors observed the performance of area inspections associated with the steam lines and the surveillance testing associated with the main steam isolation valves and main turbine control system.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations
a. Inspection Scope
The inspectors reviewed five of the licensees operability evaluations of degraded or non-conforming systems. The inspectors used the documents listed in the to accomplish the objectives of the inspection procedure. The inspectors reviewed operability evaluations affecting mitigating systems or barrier integrity to ensure that operability was properly justified and that the component or system remained available. The inspection activities included, but were not limited to, a review of the technical adequacy of the evaluation against the TSs, UFSAR, and other design information; determined whether compensatory measures, if needed, were taken; and determined whether the evaluations were consistent with the requirements of ACP-114.5, Action Request System.
The inspectors reviewed the following operability evaluations for a total of five samples:
- Operability Evaluation (OPR) 000252, Reactor Core Isolation Cooling, during the week ending January 31, 2004;
- OPR 000251, Control Rods, during the week ending January 31, 2004;
- OPR 000254, River Water Supply (RWS) System, during the week ending February 14, 2004;
- OPR 000253, Intermediate Range Monitor (IRM), during the week ending February 21, 2004; and
- OPR 000255, RHRSW 1P022A-M Upper Thrust Motor Bearing was Observed to be 2/3 Below Indicated Stand, during the week ending February 28, 2004.
b. Findings
Introduction The inspectors identified a finding of very low safety significance (Green) and an associated NCV of 10 CFR 50, Appendix B, Criterion III, Design Control, for the failure to ensure proper design control was maintained when the RHRSW/Emergency Service Water (ESW) pit Level-Indicating Switches (LISs) were downgraded to non safety-related components, thereby cross connecting a safety-related and a non safety-related circuit without the required isolation point.
Description During the week ending February 14, 2004, the inspectors identified that the licensee failed to ensure proper design control was maintained, when RHRSW/ESW pit LIS4935A and LIS4935B were downgraded from safety-related to non safety-related components. The LISs cause solenoid valves (SV) 4934 and SV4935 in the RWS to de-energize when the level in the RHRSW/ESW pits drops to approximately 20 feet.
When the SVs de-energize, the RWS make-up control valve (CV) 4914 and CV4915 go to the fail-safe open position, thereby providing a make-up water flow path from the RWS to the RHRSW/ESW pits. The RWS make-up CVs are safety-related components.
Electrical design requirements in the Institute of Electrical and Electronic Engineers (IEEE) 308 standards require isolation points between safety-related and non safety-related circuits. IEEE 308 states that an electrical isolation point will be provided to maintain the independence of Class 1E circuits and equipment so that the safety functions required during and following any design basis event can be accomplished.
This is especially important during a failure in the non safety-related circuit so that the integrity of the safety-related circuit is maintained.
The safety-related circuit of the RWS make-up CVs was cross-connected to the non safety-related circuit of the LISs, when the LISs were downgraded without the required isolation point as described in the IEEE 308. The failure to provide an isolation point in accordance with IEEE 308 standards, when the LISs were downgraded was an example of inadequate design control. The inspectors determined that although design control was not maintained when LISs were downgraded, there was a safety-related hand switch that will cause the RWS make-up CVs to open. Therefore, this finding was determined to be of very low safety significance.
Analysis The inspectors determined that the failure to ensure proper design control was maintained, when the LISs were downgraded, is a performance deficiency. Since a performance deficiency existed, the inspectors reviewed this issue against the guidance contained in Appendix B, Issue Screening, of IMC 0612, Power Reactor Inspection Reports. The inspectors compared this finding to the example findings in Appendix E, Examples of Minor Issues, of IMC 0612 to determine whether the finding was more than minor. Following that review, the inspectors concluded that the guidance in Appendix E was not applicable for the specific finding. The inspectors determined that the finding was more than minor because the failure to ensure proper design control in RWS make-up CVs has the potential to impact safety and affects the equipment performance attribute of the Mitigating Systems cornerstone. The finding potentially affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.
As a result, the inspectors reviewed this issue in accordance with IMC 0609, A, Significance Determination of Reactor Findings for At-Power Situation, using the worksheet for the Mitigating Systems cornerstone. Since the finding did not result in a loss of function per GL 91-18, the finding screened as Green.
Enforcement 10 CFR 50, Appendix B, Criterion III, Design Control, requires, in part, that design changes, including field changes, are subject to the design control measures commensurate with the original design. When the LISs were downgraded in 1992 to non safety-related components, the non safety-related circuits of the LISs and the safety-related circuits of the RWS make-up CVs were cross-connected. Design specifications standards in IEEE 308 require an isolation point between safety-related and non safety-related circuits to ensure that the safety-related circuit is independent and can perform its safety function. The failure to provide the required isolation point potentially impacted the reliability and capability of the RWS, which is an Appendix B system, to provide make-up water to the RHRSW/ESW pits. The failure to provide the required isolation point is an example where the requirements of 10 CFR 50, Appendix B, Criterion III, were not met and was a violation; however, because of its very low safety significance and because it was entered into the corrective action program, the NRC is treating this issue as an NCV 5000331/2004002-02, in accordance with Section VI.A.1 of the NRCs Enforcement Policy. This issue was entered into the licensees corrective action program as CAP030637.
Corrective actions taken included the rededication of the LISs as safety-related components.
1R16 Operator Workarounds
a. Inspection Scope
The inspectors reviewed two operator workarounds (OWAs). The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure. The inspectors verified that the selected OWA did not impact the functionality of a mitigating system. The inspection activities included, but were not limited to, a review of the selected OWAs to determine if the functional capability of the system or human reliability in responding to an initiating event was affected, including a review of the impact of the OWAs on the operators ability to execute EOPs.
The inspectors reviewed the following OWAs for a total of two samples:
- CAP030184, Pressure Safety Valve 4401 Temperature Trends from Temperature Elements 4401 and 4401A, during the week ending March 6, 2004; and
- OWA 04-004, Control Building Chiller Reliability, during the week ending March 27, 2004.
b. Findings
No findings of significance were identified.
1R17 Permanent Plant Modifications
a. Inspection Scope
The inspectors reviewed one permanent plant modification. The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure. The inspectors focused on verification that the design basis, licensing basis, and performance capability of related SSCs were not degraded by the installation of the modification. The inspectors also verified that the modifications did not place the plant in an unsafe configuration. The inspection activities included, but were not limited to, a review of the design adequacy of the modification by performing a review, or partial review, of the modifications impact on plant electrical requirements, material requirements and replacement components, response time, control signals, equipment protection, operation, failure modes, and other related process requirements.
