IR 05000269/2010003

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IR 05000269-10-003, 05000270-10-003, 05000287-10-003; 04/01/2010 - 06/30/2010; Oconee Nuclear Station Units 1, 2 and 3; Maintenance Risk Assessments and Emergent Work Control, Evaluations of Changes, Tests, or Experiments and Permanent Plan
ML102080629
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 07/27/2010
From: Bartley J
NRC/RGN-II/DRP/RPB1
To: Baxter D
Duke Energy Carolinas
References
IR-10-003
Download: ML102080629 (45)


Text

UNITED STATES uly 27, 2010

SUBJECT:

OCONEE NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000269/2010003, 05000270/2010003, 05000287/2010003

Dear Mr. Baxter:

On June 30, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Oconee Nuclear Station Units 1, 2, and 3. The enclosed inspection report documents the inspection results, which were discussed on July 1, 2010, with you and other members of your staff.

The inspection examined activities conducted under your licenses as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your licenses. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents two NRC-identified findings and one self-revealing finding of very low safety significance (Green) which were determined to be violations of NRC requirements.

However, because of the very low safety significance and because they were entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCVs)

consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Oconee. In addition, if you disagree with the cross-cutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, RII, and the NRC Senior Resident Inspector at Oconee.

DEC 2 In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Jonathan H. Bartley, Chief Reactor Projects Branch 1 Division of Reactor Projects Docket Nos.: 50-269, 50-270, 50-287, 72-04 License Nos.: DPR-38, DPR-47, DPR-55

Enclosure:

NRC Integrated Inspection Report 05000269/2010003, 05000270/2010003, 05000287/2010003 w/Attachment: Supplemental Information

REGION II==

Docket Nos: 50-269, 50-270, 50-287, 72-04 License Nos: DPR-38, DPR-47, DPR-55 Report Nos: 05000269/2010003, 05000270/2010003, 05000287/2010003 Licensee: Duke Energy Carolinas, LLC Facility: Oconee Nuclear Station, Units 1, 2 and 3 Location: Seneca, SC 29672 Dates: April 1, 2010, through June 30, 2010 Inspectors: A. Sabisch, Senior Resident Inspector E. Riggs, Resident Inspector G. Ottenberg, Resident Inspector K. Ellis, Resident Inspector J. Hamman, Resident Inspector R. Chou, Reactor Inspector (Section 1R17)

W. Loo, Health Physicist (Section 2RS1)

Approved by: Jonathan H. Bartley, Chief Reactor Projects Branch 1 Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

IR 05000269/2010-003, 05000270/2010-003, 05000287/2010-003; 04/01/2010 - 06/30/2010;

Oconee Nuclear Station Units 1, 2 and 3; Maintenance Risk Assessments and Emergent Work Control, Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications,

Radiological Hazard Assessment and Exposure Control The report covered a three-month period of inspection by the resident inspectors and two Region-based reactor inspectors. Three Green findings were identified. The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Cross-cutting aspects are determined using IMC 0310, Components Within The Cross-Cutting Areas. Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process.

Cornerstone: Initiating Events

Green.

An NRC-identified Green non-cited violation (NCV) of 10 CFR 50.65(a)(4) was identified for the licensees failure to adequately develop and effectively implement risk mitigation actions associated with lifting the Unit 2 main generator rotor. The licensee failed to establish and adhere to lift height restrictions to protect the Unit 1 and Unit 2 main feeder buses from damage in the event the rotor was dropped. The issue was entered into the licensees corrective action program as PIPs O-10-2477 and O-10-2830. Corrective actions taken included enhancing the Critical Activity and Complex Lift Plans to provide additional guidance and mitigating actions as well as assigning increased oversight for future lifts.

The performance deficiency was more than minor because it affected the Human Performance attribute and adversely impacted the Initiating Events cornerstone objective in that the risk management strategies did not minimize the consequence of a rotor drop during the Unit 2 online lifts and were not effectively implemented during the Unit 2 outage lifts. The inspectors completed a Phase 1 screening using Inspection Manual Chapter 0609, Appendix K,

Maintenance Risk Assessment and Risk Management Significance Determination Process, and determined that the finding was of very low safety significance (Green) because the Incremental Core Damage Probability increase was less than 1E-6. The finding directly involved the cross-cutting area of Human Performance under the Work Activity Coordination aspect of the Work Control component in that the licensee failed to appropriately control work activities by incorporating risk insight. H.3(a) (Section 1R13)

Cornerstone: Mitigating Systems

Green.

An NRC-identified non-cited violation (NCV) of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings was identified. The licensee failed to adhere to drawings and instructions during the installation of rebar in the Unit 3 Borated Water Storage Tank (BWST) Natural Phenomena Barrier System foundation. This issue has been entered into the licensees corrective action program as PIP O-10-4985.

The inspectors determined that the licensees failure to follow approved drawings and instructions for construction of the Unit 3 BWST Natural Phenomena Barrier System foundation was a performance deficiency. The inspectors determined that the performance deficiency was more than minor because, if left uncorrected, insufficient concrete coverage on the rebar could lead to rebar corrosion and challenge the integrity of the Unit 3 BWST Natural Phenomena Barrier System. The inspectors used Inspection Manual Chapter 0609, Significance Determination Process, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings and determined that the finding was of very low safety significance (Green) because the finding did not result in the actual loss of function of the Unit 3 BWST. This finding had a cross-cutting aspect in the area of Human Performance under the Procedural Compliance aspect of the Work Practices component because the licensee failed to effectively communicate expectations to follow procedures. H.4(b) (Section 1R17)

Cornerstone: Occupational Radiation Safety

Green.

A self-revealing non-cited violation (NCV) of 10 CFR 20.1501(a) was identified for the licensees failure to conduct an adequate area radiation survey to evaluate the magnitude and extent of radiation levels for an area located in the Radwaste Facility. This issue has been entered into the licensees corrective action program as PIPs O-09-04475 and O-10-01503.

The failure to conduct an adequate area radiation survey to evaluate the magnitude and extent of radiation levels for an area located in the Radwaste Facility is a performance deficiency. This finding is more than minor because it is associated with the Occupational Radiation Safety cornerstone attribute of exposure control and monitoring and it affected the associated cornerstone objective because the failure to conduct an adequate area radiation survey to evaluate the magnitude and extent of radiation levels for an area located in the Radwaste Facility did not ensure the adequate protection of worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. The finding was evaluated using the IMC 0609, Appendix C, and was determined to be of very low safety significance. The cause of this finding is related to the cross-cutting aspect of radiological safety in the work control component of Human Performance because the licensee did not conduct an adequate area radiation survey to evaluate the magnitude and extent of radiation levels for an area located in the Radwaste Facility. H.3(b) (Section 2RS1)

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at approximately 100 percent rated thermal power (RTP).

