IR 05000261/1987014

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Insp Rept 50-261/87-14 on 870504-08.No Violations or Deviations Noted.Major Areas Inspected:Area of Plant Chemistry,Ie Info Notices86-106 & 86-108 & Closeout of Outstanding Insp Items
ML14191A819
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 05/18/1987
From: Kahle J, Ross W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14191A818 List:
References
50-261-87-14, IEB-82-02, IEB-82-2, IEIN-86-042, IEIN-86-106, IEIN-86-108, IEIN-86-42, NUDOCS 8706010356
Download: ML14191A819 (9)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION REGION il 101 MARIETTA STREET, ATLANTA, GEORGIA 30323 Report No.:

50-261/87-14 Licensee:

Carolina Power and Light Company P. 0. Box 1551 Raleigh, NC 27602 Docket No.:

50-261 License No.:

DPR23 Facility Name: H. B. Robinson Inspection Conducted: May 4-8, 1987 Inspector:

'

n:.,

W. J. Ross Date Signed Accompanying Personnel: R. R. Marston Approved by:

j. B. Kahle, Section chief Date Signed Division of Radiation Safety and Safeguards SUMMARY Scope:

This routine unannounced inspection was conducted in the area of plant chemistry, Inspection and Enforcement Notices86-106 and 86-108, and closeout of outstanding inspection item Results:

No violations or deviations were identifie UD ADDR

REPORT DEIAILS 1. Persons Contacted Licensee Employees

  • G. P. Beatty, Vice President, Robinson Nuclear Project
  • R. E. Morgan, General Manager
  • J. M. Curley, Director, Regulatory Compliance
  • R. M. Smith, Manager, Environmental and Radiation Control (E&RC)

W. Christensen, Laboratory Foreman (E&RC)

R. Chambers, Supervisor, Performance Engineering R. Dufresne, Engineer, Design Engineering 3. A. Laddy, Chemistry Supervisor (E&RC)

J. Harrison, Principal Specialist (E&RC)

R. Hitch, Chemistry Specialist (E&RC)

J. Murray, Supervisor, Water Treatment, Operations D. Nelson, Operations Supervisor L. Smith', Chemistry Specialist, Plant Training Nuclear Regulatory Commission

.

  • Krug, Senior Resident Inspector
  • R. Latta, Resident Inspector
  • Attended exit interview 2. Exit Interview The inspection scope and findings were summarized on May 8, 1987, with those persons indicated in Paragraph 1 above. The inspector described the areas inspected and discussed the inspection finding No dissenting comments were received from the license The licensee did not identify as proprietary any of the material provided to or reviewed by the inspector during this inspectio. Licensee Action on Previous Enforcement Matters This subject was not addressed in the inspectio. Plant Chemistry This inspectio was a re-assessment of the licensee's program to prevent degradation of the primary coolant pressure boundary (specifically the steam generator tubes)

from erosion/corrosion mechanism Through discussions with cognizant personnel, review of pertinent procedures and chemistry control data, and walkdowns of key components of the secondary cooling water cycle, the inspector evaluated the effectiveness of. the design and operation of the plant as well as the efficiency of the

chemistry control program in maintaining the desired integrity of the steam generator tubes and in providing release of radioactive specie a. Review of Plant Design and Operation During this inspection the plant was in a refueling outage after fuel cycle eleven, i.e., the second fuel cycle after major modifications of the steam generators and the balance of plant had been completed (see Inspection Report 50-261/84-49 dated January 14, 1985).

During his last inspection, in September 1985, the inspector had established that these modifications had greatly increased the licensee's capability to prevent inleakage of potentially corrosive chemical species and to maintain feedwater and steam generator water at a level of purity sufficient to meet the recommendations of the Steam Generator Owners Group (SGOG)

and the Electric Power Research Institute (EPRI).