The inspectors selected the following permanent plant modification for review for a total of one sample:
- Work Order 1126796, to Modify Control Circuit for TS7538C Such That SV7539A Will Open Automatically at 105F and Circuit Operation Will Match Original Design, during the week of January 31, 2004.
b. Findings
No findings of significance were identified.
1R19 Post-Maintenance Testing
a. Inspection Scope
The inspectors reviewed nine post-maintenance testing activities. The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure. The inspectors verified that the post-maintenance test procedures and activities were adequate to ensure system operability and functional capability. Activities were selected based upon the structure, system, or component's ability to impact risk.
The inspection activities included, but were not limited to, witnessing or reviewing the integration of testing activities, applicability of acceptance criteria, test equipment calibration and control, procedural use and compliance, control of temporary modifications or jumpers required for test performance, documentation of test data, system restoration, and evaluation of test data. Also, the inspectors verified that maintenance and post-maintenance testing activities adequately ensured that the equipment met the licensing basis, TS, and UFSAR design requirements.
The inspectors selected the following post-maintenance testing activities for review for a total of nine samples:
- Corrective Work Order (CWO) A63690 on the A Control Building Chiller during the week ending January 30, 2004;
- CWO A65764 on the RCIC system during the week ending February 21, 2004;
- CWO 11291159 on the A General Service Water (GSW) Pump during the week ending February 28, 2004;
- PWO 1125621 on the A SBLC Pump, during the week ending March 6, 2004;
- CWO A60005 on the HPCI Pump Mechanical Seals during the week ending March 13, 2004;
- CWO A63477 on the HPCI Seal Water system during the week ending March 13, 2004;
- CWO A67214 on the Diesel Fire Pump during the week ending March 20, 2004;
- PWO 1126361 on the B Core Spray Pump during the week ending March 27, 2004; and
- CWO 1126683 on the HPCI Room Cooling Unit during the week ending March 27, 2004.
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors reviewed nine surveillance test activities. The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure. The inspectors reviewed surveillance testing activities to assess operational readiness and ensure that risk-significant SSCs were capable of performing their intended safety function. Activities were selected based upon risk significance and the potential risk impact from an unidentified deficiency or performance degradation that a system, structure, or component could impose on the unit if the condition were left unresolved. The inspection activities included, but were not limited to, a review for preconditioning, integration of testing activities, applicability of acceptance criteria, test equipment calibration and control, procedural use, control of temporary modifications or jumpers required for test performance, documentation of test data, TS applicability, impact of testing relative to Performance Indicator (PI) reporting, and evaluation of test data.
The inspectors selected the following surveillance testing activities for review for a total of nine samples:
- Surveillance Test Procedure (STP) 3.3.5.1-04, Functional Test of Reactor Vessel Shroud Level - Low Instrumentation, during the week ending January 24, 2004;
- STP 3.8.4-06, Battery Charger Capacity Test, during the week ending February 7, 2004;
- STP 3.7.4-02, Main Control Room Ventilation Standby Filter Unit Test, during the week ending February 7, 2004;
- STP 3.7.2-01, RWS Simulated Automatic Actuation Test, during the week ending February 7, 2004;
- STP 3.8.1-04, A Standby Diesel Generators Operability Test, during the week ending February 14, 2004;
- STP 3.5.1-04, Low Pressure Coolant Injection (LPCI) Simulated Automatic Actuation Test, during the week ending February 14, 2004;
- STP 3.3.6.1-14, Reactor Water Cleanup Isolation Logic, during the week ending March 6, 2004;
- STP 3.8.1-06, B Standby Diesel Generators Operability Test (Fast Start), during the week ending March 20, 2004; and
b. Findings
No findings of significance were identified.
1R23 Temporary Plant Modifications
a. Inspection Scope
The inspectors reviewed two temporary modifications. The inspectors used the documents listed in the Attachment to accomplish the objectives of the inspection procedure. The inspectors reviewed the temporary modifications to assess the safety function of the associated systems. The inspection activities included, but were not limited to, a review of design documents, safety screening documents, UFSAR, and applicable TS to determine that the temporary modification was consistent with modification documents, drawings and procedures. The inspectors also reviewed the post-installation test results to confirm that tests were satisfactory and the actual impact of the temporary modification on the permanent system and interfacing systems were adequately verified.
The inspectors selected the following temporary modifications for review for a total of two samples:
- Temporary Modification 04-014, Valve V38-0052 Will Be Open for Maintenance and this Valve is Connected to a Vent Which Vents Through Secondary Containment, during the week ending February 28, 2004; and
- Temporary Modification 04-21, Pressurize the Core Spray System with Demin Water per OI 151, Section 9.2, during the week ending March 27, 2004.
b. Findings
No findings of significance were identified.
1EP4 Emergency Action Level and Emergency Plan Changes
a. Inspection Scope
In February 2004, the licensee submitted revisions to portions of the Emergency Plan.
The inspectors reviewed the following revisions to determine if changes identified in these revisions reduced the Plans effectiveness, pending on-site inspection of the implementation of these changes:
- Revision 26 to Section B; and
- Revision 21 to Sections C, I, N, and Appendix 2.
b. Findings
No findings of significance were identified.
1EP6 Drill Evaluation
a. Inspection Scope
On January 14, 2004, the inspectors observed an Emergency Preparedness (EP) drill for a total of one sample. The drill simulated a failure of the breaker for the B ESW pump, resulting in a fire in the 1A4 Essential Switchgear Room. The drill also simulated a reactor recirculation system leak and an ATWS. The inspectors evaluated the licensees drill conduct and the adequacy of the post-drill performance critique to identify weaknesses and deficiencies. The inspectors used the documents listed in the to accomplish the objectives of the inspection procedure. The inspectors selected exercises that the licensee had scheduled as providing input to the Drill/Exercise PI. The inspection activities included, but were not limited to, the classification of events, notifications to off-site agencies, protective action recommendation development, and drill critiques. Observations were compared with the licensees observations and corrective action program entries. The inspectors verified that there were no discrepancies between observed performance and reported PI statistics.
b. Findings
No findings of significance were identified.
2. Radiation Safety
Cornerstone: Occupational Radiation Safety
2OS1 Access Control to Radiologically Significant Areas (71121.01)
.1 Review of Licensee Performance Indicators for the Occupational Exposure Cornerstone
a. Inspection Scope
The inspectors reviewed the licensees occupational exposure control cornerstone PI to determine whether or not the conditions surrounding the PI had been evaluated, and identified problems had been entered into the corrective action program for resolution.