On June 6, 2010, power was reduced to approximately 88 percent RTP to conduct main turbine valve movement testing. The unit was returned to approximately 100 percent RTP and remained there for the remainder of the inspection period.

Unit 2 began the inspection period at approximately 100 percent RTP and remained there until the unit was removed from service for the 2 EOC 24 refueling outage on April 25. It was returned to service early on May 30, but was removed from service to address excessive pressurizer spray valve leakage. The unit returned to service on June 3, and reached approximately 100 percent RTP on June 5 and remained there for the remainder of the inspection period.

Unit 3 began the inspection period at approximately 100 percent RTP. The unit was placed in Mode 4 on April 18, to repair a leak in the 3F2 feedwater heater. The unit was returned to 100 percent RTP on April 26 and remained there for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection

a. Inspection Scope

Hot Weather Preparations: The inspectors reviewed the licensees preparations for adverse weather associated with high ambient temperatures to ensure equipment used in the licensees procedures were capable of functioning as intended. This included field walkdowns to assess the material condition and operation of ventilation and cooling equipment, as well as a review of procedures designed to align equipment to support operation during the summer months. Risk-significant systems and areas reviewed included the standby shutdown facility (SSF), the auxiliary building, portions of the turbine building and the Essential Siphon Vacuum Building. In addition, the inspectors conducted discussions with operations, engineering, and maintenance personnel in order to assess the licensees ability to identify and resolve deficient conditions associated with hot weather protection equipment prior to actual hot weather being experienced at the site. The Documents reviewed are listed in the Attachment.

External Flooding: The inspectors conducted a walkdown of the SSF facility to inspect the below-grade conduits and penetrations that could provide a pathway for water to enter the facility. The drainage system including installed sump pumps was inspected to verify it was functional and able to remove water that entered the facility. Discussions were held with the system engineers responsible for the equipment within the SSF structure. Documents reviewed are listed in the Attachment.

Evaluation of Summer Readiness of Offsite and Alternate AC Power Systems: The inspectors reviewed the licensees procedures used to respond to changing offsite grid conditions, including actions to be taken when notified by the Transmission Control Center that a Real Time Contingency Analysis (RTCA) shows inadequate post trip voltage to verify the implementation of the procedures protect mitigating systems from adverse weather affects. The inspectors also reviewed the procedural guidance for monitoring switchyard voltage and frequency when the RTCA tool is non-functional. The assessment of plant risk for maintenance activities that could affect grid reliability or offsite activities which could affect the transmission systems ability to provide adequate offsite power was discussed with the appropriate plant personnel. The inspectors also reviewed related work orders and performed a walkdown of the plant switchyards to verify the material condition of the offsite power sources. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R04 Equipment Alignment

a. Inspection Scope

The inspectors performed partial walkdowns of the six systems listed below to assess the operability of redundant or diverse trains and components when safety-related equipment was inoperable or out-of-service and to identify any discrepancies that could impact the function of the system potentially increasing overall risk. The inspectors reviewed applicable operating procedures and walked down system components, selected breakers, valves, and support equipment to determine if they were correctly aligned to support system operation. The inspectors reviewed protected equipment sheets, maintenance plans, and system drawings to determine if the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the Corrective Action Program (CAP). Documents reviewed are listed in the

.

  • Designated protected equipment associated with work tied to the Natural Phenomena Barrier System and High Energy Line Break projects during the week of April 12, 2010
  • Verification of protected equipment identified for planned maintenance activities at the start of the week of April 25, 2010
  • Additional equipment identified for protection following declaring the SSF inoperable based on high service water strainer differential pressure indications
  • Decay heat removal systems placed in-service prior to the start of core reloading activities on Unit 2
  • Keowee Hydro Unit (KHU)-1 while KHU-2 was out of service for quarterly Preventive Maintenance (PM)

b. Findings

No findings were identified.

1R05 Fire Protection

a. Inspection Scope

Fire Area Tours: The inspectors walked down accessible portions of the five plant areas listed below to assess the licensees control of transient combustible material and ignition sources, fire detection and suppression capabilities, fire barriers, and any related compensatory measures. The inspectors observed the fire protection suppression and detection equipment to determine if any conditions or deficiencies existed which could impair the operability of that equipment. The inspectors selected the areas based on a review of the licensees safe shutdown analysis probabilistic risk assessment and sensitivity studies for fire-related core damage accident sequences. Documents reviewed are listed in the Attachment.

  • Turbine Building Ground Floor
  • Turbine Building Operating Deck
  • Unit 2 Reactor Building
  • Unit 1 Cable Room Fire Drill Observation: On June 11, 2010, the licensee conducted a shift fire drill simulating an oil leak on the SSF generator resulting in a fire. The inspectors observed this drill to verify the fire brigades use of protective gear and firefighting equipment; that fire fighting pre-plan procedures and appropriate fire fighting techniques were used; and that the directions of the fire brigade leader were thorough, clear, and effective. The inspectors also observed the post-drill critique to assess if it was appropriately critical, included discussions of drill observations, and identified any areas requiring corrective action. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R06 Flood Protection Measures

a. Inspection Scope

Internal Flood Protection: The inspectors reviewed the following activity to verify that the licensees turbine building flood control measures were implemented while performing Unit 2 condenser maintenance during the refueling outage. The inspectors reviewed the applicable portions of OP/2/A/1104/012 E, Isolation and Re-Flooding Condenser Circulating Water (CCW) Inlet Piping. The inspectors verified that Selected Licensee Commitments 16.9.11, Turbine Building Flood Protection Measures were met.