This followup inspection revealed that continued improvement had been made in achieving and maintaining high quality secondary cooling wate The effectiveness of the principal components of the secondary cooling water system and summarized belo (1) Main Condenser - No problems had been encountered from inleakage of air or condenser cooling water into the condenser hotwell Consequently, chemistry control parameters had been maintained at levels considerably below SGOG/EPRI limits; e.g., cation conductivity approximately 0.06-0.07 umho/cm, dissolved oxygen approximately 5 ppb, and pH approximately Air inleakage had been less than 10 SCFM (standard cubic feet per minute) and was readily removed by the condenser air ejector syste (2) Service Water System -

As reported in Inspection Report 50-261/84-49, January 14, 1985, severe attack of stainless steel pipe that provide flow of Service Water to containment fan coolers had been observed during the steam generator replacement outag Ihe degradation of these pipes was attributed to microbiological induced corrosion (MIC).

During the current refueling outage the Service Water System was being flushed with water that contained hydrogen peroxide to eliminate all bacteria and environments that facilitate microbiologically induced corrosion (MIC).

The inspector was informed that a "MIC Tracking Program" had been established to identify environmental and operating conditions that might be conducive to growth of bacteria within plant system (3) Water Treatment Plant - Although purification of well water for condensate makeup and other plant uses had been complicated by the presence of relatively high levels of silica, the product of the water treatment plant had been essentially pure water (i.e.,

a specific conductivity of approximately 0.06 unho/cm).

The

licensee had previously added hydrazine to the water in the condensate storage tank to counteract inleakage of air (oxygen)

into this tank. This practice was no longer in effect because the presence of thermal-degradation products of hydrazine (especially ammonia) had complicated the use of this water for regeneration of ion-exchange resins in the deep-bed condensate polishers (i.e.,

conductivity measurements could not differentiate between ammonia and ionic impurities being washed off of the resins).

The inspector was informed that the dissolved oxygen level of water in the CST continued to be less than 100 ppb - a level that could be efficiently removed by the condenser air ejector when CST water was pumped to the hotwell for condensate makeu (4) Condensate Cleanup System - Because of the high purity of both the condensate and makeup water the licensee had been able to maintain full-flow polishing of the condensate with minimal regeneration of the deep-bed demineralizers; i.e., usually only one of the six beds were regenerated per week. The regeneration procedure had been routinely performed without contaminating.the feedwater with regenerant chemicals (sulfuric acid and sodium hydroxide) or by leakage of ion exchange resin beads from the demineralizers. The inspector attributed this excellent record, in part, to the design of the regeneration tanks, the use of neutral ion exchange resins to maintain separation between the cation and anion resin beads, and to the high level of training and competence of the radwaste operators. These operators had been dedicated to the operation of this system since it.was installed during the steam generator replacement outag (5) Feedwater -

An audit of chemistry control data that had been acquired since the inspector's last site visit in 1985 showed that, except for the presence of hydrazine and ammonia that had been continuously added for chemistry control of pH and oxygen, the feedwater was essentially pure water; i.e., cation conductivity of approximately 0.06 umho/cm. This condition had been achieved by continuously polishing the condensate and by recycling the water from the feedwater heater drains back to the hotwell until this drain water was sufficiently pure to pump forward to the feedwater pumps for augmented feedwater flo (6) Steam Generator Cleanliness - The continuous improvement in the licensee's capability to clean-up the water in the steam generator by means of both the condensate polishers and the steam generator blowdown system had been reflected in a decrease in the cation conductivity of the steam generator blowdown from 0.6 to approximately 0.2 umho/cm during the tenth fuel cycle and 0I further decrease to approximately 0.15 umho/cm during the eleventh fuel cycl Likewise, transport of solid ion oxide

"sludge" from carbon steel pipe, throughout the balance of plant, to the steam generators had been relatively small during

the tenth fuel cycle (approximately 80 pounds per steam generator) and even less during the eleventh fuel cycle (45 lbs, 28 lbs, and 16 lbs of sludge removed from Steam Generators A, B and C respectively). Finally, an audit of chemistry data during periods of plant cooldown during the eleventh fuel cycle indicated that very low levels (less than 10 ppb) of "hideout" as sulfate, chloride, or sodium -

remained in the steam.