This review represented one sample.
b. Findings
No findings of significance were identified.
.2 Plant Walkdowns and Radiation Work Permit (RWP) Reviews
a. Inspection Scope
The inspectors reviewed licensee controls and surveys in the following three radiologically significant work areas within radiation areas, high radiation areas and airborne radioactivity areas in the plant, and reviewed work packages which included associated licensee controls and surveys of these areas to determine if radiological controls including surveys, postings and barricades were acceptable:
- Build and Move Scaffold for MO2723 Inspect and Lube;
- Control Valve (CV) 3754 Operator Work; and
- Vent HPCI Suction.
The inspectors reviewed the RWPs and work packages used to access these three areas and other high radiation work areas to identify the work control instructions and control barriers that had been specified. Electronic dosimeter alarm set points for both integrated dose and dose rate were evaluated for conformity with survey indications and plant policy. Workers were interviewed to verify that they were aware of the actions required when their electronic dosimeters noticeably malfunctioned or alarmed.
The inspectors walked down and surveyed (using an NRC survey meter) one of these three areas to verify that the prescribed RWP, procedure, and engineering controls were in place, that licensee surveys and postings were complete and accurate, and that air samplers were properly located. This review represented three samples.
b. Findings
No findings of significance were identified.
.3 Problem Identification and Resolution
a. Inspection Scope
The inspectors reviewed the licensees self-assessments, audits, Licensee Event Reports (LERs), and Special Reports related to the access control program to verify that identified problems were entered into the corrective action program for resolution.
The inspectors reviewed 15 CAPs related to access controls and high radiation area radiological incidents (non-PIs identified by the licensee in high radiation areas <1R/hr).
Staff members were interviewed and corrective action documents were reviewed to verify that follow-up activities were being conducted in an effective and timely manner commensurate with their importance to safety and risk based on the following:
Initial problem identification, characterization, and tracking;
Disposition of operability/reportability issues;
Evaluation of safety significance/risk and priority for resolution;
Identification of repetitive problems;
Identification of contributing causes;
6. Identification and implementation of effective corrective actions;
Resolution of NCVs tracked in the corrective action system; and
Implementation/consideration of risk significant operational experience feedback.
The inspectors evaluated the licensees process for problem identification, characterization, prioritization, and verified that problems were entered into the corrective action program and resolved. For repetitive deficiencies and/or significant individual deficiencies in problem identification and resolution, the inspectors verified that the licensees self-assessment activities were capable of identifying and addressing these deficiencies.
The inspectors reviewed licensee documentation packages for all PI events occurring since the last inspection to determine if any of these PI events involved dose rates
>25 R/hr at 30 centimeters or >500 R/hr at 1 meter. Barriers were evaluated for failure and to determine if there were any barriers left to prevent personnel access.
Unintended exposures >100 millirem total effective dose equivalent (or >5 rem shallow dose equivalent or >1.5 rem lens dose equivalent), were evaluated to determine if there were any regulatory overexposures or if there was a substantial potential for an overexposure. This review represented four samples.
b. Findings
No findings of significance were identified.
.4 Job-In-Progress Reviews
a. Inspection Scope
The inspectors observed the following two jobs that were being performed in radiation areas, airborne radioactivity areas, or high radiation areas for observation of work activities that presented the greatest radiological risk to workers:
- CV 3754 Operator Work; and
- Vent HPCI Suction.
The inspectors reviewed radiological job requirements for these two activities including RWP requirements and work procedure requirements.
Job performance was observed with respect to these requirements to verify that radiological conditions in the work area were adequately communicated to workers through pre-job briefings and postings. The inspectors also verified the adequacy of radiological controls including required radiation, contamination, and airborne surveys for system breaches; radiation protection job coverage which included audio and visual surveillance for remote job coverage; and contamination controls.
Radiological work in high radiation work areas having significant dose rate gradients was reviewed to evaluate the application of dosimetry to effectively monitor exposure to personnel and to verify that licensee controls were adequate. These work areas involved areas where the dose rate gradients were severe (diving activities and the Reactor Water Clean-Up (RWCU) Heat Exchanger Room) which increased the necessity of providing multiple dosimeters and/or enhanced job controls. This review represented three samples.
b. Findings
No findings of significance were identified.
.5 High Risk Significant, High Dose Rate High Radiation Area (HRA) and Very High
Radiation Area (VHRA) Controls
a. Inspection Scope
The inspectors held discussions with the Radiation Protection Manager concerning high dose rate/high radiation area and very high radiation area controls and procedures, including procedural changes that had occurred since the last inspection, in order to verify that any procedure modifications did not substantially reduce the effectiveness and level of worker protection.
The inspectors conducted plant walkdowns to verify the posting and locking of entrances to high dose rate HRAs and VHRAs. This review represented two samples.
b. Findings
No findings of significance were identified
.6 Radiation Worker Performance
a. Inspection Scope
During job performance observations, the inspectors evaluated radiation worker performance with respect to stated radiation protection work requirements and evaluated whether workers were aware of the significant radiological conditions in their workplace, the RWP controls and limits in place, and that their performance had accounted for the level of radiological hazards present.
The inspectors reviewed radiological problem reports which found that the cause of the event was due to radiation worker errors to determine if there was an observable pattern traceable to a similar cause, and to determine if this perspective matched the corrective action approach taken by the licensee to resolve the reported problems. These problems, along with planned and taken corrective actions were discussed with the Radiation Protection Manager. This review represented two samples.
b. Findings
No findings of significance were identified.
.7 Radiation Protection Technician (RPT) Proficiency
a. Inspection Scope
During job performance observations, the inspectors evaluated RPT performance with respect to radiation protection work requirements and evaluated whether they were aware of the radiological conditions in their workplace, the RWP controls and limits in place, and if their performance was consistent with their training and qualifications with respect to the radiological hazards and work activities.
The inspectors reviewed eleven radiological CAPs associated with RPT errors, to determine if there was an observable pattern traceable to a similar cause, and to determine if this perspective matched the corrective action approach taken by the licensee to resolve the reported problems. This review represented two samples.
b. Findings
No findings of significance were identified.
2OS2 As Low As Is Reasonably Achievable Planning And Controls (ALARA) (71121.02)
.1 Inspection Planning
a. Inspection Scope
The inspectors reviewed plant collective exposure history, current exposure trends, ongoing and planned activities in order to assess current performance and exposure challenges. This included determining the plants current 3-year rolling average for collective exposure in order to help establish resource allocations and to provide a perspective of significance for any resulting inspection finding assessment. The inspectors determined site specific trends in collective exposures and source-term measurements. The inspectors reviewed procedures associated with maintaining occupational exposures ALARA and processes used to estimate and track work activity specific exposures. This review represented three samples.
b. Findings
No findings of significance were identified.