Submerged or Buried Cable Inspection: The inspectors inspected the condition of the Unit 1 SSF Trench (Cover 34) through direct observation. The inspectors verified the trench contained no standing water and that the cables were intact and in good condition.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification

a. Inspection Scope

Resident Review: The inspectors observed one active simulator exam, to assess the performance of licensed operators during a simulator training session. The scenario included a group of control rods inadvertently de-energizing requiring a manual reactor trip, failure of the Main Turbine to automatically or manually trip requiring the operators to secure both electro-hydraulic turbine control pumps, Loss of Main Feedwater, Emergency Feedwater, and the Condensate Booster Pumps requiring the crew to implement High Pressure Injection Forced Cooling. The inspection focused on high-risk operator actions performed during implementation of the abnormal and emergency operating procedures, and the incorporation of lessons learned from previous plant and industry events. The classification and declaration of the Emergency Plan was also observed during the scenario. The post-scenario critique conducted by the training instructor and the crew was observed. Documents reviewed are listed in the

.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the licensees effectiveness in performing the following three corrective maintenance activities. These reviews included an assessment of the licensees practices pertaining to the identification, scoping, and handling of degraded equipment conditions, as well as common cause failure evaluations. For each activity selected, the inspectors performed a detailed review of the problem history and surrounding circumstances, evaluated the extent of condition reviews as required, and reviewed the generic implications of the equipment and/or work practice problem. For those structures, systems and components (SSCs) scoped in the Maintenance Rule per 10 CFR 50.65, the inspectors verified that reliability and unavailability were properly monitored and that 10 CFR 50.65 (a)(1) and (a)(2) classifications were justified in light of the reviewed degraded equipment condition. Documents reviewed are listed in the

.

  • Assessment of unexpected refueling canal seal leakage following canal flood-up, actions taken to drain back down, maintenance work done to replace the seal and verify that no leakage existed to support the core offload work
  • Repair of CCW-284, SSF Diesel Engine Service Water pump discharge check valve following its failure to close resulting in inoperability of the SSF heating, ventilation, and air conditioning (HVAC) System
  • Relocation of the low pressure tap associated with the differential pressure gauge of the SSF service water strainer following clogging of the tap

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors evaluated the following attributes for the nine activities listed below:

(1) the effectiveness of the risk assessments performed before maintenance activities were conducted;
(2) the management of risk;
(3) that, upon identification of an unforeseen situation, necessary steps were taken to plan and control the resulting emergent work activities; and
(4) that maintenance risk assessments and emergent work problems were adequately identified and resolved. Documents reviewed are listed in the

.

  • Unit 2 Electrical Generator Rotor Lift to support rotor replacement from the truck bay to the Unit 2 operating deck laydown area
  • Failure of 1HP-417 Reactor Coolant Makeup Unit Pump (RCMUP) recirculation path to Spent Fuel Pool to open during SSF RCMUP test concurrent with breaker 1KE-9 failure
  • Replacement of reactor vessel plenum during the 2 EOC 24 refueling outage
  • Critical Plan covering the restart of work associated with the Natural Phenomena Barrier System (NPBS) around the Borated Water Storage Tank (BWST)
  • Unplanned Red PRA condition due to the simultaneous unavailability of Station Auxiliary Service Water (ASW) and SSF ASW on April 28, 2010
  • Unplanned Red PRA condition due to the simultaneous unavailability of Station ASW and SSF ASW (failure of 0CCW-284) on May 4, 2010
  • Response to low seal dP indications on the 2A1 reactor coolant pump (RCP) during startup, the decision to return to Mode 5 to replace the RCP seal package and the associated schedule review and resequencing required to support the emergent work
  • Unit 2 Electrical Generator Rotor Lift to support rotor replacement from the Unit 2 operating deck laydown area to the truck bay

b. Findings

Introduction:

An NRC-identified Green NCV of 10 CFR 50.65(a)(4) was identified for the licensees failure to adequately develop and effectively implement risk mitigation actions associated with lifting the Unit 2 main generator rotor. The licensee failed to establish and adhere to lift height restrictions to protect the Unit 1 and Unit 2 main feeder buses from damage in the event the rotor was dropped.

Description:

During the Unit 2 refueling outage, the main generator rotor was replaced.

The installation process included six overcapacity lifts which required lifting the 190-ton rotor over the Unit 1 and Unit 2 main electrical feeder buses. Two lifts were scheduled while both Unit 1 and Unit 2 were operating and the remaining four lifts were scheduled while Unit 2 was shutdown. The licensee developed a Critical Activity Plan for the two lifts conducted while Unit 1 and Unit 2 were at power and a Complex Lift Plan for the lifts that occurred during the Unit 2 outage. The following deficiencies related to the development and execution of these plans were identified by the inspectors and represented a failure to meet the requirements in 10 CFR 50.65(a)(4):

  • The licensees Critical Activity Plan addressed the risk mitigation of a potential drop of the rotor by stating that the Safe Shutdown Facility could be used to mitigate the consequences of a load drop event. However, the licensee failed to consider limiting the lift height while over Unit 1 and Unit 2 main electrical feeder buses to a height which would not have damaged the buses in the event the rotor was dropped. The licensee had previously calculated that a drop of the rotor of less than six inches would prevent damaging the electrical buses beneath the east-west portion of the designated travel path. Without applying this limitation, the rotor was lifted greater than two feet above the floor.
  • In the Complex Lift Plan, the licensee restricted the rotor from being lifted more than six inches above the floor to prevent damage to the main electrical feeder buses located directly beneath the travel path in the event the rotor was dropped. This limitation was discussed in the pre-job brief for the activity. While performing the first lift, the rotor was raised above the six inch height restriction. The lift was stopped and the rotor lowered to within the prescribed height limit prior to completing the lift.

The issue was entered into the licensees corrective action program as PIPs O-10-2477 and O-10-2830. Corrective actions taken included enhancing the Critical Activity and Complex Lift Plans to provide additional guidance and mitigating actions as well as assigning increased oversight for future lifts.

Analysis:

The failure to adequately manage the increased risk associated with the Unit 2 rotor lifts was a performance deficiency. The performance deficiency was more than minor because it affected the Human Performance attribute and adversely impacted the Initiating Events cornerstone objective in that the risk management strategies did not minimize the consequence of a rotor drop during the Unit 2 online lifts and were not effectively implemented during the Unit 2 outage lifts. The inspectors completed a Phase 1 screening using Inspection Manual Chapter 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance Determination Process, and determined that the finding was of very low safety significance (Green) because the Incremental Core Damage Probability increase was less than 1E-6. The finding directly involved the cross-cutting area of Human Performance under the Work Activity Coordination aspect of the Work Control component in that the licensee failed to appropriately control work activities by incorporating risk insight. H.3.a]

Enforcement:

10 CFR 50.65(a)(4), Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, requires in part, that the licensee assess and manage the increase in risk that may result from the proposed maintenance activities.