generator The inspector considered that the licensee had attained a level of cleanliness in the steam generators that should prevent formation of local corrosive environment Although the licensee had not tested the integrity of the steam generator tubes by eddy current measurements during the current refueling outage, no evidence of cracks of other types of degradation had been observed during the outage after cycle ten (the initial fuel cycle with the new steam generator tube (7) Steam Generator Blowdown - The inspector was informed that, during the current refueling outage, modifications of the steam generator blowdown systems were being made so that this water could be cycled back to the hotwell and reclaimed rather than wasted as in the pas These modifications should not only conserve thermal energy and water but should reduce the demand for condensate makeup and, therefore, further reduce the probability for ingress of contaminants into the secondary water syste (8) Replacement of Low-Pressure Turbine Rotors -

The inspector observed the replacement of the plant's low-pressure rotors (shrunk-on turbine disks) with rotors of a new design that, among other advantages, will reduce the probability of disk failure from stress corrosion crackin The new rotors were cast as an integral unit of disks and bore and, therefore, without keyways and crevices that had become the locale for the initiation of cracks in the shrunk-on model No violations or deviations were identifie b. Review of the Licensee's Chemistry Program The following elements of the licensee's water chemistry program were reviewed during this inspectio (1) Staff - Since the inspector's last site visit the 21-person Chemistry Staff that is under the direction of the Manager of Environmental and Radiation Control had been reorganized into an analytical staff under the Laboratory Supervisor and a specialist staff under the Principal Specialis After discussions with key personnel from the Chemistry staff, the inspector concluded that the licensee had sufficient personnel resources and expertise to fully implement the type of chemistry

program recommended by the SGOG as well as to comprehend and resolve potential and/or actual site specific chemistry problem The analytical staff had been divided into five shifts that worked on the same schedules as the corresponding operations staff so that a "team" concept could be develope (2) Training -

A continuing training course that encompassed eighteen modules was being implemented by the Plant Training Department to supplement the on-the-job training being provided to chemical technician All subjects covered by the qualification cards required to perform all chemistry control responsibilities were to be taught throughout a five-year cycle and subsequent two-year requalification period (3) Procedures - The Chemistry staff had developed a draft of a new PWR Chemistry Guidelines Manual for H. B. Robinson Steam Electric Plan The inspector established that this draft manual implemented corporate policy and guidance for the development of a chemistry program that fulfills all Technical Specification requirements and which endorses and implements SGOG recommendations for both primary and secondary chemistr (4)

Primary Chemistry Control -

The inspector verified that the criteria for purity of the reactor coolant required by Technical Specification 3.1 had been met during the interval since the inspector's last site visit. The chemistry staff, with the help of personnel from the corporate support group, had been reviewing the information recently provided in the EPRI Primary Chemistry Guidelines as well as performing other studies in an effort to reduce the radiation levels of activation products in the reactor coolant. The inspector was informed that cobalt-58 had been the major source of radiation in the RCS since new Inconel tubes had been installed in the steam generators. The cobalt-58/cobalt-60 ratio. had been decreasing during the last two years as the tubes became passivated with oxide film and less nickel-58 was being transported to the reactor and activated to cobalt-5 (5) Secondary Chemistry Control -

As discussed earlier in this report, the key chemistry parameters recommended by the SGOG and EPRI for control and diagnostic purposes had been routinely monitored by the Chemistry staff. Both inline and grab sampling procedures had been use The inspector observed that additional chemistry technicians were continuing to become qualified in the use of state-of-the-art analytical instrumentation such as ion chromatography and atomic spectrophotometry for analyzing grab samples for trace levels of anions and metal ion Through an audit of secondary chemistry control data the inspector established that the licensee had been able to maintain the level of impurities, both solid and soluble, in the secondary cooling system at essentially the purity of demineralized water. Consequently, the criteria recommended by the SGOG had been significantly improved upon, so that the secondary water system was considered to be well protected against the various types of corrosion that were encountered before the steam generator tubes were replace No violations or deviations were identifie. IE Notice 86-106, Feedwater Line Break The inspector reviewed the licensee's actions that had been taken in response to this Notice that described the degradation and failure of feedwater lines at the Surry Nuclear Power Plant in December 198 These actions are summarized as follows:

a. A special pipewall-thinning examination was performed on pipes that were considered to be similar to the degraded pipes at Surr Errosion was found to be negligibl Pipe design changes were not considered to be either necessary or a viable option for wall thinnin c. Water temperature changes were not considered to be necessary or a viable option to prevent wall thinnin d. The feasibility of increasing the pH feedwater to 9.3-9.6 is being considered as a means to reduce corrosion of carbon steel pip e. A new procedure (MI10)

for surveillance of steam and steam/water pipes was implemented during the last two refueling outage Corrosion of feedwater drain lines was identified, and some of this piping has been scheduled for replacement during the current refueling outag f. This Notice had been discussed with several other utilities that had experienced erosion/corrosion in two-phase (wet steam) pipe. IE Notice 86-108, Degradation of Reactor Coolant System Pressure Boundary Resulting from Boric Acid Corrosion The inspector established that the licensee had completed a review of this Notice with the following results:

a. All RCS piping and nozzles in HBR2 were verified to have been fabricated from stainless steel

7 A review of the maintenance history and the program for lubricating threaded fasteners had been completed in 1982 in response to IE Bulletin 82-02 (which addressed the same subject). No problem areas were identifie Subsequent reviews were performed in 1983 and 1984 in response to INPO reports. Again, no further problems were foun c. Although the plant ISI program was based on an earlier Edition of the ASME Code, the licensee reviewed its program versus the 1986 Edition which has more stringent requirements for the inspection of bolted joints. This review did not identify any need for further actio Present procedures require that complete walkdown inspection of the primary coolant boundary be made before startup of the plant from a refueling outage and during shutdown for a refueling outage (before cooldown).

During the current refueling outage the licensee had observed a pinhole leak in the weld of CRD No. K6. When the insulation had been removed from the reactor vessel no damage to the carbon steel head had been observe The faulty weld had been cut out and replace Photographs of the affected area indicated that boric acid crystals had not been widespread; however, the containment fan cooler had been plugged with boric acid crystals that had been deposited from steam that had been swept into the head ventilation duct The inspector was informed that several similar pinhole leaks had been encountered in the pas. Inspector Followup Items (92701)

a. (Closed)

86-IN42:

IE Information Notice No. 86-42, Improper Maintenance of, Radiation Monitoring Systems. The inspector verified that plant procedures required independent verification of restoration lineup for ESF system b. (Closed)

Inspector Followup Item (IFI)

85-15-01:

Evaluate PASS Shielding Studies with Respect to Sample Piping External to PASS Panel, Access Areas, and Operator Location. The inspector discussed this item with cognizant licensee personnel and reviewed documentation pertaining to the ite The evaluation had been completed, and the work was scheduled to be completed by the end of the current calendar yea c. (Closed)

IFI 86-19-02:

Review Licensee's Evaluation of Cobalt-58 Results in RCS and Liquid Wastes. The inspector established that the licensee had determinated that inconsistencies between detectors had resulted from Co-58 being in suspension in RCS and had proposed methods for accurately determining cobalt-58 concentration d. (Closed) IFI 86-14-01:

Correct Typos in Second Half 1985 Semi-Annual Report; Evaluate Total Error Estimate; Provide Analytical LLD Values

Instead of Zero in the Semi-Annual Report. The inspector noted that the Semi-Annual Report for the second half of 1986 provided a table of LLDs and used the terminology "less than LLD," instead of "0" or

"not detected."

The licensee provided corrected pages for the two 1984 reports and the two 1985 reports. The licensee also provided an analysis of the individual and total measurement error