.2 Radiological Work Planning
a. Inspection Scope
The inspectors evaluated the licensees list of work activities ranked by estimated exposure that were in progress and reviewed the following five work activities of highest exposure significance:
- V23-0009 Replace Stem and Disc;
- Build and Move Scaffold for MO2723 Inspect and Lube;
- CV 3754 Operator Work;
- Replace 1P211B Core Spray Pump Seal; and
- Vent HPCI Suction.
For these five activities, the inspectors reviewed the ALARA work activity evaluations, exposure estimates, and exposure mitigation requirements in order to verify that the licensee had established procedures, and engineering and work controls that were based on sound radiation protection principles in order to achieve occupational exposures that were ALARA. This also involved determining that the licensee had reasonably grouped the radiological work into work activities, based on historical precedence, industry norms, and/or special circumstances.
The inspectors compared the results achieved including dose rate reductions and person-rem used with the intended dose established in the licensees ALARA planning for these five work activities. Reasons for inconsistencies between intended and actual work activity doses were reviewed. This review represented three samples.
b. Findings
No findings of significance were identified.
.3 Verification of Dose Estimates and Exposure Tracking Systems
a. Inspection Scope
The inspectors reviewed the assumptions and bases for the current annual collective exposure estimate including procedures, in order to evaluate the licensees methodology for estimating work activity-specific exposures and the intended dose outcome. Dose rate and man-hour estimates were evaluated for reasonable accuracy.
The licensees process for adjusting exposure estimates or re-planning work, when unexpected changes in scope, emergent work or higher than anticipated radiation levels were encountered, was evaluated. This included determining that adjustments to estimated exposure (intended dose) were based on sound radiation protection and ALARA principles and not adjusted to account for failures to control the work. The frequency of these adjustments was reviewed to evaluate the adequacy of the original ALARA planning process.
The licensees exposure tracking system was evaluated to determine whether the level of exposure tracking detail, exposure report timeliness, and exposure report distribution was sufficient to support control of collective exposures. RWPs were reviewed to determine if they covered too many work activities to allow work activity specific exposure trends to be detected and controlled. During the conduct of exposure significant work, the inspectors evaluated if licensee management was aware of the exposure status of the work and would intervene if exposure trends increased beyond exposure estimates. This review represented two samples.
b. Findings
No findings of significance were identified.
.4 Job Site Inspections and ALARA Control
a. Inspection Scope
The inspectors observed the following five jobs that were being performed in radiation areas, airborne radioactivity areas, or HRAs for observation of work activities that presented the greatest radiological risk to workers:
- V23-0009 Replace Stem and Disc;
- Build and Move Scaffold for MO2723 Inspect and Lube;
- CV 3754 Operator Work;
- Replace 1P211B Core Spray Pump Seal; and
- Vent HPCI Suction.
The licensees use of ALARA controls for these work activities was evaluated using the following:
The licensees use of engineering controls to achieve dose reductions was evaluated to verify that procedures and controls were consistent with the licensees ALARA reviews, that sufficient shielding of radiation sources was provided for and that the dose expended to install/remove the shielding did not exceed the dose reduction benefits afforded by the shielding. This review represented one sample.
b. Findings
No findings of significance were identified.
.5 Source-Term Reduction and Control
a. Inspection Scope
The inspectors reviewed licensee records to determine the historical trends and current status of tracked plant source terms and determined that the licensee was making allowances and had developing contingency plans for expected changes in the source term due to changes in plant fuel performance issues or changes in plant primary chemistry. This review represented one sample.
b. Findings
No findings of significance were identified.
.6 Radiation Worker Performance
a. Inspection Scope
Radiation worker and RPT performance was observed during work activities being performed in radiation areas, airborne radioactivity areas, and HRAs that presented the greatest radiological risk to workers. The inspectors evaluated whether workers demonstrated the ALARA philosophy in practice by being familiar with the work activity scope and tools to be used, by utilizing ALARA low dose waiting areas and that work activity controls were being complied with. Also, radiation worker training and skill levels were reviewed to determine if they were sufficient relative to the radiological hazards and the work involved. This review represented one sample.
b. Findings
No findings of significance were identified.
.7 Problem Identification and Resolution
a. Inspection Scope
The inspectors reviewed the licensees self-assessments and audits related to the ALARA program since the last inspection to determine if the overall audit programs scope and frequency for all applicable areas under the Occupational Exposure Cornerstone met the requirements of 10 CFR 20.1101(c).
The licensees corrective action program was also reviewed to determine if repetitive deficiencies and/or significant individual deficiencies in problem identification and resolution had been addressed. This review represented two samples.
b. Findings
No findings of significance were identified.
Cornerstone: Public Radiation Safety
2PS1 Radioactive Gaseous And Liquid Effluent Treatment And Monitoring Systems (71122.01)
.1 Inspection Planning
a. Inspection Scope
The inspectors reviewed the most current Radiological Effluent Release Report to verify that the program was implemented as described in the Radiological Environmental Technical Specifications/Offsite Dose Assessment Manual (RETS/ODAM) and the UFSAR. The effluent report was also evaluated to determine if there were any significant changes to the ODAM or to the radioactive waste system design and operation. The inspectors verified that any changes to the ODAM were technically justified, documented, and made in accordance with Regulatory Guide 1.109 and NUREG-0133. Modifications (if any) made to the radioactive waste system design and operation were evaluated to determine if these alterations changed the dose consequence to the public. The inspectors also verified that technical and/or 10 CFR 50.59 reviews were performed when required, and determined whether radioactive liquid and gaseous effluent radiation monitor set point calculation methodology had changed since completion of the modifications. The inspectors evaluated the effluent report for any anomalous results and verified that any such results were adequately resolved.
The RETS/ODAM and UFSAR were reviewed to identify the effluent radiation monitoring systems and associated flow measurement devices. There were no radiological effluent performance indicator occurrences for onsite follow-up. The UFSAR description of all radioactive waste systems was reviewed. This review represented one sample.
b. Findings
No findings of significance were identified.
.2 Onsite Inspection
a. Inspection Scope
The inspectors walked down the major components of the gaseous and liquid release systems, including radiation and flow monitors, demineralizers, filters, tanks, and vessels. This was done to observe current system configuration with respect to the description in the UFSAR, ongoing activities, and equipment material condition.