Nuclear System Directive (NSD) 415, Operational Risk Management (Modes 1-3) per 10CFR50.65(a)(4), implements the requirements of 10FR50.65(a)(4) during power operation. NSD 213, Risk Management Process, defines the requirements of station personnel to identify, direct, control, and manage risk-significant activities at the station, including the development of Critical Activity Plans to manage and minimize the risk resulting from the planned activity. Contrary to the above, on April 10, 2010, and April 26, 2010, the licensee failed to adequately assess and manage the increase in risk associated with maintenance activities. Specifically, for the planned Unit 2 main generator rotor lifts the licensee did not establish a height restriction during the rotor lift while Unit 2 was online and exceeded the established height restriction during a rotor lift while Unit 2 was shutdown. Consequently, the Unit 1 and Unit 2 main electrical feeder buses could have been damaged in the event the rotor was dropped. Because this finding is of very low safety significance and has been entered into the licensees corrective action program as PIPs O-10-2477 and O-10-2830, this violation is being treated as an NCV consistent with Section VI.A of the NRC Enforcement Manual: NCV 05000269, 270/2010003-01, Inadequate Risk Management Associated with the Unit 2 Electrical Generator Rotor Lift.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following eight operability evaluations affecting risk significant systems to assess:

(1) the technical adequacy of the evaluations;
(2) whether continued system operability was warranted;
(3) whether other existing degraded conditions were considered;
(4) if compensatory measures were involved, whether the compensatory measures were in place, would work as intended, and were appropriately controlled; and
(5) where continued operability was considered unjustified, the impact on Technical Specifications (TS) limiting condition for operations.
  • PIP O-10-2172, Unevaluated Single Failure of Control Room Ventilation System
  • PIP O-10-2608, Following successful as-found testing, the pilot spindle/disc assembly of 1RC-66 removed during 1 EOC 25 was found in unexpected condition
  • PIP O-10-2842, Troubleshooting the cause of the 3A hotwell pump failure to start
  • PIP O-10-2707, 2MS-161 (2A MS line Atmospheric Dump Block Bypass) chain broke during operation
  • PIP O-10-3167, Keowee ambient air temperature may exceed piping design temperatures during loss of all ventilation
  • PIP O-10-3285, Excessive cooling water temperature required shutdown of SSF HVAC Compressors
  • PIP O-10-2448, Valve 1HP-417 (isolation valve in the RCMUP recirculation flowpath to the Spent Fuel Pool) would not operate from the SSF control room switch during testing
  • PIP O-10-3825, Design Change EC103784 did not document expected impact on SSF Service Water strainer differential pressure measurement

b. Findings

No findings were identified.

1R17 Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed ductbank construction and examined the brick and concrete block wall condition for Units 1 and 3 in Auxiliary Building after the siding removed in preparing for the installation of the Fiber Reinforced Protection. The inspectors examined installation of the reinforcing steel and form work configuration for the Unit 3 BWST and North and South Entrance Foundations in the Protective Service Water (PSW) Building. The inspectors observed the concrete placement, testing, and standard cylinder preparation for the compressive testing for the Unit 3 BWST Foundation and North and South Entrance Foundations and Wall W-12 of PSW Building. The inspectors reviewed procedures, specifications, construction documents, and corrective actions such as PIPs generated by the licensee and Nonconformance Reports (NCR) generated by the contractor related to the rebar installation, concrete mix testing, and concrete pour.

The inspectors examined the rebar installation to ensure that the licensee had measured the reinforcing steel size, spacing, splice length, and the concrete minimum protection coverage in accordance with the requirements of the design drawings and the American Concrete Institute (ACI) 301-89 and -05, Code Requirements for Structural Concrete.

The inspectors reviewed the concrete pre-placement inspection checklist prior to the concrete pour. The inspectors reviewed the procedures, specifications, and documents related to the concrete construction activities.

The inspectors observed placement activities to verify that activities pertaining to concrete delivery time, flow distance, layer thickness and concrete consolidation or vibration conformed to industry standards established by the American Concrete Institute. Concrete batch tickets were examined to verify that the specified concrete mix was being delivered to the site. The inspectors observed that concrete placement activities were continuously monitored by the Duke and contractor quality control personnel and engineers. The inspectors witnessed in-process testing and reviewed the results for slump, air content, temperature, unit weight, and molding of the concrete cylinders for compressive strength testing, and also witnessed sample points and truck loads to verify that concrete samples for the field testing and cylinders for the testing were obtained at the point of placement (end of chute line) and the middle portion of the truck loads. The inspectors reviewed cylinders to determine whether they were molded in accordance with applicable American Society for Testing and Materials (ASTM)requirements of ASTM C 172, Standard Method of Sampling Freshly Mixed Concrete, and determined whether concrete field testing was performed by Quality Control (QC)inspectors from the contractor or Duke. Documents reviewed are listed in the

.

b. Findings

Introduction:

An NRC-identified Green NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings was identified. The licensee failed to adhere to drawings and instructions during the installation of rebar in the Unit 3 BWST Natural Phenomena Barrier System foundation.

Description:

The licensee was constructing a Natural Phenomena Barrier System to protect the BWST against damage from windborne debris. The initial phase of the project involved pouring a concrete foundation that encased an internal framework of steel rebar. The modification package contained drawing A31Q-2153-15-01, Revision 2, which required three inches of concrete coverage for all rebar subject to soil contact based on ACI Code 301-89. On June 16, 2010, after all the required rebar was placed a QC inspection was performed on the Unit 3 BWST foundation rebar to verify that it would meet the coverage requirement. The QC inspectors documented that the rebar met dimensional requirements.

On June 17, 2010, prior to the actual concrete pour the inspectors performed a walkdown of the foundation. The inspectors identified several rebars on the lower section that did not meet the coverage requirement. Some of the rebars only had approximately one-half inch clearance from the mud mat. Following discussions with project personnel, the licensee issued Advance Work Authorization (AWA) 97958-F to modify the minimum concrete coverage requirement for the lower section of rebar to two inches based on ACI Code 301-05, Specifications for Structural Concrete, for concrete to be poured on the top of existing mud mat. The licensee then performed rework to provide a two-inch coverage. QC then performed another inspection and approved the structure for concrete pour.

On June 18, 2010, the inspectors again walked down the area and identified that many rebars on the upper section did not meet the required concrete coverage of two inches specified by ACI Code 301-89, referred to by Specification No.OSS-0160.00-00-0002, Specification for Receiving and Placing Concrete for QA Condition Structure. The licensee performed additional rework on the upper section to provide the required concrete coverage. Following rework and re-inspection, the Unit 3 BWST concrete pour was completed.

