08-09-2016 | On June 12, 2016, with Millstone Power Station Unit 3 operating in MODE 1 at 100% power, operators identified the third stage of the "A" Reactor Coolant Pump ( RCP) seal had failed, which resulted in an unidentified Reactor Coolant System leak greater than the Technical Specification (TS) limit of 1 gallon per minute. Operators initiated a plant shutdown as required by TS 3.4.6.2 ACTION Statement b. During the downpower, steam generator levels were not adequately maintained and the Engineered Safety Features Actuation System generated a Turbine Trip and Feed Water Isolation on Steam Generator Water Level - High-High being exceeded on the 'B' steam generator.
In response, operators manually tripped the reactor at 23:37 (MODE 1, at approximately 20 % power). The auxiliary feedwater system started as designed.
Safety systems functioned as expected. There were no radiological challenges as a result of the event. The plant entered COLD SHUTDOWN on June 14, 2016 at 01:29.
The cause of the unidentified leak was a failed third stage on the "A" RCP seal. The seal was replaced.
The cause of the feedwater transient and resultant manual reactor trip was due to operator performance in controlling steam generator level. This is being addressed in the Corrective Action Program.
This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in manual or automatic actuation of systems listed in 10 CFR 50.73(a)(2)(iv)(B). Additionally, the plant shutdown is being reported in accordance with 10 CFR 50.73 (a)(2)(i)(A) as the completion of any nuclear plant shutdown required by the plant's Technical Specifications. |
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Category:Letter
MONTHYEARIR 05000336/20240032024-11-0707 November 2024 Integrated Inspection Report 05000336/2024003 and 05000423/2024003 and Apparent Violation and Independent Spent Fuel Storage Installation Inspection Report 07200008/2024001 ML24289A0152024-10-21021 October 2024 Review of the Fall 2023 Steam Generator Tube Inspection Report 05000423/LER-2024-001, Loss of Safety Function and Condition Prohibited by Technical Specifications for Loss of Secondary Containment Boundary2024-10-14014 October 2024 Loss of Safety Function and Condition Prohibited by Technical Specifications for Loss of Secondary Containment Boundary IR 05000336/20244022024-10-0808 October 2024 Security Baseline Inspection Report 05000336/2024402 and 05000423/2024402 (Cover Letter Only) ML24281A1102024-10-0707 October 2024 Requalification Program Inspection 05000423/LER-2023-006-02, Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications2024-09-26026 September 2024 Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications ML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24260A2192024-09-16016 September 2024 Decommissioning Trust Fund Disbursement - Revision to Previous Thirty-Day Written Notification ML24260A1952024-09-16016 September 2024 Response to Request for Additional Information Regarding Proposed Amendment to Support Implementation of Framatome Gaia Fuel ML24248A2272024-09-0404 September 2024 Operator Licensing Examination Approval ML24240A1532024-09-0303 September 2024 Summary of Regulatory Audit Supporting the Review of License Amendment Request for Implementation of Framatome Gaia Fuel IR 05000336/20240052024-08-29029 August 2024 Updated Inspection Plan for Millstone Power Station, Units 2 and 3 (Reports 05000336/2024005 and 05000423/2024005 IR 05000336/20240022024-08-13013 August 2024 Integrated Inspection Report 05000336/2024002 and 05000423/2024002 ML24221A2872024-08-0808 August 2024 Independent Spent Fuel Storage Installation (ISFSI) - Submittal of Cask Registration for Spent Fuel Storage IR 05000336/20244412024-08-0606 August 2024 Supplemental Inspection Report 05000336/2024441 and 05000423/2024441 and Follow-Up Assessment Letter (Cover Letter Only) ML24212A0742024-08-0505 August 2024 Request for Withholding Information from Public Disclosure - Millstone Power Station, Unit No. 3, Proposed Alternative Request IR-4-13 to Support Steam Generator Channel Head Drain Modification ML24211A1712024-07-25025 July 2024 Associated Independent Spent Fuels Storage Installation, Revision to Emergency Plan - Report of Change IR 05000336/20244032024-07-22022 July 2024 Information Request for the Cybersecurity Baseline Inspection, Notification to Perform Inspection 05000336/2024403 and 05000423/2024403 IR 05000336/20245012024-07-0101 July 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000336/2024501 and 05000423/2024501 ML24180A0932024-06-28028 June 2024 Readiness for Additional Inspection: EA-23-144 IR 05000336/20240102024-06-26026 June 2024 Biennial Problem Identification and Resolution Inspection Report 