The inspectors observed the routine processing (including sample collection and analysis) of radioactive liquid waste to verify that appropriate treatment equipment was used and that radioactive liquid waste was processed in accordance with procedural requirements. As the licensee maintains a zero release program for liquid radioactive waste, there were no liquid effluent releases to observe or liquid effluent release packages to review, and thus no projected dose to the public from liquid releases. The inspectors observed the routine processing, sampling and release of radioactive gaseous effluent to verify that appropriate treatment equipment was used and that the radioactive gaseous effluent was processed and released in accordance with RETS/ODAM requirements. Radioactive gaseous effluent release data, including the projected doses to members of the public, was evaluated.
The inspectors reviewed any records of abnormal releases or releases made with inoperable effluent radiation monitors and reviewed the licensees actions for these types of releases to ensure an adequate defense-in-depth was maintained against an unmonitored, unanticipated release of radioactive material to the environment.
The inspectors reviewed the licensees technical justification for any changes made by the licensee to the ODAM as well as to the liquid or gaseous radioactive waste system design, procedures, or operation since the last inspection to determine whether the changes affected the licensees ability to maintain effluents ALARA and whether changes made to monitoring instrumentation resulted in a non-representative monitoring of effluents. The inspectors also reviewed the licensees offsite dose calculations and evaluated any significant changes in dose values reported in the Radiological Effluent Release Report from values in the previous report.
The inspectors reviewed a selection of monthly, quarterly, and annual dose calculations to ensure that the licensee properly calculated the offsite dose from radiological effluent releases and to determine if any annual RETS/ODAM (i.e., Appendix I to 10 CFR Part 50 values) were exceeded.
The inspectors reviewed air cleaning system surveillance test results to ensure that the system was operating within the licensees acceptance criteria. The inspectors reviewed surveillance test results (or methodology) the licensee uses to determine the stack and vent flow rates. The inspectors verified that the flow rates were consistent with RETS/ODAM or UFSAR values.
The inspectors reviewed records of instrument calibrations performed since the last inspection for each point of discharge effluent radiation monitor and flow measurement device and reviewed any completed system modifications and the current effluent radiation monitor alarm set point value for agreement with RETS/ODAM requirements.
The inspectors also reviewed calibration records of radiation measurement instrumentation associated with effluent monitoring and release activities, along with the quality control records for the radiation measurement instruments.
The inspectors reviewed the results of the inter-laboratory comparison program to verify the quality of radioactive effluent sample analyses performed by the licensee. The inspectors reviewed the licensees quality control evaluation of the inter-laboratory comparison test and associated corrective actions for any deficiencies identified. In addition, the inspectors reviewed the results from the licensees quality assurance audits to determine whether the licensee met the requirements of the RETS/ODAM. This review represented eight samples.
b. Findings
No findings of significance were identified.
.3 Identification and Resolution of Problems
a. Inspection Scope
The inspectors reviewed the licensees self assessments, audits, LERs, and Special Reports related to the radioactive effluent treatment and monitoring program since the last inspection to determine if identified problems were entered into the corrective action program for resolution. The inspectors also verified that the licensee's self-assessment program was capable of identifying repetitive deficiencies or significant individual deficiencies that were identified in problem identification and resolution.
The inspectors also reviewed corrective action reports from the radioactive effluent treatment and monitoring program since the previous inspection, interviewed staff and reviewed documents to determine if the following activities were being conducted in an effective and timely manner commensurate with their importance to safety and risk:
Initial problem identification, characterization, and tracking;
Disposition of operability/reportability issues;
Evaluation of safety significance/risk and priority for resolution;
Identification of repetitive problems;
Identification of contributing causes;
Identification and implementation of effective corrective actions;
Resolution of NCVs tracked in the corrective action system; and
Implementation/consideration of risk significant operational experience feedback.
This represented one sample.
b. Findings
No findings of significance were identified.
2PS2 Radioactive Material Processing and Transportation (71122.02)
.1 Radioactive Waste System
a. Inspection Scope
The inspectors reviewed the liquid and solid radioactive waste system description in the UFSAR for information on the types and amounts of radioactive waste generated and disposed. The inspectors reviewed the scope of the licensees audit program with regard to radioactive material processing and transportation programs to verify that it met the requirements of 10 CFR 20.1101(c). This review represented one sample.
b. Findings
No findings of significance were identified.
.2 Radioactive Waste System Walkdowns
a. Inspection Scope
The inspectors performed walkdowns of the liquid and solid radioactive waste processing systems to verify that the systems agreed with the descriptions in the UFSAR and the Process Control Program, and to assess the material condition and operability of the systems. The inspectors reviewed the status of radioactive waste process equipment that was not operational and/or was abandoned in place. The inspectors reviewed the licensees administrative and physical controls to ensure that the equipment would not contribute to an unmonitored release path or be a source of unnecessary personnel exposure.
The inspectors reviewed changes to the waste processing system to verify the changes were reviewed and documented in accordance with 10 CFR 50.59 and to assess the impact of the changes on radiation dose to members of the public. The inspectors reviewed the current processes for transferring waste resin into shipping containers to determine if appropriate waste stream mixing and/or sampling procedures were utilized.
The inspector also reviewed the methodologies for waste concentration averaging to determine if representative samples of the waste product were provided for the purposes of waste classification in 10 CFR 61.55. This review represented one sample.
b. Findings
No findings of significance were identified.
.3 Waste Characterization and Classification
a. Inspection Scope
The inspectors reviewed the licensees radiochemical sample analysis results for each of the licensees waste streams, including Dry Active Waste (DAW), spent resins and filters. The inspectors also reviewed the licensees use of scaling factors to quantify difficult-to-measure radionuclides (e.g., pure alpha- or beta-emitting radionuclides). The reviews were conducted to verify that the licensees program assured compliance with 10 CFR 61.55 and 10 CFR 61.56, as required by Appendix G of 10 CFR Part 20. The inspectors also reviewed the licensees waste characterization and classification program to ensure that the waste stream composition data accounted for changing operational parameters and thus remained valid between the annual sample analysis updates. This review represented one sample.
b. Findings
No findings of significance were identified.
.4 Shipment Preparation
a. Inspection Scope
The inspectors reviewed the training records provided to personnel responsible for the conduct of radioactive waste processing and radioactive shipment preparation activities.
The review was conducted to verify that the licensees training program provided training consistent with NRC and Department of Transportation (DOT) requirements. This review represented one sample.
b. Findings
No findings of significance were identified.
.5 Shipping Records
a. Inspection Scope
The inspectors reviewed five non-excepted package shipment manifests/documents completed in 2002/2003 to verify compliance with NRC and DOT requirements (i.e., 10 CFR Parts 20 and 71, and 49 CFR Parts 172 and 173). This review represented one sample.
b. Findings
No findings of significance were identified.