Analysis:

The inspectors determined that the licensees failure to follow approved drawings and instructions for construction of the Unit 3 BWST Natural Phenomena Barrier System foundation was a performance deficiency. The inspectors determined that the finding was more than minor because, if left uncorrected, insufficient concrete coverage on the rebar could lead to rebar corrosion and challenge the integrity of the Unit 3 BWST Natural Phenomena Barrier System. The inspectors used Inspection Manual Chapter 0609, Significance Determination Process, Attachment 4, Phase 1 -

Initial Screening and Characterization of Findings and determined that the finding was of very low safety significance (Green) because the finding did not result in the actual loss of function of the Unit 3 BWST. This finding had a cross-cutting aspect in the area of Human Performance under the Procedural Compliance aspect of the Work Practices component because the licensee failed to effectively communicate expectations to follow procedures. H.4(b)

Enforcement:

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings required, in part, that activities affecting quality shall be accomplished in accordance with instructions, procedures, or drawings appropriate to the circumstances.

Drawing A31Q-2153-15-01, Revision 2, and ACI Code 301-89 required rebar installation to provide for a minimum of three inches of concrete coverage for all reinforced concrete subject to soil contact for the lower section of rebars. ACI Code 301-89, Specifications for Structural Concrete for buildings, required a two-inch concrete coverage for the top section of rebars. Contrary to the above, between June 16, 2010, and June 18, 2010, the licensee did not accomplish rebar installation, an activity affecting quality, in accordance with approved drawings and instructions for the construction of the Unit 3 BWST Natural Phenomena Barrier System foundation. The inspectors observed rebar installations that did not provided the required concrete coverage of A31Q-2153-15-01, Revision 2 or ACI Code 301-89. Because this finding is of very low safety significance and has been entered into the licensees corrective action program as PIP O-10-4985, this violation is being treated as a NCV consistent with Section VI.A of the NRC Enforcement Manual: NCV 05000287/2010003-02, Failure to Install Structural Rebar as Required by Instructions and Drawings.

1R18 Plant Modifications

a. Inspection Scope

The inspectors reviewed three permanent plant modifications and one temporary modification to verify the adequacy of the modification packages, as well as 10 CFR 50.59 screenings, and to evaluate the modifications for adverse affects on system availability, reliability and functional capability, or potential impact to fuel in the core.

Documents reviewed are listed in the Attachment.

Permanent Plant Modifications

  • EC 103784, Add cross-connect between 0CCW PG-0433 and 0CCW PG-0535 instrument lines
  • High Energy Line Break (HELB) Commitments 29H, 37H and 43H, Closure of Plant Heating Isolation Valves thereby Eliminating Potential HELBs Temporary Plant Modifications

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following eight post-maintenance test procedures and/or test activities to assess if:

(1) the effect of testing on the plant had been adequately addressed by control room and/or engineering personnel;
(2) testing was adequate for the maintenance performed;
(3) acceptance criteria were clear and demonstrated operational readiness consistent with design and licensing basis documents;
(4) test instrumentation had current calibrations, range, and accuracy consistent with the application;
(5) tests were performed as written with applicable prerequisites satisfied;
(6) jumpers installed or leads lifted were properly controlled;
(7) test equipment was removed following testing; and
(8) equipment was returned to the status required to perform its safety function. Documents reviewed are listed in the Attachment.
  • 1BS-1 (Unit 1 A Reactor Building Spray header isolation valve) Valve Stroke Test following actuator mechanical/electrical PM
  • 1LP-22 (Unit 1 B Low Pressure Injection train BWST suction valve) Valve Stroke Test following actuator mechanical/electrical PM
  • A Chiller 24-hour run following power supply circuit board and diode bridge replacement
  • Unit 2 pressurizer spray valve (2RC-1) testing following valve replacement
  • SSF Diesel Engine Service Water Pump Test following inline strainer cleaning
  • Keowee Hydro Unit 2 Test following quarterly PMs
  • Keowee Hydro Unit 2 Air Circuit Breaker-4 relief valve pressure set test and IST surveillance following relief valve replacement

b. Findings

No findings were identified.

1R20 Refueling and Outage Activities

a. Inspection Scope

Unit 2 EOC 24 Refueling Outage: The inspectors evaluated licensee outage activities to determine if the licensee considered risk in developing outage schedules; adhered to administrative risk reduction methodologies they developed to control plant configuration; adhered to operating license, TS and Selected Licensee Commitment requirements and procedural guidance that maintained defense-in-depth; and developed mitigation strategies for losses of the key safety functions. The inspectors reviewed the licensees outage risk control plan to assess the adequacy of the risk assessments that had been conducted and that the licensee had implemented appropriate risk management strategies as required by 10 CFR 50.65(a)(4). The inspectors conducted portions of the following activities associated with the refueling outage. Documents reviewed are listed in the Attachment.

  • Observed Just-in-Time training conducted for the shift involved in the unit cooldown which simulated bringing the unit from Mode 3 to Mode 5
  • Observed power reduction process, removing the reactor from service and cooldown from normal operating pressure and temperature to ensure that the requirements in the TS and Selected Licensee Commitments were followed
  • Conducted a containment entry once Mode 3 had been reached to observe the condition of major, normally-inaccessible equipment and check for indications of previously unidentified leakage from the reactor coolant system including the reactor vessel upper and bottom head penetrations were not present
  • Observed the cooldown process to verify that TS cooldown restrictions and administrative guidelines were followed
  • Reviewed the licensees responses to emergent work and unexpected conditions to verify that resulting configuration changes were controlled in accordance with the outage risk control plan
  • Observed the removal and reinstallation of the reactor vessel head to ensure the lift was conducted in accordance the station procedures and heavy lift guidance
  • Observed fuel handling operations during new fuel receipt, movement into the spent fuel pool, and reactor core offload to verify that those operations and activities were being performed in accordance with TS and procedural guidance
  • Reviewed system lineups and/or control board indications to substantiate that TS, license conditions, and other requirements, commitments, and administrative procedure prerequisites for mode changes were met prior to changing modes or plant configurations
  • Observed refueling activities to substantiate that the location of the fuel assemblies was tracked through core offload including review of the videotape core loading verification with Reactor Engineering personnel
  • Observed Just-in-Time training covering the approach to criticality and Zero Power Physics Testing for the personnel involved in these activities
  • Periodically reviewed the setting and maintenance of containment integrity, to establish that the Reactor Coolant System and containment boundaries were in place and had integrity when necessary
  • Conducted containment walkdown to inspect for overall cleanliness and material condition of plant equipment after the licensee completed their closeout inspection
  • Observed the approach to criticality, placing the main generator on-line which completed the refueling outage and portions of the power ascension activities
  • Reviewed the items that had been entered into the CAP to verify that the licensee had identified outage related problems at an appropriate threshold
  • Observed activities to verify that the licensee maintained defense-in-depth commensurate with the outage risk control plan for key safety functions and applicable TS when taking equipment out of service Unit 3 EOC-24B Forced Outage Due to the 3F-2 Feedwater Heater Leak: The inspectors observed portions of the Unit 3 shutdown on April 18, 2010, from 100 percent RTP to Mode 4 and subsequent forced outage activities resulting from tube leakage in the 3F-2 feedwater heater. Activities observed by the inspectors included the unit shutdown to Mode 4, taking the turbine offline, portions of the feedwater heater repair, and reviewed Low Temperature Overpressure controls in place while in the mode of applicability. An inspector accompanied licensee personnel on a containment walkdown prior to unit startup to assess the overall material condition of safety related and risk significant SSCs. Inspectors reviewed the items entered into the licensees CAP, to establish that the licensee identified problems related to the outage activities at an appropriate threshold and had entered them into the CAP. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors either witnessed and/or reviewed test data for the nine surveillance tests listed below to assess if the SSCs met TS, Updated Final Safety Analysis Report (UFSAR), and licensee procedure requirements. In addition, the inspectors determined if the testing effectively demonstrated that the SSCs were ready and capable of performing their intended safety functions. Documents reviewed are listed in the