05000336/2024010 and 05000423/2024010 ML24178A2422024-06-25025 June 2024 2023 Annual Report of Emergency Core Cooling System (ECCS) Model, Changes Pursuant to the Requirements of 10 CFR 50.46 IR 05000336/20244402024-06-24024 June 2024 Final Significance Determination for Security-Related Greater than Green Finding(S) with Assessment Follow-up; IR 05000336/2024440 and 05000423/2024440 and Notice of Violation(S), NRC Investigation Rpt 1-2024-001 (Cvr Ltr Only) ML24176A1782024-06-20020 June 2024 Update to the Final Safety Analysis Report ML24176A2622024-06-20020 June 2024 Update to the Final Safety Analysis Report, Revision 37 ML24177A2792024-06-20020 June 2024 Preparation and Scheduling of Operator Licensing Examinations ML24280A0012024-06-20020 June 2024 Update to the Final Safety Analysis Report (Redacted Version) ML24281A2072024-06-20020 June 2024 Update to the Final Safety Analysis Report, Revision 37 (Redacted Version) 05000336/LER-2024-001, Control Room Air Conditioning Unit Inoperable Due to Refrigerant Overcharge Resulting in a Condition Prohibited by Technical Specifications2024-06-10010 June 2024 Control Room Air Conditioning Unit Inoperable Due to Refrigerant Overcharge Resulting in a Condition Prohibited by Technical Specifications ML24170B0532024-06-10010 June 2024 DOM-NAF-2-P/NP-A, Revision 0.5, Reactor Core Thermal-Hydraulics Using the VIPRE-D Computer Code ML24165A1292024-06-0505 June 2024 ISFSI, 10 CFR 50.59 Annual Change Report for 2023 Annual Regulatory Commitment Change Report for 2023 ML24128A2772024-06-0404 June 2024 Issuance of Amendment No. 290 to Revise TSs for Reactor Core Safety Limits, Fuel Assemblies, and Core Operating Limits Report for Use of Framatome Gaia Fuel (EPID L-2023-LLA-0074) (Non-Proprietary) ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities ML24110A0562024-05-21021 May 2024 Exemption from the Requirements of 10 CFR Part 50, Section 50.46, and Appendix K Regarding Use of M5 Cladding Material (EPID L-2023-LLE-0013) (Letter) ML24109A0032024-05-21021 May 2024 Issuance of Amendment No. 289 to Revise Technical Specifications to Use Framatome Loss of Coolant Accident Evaluation Methodologies for Establishing Core Operating Limit (EPID L-2023-LLA-0065) (Non-Proprietary) ML24142A0952024-05-20020 May 2024 End of Cycle 22 Steam Generator Tube Inspection Report 05000423/LER-2023-006-01, Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications2024-05-20020 May 2024 Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications ML24141A2432024-05-20020 May 2024 Response to Request for Additional Information Regarding Alloy 600 Aging Management Program Submittal Related to License Renewal Commitment No. 15 IR 05000336/20240012024-05-14014 May 2024 Integrated Inspection Report 05000336/2024001 and 05000423/2024001 and Apparent Violation ML24123A2042024-05-0202 May 2024 Pre-Decisional Replay to EA-23-144 05000423/LER-2023-006, Pressurizer Power Operated Relief Valve Failed to Stroke Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications2024-05-0202 May 2024 Pressurizer Power Operated Relief Valve Failed to Stroke Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications IR 05000336/20244012024-04-30030 April 2024 Security Baseline Inspection Report 05000336/2024401 and 05000423/2024401 (Cover Letter Only) ML24123A1222024-04-30030 April 2024 Inservice Inspection Program - Owners Activity Report, Refueling Outage 22 ML24116A0452024-04-25025 April 2024 Special Inspection Follow-Up Report 05000336/2024440 and 05000423/2024440 and Preliminary Finding(S) of Greater than Very Low Significance and NRC Investigation Report No. 1-2024-001 (Cover Letter Only) ML24116A1742024-04-24024 April 2024 Annual Radiological Environmental Operating Report ML24114A2662024-04-24024 April 2024 Submittal of 2023 Annual Radioactive Effluent Release Report ML24103A0202024-04-22022 April 2024 Summary of Regulatory Audit in Support of License Amendment Request to Use Framatome Small Break and Realistic Large Break Loss of Coolant Accident Evaluation Methodologies for Establishing Core Operating Limits ML24106A2032024-04-15015 April 2024 2023 Annual Environmental Operating Report ML24088A3302024-04-0404 April 2024 Regulatory Audit Plan in Support of License Amendment Request to Implement Framatome Gaia Fuel ML24093A2162024-04-0101 April 2024 Response to Request for Additional Information Regarding License Amendment Request to Use Framatome Small Break and Realistic Large Break Loss of Coolant Accident Evaluation Methodologies for Establishing Core Operating Limits 2024-09-04