.6 Identification and Resolution of Problems
a. Inspection Scope
The inspectors reviewed CAPs and Nuclear Oversight Department observations that addressed radioactive waste and radioactive materials shipping program deficiencies since the last inspection, to verify that the licensee had effectively implemented the corrective action program and that problems were identified, characterized, prioritized and corrected. The inspectors also verified that the licensee's self-assessment program was capable of identifying repetitive deficiencies or significant individual deficiencies in problem identification and resolution.
The inspectors also reviewed corrective action reports from the radioactive material and shipping programs since the previous inspection, interviewed staff and reviewed documents to determine if the corrective measures were being conducted in an effective and timely manner commensurate with their importance to safety and risk. This review represented one sample.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
Cornerstones: Initiating Events and Mitigating Systems
.1 Reactor Safety Strategic Area
a. Inspection Scope
The inspectors reviewed recent licensee PI submittals. The inspectors used PI guidance and definitions contained in Nuclear Energy Institute Document 99-02, Revision 2, Regulatory Assessment Performance Indicator Guideline, to verify the accuracy of the PI data. As part of the inspection, the documents listed in the Appendix were used to evaluate the accuracy of PI data. The inspectors review included, but was not limited to, conditions and data from logs, LERs, CAPs, and calculations for each PI specified.
The following PIs were reviewed for a total of five samples:
- Unplanned Scrams per 7000 Critical Hours, for the period of January 2003, through December 2003, during the week of March 6, 2004;
- Unplanned Scrams with Loss of Normal Heat Removal, for the period of January 2003, through December 2003, during the week of March 6, 2004;
- Unplanned Power Changes per 7000 Critical Hours, for the period of January 2003, through December 2003, during the week of March 6, 2004;
- Safety System Unavailability for High Pressure Injection System, for the period of January 2003, through December 2003, during the week of February 28, 2004; and
- Safety System Unavailability for Heat Removal Systems, for the period of January 2003, through December 2003, during the week of February 28, 2004.
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity, and
.1 Routine Review of Identification and Resolution of Problems
a. Inspection Scope
For inspections performed and documented in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Minor issues entered into the corrective action program as a result of the inspectors observations are included in the attached list of documents reviewed.
b. Findings
No findings of significance were identified.
.2 Risk Assessment and Management
Introduction The inspectors have identified several issues in the area of risk assessment and risk management over the past 18 months. Two of the issues have resulted in NCVs of 10 CFR 50.65(a)(4) for failures to perform adequate risk assessments. The NCVs were described in inspection reports 5000331/2002006 and 5000331/2003008. These issues have resulted in various corrective actions being taken.
The inspectors selected the following CAPs for review:
Action Request (AR) 32344, Actual Plant Overall Risk was Yellow, August 29, 2002; CAP 27704, Unavailability of Inverter not included in Risk Review, June 3, 2003; CAP 29259, Missed Risk Analysis for C Torus to Drywell Vacuum Breaker, October 3, 2003; CAP 29394, Risk Assessment, October 14, 2003; and CAP 29421, ORAM/SENTINEL review not performed, October 16, 2003.
a.
Effectiveness of Corrective Actions
- (1) Inspection Scope The inspectors reviewed multiple related CAPs to determine if they addressed generic implications and that corrective actions were appropriately focused to correct the problem.
- (2) Issues Corrective actions related to each CAP appeared to be adequate to ensure that specific issue was appropriately addressed. Corrective actions taken for the August 29, 2002, issue included changing the on-line risk assessment process to require the Shift Technical Advisor to perform real-time risk assessments as system equipment availability changes. Additionally, these risk assessments are now documented on a new worksheet which provides appropriate risk assessment guidelines. Corrective actions taken for the June 3, 2003, issue included changes in the plants risk model, which resulted in improvements to the overall plant risk evaluation. The inspectors noted that changes made by the licensee focused on improving the risk assessment process.
On October 3, 2003, the inspectors observed that the Control Room staff had considered the overall plant risk condition as Green, although problems with the C torus-drywell vacuum breaker resulted in it being considered unavailable. The Control Room staff performed an on-line risk assessment using ORAM/SENTINEL, after being prompted by the inspectors. ORAM/SENTINEL calculated the overall risk condition as Red with a core damage frequency of 9.412 x 10-6 . The Red risk profile was due to the Safety Function Assessment Tree parameter which considered the unavailable vacuum breaker as a degradation to containment integrity. An overall Red risk condition requires appropriate risk management activities to be performed to ensure that redundant systems remain available. Since the evaluation was not performed, the associated risk management activities were also not performed.
An overall assessment of the plants risk conditions was performed by the licensees risk assessment engineers and the assessment determined that the risk condition was actually Green since the vacuum breaker was failed in the closed position, maintaining containment integrity. However, the model in ORAM/SENTINEL had considered the vacuum breaker as failed open. Corrective actions included placing risk assessment activities in the work order and equipment tagging process. The licensee also conducted additional training for Operations Department staff on the ORAM/SENTINEL and risk model program.
The cumulative effect of the corrective actions associated with evaluations and management of risk have decreased the number of NRC-identified problems with the licensees on-line risk assessment and management.
.3 Measurement and Test Equipment (M&TE) Management
Introduction The inspectors identified that timely corrective actions associated with the evaluation of failed M&TE utilized to calibrate the IRMs in March 2003 were not performed. The M&TE had failed its periodic calibration in October 2003, but no corrective actions were taken by the licensee until February 2004, even though the plant had gone through four forced outages during November 2003 where the IRMs were considered operable and utilized for plant startup. Guidance for the M&TE program is listed in ACP 1408.8, Control of Measuring and Test Equipment. The procedure states, in part, that out-of-tolerance conditions and use history evaluations will be performed in a timely manner. In this particular case the evaluations were not timely, since the evaluations were not performed prior to relying on the IRMs in Mode Two (Startup) operations and also not within the standard 30 days. The licensees review of the failed test equipment utilized in the calibration of the IRMs was determined not to have produced significant offsets in the display meters since only a one percent error in the calibrated power supply was identified, therefore instrument overlaps were provided. In addition, the trip circuit was not affected in the calibration. Proper instrument overlaps and trip settings provided by the IRMs ensure plant safety. The process of ensuring that M&TE is fully functional and capable of performing its intended function is critical to the safe operation of the plant. Part of that process is confirming that the associated calibration equipment for M&TE remains capable of being used as a valid standard. When a problem is found with the calibration equipment, an associated evaluation must be performed in a timely manner to ensure the plant is operated safely. Based on this issue, the inspectors reviewed additional out-of-tolerance evaluations to ensure appropriate resolution timeliness.