.

Routine Surveillances

  • PT/2/A/0610/001L, Load Shed Channel Verification, Rev. 12
  • MP/0/A/1150/030, Reactor Vessel - Lower Head Penetrations - Visual Inspection, Rev. 4
  • PT/2/A/0600/013, Motor Driven Emergency Feedwater Pump Test, Rev. 63
  • PT/2/A/0400/020, SSF RC Letdown Line Discharge Test, Rev. 1 In-Service Tests
  • PT/1/A/0600/012, Turbine Driven Emergency Feedwater Pump Test, Rev. 95 Containment Isolation Valve Testing
  • PT/2/A/0151/019, Penetration 19 Leak Rate Test, Rev. 14
  • PT/2/A/0151/020, Penetration 20 Leak Rate Test, Rev. 12
  • CP/3/A/2002/001, Unit 3 Primary Sampling System, Rev. 62

b. Findings

No findings were identified.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety and Public Radiation Safety

2RS1 Radiological Hazard Assessment and Exposure Control

a. Inspection Scope

Radiological Hazard Assessment: The inspectors reviewed a number of radiological surveys, including those performed for airborne areas, of locations throughout the facility including the Unit 2 containment, Unit 1, Unit 2, and Unit 3 reactor buildings, the turbine building, the Radwaste Facility, and the independent spent fuel storage installation (ISFSI). The inspectors also walked down those same areas and select radioactive material storage locations with a survey instrument, evaluating material condition, postings, and radiological controls. The inspectors observed jobs in radiologically risk-significant areas including high radiation areas (HRAs) and areas with, or with the potential for, airborne activity. The inspectors determined that the surveys were adequate in thoroughness and frequency for the identified hazards.

Instructions to Workers: During plant walk downs, the inspectors observed labeling and radiological controls on containers of radioactive material. The inspectors also reviewed radiation work permits (RWP) used for accessing HRAs and airborne areas, verifying that appropriate work control instructions and electronic dosimeter (ED) setpoints had been provided and to assess the communication of radiological control requirements to workers. For selected tasks, the inspectors attended pre-job briefings that reviewed RWP details with the workers. The inspectors reviewed selected ED dose and dose rate alarms, to verify workers properly responded to the alarms and that the licensees review of the events was appropriate. Through observation of pre-job RWP briefings and health physics technician (HPT) coverage of workers, the inspectors determined the licensee had established adequate means to notify workers of changing radiological conditions.

Contamination and Radioactive Material Control: The inspectors observed the release of potentially contaminated items from the radiologically controlled area (RCA) and from contaminated areas such as the Unit 2 containment personnel hatch. The inspectors also reviewed the procedural requirements for, and equipment used to perform, the radiation surveys for release. During plant walk downs, the inspectors evaluated radioactive material storage areas and containers to include satellite RCAs, assessing material condition, posting/labeling, and control of materials/areas. In addition, the inspectors reviewed the sealed source inventory and verified labeling, storage conditions, and leak testing of selected sources located in Room Numbers (Nos.) 332 and 362 of the U2 Auxiliary Building.

The inspectors walked-down the ISFSI facility, observing the physical condition of the casks, radiological postings, and barriers. The inspectors performed independent gamma radiation surveys of the area and reviewed gamma radiation surveys of the ISFSI facility performed by licensee personnel. Inspectors compared the independent survey results to previous surveys and against procedural and TS limits. The inspectors evaluated implementation of radiological controls, including labeling and posting, and discussed controls with radiation protection (RP) staff. Environmental monitoring results for direct radiation from the ISFSI were reviewed and inspectors observed the placement and physical condition of thermoluminescent dosimeters around the facility.

Radiological Hazards Control and Work Coverage: The inspectors evaluated licensee performance in controlling worker access to radiologically significant areas and monitoring jobs in-progress associated with the U2 EOC 24 refueling outage.

Established radiological controls were evaluated for selected tasks including alloy 600 weld overlay, steam generator (S/G) eddy current testing (ECT), pressurizer piping work activities, and RCP B work activities. The inspectors evaluated the effectiveness of radiation exposure controls, including air sampling, barrier integrity, engineering controls, and postings through a review of both internal and external exposure results.

During walk downs with a radiation survey meter, the inspectors independently verified ambient radiological conditions were consistent with licensee performed surveys, RWPs, and pre-job briefings; observed the adequacy of radiological controls; and observed controls for radioactive materials stored in the spent fuel pool. The inspectors also reviewed the procedural guidance for multi- and extremity badging. Select multi-badge packets were reviewed to verify consistency with procedural and regulatory guidance.

For high radiation area tasks involving significant dose rate gradients, the inspectors evaluated the use and placement of whole body and extremity dosimetry to monitor worker exposure. The inspectors also reviewed and discussed selected whole-body count analyses conducted during 2009 and the Unit 2 refueling outage. The inspectors reviewed RWPs for use in airborne areas, ensuring the prescribed controls were appropriate for the conditions as identified in radiological surveys and air samples. ED alarm set points and worker stay times were evaluated against area radiation survey results for drywell and refueling floor activities.

Risk-Significant HRA and Very HRA (VHRA) Controls: The inspectors discussed the controls and procedures for locked-high radiation areas (LHRAs) and VHRAs with health physics supervisors and the RP Manager. The inspectors observed the issuance of LHRA keys and evaluated the storage, inventory, and handling of LHRA/VHRA keys.

During plant walk downs, the inspectors verified the posting/locking of LHRA/VHRA areas.