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000423/LER-2024-001, Loss of Safety Function and Condition Prohibited by Technical Specifications for Loss of Secondary Containment Boundary2024-10-14014 October 2024 Loss of Safety Function and Condition Prohibited by Technical Specifications for Loss of Secondary Containment Boundary 05000423/LER-2023-006-02, Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications2024-09-26026 September 2024 Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications 05000336/LER-2024-001, Control Room Air Conditioning Unit Inoperable Due to Refrigerant Overcharge Resulting in a Condition Prohibited by Technical Specifications2024-06-10010 June 2024 Control Room Air Conditioning Unit Inoperable Due to Refrigerant Overcharge Resulting in a Condition Prohibited by Technical Specifications 05000423/LER-2023-006-01, Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications2024-05-20020 May 2024 Pressurizer Power Operated Relief Valve Failed to Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications 05000423/LER-2023-006, Pressurizer Power Operated Relief Valve Failed to Stroke Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications2024-05-0202 May 2024 Pressurizer Power Operated Relief Valve Failed to Stroke Open During Surveillance Testing Resulting in a Condition Prohibited by Technical Specifications 05000423/LER-2023-005, Oil Leakage from C RSS Pump Motor Challenged Meeting Its Mission Time Resulting in a Condition Prohibited by Technical Specifications2024-02-0808 February 2024 Oil Leakage from C RSS Pump Motor Challenged Meeting Its Mission Time Resulting in a Condition Prohibited by Technical Specifications 05000423/LER-2023-004, For Millstone Power Station, Unit 3 Regarding Reactor Coolant System Pressure Isolation Valves Operational Leakage Exceeded the Acceptance Criteria Resulting in a Condition Prohibited by Technical Specifications2023-12-19019 December 2023 For Millstone Power Station, Unit 3 Regarding Reactor Coolant System Pressure Isolation Valves Operational Leakage Exceeded the Acceptance Criteria Resulting in a Condition Prohibited by Technical Specifications 05000423/LER-2023-003, RCS Temperature Detector Exceeded Time Response Acceptance Criteria Resulting in a Condition Prohibited by Technical Specifications2023-12-0808 December 2023 RCS Temperature Detector Exceeded Time Response Acceptance Criteria Resulting in a Condition Prohibited by Technical Specifications 05000423/LER-2023-002, Auxiliary Feedwater Control Valve Failure Resulting in a Condition Prohibited by Technical Specifications2023-11-30030 November 2023 Auxiliary Feedwater Control Valve Failure Resulting in a Condition Prohibited by Technical Specifications ML23334A1522023-11-30030 November 2023 Auxiliary Feedwater Control Valve Failure Resulting in a Condition Prohibited by Technical Specifications 05000336/LER-2023-002, Failed Check Valve Resulted in an Unanalyzed Condition2023-08-31031 August 2023 Failed Check Valve Resulted in an Unanalyzed Condition 05000423/LER-2023-001, Automatic Reactor Trip Due to Main Generator Output Breaker Ground Fault2023-07-27027 July 2023 Automatic Reactor Trip Due to Main Generator Output Breaker Ground Fault 05000336/LER-2023-001, For Millstone, Unit 2, Structural Integrity of a Train Service Water Header Piping Could Not Be Demonstrated Causing the Unit to Operate in a Condition Prohibited by Technical Specifications2023-07-0707 July 2023 For Millstone, Unit 2, Structural Integrity of a Train Service Water Header Piping Could Not Be Demonstrated Causing the Unit to Operate in a Condition Prohibited by Technical Specifications 05000423/LER-2022-002, Two Main Steam Safety Valves Installed in Wring Location Resulting in Failure to Lift within the Technical Specification Acceptance Criteria2022-05-31031 May 2022 Two Main Steam Safety Valves Installed in Wring Location Resulting in Failure to Lift within the Technical Specification Acceptance Criteria 05000423/LER-2022-001, Emergency Core Cooling and Reactor Plant Component Cooling Water Systems Inoperable for Time Greater than Allowed by Technical Specifications2022-03-24024 March 2022 Emergency Core Cooling and Reactor Plant Component Cooling Water Systems Inoperable for Time Greater than Allowed by Technical Specifications 05000336/LER-2022-001, Structural Integrity of Reactor Building Component Cooling Water Cracked Threaded Fitting Could Not Be Established Resulting in System Inoperable Longer than Allowed by Technical Specifications2022-03-18018 March 2022 Structural Integrity of Reactor Building Component Cooling Water Cracked Threaded Fitting Could Not Be Established Resulting in System Inoperable Longer than Allowed by Technical Specifications 05000336/LER-2021-002, Failed Check Valve Resulting in Unnalyzed and Operation Prohibited by Technical Specifications2022-01-0505 January 2022 Failed Check Valve