The inspectors selected the following CAPs for review:
CAP 27165, As found out of tolerance for P641, April 24, 2003; CAP 27168, As found out of tolerance for Q560, April 24, 2003; CAP 29594, M&TE V121 was found out of tolerance, October 30, 2003; CAP 29062, M&TE Q589 was found out of tolerance, September 17, 2003; and CAP 29061, M&TE A019 was found out of tolerance, September 17, 2003.
a.
Effectiveness of Corrective Actions
- (1) Inspection Scope The inspectors reviewed multiple related CAPs to determine if the condition reports addressed generic implications and that corrective actions were appropriately focused to correct the problem and performed in a timely manner.
- (2) Issues Corrective actions related to each CAP appeared to be adequate to ensure that issue was appropriately addressed. When the piece of test equipment failed, a corrective action document was written. The document resulted in a condition evaluation being performed to evaluate the use history of the equipment. Work orders were written to have data or measurements re-performed to ensure compliance, when necessary.
The inspectors did identify documentation deficiencies associated with the metrology laboratory quality records. Records did not contain all of the required information on the data sheets. The ability to verify the actual trail of the corrective action documents that performed the evaluation for the failure of the individual test equipment was not always available on the associated data sheet. The missing information was able to be obtained through additional sources such as the corrective action program. Licensee management is performing an overall assessment of the program based on issues raised by the inspectors.
4OA3 Event Follow-up
.1 (Closed) LER 050000331/2003-005-0: Unplanned Manual Reactor Scram due to High
Reactor Coolant Conductivity.
a. Inspection Scope
The inspectors evaluated LER 050000331/2003-005-0: Unplanned Manual Reactor Scram due to High Reactor Coolant Conductivity.
b. Findings
Introduction A finding of very low safety significance (Green) was identified due to the failure of the licensee to ensure that the E condensate demineralizer was properly reassembled following maintenance. This was identified through a self-revealing event.
Description On November 7, 2003, a manual reactor scram was inserted due to increasing reactor water conductivity. The licensee conducted extensive evaluations to determine why reactor water conductivity increased and concluded that the cause was attributed to a resin intrusion. Troubleshooting activities were then performed to determine how the resin intrusion occurred. During the troubleshooting, the licensee determined that deficiencies with the E condensate demineralizer had allowed resin leakage into the reactor vessel. Several deficiencies were identified with the E demineralizer. It had one septum that was disengaged from the quick-disconnect fitting, two septa that were loose with leak paths from the bottom seals, and 72 septa of incorrect length. The deficiencies occurred during the septum replacement and subsequent reassembly of the E condensate demineralizer, which was performed on November 6, 2003.
The licensee also performed root cause evaluation (RCE) 001016 for the resin intrusion.
Three overall root causes were identified as part of that RCE. They were that the critical characteristics to ensure that the septa function were maintained were not identified, post maintenance testing did not identify the failure mode, and maintenance personnel did not demonstrate a questioning attitude during the assembly of the condensate demineralizer. All three causes demonstrate the failure to ensure that the E condensate demineralizer was properly reassembled following the septa replacement.
The failure to ensure that the demineralizer was properly reassembled is a performance deficiency that caused resin leakage which resulted in a reactor scram. This finding was determined to be of very low safety significance, since it did not impact any mitigating systems capability.
Analysis The inspectors determined that a performance deficiency existed, because the E condensate demineralizer was not properly reassembled following maintenance, thereby allowing a resin intrusion to occur. Since there was a performance deficiency, the inspectors reviewed this finding against the guidance contained in Appendix B, Issue Screening, of IMC 0612, Power Reactor Inspection Reports. The inspectors concluded that the guidance in Appendix E, Examples of Minor Issues, of IMC 0612 was not applicable or useful for the specific finding. The inspectors determined that the finding was more than minor, since it had an actual impact on safety and resulted in a reactor scram.
The inspectors reviewed this finding in accordance with IMC 0609, Attachment A, Significance Determination of Reactor Findings for At-Power Situations, using the Initiating Events worksheet. Since the finding did not contribute to the likelihood of a primary or secondary Loss of Coolant Accident (LOCA), affect mitigating equipment, or increase the likelihood of a fire or flood, it therefore screened as Green.
Enforcement The inspectors determined that no violations of NRC requirements occurred during the evaluation of the resin intrusion from the E condensate demineralizer or the resultant reactor scram on November 7, 2003. This determination was based on the fact that the condensate demineralizer is not classified as a safety-related SSC. The licensee entered this into the corrective action program as CAP 29719. (FIN 5000331/2004002-05)
Corrective actions taken included repairs to the E condensate demineralizer, revisions to the procedure for the purchase and inspection of septa, and revisions to the procedure for returning the demineralizers to service.
.2 (Closed) LER 050000331/2003-006-0: Unplanned Manual Reactor Scram due to
Degrading Condenser Vacuum.
On November 25, 2003, a manual reactor scram was inserted due to a degrading condenser vacuum. Extensive testing and evaluations conducted by the licensee determined the cause of the degrading vacuum was excessive air in-leakage due to a failed welded seam between the high pressure condenser and the crossover loop seal.
Corrective actions included replacing the failed weld and its companion weld in the low pressure condenser with full penetration welds. Other condenser welds on the sides and bottom of the loop seal were evaluated and determined to be acceptable. The safety significance of this event was minimal, since the condenser remained available for heat removal throughout the event and the availability of other mitigating systems was not affected. The LER was reviewed by the inspectors and no findings of significance were identified. The licensee documented the issue in CAP 030391.
4OA5 Other Activities
.1 (Closed) Unresolved Item (URI) 050000331/2003-008-03: Operation of the Drywell
Cooler Motor Operated Valves (MOVs) Under Reduced Voltage.
This URI was originally opened because additional information on the safety function of the drywell coolers MOVs was needed. The inspectors reviewed the list of drywell coolers MOVs against the criteria contained in GL 89-10, Safety-Related Motor-Operated Valve Testing and Surveillance, and licensee document MOV 2.1, GL 89-10 MOV Program Scope. Using these criteria, the inspectors determined that drywell coolers MOVs are not classified as safety-related, and thus are not within the scope of GL 89-10. Therefore this URI was closed.