Radiation Worker Performance and Radiation Protection Technician Proficiency: The inspectors observed radiation worker performance through direct observation, via remote camera monitoring, and via telemetry. Jobs observed associated with the U2 EOC 24 outage included S/G ECT, alloy 600 welding overlays, pressurizer piping work activities, and RCP B work activities. These jobs were performed in high radiation, airborne, and/or contaminated areas. The inspectors also observed HPTs providing field coverage of jobs and providing remote coverage.

Problem Identification & Resolution: Licensee CAP documents associated with radiation monitoring and exposure control were reviewed and assessed. This included review of selected CAP records related to radiation worker and HPT performance. The inspectors evaluated the licensees ability to identify, characterize, prioritize, and resolve the identified issues in accordance with procedure NSD 208, Problem Investigation Process, Revision 31. The inspectors also evaluated the scope of the licensees internal audit program and reviewed recent assessment results. Documents reviewed are listed in the

.

RP activities were evaluated against the requirements of UFSAR Section 12; TS Section 5.7; 10 CFR Parts 19 and 20; and approved licensee procedures. Radiological control activities for ISFSI areas were evaluated against 10 CFR Part 20, 10 CFR Part 72, and TS details. Documents reviewed are listed in the Attachment.

The inspectors completed 1 sample, as described in Inspection Procedure (IP)71124.01. The inspectors also completed the RP line-item sample activities specified in IP 60855.1.

b. Findings

Introduction:

A self-revealing NCV of 10 CFR 20.1501(a) was identified for the licensees failure to conduct an adequate area radiation survey to evaluate the magnitude and extent of radiation levels for an area located in the Radwaste Facility.

Description:

On June 23, 2009, an individual checked in at the Surveillance and Control Single Point of Access window and informed the HPT that he had to go into Room No.

RW-227 of the Radwaste Facility to manipulate some valves. Also, the individual informed the HPT that on a previous day he had entered the same area and had received a ED dose rate alarm of 76 mrem/hr on a dose rate setting of 75 mrem/hr. The HPT reviewed the last area radiation survey of the area conducted on June 18, 2009, and noted that the dose rates in the area were found to be 70 mrem/hr at the location where the individual had to work. Based on those discussions with the individual and the most recent area radiation in that area, the HPT along with RP supervision decided to raise the RWP ED setpoint for that individual from 75 mrem/hr to 100 mrem/hr. The worker proceeded to go to Room No. RW-227 of the Radwaste Facility to manipulate the valves and received an ED dose rate alarm and immediately left the area and went to RP. RP reviewed the EDs histogram and determined that he had entered a radiation field of 112 mrem/hr. An HPT and supervisor resurveyed the area and identified dose rates of 120 mrem/hr at 30 centimeters

(cm) and 350 mrem/hr at contact in the work area near the G demineralizer. Based on those dose rates RP controlled and posted the area as a HRA. A plan was developed and implemented to backwash the solids from H and G demineralizers which reduced the dose rates in the area to 80 mrem/hr at 30 cm and 205 mrem/hr at contact. In addition to the two remote monitoring devices that were already in the room, RP installed two more remote monitoring devices one foot in front of the H and G demineralizers to provide additional live time radiation dose data in the area.
Analysis:

The failure to conduct an adequate area radiation survey to evaluate the magnitude and extent of radiation levels for an area located in the Radwaste Facility is a performance deficiency. This finding is more than minor because it is associated with the Occupational Radiation Safety cornerstone attribute of exposure control and monitoring and it affected the associated cornerstone objective because the failure to conduct an adequate area radiation survey to evaluate the magnitude and extent of radiation levels for an area located in the Radwaste Facility did not ensure the adequate protection of worker health and safety from exposure to radiation from radioactive material during routine civilian nuclear reactor operation. The finding was evaluated using IMC 0609, Appendix C, and was determined to be of very low safety significance.

The failure to conduct an adequate area radiation survey of the room did not pose a substantial potential for overexposure and did not affect the ability to assess doses because the involved individual was monitored for exposure from external radiation fields using an alarming ED. The cause of this finding is related to the cross-cutting aspect of radiological safety in the work control component of Human Performance because the licensee did not conduct an adequate area radiation survey to evaluate the magnitude and extent of radiation levels for an area located in the Radwaste Facility.

H.3(b)

Enforcement:

10 CFR 20.1501(a) states that each licensee shall make or cause to be made, surveys that:

(1) may be necessary for the licensee to comply with the regulations in this part; and
(2) are reasonable under the circumstances to evaluate:
(i) the magnitude and extent of radiation levels;
(ii) concentrations or quantities of radioactive material; and (iii) the potential radiological hazards. Contrary to the above, on June 23, 2009, the licensee failed to make an adequate survey to evaluate the magnitude and extent of radiation levels for an area located in the Radwaste Facility. The finding was documented in the licensees corrective action program as PIPs O-09-04475 and O-10-01503. Because this violation was of very low safety significance and was entered into the licensees corrective action program, it is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy: NCV 50-269, 270,287/2010003-03, Failure to conduct an adequate area radiation survey of a room in the Radwaste Facility.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

a. Inspection Scope

The inspectors sampled licensee data to confirm the accuracy of reported PI data for the nine indicators during periods listed below. To determine the accuracy of the report PI elements, the reviewed data was assessed against PI definitions and guidance contained in Nuclear Energy Institute 99-02, Regulatory Assessment Indicator Guideline, Revision 5. Documents reviewed are listed in the Attachment.

Cornerstone: Mitigating Systems

  • Mitigating System Performance Index (MSPI) - High Pressure Injection (3 units)
  • MSPI - Support Cooling Water Systems (3 units)

Cornerstone: Barrier Integrity

For the period April 1, 2009, through March 31, 2010, the inspectors reviewed Operating Logs, Train Unavailability Data, Maintenance Records, Maintenance Rule Data, PIPs, Consolidated Derivation Entry Reports, and System Health Reports to verify the accuracy of the PI data reported for each PI.

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems

.1 Daily Screening of Corrective Action Reports

In accordance with IP 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed daily screening of items entered into the licensees CAP. This review was accomplished by reviewing copies of PIPs, attending daily screening meetings, and accessing the licensees computerized database.