Resulting in Unnalyzed and Operation Prohibited by Technical Specifications 05000336/LER-2021-001, Incorrectly Placed Spent Fuel Assemblies in Unit 2 Spent Fuel Pool2021-09-23023 September 2021 Incorrectly Placed Spent Fuel Assemblies in Unit 2 Spent Fuel Pool 05000423/LER-2019-0012020-02-13013 February 2020 LER 2019-001-00 for Millstone Power Station Unit 3 Regarding Plant Shutdown Required by Technical Specifications, Emergency Diesel Generator Exceeded Allowed Outage Time 05000423/LER-2017-0012017-03-20020 March 2017 Loss of Safety Function - Secondary Containment, LER 17-001-00 for Millstone, Unit 3 Regarding Loss of Safety Function - Secondary Containment 05000336/LER-2016-0022016-09-20020 September 2016 Manual Reactor Trip Due to Loss of Two Circulating Water Pumps, LER 16-002-00 for Millstone Power Station Unit 2 Regarding Manual Reactor Trip Due Loss Of Two Circulating Water Pumps 05000423/LER-2016-0052016-08-0909 August 2016 Technical Specification Required Shutdown and Manual Reactor Trip Due to Steam Generator Level Oscillation, LER 16-005-00 for Millstone Power Station Unit 3 RE: Technical Specification Required Shutdown and Manual Reactor Trip Due to Steam Generator Level Oscillation 05000423/LER-2016-0042016-07-13013 July 2016 Manual Reactor Trip Due to Low Hydrogen Gas Pressure In Main Generator, LER 16-004-00 for Millstone Power Station Unit 3 RE: Manual Reactor Trip Due to Low Hydrogen Gas Pressure In Main Generator 05000336/LER-2016-0012016-06-27027 June 2016 Turbine Driven Auxiliary Feedwater Putnp Room HELB Door Left Open, LER 16-001-00 for Millstone Power Station Unit 2 RE: Turbine Driven Auxiliary Feedwater Pump Room HELB Door Left Open 05000423/LER-2016-0032016-06-0808 June 2016 Loss of Safety Function- Supplementary Leak Collection and Release System, LER 16-003-00 for Millstone Power Station, Unit 3, Regarding Loss of Safety Function-Supplementary Leak Collection and Release System 05000423/LER-2016-0022016-03-23023 March 2016 Feedwater Isolation Signal Defeated Due to Wiring Error, LER 16-002-00 for Millstone Power Station Unit 3 Regarding Feedwater Isolation Signal Defeated Due to Wiring Error 05000423/LER-2016-0012016-03-16016 March 2016 Automatic Reactor Trip on Reactor Coolant System Low Flow Due to Loss of 'B' Reactor Coolant Pump, LER 16-001-00 for Millstone Power Station Unit 3, Regarding Automatic Reactor Trip on Reactor Coolant System Low Flow Due to Loss of 'B' Reactor Coolant Pump 05000336/LER-2015-0032016-01-0707 January 2016 Valid Actuation of the Reactor Protection System, LER 15-003-00 for Millstone, Unit 2, Regarding Valid Actuation of the Reactor Protection System ML0925900552009-09-0808 September 2009 Special Report for Seismic Instrumentation ML0719302812007-04-11011 April 2007 Final ASP Analysis- Millstone (LER 336/06-002) ML0622802402006-08-0808 August 2006 Special Report for Inoperable Radiation Monitor 2024-09-26
[Table view] |
1. EVENT DESCRIPTION:
On June 12, 2016 at approximately 19:55, with Millstone Power Station Unit 3 (MPS3) operating in MODE 1 at 100% power, operators identified the third stage on the "A" Reactor Coolant Pump (RCP) seal had failed, which resulted in an unidentified Reactor Coolant System (RCS) leak greater than the Technical Specification (TS) limit. The leak was going to the containment sump at a leakage rate of approximately 2 gallons per minute (gpm) which exceeded the TS 3.4.6.2.b limit of 1 gpm UNIDENTIFIED LEAKAGE. Operators entered TS 3.4.6.2 ACTION Statement b, "With any RCS operational LEAKAGE not within limits, other than PRESSURE BOUNDARY LEAKAGE, LEAKAGE from Reactor Coolant System Pressure Isolation Valves or primary to secondary LEAKAGE, reduce the leakage rate to within limits within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> or be in at least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SHUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />", and commenced a downpower at 1% per minute in accordance with station procedures. During the downpower, steam generator levels were not adequately maintained. As a result, the Engineered Safety Features Actuation System generated a Turbine Trip and Feed Water Isolation on Steam Generator Water Level — High-High being exceeded on the 'B' steam generator. In response to the turbine trip and feedwater isolation, operators manually tripped the reactor at 23:37 (MODE 1, at approximately 20 )`/0 power). The auxiliary feedwater system started as designed and maintained steam generator levels. Safety systems functioned as expected. There were no radiological challenges as a result of the event. The plant completed the Shutdown required by Technical Specifications and entered COLD SHUTDOWN on June 14, 2016 at 01:29.