.2 Spent Fuel Material Control and Accounting At Nuclear Power Plants (TI [Temporary
Instruction] 2515/154)
a. Inspection Scope
The inspectors interviewed the licensees Special Nuclear Material (SNM) custodian using the questions in TI 2515/154 as a guideline. The inspectors reviewed licensee procedures governing the movement and accounting of SNM, and verified the procedures were adequate for the relevant task, approved at an appropriate management level, and controlled in accordance with the licensees document control policy. The inspectors reviewed inventory records for SNM as well as non-fuel items stored in the spent fuel pool. The inspectors noted the adequate segregation of spent fuel assemblies and non-fuel items in the spent fuel pool. The inspectors verified that licensee staff was cognizant of regulatory guidance for completing Nuclear Material Transaction Reports (NRC Form 741) and Nuclear Material Balance Reports (NRC Form 742), and that samples of completed reports were accurate and in accordance with the guidance. Lastly, the inspectors verified that software used to generate past and present inventories were controlled at the appropriate level, and subject to quality assurance requirements. Documents reviewed as part of this TI are listed in the
. This TI was not a part of the baseline inspection program and was therefore not considered a sample. Phases I and II of the TI are considered complete for the licensee.
b. Findings
No findings of significance were identified.
4OA6 Meetings
.1 Exit Meeting
The inspectors presented the inspection results to Mr. M. Peifer and other members of licensee management on April 5, 2004. The licensee acknowledged the findings presented. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
.2 Interim Exit Meetings
An interim exit was conducted for:
- Emergency Preparedness inspection with Mr. P. Sullivan on March 3, 2004;
- Occupational radiation safety, radiological access control, and ALARA inspection with Mr. D. Curtland on March 12, 2004.
4OA7 Licensee-Identified Violations
Cornerstone: Mitigating Systems
.1 10 CFR 50, Appendix B, Criterion III, Design Control, requires that the SSCs to which
this appendix applies are correctly translated into specifications, drawings, procedures, and instructions. That design changes, including field changes, shall be subject to design control measures commensurate with those applied to the original design.
Contrary to these requirements, the licensee changed the design of the un-interruptible instrument alternating current (AC) power system in Design Change Package (DCP) 1411 without proper design control being maintained. When DCP 1411 was installed into the plant, the licensees design and safety analysis failed to properly evaluate the effect of losing a specific direct current (DC) panel and a Loss of Offsite Power (LOOP) on the operation of RWS make-up CV4914 and CV4915.
DCP 1411 installed three independent inverter power systems consisting of a battery charger, an inverter, a voltage regulator, a static switch, and a manual bypass switch.
The systems replaced the un-interruptible AC system, the Division 1 and Division 2 instrument AC systems. The original design of the system did not have batteries providing backup system power. SV4934 and SV4935, which determine the position of the RWS make-up CVs, were electrically connected to the opposite train so that a loss of DC divisional power 1D13 and 1D23 and a LOOP would cause the SVs to de-energize, which caused the RWS make-up CVs to open. The installation of inverter power systems 1D15 and 1D25 changed the loss of DC divisional power and LOOP Scenario, since the inverter kept the instrument AC division powered. With the instrument AC division powered, the SVs remain energized, which keeps the RWS make-up CVs closed. The fail-safe position for the make-up CVs is open.
The safety evaluation performed by the licensee during this modification did not properly evaluate this scenario, since it stated that there would be no impact. There was an impact since the valves no longer went to there open fail safe condition during a loss of DC with a LOOP. The inspectors determined that although the evaluation and design utilized for the installation of DCP 1411 were inadequate, there was a safety-related hand switch in the RWS make-up circuit that will cause the RWS make-up CVs to open.
Therefore, this violation is not more than very low safety significance, and is being treated as an NCV. The licensee entered this issue into the corrective action program as CAP 30637.
Cornerstone: Emergency Preparedness
discovery that information technology (IT) contractor staff had made changes to the Emergency Response Data System (ERDS) software, and these changes were not communicated to the NRC as required by 10 CFR 50, Appendix E, Emergency Planning and Preparedness for Production and Utilization Facilities. The EP staff discovered this violation by evaluating an operating experience information transmittal from another licensee which described a similar situation at the other facility. Upon questioning by the EP staff, the IT contractor staff confirmed that they had made changes to ERDS software in the past, but were unaware of the notification requirements in 10 CFR 50 Appendix E.
The inspectors verified that corrective actions have been taken to ensure compliance with the Appendix E notification requirements. These measures included transferring ownership of ERDS to the EP group, and researching and documenting all the changes made by IT contractors to ERDS. The inspectors further verified that past unreported changes to ERDS did not compromise its accurate functioning at both the licensees emergency response facilities as well as the NRC Headquarters Operations Center.
This was of low safety significance due to the fact that the accuracy of ERDS information was not compromised, and the unreported changes were relatively minor.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
- M. Peifer, Site Vice President
- J. Bjorseth, Plant Manager
- S. Catron, Regulatory Affairs Manager
- D. Curtland, Site Engineering Director
- T. Evans, Operations Manager
- B. Kindred, Security Manager
- C. Kress, Training Manager
- W. Simmons, Maintenance Manager
- D. Wheeler, Chemistry Manager
- J. Windschill, Radiation Protection Manager
Nuclear Regulatory Commission
- D. Beaulieu, Project Manager, NRR
- B. Burgess, Chief, Reactor Projects Branch 2
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
5000331/2004002-01 NCV Inadequate Acceptance Criteria for Emergency Diesel Generator Heat Exchangers Inspections (1R07)5000331/2004002-02 NCV Failure to Maintain Adequate Design Control when the Residual Heat Removal Service Water/Emergency Service Water Pit Level Indicating Switches were Downgraded (1R15)5000331/2004002-03 FIN Failure to Ensure Proper Reassembly of the E Condensate Demineralizer Resulted in a Manual Reactor SCRAM (4AO3)
Closed
5000331/2004002-01 NCV Inadequate Acceptance Criteria for Emergency Diesel Generator Heat Exchanger Inspections (1R07)5000331/2004002-02 NCV Failure to Maintain Adequate Design Control when the Residual Heat Removal Service Water/Emergency Service Water Pit Level Indicating Switches were Downgraded (1R15)
Attachment
- 05000331/2004002-03 FIN Failure to Ensure Proper Reassembly of the E Condensate Demineralizer Resulted in a Manual Reactor SCRAM (4AO3)
- 050000331/2003-005-0 LER Unplanned Manual Reactor Scram due to High Reactor Coolant Conductivity (4OA3)
- 050000331/2003-006-0 LER Unplanned Manual Reactor Scram due to Degrading Condenser Vacuum (4OA3)
Discussed
None.
Attachment