.2 Annual Sample

a. Inspection Scope

The inspectors reviewed PIPs O-09-5082 and O-10-1108 and the associated corrective actions to assess the effectiveness of the actions that had been implemented to address issues identified in the December 2009 to January 2010 time frame related scaffold construction and placement at Oconee. The sample activities included conducting walkdowns and inspections of scaffolds erected throughout the plant, performing a review of the recently implemented Duke Nuclear Scaffold Manual and interviewing personnel associated with the scaffold program within the station and Oconee Major Projects work groups. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

.3 Operator Workarounds

a. Inspection Scope

The inspectors reviewed the cumulative effects of deficiencies that constituted operator workarounds to determine whether or not they could: affect the reliability, availability, and potential for misoperation of a mitigating system; affect multiple mitigating systems; or affect the ability of operators to respond in a correct and timely manner to plant transients and accidents. The inspectors also assessed whether operator workarounds were being identified and entered into the licensees corrective action program at an appropriate threshold.

b. Findings

No findings were identified.

.4 Semi-Annual Trend Review

a. Inspection Scope

As required by IP 71152, Identification and Resolution of Problems, the inspectors performed a review of the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screenings discussed in section 4OA2.1 above, licensee trending efforts, licensee human performance results and inspector observations made during in-plant inspections and walk-downs. The inspectors review primarily considered the six-month period of January 2010 through June 2010, although some examples expanded beyond those dates when the scope of the trend warranted. The review also included issues documented outside the normal CAP in major equipment problem lists, plant health team lists, Independent Nuclear Oversight reports, system and component health reports, self-assessment reports, and maintenance rule reports. The inspectors compared and contrasted their results with the results contained in the licensees latest quarterly trend reports. Corrective actions associated with a sample of the issues identified in the licensees trend report were reviewed for adequacy.

b. Observations and Findings

No findings were identified. In general, the licensee has identified trends and has appropriately addressed the trends with their CAP. However, the inspectors identified the following three trends that the licensee had not previously recognized. The inspectors will continue to monitor this area and assess the effectiveness of the licensees corrective actions. Documents reviewed are listed in the Attachment.

Capturing Plant Issues in the Corrective Action Program: The inspectors identified a trend during the second half of 2009 associated with weaknesses in the implementation of the PIP program. The trend was related to the inconsistent initiation of PIPs when the criteria in the licensee CAP implementing guidance document was met or not fully describing the issue to allow appropriate corrective actions to be developed or trends identified. As a result of this NRC-identified trend, the licensee initiated PIP O-10-0182.

The licensee has implemented corrective actions to address these aspects of the CAP; however, examples continue to be noted in both the inconsistent initiation of PIPs when required and describing the issue in sufficient detail and clarity to enable the appropriate corrective actions to be developed and trends identified in a timely manner. The inspectors will continue to monitor the licensees progress in this area.

Control of Vehicles Within the Protected Area (PA): The inspectors identified a trend during the second half of 2009 associated with the failure to properly control vehicles within the PA. As a result of this NRC-identified trend, the licensee initiated PIP O-10-0225. Although improvement was noted during the first half of 2010, additional examples have occurred. As a result, the inspectors will continue to monitor this trend and assess the effectiveness of the licensees corrective actions.

Contractor Activities Impacting Plant Security Measures: The inspectors identified a trend during the second half of 2009 associated with the failure of Oconee Major Project vendors to comply with site security requirements. As a result of this NRC-identified trend, the licensee initiated PIP O-10-0232. Although improvement was noted during the first half of 2010, the inspectors will continue to monitor this trend and assess the effectiveness of the licensees corrective actions.

Coordination of Outage Activities: The inspectors identified a trend during the second half of 2008 that the licensee had not previously recognized associated with the coordination of outage activities. Improvement was noted during the 2009 Unit 1 and Unit 3 refueling outage; however, the inspectors continued to monitor this area during the Unit 2 refueling outage to assess the effectiveness of corrective actions. While isolated coordination issues were noted during the Unit 2 outage, the additional oversight provided by the stations Outage organization and the formalized look-aheads documented in turnover and update sheets resulted in a significant reduction in the number of unplanned system interactions or schedule delays. Accordingly, this trend statement will no longer be followed in subsequent integrated inspection reports.

4OA3 Event Follow-up

Fire Brigade Response to Two Fires Within the Turbine Building

a. Inspection Scope

On April 30, 2010, two separate fires were reported within the turbine building. The first involved a motor on a permanent space heater and the second was a portable welding machine that shorted internally. In both cases the station fire brigade responded promptly and extinguished the fires in less than the 15-minute time frame at which the Emergency Plan would have been activated. The resident inspectors responded to the scene of both fires and observed the fire brigade performance in extinguishing the fires.

The inspectors also attended one of the post-fire response critiques and reviewed the PIPs associated with both events. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

4OA5 Other Activities

Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.

b. Findings

No findings were identified.

4OA6 Management Meetings (Including Exit Meeting)

Exit Meeting Summary

The resident inspectors presented the inspection results to Mr. David A. Baxter and other members of licensee management at the conclusion of the inspection period on July 1, 2010. The licensee acknowledged the findings presented. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary and no proprietary information was identified.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

K. Alter, Regulatory Compliance Manager
S. Batson, Engineering Manager
D. Baxter, Site Vice President
S. Boggs, Emergency Services Coordinator
J. Bohlmann, Organization Effectiveness Manager
R. Brown, Emergency Preparedness Manager
E. Burchfield, Superintendent of Operations
C. Cash, PSW Building Superintendent
P. Culbertson, Maintenance Manager
W. Edge, Engineering Supervisor II

P. Fisk; Mechanical/Civil Engineering Manager

D. Galloway, BWST Implementation Manager
P. Gillespie, Station Manager
J. Kammer, Modification Engineering Manager
T. King, Acting Safety Assurance Manager
W. Lindsay, Duck Bank Superintendent
R. Medlin, HELB Tornado-Project Manager
B. Meixell, Regulatory Compliance
K. Nicholson, Technical Specialist, Reg Compliance
W. Pursley, General Supervisor, Radiation Protection
D. Robinson, Manager, Radiation Protection
J. Schwalm, BWST Superintendent
S. Severance, Regulatory Compliance
J. Smith, Regulatory Compliance
B. Stares, Civil Engineer
D. White, Surveillance and Control, Radiation Protection

NRC

J. Stang, Project Manager, NRR

LIST OF REPORT ITEMS

Opened and Closed

05000269, 270/2010003-01 NCV Inadequate Risk Management Associated With the Unit 2 Electrical Generator Rotor Lifts (Section 1R13)
05000287/2010003-02 NCV Failure to Install Structural Rebar as Required by Instructions and Drawings (Section 1R17)
05000269, 270, 287/2010003-03 NCV Failure to Conduct an Adequate Area Radiation Survey of a Room in the Radwaste Facility (Section 2RS1)

DOCUMENTS REVIEWED