This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in manual or automatic actuation of systems listed in 10 CFR 50.73(a)(2)(iv)(B).
Additionally, the plant shutdown is being reported in accordance with 10 CFR 50.73 (a)(2)(i)(A) as the completion of any nuclear plant shutdown required by the plant's Technical Specifications.
2. CAUSE:
The cause of the UNIDENTIFIED LEAKAGE exceeding plant technical specification requirements was a failed third stage on the "A" RCP seal. Failure of the "A" RCP seal stage was caused by gradual pitting and degradation of the seal stationary faces.
The cause of the Engineered Safety Features Actuation System generated turbine trip and feedwater isolation was inadequate control of feedwater flow by the feedwater station operator which resulted in all four steam generator levels increasing and the "B" SG reaching the 80% Hi- Hi trip setpoint.
3. ASSESSMENT OF SAFETY CONSEQUENCES:
The failure of the third stage of the 'A' RCP seal followed by an excess feedwater flow transient and manual reactor trip during the rapid downpower, was bounded by the analysis presented in Final Safety Analysis Report Chapter 15.1.2, "Feedwater System Malfunctions that Result in an Increase in Feedwater Flow". Therefore, the event had a very low safety significance.
The leak resulted from failure of only the upper third stage of the three stage Flowserve RCP seal design. Pressure breakdown and flow restriction from the first two seal stages continued. The resultant leak rate from the "A" RCP seal, approximately 2 gpm, was within the capability of the charging system to maintain pressurizer level. The leakage from the seal was collected in the containment sump with no releases to the environment.
4. CORRECTIVE ACTION:
The 'A' RCP seal was replaced. Additional corrective actions will be taken in accordance with the corrective action program.
Operator performance issues for the impacted positions are being addressed in the Corrective Action Program.
5. PREVIOUS OCCURRENCES:
There are no previous occurrences with the same underlying reason or consequences.
6. ENERGY INDUSTRY IDENTIFICATION SYSTEM (EIIS) CODES:
- Solid State Protection System — JG
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05000423/LER-2016-001 | Automatic Reactor Trip on Reactor Coolant System Low Flow Due to Loss of 'B' Reactor Coolant Pump LER 16-001-00 for Millstone Power Station Unit 3, Regarding Automatic Reactor Trip on Reactor Coolant System Low Flow Due to Loss of 'B' Reactor Coolant Pump | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000336/LER-2016-001 | Turbine Driven Auxiliary Feedwater Putnp Room HELB Door Left Open LER 16-001-00 for Millstone Power Station Unit 2 RE: Turbine Driven Auxiliary Feedwater Pump Room HELB Door Left Open | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000423/LER-2016-002 | Feedwater Isolation Signal Defeated Due to Wiring Error LER 16-002-00 for Millstone Power Station Unit 3 Regarding Feedwater Isolation Signal Defeated Due to Wiring Error | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2016-002 | Manual Reactor Trip Due to Loss of Two Circulating Water Pumps LER 16-002-00 for Millstone Power Station Unit 2 Regarding Manual Reactor Trip Due Loss Of Two Circulating Water Pumps | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000423/LER-2016-003 | Loss of Safety Function- Supplementary Leak Collection and Release System LER 16-003-00 for Millstone Power Station, Unit 3, Regarding Loss of Safety Function-Supplementary Leak Collection and Release System | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000423/LER-2016-004 | Manual Reactor Trip Due to Low Hydrogen Gas Pressure In Main Generator LER 16-004-00 for Millstone Power Station Unit 3 RE: Manual Reactor Trip Due to Low Hydrogen Gas Pressure In Main Generator | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000423/LER-2016-005 | Technical Specification Required Shutdown and Manual Reactor Trip Due to Steam Generator Level Oscillation LER 16-005-00 for Millstone Power Station Unit 3 RE: Technical Specification Required Shutdown and Manual Reactor Trip Due to Steam Generator Level Oscillation | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown |
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